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#REDIRECT [[IR 05000228/2014201]]
{{Adams
| number = ML14351A262
| issue date = 12/19/2014
| title = IR: 05000228/2014201 on November 17-19, 2014 at the Aerotest Operations, Inc. Facility - NRC Routine Inspection Report No. 50-228/2014-201 and Notice of Violation
| author name = Hsueh K
| author affiliation = NRC/NRR/DPR
| addressee name = Warren S
| addressee affiliation = Aerotest Operations, Inc
| docket = 05000228
| license number = R-098
| contact person = C Bassett
| document report number = IR 2014201
| document type = Inspection Report, Letter, Notice of Violation
| page count = 13
}}
See also: [[see also::IR 05000228/2014201]]
 
=Text=
{{#Wiki_filter:December 19, 2014
Ms. Sandra Warren, General Manager
Aerotest Operations, Inc.
3455 Fostoria Way
San Ramon, CA 94583
SUBJECT:        AEROTEST OPERATIONS, INC. - NRC ROUTINE INSPECTION REPORT
                NO. 50-228/2014-201 AND NOTICE OF VIOLATION
Dear Ms. Warren:
On November 17-19, 2014, the U.S. Nuclear Regulatory Commission (NRC, the Commission)
completed an inspection at the Aerotest Radiography and Research Reactor facility (Inspection
Report No. 50-228/2014-201). The enclosed report documents the inspection results which
were discussed on November 19, 2014, with you and Mr. Alfredo Meren, Manager of Reactor
Operations.
The inspection examined activities conducted under your license as they relate to safety and
compliance with the Commissions rules and regulations and with the conditions of your license.
The inspector reviewed selected procedures and records, observed activities, and interviewed
personnel.
Based on the results of this inspection, the NRC has determined that a Severity Level IV
violation of NRC requirements occurred. The violation was evaluated in accordance with the
NRC Enforcement Policy. The current Enforcement Policy is included on the NRC's Web site at
http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html. The violation is cited in
the enclosed Notice of Violation (Notice) and the circumstances surrounding it are described in
detail in the subject inspection report. The violation is being cited in the Notice because it
constitutes a failure to meet regulatory requirements that has more than minor safety
significance and the violation was identified by the NRC.
You are required to respond to this letter and should follow the instructions specified in the
enclosed Notice when preparing your response. The NRC will use your response in part, to
determine whether further enforcement action is necessary to ensure compliance with
regulatory requirements.
 
S. Warren                                    -2-
In accordance with Title 10 of the Code of Federal Regulations Section 2.390 of the NRCs
Agency Rules of Practice and Procedure, a copy of this letter, its enclosure, and your
response (if any) will be available electronically for public inspection in the NRC Public
Document Room or from the NRCs document system (Agencywide Documents Access and
Management System (ADAMS)). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html. To the extent possible, your response should not
include any personal privacy or proprietary information so that it can be made available to the
public without redaction.
Should you have any questions concerning this inspection, please contact Mr. Craig Bassett at
(301) 466-4495 or by electronic mail at Craig.Bassett@nrc.gov.
                                              Sincerely,
                                              /RA/
                                              Kevin Hsueh, Chief
                                              Research and Test Reactors Oversight Branch
                                              Division of Policy and Rulemaking
                                              Office of Nuclear Reactor Regulation
Docket No. 50-228
License No. R-98
Enclosures:
1. Notice of Violation
2. NRC Inspection Report No. 50-228/2014-201
cc: See next page
 
Aerotest Operations, Inc.                        Docket No. 50-228
cc:
Mr. Michael Anderson, President
Aerotest Operations, Inc.
Autoliv ASP, Inc.
1320 Pacific Drive
Auburn Hills, MI 48326
Mr. Alfredo Meren, Manager of Reactor Operations
Aerotest Operations, Inc.
3455 Fostoria Way
San Ramon, CA 94583
California Energy Commission
1516 Ninth Street, MS-34
Sacramento, CA 95814
Radiological Health Branch
P.O. Box 997414, MS 7610
Sacramento, CA 95899-7414
Test, Research, and Training
Reactor Newsletter
University of Florida
202 Nuclear Sciences Center
Gainesville, FL 32611
 
