ML19309H872: Difference between revisions
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O THIS DOCUMENT CONTAINS gooa cuauTv enats j 800526067I NARRATIVE SIM4ARY OF OPERATING EXPERIENG DOCKET NO. 50-263 INIT , A nticello DATE 5-2-80 COMPLETED BY A. L. Myrabo TELEPHONE '612/295-5151 f.0VIII _ | |||
April 4-1-80 to Continuation of 1980 refueling outage. | April 4-1-80 to Continuation of 1980 refueling outage. | ||
4-3-80 4-4-80 Reactor critical for physics testing and reactor heat-up. | 4-3-80 4-4-80 Reactor critical for physics testing and reactor heat-up. | ||
Line 28: | Line 27: | ||
4-28-80 Generator on-line for power operation. | 4-28-80 Generator on-line for power operation. | ||
4-29-80 Orderly shutdown due to failure of recirc pump seal, to 4-30-80 | 4-29-80 Orderly shutdown due to failure of recirc pump seal, to 4-30-80 | ||
s | s | ||
. MAY 1 3 1980 | . MAY 1 3 1980 OPERATING DATA REPORT DOCKET NO. 50-263_______ | ||
OPERATING DATA REPORT DOCKET NO. 50-263_______ | |||
DATE 5- 2-80____ | DATE 5- 2-80____ | ||
COMPLETED BY A. L. Myrabo TELEPHONE 612/295-5151 OPERATING STATUS _ _ .._._ ___ ________ ____ | COMPLETED BY A. L. Myrabo TELEPHONE 612/295-5151 OPERATING STATUS _ _ .._._ ___ ________ ____ | ||
Line 44: | Line 39: | ||
: 7. tu rinnua Dependahle Capacity (Net hdGl _ _S36 I.__.._.__.__.____-_--._----.-I | : 7. tu rinnua Dependahle Capacity (Net hdGl _ _S36 I.__.._.__.__.____-_--._----.-I | ||
.l. It Chan9es Occur in Capacity Ratings (Iterns Nurnber 3 1hrough 7) Since Last Repnr t , Give Rea<ons: _ _. N / A _ .. . .,..__ ___ ___ _ _ ._ ____ __ __ | .l. It Chan9es Occur in Capacity Ratings (Iterns Nurnber 3 1hrough 7) Since Last Repnr t , Give Rea<ons: _ _. N / A _ .. . .,..__ ___ ___ _ _ ._ ____ __ __ | ||
Pow r> r ievel 1.6 Which i<estracted, 'i | Pow r> r ievel 1.6 Which i<estracted, 'i | ||
* c. ; (Net NWo) __tUA________.__.__._..__ | * c. ; (Net NWo) __tUA________.__.__._..__ | ||
,( R. m 3 0.. . For 1' .tvicttons, If Any* .tUA___.__________.___.____.______*_ | ,( R. m 3 0.. . For 1' .tvicttons, If Any* .tUA___.__________.___.____.______*_ | ||
__.._ __. ___ ___ ____.___._-.. _. ._. _.__._ _ _._ _ _.--..- -_ -- -_.. -.L | __.._ __. ___ ___ ____.___._-.. _. ._. _.__._ _ _._ _ _.--..- -_ -- -_.. -.L This Month Yr.-to-Date Curnulative i1. Hours In Reporting Period _____719 ____2903 ___ 77440 | ||
This Month Yr.-to-Date Curnulative i1. Hours In Reporting Period _____719 ____2903 ___ 77440 | |||
: 12. N urnber Of Hours Reactor Was Critical ___415.5 __ 1639.1 __ 63170.0 | : 12. N urnber Of Hours Reactor Was Critical ___415.5 __ 1639.1 __ 63170.0 | ||
: 13. Reactor Reserve Shutdown Hours _ 0.0 ___ __0.0 _._ ._._ 9 4 0 . 7 | : 13. Reactor Reserve Shutdown Hours _ 0.0 ___ __0.0 _._ ._._ 9 4 0 . 7 | ||
Line 67: | Line 58: | ||
: 24. Shutdowns Scheduled Over Next 12 Months (Ty' Date, and Duration of Each) | : 24. Shutdowns Scheduled Over Next 12 Months (Ty' Date, and Duration of Each) | ||
__ March 20, 1981 - Refueling Outage - 56 days ____ ___.___.________________ _ | __ March 20, 1981 - Refueling Outage - 56 days ____ ___.___.________________ _ | ||
: 25. If Shut Down At End Of Report Period, Estirnated Date Of Startup:__05-16-80__ | : 25. If Shut Down At End Of Report Period, Estirnated Date Of Startup:__05-16-80__ | ||
: 26. Units In Test Status (Prior to Corarnerc i a l Opera t lon) . N/A Forecast Achieved | : 26. Units In Test Status (Prior to Corarnerc i a l Opera t lon) . N/A Forecast Achieved INITIAL CRITICALITY _ __ _.. __ _____ | ||
INITIAL CRITICALITY _ __ _.. __ _____ | |||
INITIAL ELECTRICITY _ _____ ________ | INITIAL ELECTRICITY _ _____ ________ | ||