S. Warren                                    -2-
In accordance with Title 10 of the Code of Federal Regulations Section 2.390 of the NRCs
Agency Rules of Practice and Procedure, a copy of this letter, its enclosure, and your
response (if any) will be available electronically for public inspection in the NRC Public
Document Room or from the NRCs document system (Agencywide Documents Access and
Management System (ADAMS)). ADAMS is accessible from the NRC Web site at
http://www.nrc.gov/reading-rm/adams.html. To the extent possible, your response should not
include any personal privacy or proprietary information so that it can be made available to the
public without redaction.
Should you have any questions concerning this inspection, please contact Mr. Craig Bassett at
(301) 466-4495 or by electronic mail at Craig.Bassett@nrc.gov.
                                              Sincerely,
                                              /RA/
                                              Kevin Hsueh, Chief
                                              Research and Test Reactors Oversight Branch
                                              Division of Policy and Rulemaking
                                              Office of Nuclear Reactor Regulation
Docket No. 50-228
License No. R-98
Enclosures:
1. Notice of Violation
2. NRC Inspection Report No. 50-228/2014-201
cc: See next page
DISTRIBUTION:
PUBLIC                        PROB r/f                RidsNrrDprPrta Resource
RidsNrrDprPrtb Resource        CBassett, NRR            STraiforos, NRR
MNorris, NSIR                  MCompton, NRR
ACCESSION NO.: ML14351A262                          *concurred via e-mail      NRC-002
OFFICE                  NRR/DPR/PROB*                            NRR/DPR/PROB
NAME                    CBassett                                  KHsueh
DATE                    12/18/2014                                12/19/2014
                                    OFFICIAL RECORD COPY
 
                                      NOTICE OF VIOLATION
Aerotest Operations, Inc.                                                      Docket No.      50-228
Aerotest Radiography and Research Reactor                                      License No.      R-98
During a U.S. Nuclear Regulatory Commission (NRC) inspection conducted on
November 17-19, 2014, a violation of NRC requirements was identified. In accordance with the
NRC Enforcement Policy, the violation is listed below:
Title 10 of the Code of Federal Regulations Part 55.21, Medical Examination, states that a
licensee shall have a medical examination by a physician every two years.
Contrary to the above, a Senior Reactor Operator at the Aerotest Radiography and Research
Reactor facility had a medical examination on November 12, 2010, but did not have another
medical examination until September 18, 2013, a period greater than two years and a period
greater than 30 months which includes a grace period of 6 months typically allowed for licensed
operators at Research and Test Reactor facilities.
This has been determined to be a Severity Level IV violation (Section 6.4.d.1(c)).
Pursuant to the provisions of 10 CFR 2.201, Aerotest Operations, Inc. is hereby required to
submit a written statement or explanation to the U.S. Nuclear Regulatory Commission,
ATTN: Document Control Desk, Washington, D.C. 20555-0001 with a copy to the responsible
inspector, within 30 days of the date of the letter transmitting this Notice of Violation (Notice).
This reply should be clearly marked as a "Reply to a Notice of Violation" and should
include: (1) the reason for the violation, or, if contested, the basis for disputing the violation or
severity level, (2) the corrective steps that have been taken and the results achieved, (3) the
corrective steps that will be taken to avoid further violations, and (4) the date when full
compliance will be achieved. Your response may reference or include previous docketed
correspondence, if the correspondence adequately addresses the required response. If an
adequate reply is not received within the time specified in this Notice, an order or Demand for
Information may be issued as to why the license should not be modified, suspended, or
revoked, or why such other action as may be proper should not be taken. Where good cause is
shown, consideration will be given to extending the response time.
If you contest this enforcement action, you should also provide a copy of your response,
with the basis for your denial, to the Director, Office of Enforcement, U.S. Nuclear Regulatory
Commission, Washington, D.C. 20555-0001.
Because your response will be made available electronically for public inspection in the NRC
Public Document Room or from the Publicly Available Records component of the NRCs
Agencywide Documents Access and Management System (ADAMS), to the extent possible, it
should not include any personal privacy, proprietary, or safeguards information so that it can be
made available to the public without redaction. ADAMS is accessible from the NRC Web site at
(the Public Electronic Reading Room) http://www.nrc.gov/reading-rm/adams.html. If personal
privacy or proprietary information is necessary to provide an acceptable response, then please
provide a bracketed copy of your response that identifies the information that should be
protected and a redacted copy of your response that deletes such information. If you request
                                                                                          Enclosure 1
 
                                                -2-
withholding of such material, you must specifically identify the portions of your response that
you seek to have withheld and provide in detail the bases for your claim of withholding
(e.g., explain why the disclosure of information will create an unwarranted invasion of personal
privacy or provide the information required by 10 CFR 2.390(b) to support a request for
withholding confidential commercial or financial information). If safeguards information is
necessary to provide an acceptable response, please provide the level of protection described
in 10 CFR 73.21.
In accordance with 10 CFR 19.11, you may be required to post this Notice within two working
days.
Dated this 19th day of December, 2014
 
                  U.S. NUCLEAR REGULATORY COMMISSION
                OFFICE OF NUCLEAR REACTOR REGULATION
Docket No:      50-228
License No:    R-98
Report No:      50-228/2014-201
Licensee:      Aerotest Operations, Inc.
Facility:      Aerotest Radiography and Research Reactor
Location:      3455 Fostoria Way
                San Ramon, CA 94583
Dates:          November 17-19, 2014
Inspector:      Craig Bassett
Accompanied by: Kevin Hsueh, Chief
                Research and Test Reactors Oversight Branch
                William Schuster, Project Manager
                Research and Test Reactors Oversight Branch
Approved by:    Kevin Hsueh, Chief
                Research and Test Reactors Oversight Branch
                Division of Policy and Rulemaking
                Office of Nuclear Reactor Regulation
                                                            Enclosure 2
 
                                      EXECUTIVE SUMMARY
                                      Aerotest Operations, Inc.
                            Aerotest Radiography and Research Reactor
                                    Report No: 50-228/2014-201
The primary focus of this routine, announced inspection was the on-site review of selected
aspects of the Aerotest Operations, Inc. (the licensees) Class II research and test reactor safety
program including: 1) organization and staffing, 2) review and audit and design change
functions, 3) facility operations, 4) procedures, 5) operator requalification, 6) maintenance and
surveillance, 7) fuel handling, and 8) experiments since the last U.S. Nuclear Regulatory
Commission (NRC) inspection of these areas.
Organization and Staffing
      The licensee's organization and staffing were in compliance with the requirements
        specified in Section 12 of the facility Technical Specifications.
Review and Audit and Design Change Functions
      Review and oversight functions required by Technical Specifications Section 12.1.3 were
        acceptably completed by the Reactor Safeguards Committee.
      No changes had been made at the facility since the last NRC inspection but a process
        for design change was in place and would be followed if changes were initiated.
Reactor Operations
      Reactor operations had ceased in 2010.
Procedures
      Facility procedures were being reviewed by the licensee and reviewed and approved by
        the Reactor Safeguards Committee as required by Technical Specifications and
        administrative procedures.
Operator Requalification
      Operator requalification was being conducted and completed as required by the
        Operator Requalification Program.
      One violation was noted for failure to have an operator with an active license complete a
        medical examination biennially as required.
 
                                              -2-
Maintenance and Surveillance
      Maintenance was being completed in accordance with Technical Specifications and
      procedural requirements.
      The program for completing surveillance checks, tests, verifications, and calibrations
      was being implemented in accordance with Technical Specifications requirements.
Fuel Handling
      Following a fuel inspection in 2013, the total number of fuel elements with cracked or
      damaged cladding has been determined.
      Fuel movements and weighing of those elements in canisters were completed and
      documented in accordance with the requirements specified by procedure.
Experiments
      No experiments or irradiations have been conducted since October 15, 2010.
 