COMMERCIAL OPERATION ___ ___ __.___2_ | COMMERCIAL OPERATION ___ ___ __.___2_ | ||
= | = | ||
\ | \ | ||
f AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-263 ._ .__ | f AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-263 ._ .__ | ||
UNII MonticeLLo DATE 5- 2-00_____ | UNII MonticeLLo DATE 5- 2-00_____ | ||
Line 91: | Line 76: | ||
l | l | ||
_365__.__. | _365__.__. | ||
.{ _.._._-5.._._.. 19 __ ___ -_..__ | .{ _.._._-5.._._.. 19 __ ___ -_..__ | ||
l | l 20 -5 4 _.__-5..~._.__.__.._ _ ___ .. __ _._____ | ||
20 -5 4 _.__-5..~._.__.__.._ _ ___ .. __ _._____ | |||
S- _ _ . _ . . 79__ _ __ ___ | S- _ _ . _ . . 79__ _ __ ___ | ||
'i _ ._ _ ._ -5__ _.____ __ | 'i _ ._ _ ._ -5__ _.____ __ | ||
6 .... .. _370.. _ ._.__. | 6 .... .. _370.. _ ._.__. | ||
22 _ .___. _ _ -4 __._ _ __ | 22 _ .___. _ _ -4 __._ _ __ | ||
,. 7 ;....._ ._506 . _. . | ,. 7 ;....._ ._506 . _. . | ||
23- ._ _- -3_ _ _._ - | 23- ._ _- -3_ _ _._ - | ||
O _ __...__.. .527._ _ _ __.__._ | O _ __...__.. .527._ _ _ __.__._ | ||
24 _______-4_.________. | 24 _______-4_.________. | ||
Line 114: | Line 91: | ||
26 -4 2 | 26 -4 2 | ||
7 10 _ _ _ .. _ ._ _ S. i B - _. _ | 7 10 _ _ _ .. _ ._ _ S. i B - _. _ | ||
, 11 _ . ._ _ _ _ _ 5 1 7 . ._ ._ _. . . ._ _ 27 _ _ _ . -5._ _-.___ _ | , 11 _ . ._ _ _ _ _ 5 1 7 . ._ ._ _. . . ._ _ 27 _ _ _ . -5._ _-.___ _ | ||
i'& _ ___.. _ _508 __. __ _ | i'& _ ___.. _ _508 __. __ _ | ||
Line 120: | Line 96: | ||
13 _.___ _ _473-_._____ __ , | 13 _.___ _ _473-_._____ __ , | ||
29 _____._2i______.__._ | 29 _____._2i______.__._ | ||
___.._ _ -4 | ___.._ _ -4 30 3 | ||
30 | |||
3 | |||
'14 ._ __.____ _547 ...__ ._ _ | '14 ._ __.____ _547 ...__ ._ _ | ||
15 .._.___ _ 551 _._ _____.___. 31 _ _ _ . . _ _ _ _ _ . . _ _ _ . _ | 15 .._.___ _ 551 _._ _____.___. 31 _ _ _ . . _ _ _ _ _ . . _ _ _ . _ | ||
. 16 __________547____________ | . 16 __________547____________ | ||
t INSTRUCTIONS-On this format, tist~the average daily unit power level in MWe-Net for e-Och ddy in.the, reporting-Month. Compute to the nearest whole megawatt. | |||
t | |||
INSTRUCTIONS- | |||
On this format, tist~the average daily unit power level in MWe-Net for e-Och ddy in.the, reporting-Month. Compute to the nearest whole megawatt. | |||
.. 1 0, y. | .. 1 0, y. | ||
. DOCKET NO. 50-263 UNIT SIIUTDOWNS \ND POhER REDUCliONS , | . DOCKET NO. 50-263 UNIT SIIUTDOWNS \ND POhER REDUCliONS , | ||
Line 156: | Line 119: | ||
* 4 F: Forced Reason: Method: Edubii G - Inst ructions S Schedulet! A Equ;pment Failure (Explain) !-Manual ' for Preparation of Data B. Maintenance or Test 2 Manual Scram. Entry Sheets fer Licensee | * 4 F: Forced Reason: Method: Edubii G - Inst ructions S Schedulet! A Equ;pment Failure (Explain) !-Manual ' for Preparation of Data B. Maintenance or Test 2 Manual Scram. Entry Sheets fer Licensee | ||
- C Refueling 3 Automatic Scram. Esent Report (LER) File t NUREG. | - C Refueling 3 Automatic Scram. Esent Report (LER) File t NUREG. | ||
D Regulator) Restriction 4 Other (Explaini 0161) | D Regulator) Restriction 4 Other (Explaini 0161) | ||
E-Operator Training & License Examination . | E-Operator Training & License Examination . | ||
F-Administrati.e . | F-Administrati.e . | ||
5 G. Operational Error (Explain t Exhibit I - Same Source 19/77) Il Other (Explaint}} | 5 G. Operational Error (Explain t Exhibit I - Same Source 19/77) Il Other (Explaint}} |
Latest revision as of 10:49, 1 February 2020
ML19309H872 | |
Person / Time | |
---|---|
Site: | Monticello ![]() |
Issue date: | 05/02/1980 |
From: | Myrabo A NORTHERN STATES POWER CO. |
To: | |
Shared Package | |
ML113110980 | List: |
References | |
NUDOCS 8005200578 | |
Download: ML19309H872 (4) | |
Text
.