                                          REPORT DETAILS
Summary of Facility Status
Aerotest Operations, Inc. (Aerotest, the licensee) 250 kilowatt (kW) TRIGA conversion research
reactor, known as the Aerotest Radiography and Research Reactor (ARRR), had been operated
in the past in support of neutron radiography experiments and reactor operator training.
However, the licensee had voluntarily ceased to operate the research reactor on October 15,
2010, because of foreign ownership issues. During this inspection, the reactor remained shut
down and was not operated.
1.      Organization and Staffing
        a.      Inspection Scope (Inspection Procedure [IP] 69001)
                The inspector reviewed the following regarding the licensee's organization and
                staffing to ensure that the requirements of Technical Specifications (TS) Sections
                10.1 and 12.1 were being met:
                      Current staffing of the ARRR
                      Management responsibilities and organizational structure indicated in
                        Section 12 of the TS, as implemented through the latest revision to the
                        Facility License Number (No.) 98, Amendment No. 4, dated January 28,
                        1981
                      Section II of the ARRR Procedures Manual entitled, Operating
                        Procedures, Procedure Change Notice (PCN) No. 2, RSC approval
                        dated June 28, 1990
                      Annual Summary of Changes, Tests, and Experiments at Aerotest
                        Radiography and Research Reactor (ARRR) for the period from July 1,
                        2012, to June 30, 2013, issued July 30, 2013, and for the period from
                        July 1, 2013, to June 30, 2014, issued July 8, 2014 (the facility annual
                        reports)
        b.      Observations and Findings
                Through discussions with licensee representatives, the inspector determined that
                management responsibilities at the facility had not changed since the previous
                routine NRC inspection conducted in December 2012 (NRC Inspection Report
                No. 50-228/2012-206). The inspector noted that the General Manager remained
                the local official in charge of day-to-day activities at the facility. The Reactor
                Supervisor (who was also assigned the duties of the Reactor Operations
                Manager) retained direct control over, and overall responsibility for, management
                of the reactor as specified in the TS. The General Manager and the Reactor
                Supervisor reported to the President, Aerotest Operations, Inc.
                Through review of records and discussions with licensee personnel, the inspector
                determined that the staffing at the facility had been cut in 2010 due to issues
                involving foreign ownership. The current staffing at the ARRR consisted of the
 
                                          -2-
        General Manager (who was also the Security Officer, the Radiation Safety
        Officer, and a Senior Reactor Operator), the Reactor Supervisor (who was also
        the Manager of Reactor Operations and a Senior Reactor Operator), a Nuclear
        Engineer (who was also a Senior Reactor Operator), the Manager of Nuclear
        Radiography, and the Manager of Quality Assurance. The employees were
        monitoring the facility and conducting maintenance and surveillance duties as
        required by the TS.
  c. Conclusion
        The licensee's organization was as specified in the TS. The employees were
        monitoring the facility and conducting maintenance and surveillance duties as
        required by the TS.
2. Review and Audit and Design Change Functions
  a.    Inspection Scope (IP 69001)
        In order to ensure that the audits and reviews were being completed as required
        by TS Section 12.1.3 and to verify that any modifications to the facility were
        consistent with 10 CFR 50.59, the inspector reviewed the following:
                Completed audits for 2013 and 2014
                Changes made under the licensees 10 CFR 50.59 change process
                Reactor Safeguards Committee meeting minutes for 2013 and 2014
                Duties of the Reactor Safeguards Committee detailed in TS Section 12
                Charter of the Reactor Safeguards Committee outlined in Section I of the
                ARRR Procedures Manual entitled, Administrative Procedures, PCN
                No. 2, RSC approval dated June 28, 1990
                The last two ARRR annual reports
  b.    Observations and Findings
        (1)    Review and Audits Functions
                The Reactor Safeguards Committee (RSC) met at least once per year in
                accordance with TS requirements with the last two meetings held on
                November 19, 2013, and on November 5, 2014. The inspector reviewed
                the RSC's meeting minutes for these meetings. The meeting minutes
                showed that the RSC had considered the types of topics stipulated by the
                TS. It was noted that the meetings were attended by all members of the
                committee. Review of the minutes also indicated that the committee
                provided guidance and direction to ensure suitable oversight of the
                facility.
                The inspector verified that the periodic audits specified by TS Section
                12.1.3 were being completed as required. The RSC minutes and audit
                records indicated that the Chair of the RSC and generally another RSC
 
                                            -3-
                member conducted unannounced audits of facility operations annually
                and submitted the results to the President, Aerotest Operations, Inc. The
                inspector noted that current issues and the facility status were reviewed
                and that the licensee took appropriate corrective actions in response to
                those audit findings or recommendations as needed.
        (2)    Design Change Functions
                Through review of applicable records and interviews with licensee
                personnel, the inspector determined that some design changes had been
                considered at the facility but that none had actually been initiated or
                completed since the last NRC inspection. It was noted that TS and
                procedural requirements were in place to ensure that changes, if
                proposed, would be reviewed by the RSC and in accordance with 10 CFR
                50.59 as required.
  c.  Conclusion
        Review and oversight functions required by TS Section 12.1.3 were acceptably
        completed by the RSC. No changes had been made at the facility since the last
        NRC inspection but a process for design change was in place and would be
        followed if changes were initiated.
3. Operations
  a.    Inspection Scope (IP 69001)
        The inspector reviewed selected portions and/or aspects of the following to
        ensure compliance with TS Sections 10 and 12:
                ARRR Operational Log Sheets and ARRR Startup/Shutdown Sheets for
                2013 and to date in 2014
                Section II of the ARRR Procedures Manual entitled, Operating
                Procedures, PCN No. 2, RSC approval dated June 28, 1990
                The last two ARRR annual reports
  b.    Observations and Findings
        The inspector reviewed ARRR Startup/Shutdown Sheets and Operational Log
        Sheets for reactor-related checks and activities dating from January 2013
        through October 2014. Since October 2010, the reactor had not been operated
        but Startup/Shutdown Sheets and Operational Log Sheets had been filled out to
        document the completion of various activities including quarterly maintenance,
        control rod inspection, fuel handling, and other checks and calibrations.
        The operating logs appeared to be complete and provided an acceptable
        indication of facility activities. The Annual Summaries of Changes, Tests, and
 