O THIS DOCUMENT CONTAINS gooa cuauTv enats j 800526067I NARRATIVE SIM4ARY OF OPERATING EXPERIENG DOCKET NO. 50-263 INIT , A nticello DATE 5-2-80 COMPLETED BY A. L. Myrabo TELEPHONE '612/295-5151 f.0VIII _
April 4-1-80 to Continuation of 1980 refueling outage.
4-3-80 4-4-80 Reactor critical for physics testing and reactor heat-up.
4-5-80 Generator on-line prior to turbine overspeed test. Turbine overspeed test completed.
4-6-80 Power operation at essentially 100% of rated power except for weekend to surveillance testing and control rod adjustments.
4-18-80 4-19-80 Reactor scram on turbine trip due to reactor high level. Trip was received while attempting orderly shutdown because of failed recirc pump seals.
4-26-80 Scheduled outage to repair recirc pump seals-hUfE: Reactor was in a shutdown condition prior to the start of this outage.
4-28-80 Generator on-line for power operation.
4-29-80 Orderly shutdown due to failure of recirc pump seal, to 4-30-80
s
. MAY 1 3 1980 OPERATING DATA REPORT DOCKET NO. 50-263_______
DATE 5- 2-80____
COMPLETED BY A. L. Myrabo TELEPHONE 612/295-5151 OPERATING STATUS _ _ .._._ ___ ________ ____
l Notes l 1 Unii h o.io . . . _ __..__ __ __. __itonticelto l l
' . ' . Reportinq peitod: __._. _._ _. .. __.. APRIL l l
.5 . L i c tmsed Therraa l Power (MWt): _ ____ _ __ 1670 l l
- 4. Naraepiate Ratang (Gioss Mue) _.__..__ __ 569 l l S. im s 9 n Electrical Rating (Net MWe) _. ___545.4 l l
- 6. M a x iva.ua Dependable Copacity (Gross MWe) __564 l l
- 7. tu rinnua Dependahle Capacity (Net hdGl _ _S36 I.__.._.__.__.____-_--._----.-I
.l. It Chan9es Occur in Capacity Ratings (Iterns Nurnber 3 1hrough 7) Since Last Repnr t , Give Rea<ons: _ _. N / A _ .. . .,..__ ___ ___ _ _ ._ ____ __ __
Pow r> r ievel 1.6 Which i<estracted, 'i
- c. ; (Net NWo) __tUA________.__.__._..__
,( R. m 3 0.. . For 1' .tvicttons, If Any* .tUA___.__________.___.____.______*_
__.._ __. ___ ___ ____.___._-.. _. ._. _.__._ _ _._ _ _.--..- -_ -- -_.. -.L This Month Yr.-to-Date Curnulative i1. Hours In Reporting Period _____719 ____2903 ___ 77440
- 12. N urnber Of Hours Reactor Was Critical ___415.5 __ 1639.1 __ 63170.0
- 13. Reactor Reserve Shutdown Hours _ 0.0 ___ __0.0 _._ ._._ 9 4 0 . 7
- 14. Hours Generator On-Line ___360.6 ___i571.7 _. 61541.0
- 15. Unit Reserve Shutdown Hours _____0.0 .___ _ 0.0 ____ __0.0
- 16. Gross Therrna l Energy Generated (MWH) ._ 536251 _ 2090129 _101032991
- 17. Gross Electrical Energy Generated (MWH) _ 182410 __ 703560 _ 31681620
- 10. Net Electrical Energy Generated (MWH) _ 173908 __ 668750 __30300954
- 19. Unit Service Factor __ 50.2% _._ 54.1% __ _ 79.5%
- 20. Unit Availability Factor __ 50.2% ___ 54.1% '
____ 79.5%
- 21. Unit Capacity Factor (Using .MDC Net) __ 45.1% __ 43.0% ._. 73.0%
- 22. Unit Capacity Factor (Using DER Net) _ 44.3% __ 42.2% _ __ 71.7%
- 23. Unit Forced Outage Rate _ 35.2% __ 11.5% ____ 6.6%
- 24. Shutdowns Scheduled Over Next 12 Months (Ty' Date, and Duration of Each)
__ March 20, 1981 - Refueling Outage - 56 days ____ ___.___.________________ _
- 25. If Shut Down At End Of Report Period, Estirnated Date Of Startup:__05-16-80__
- 26. Units In Test Status (Prior to Corarnerc i a l Opera t lon) . N/A Forecast Achieved INITIAL CRITICALITY _ __ _.. __ _____
INITIAL ELECTRICITY _ _____ ________
COMMERCIAL OPERATION ___ ___ __.___2_
=
\
f AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-263 ._ .__
UNII MonticeLLo DATE 5- 2-00_____
COMPLETED BY A. L. Myrabo TELEPHONE 612/295-5151 hfir4 l Il ....APhlL . _ _ . _
I> A Y AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL.
1 4
( ttWe-Ne t > (MWe-Net) 1 .- . _ _ 3..- . -,_._ -
17 _ _____ 550_ - _ - _ __
< ."a _ _ _ _ . _ _ . _ . -~4____- _._ __
10 _ _- __546_ ______ _
l
_365__.__.
.{ _.._._-5.._._.. 19 __ ___ -_..__
l 20 -5 4 _.__-5..~._.__.__.._ _ ___ .. __ _._____
S- _ _ . _ . . 79__ _ __ ___
'i _ ._ _ ._ -5__ _.____ __
6 .... .. _370.. _ ._.__.
22 _ .___. _ _ -4 __._ _ __
,. 7 ;....._ ._506 . _. .
23- ._ _- -3_ _ _._ -
O _ __...__.. .527._ _ _ __.__._
24 _______-4_.________.
V . _ __ _5i9 .. ._ __ _
25 ___._ ___ -4 _ _ __._ _.__
P i
26 -4 2
7 10 _ _ _ .. _ ._ _ S. i B - _. _
, 11 _ . ._ _ _ _ _ 5 1 7 . ._ ._ _. . . ._ _ 27 _ _ _ . -5._ _-.___ _
i'& _ ___.. _ _508 __. __ _
28 -. ___.137__ - _ _. _
13 _.___ _ _473-_._____ __ ,
29 _____._2i______.__._
___.._ _ -4 30 3
'14 ._ __.____ _547 ...__ ._ _
15 .._.___ _ 551 _._ _____.___. 31 _ _ _ . . _ _ _ _ _ . . _ _ _ . _
. 16 __________547____________
t INSTRUCTIONS-On this format, tist~the average daily unit power level in MWe-Net for e-Och ddy in.the, reporting-Month. Compute to the nearest whole megawatt.
.. 1 0, y.
. DOCKET NO. 50-263 UNIT SIIUTDOWNS \ND POhER REDUCliONS ,
UNIT N etE Moriticello DATE 5-Z-80 April CO%1PLETED BY A. L. Myrabo REPORT \10NTil TELEPHONE 612/295-5151 I
"w _
N... DJie 1, 5 $#""'~ I'2 g cause a coneciise y a e-= R e ort :
1.5 4 .- A ..en ...
== -z 32g v: s
,} - Present Recurrence
- 5 4' 4-1-80 S 101.6 C 4 N/A ZZ ZZZZZZ Continuation of 1980 Refueling Outage.
5 4-5-80 S 3.2 B 1 N/A IIA 'IURBIN Turbine overspeed test 6 4-19-80 F 151.2 A 3 N/A CB PtNPXX Turbine' trip on high level while re-ducing power after recirc pump seal failure. Seals on both recirc pumps replaced.
17, .4-26-80 S- 57.5 A 4 N/A CB IWIPXX Outage taken to repair recirc punp seal.
N0lI: Reactor was in s shutdown con dition prior tothe start of i
this outage.
8 4-29-80 F 44.8 A 1 N/A CB PtNPXX Plant shutdown to repair recirc punp seal.
I 2 3
- 4 F: Forced Reason: Method: Edubii G - Inst ructions S Schedulet! A Equ;pment Failure (Explain) !-Manual ' for Preparation of Data B. Maintenance or Test 2 Manual Scram. Entry Sheets fer Licensee
- C Refueling 3 Automatic Scram. Esent Report (LER) File t NUREG.
D Regulator) Restriction 4 Other (Explaini 0161)
E-Operator Training & License Examination .
F-Administrati.e .
5 G. Operational Error (Explain t Exhibit I - Same Source 19/77) Il Other (Explaint