                                            -4-
          Experiments (the licensees annual reports to the NRC) documented the fact that
          no operations had occurred during the past two years.
    c.    Conclusions
          Reactor operations had ceased in 2010. The operating logs appeared to be
          complete and provided an acceptable indication of facility activities.
4. Procedures
    a.    Inspection Scope (IP 69001)
        The inspector reviewed the following to ensure that the requirements of TS
        Section 12.2 were being met concerning written procedures:
                  Varioius ARRR procedures
                  Procedure Approval Sheets
                  Procedure Change Notice forms
                  ARRR procedure review sign-off forms
                  Section I of the ARRR Procedures Manual entitled, Administrative
                  Procedures, which detailed the process used to review, revise, and
                  approve all facility procedures
    b.    Observations and Findings
          The inspector noted that procedures had been developed for reactor operations
          and safety as required by the TS. The licensees procedures were found to be
          acceptable even though no operations were currently in progress. The inspector
          noted that the administrative procedure specified the responsibilities of the RSC.
          The inspector verified that a designated member of the RSC had completed
          biennial reviews of the facility procedures as required. It was noted that the last
          review of all procedures had occurred on May 15, 2013. The licensee verified
          that any substantive revisions to procedures would be presented to the RSC for
          review and approval as required by TS.
    c.    Conclusion
          Facility procedures satisfied TS and administrative procedure requirements
          which included being reviewed by the licensee and reviewed and approved by
          the RSC.
5.  Operator Requalification Program
    a.    Inspection Scope (IP 69001)
          To verify compliance with the Operator Requalification Program for the ARRR,
          which was submitted to the NRC on July 13, 2000, the inspector reviewed:
 
                                  -5-
        Status of all qualified operators licenses
        Operator physical examination records for 2012 and 2014
        Selected ARRR Operational Log Sheets documenting reactivity
        manipulations for 2013 and 2014
        SRO Licensed Activities Log documenting active operator supervisory
        and related functions for 2013 and 2014
        2014 Senior Reactor Operator Biennial Written Examinations and related
        records
        2013 and 2014 Senior Reactor Operator Annual Operating test results
        and related records
b. Observations and Findings
  (1)  Active Duty Status
        There were three people who maintained an SRO license at the facility.
        The inspector verified that the SROs licenses were current. It was noted
        that the paperwork for one individual had been submitted in a timely
        manner for a license renewal. Records showed that operators were given
        biennial requalification examinations and annual operations tests as
        required. Logs indicated that operators maintained active duty status as
        required by performing the required maintenance and inspections of
        reactor components or by completing supervisory and related licensed
        operator duties. The Operator Requalification Program was being
        maintained up to date. The inspector also verified that the operators were
        reviewing the contents of all abnormal and emergency procedures on a
        regularly scheduled basis as indicated by a sign off sheet located in the
        emergency procedures folder.
  (2)  Medical Examinations
        10 CFR Part 55.21 states that a licensee shall have a medical
        examination by a physician every two years.
        The inspector examined medical records to verify that each operator had
        received a biennial physical examination as required. It was noted that
        two of the Senior Reactor Operators had received a medical examination
        every two years as required by 10 CFR 55.21. The third SRO had had an
        examination on November 12, 2010, but had not had another examination
        until September 18, 2013.
        The inspector noted that the third SRO and the other two SROs had been
        actively engaged in completing maintenance and surveillance activities
        associated with the reactor, conducting periodic security tests, and
        performing SRO-related functions such as supervising others during the
        entire period from November 2010 through September 2013. This
        included the period from May 2013 to September 2013 which was the
 
                                            -6-
                  time period in excess of the 30 months allowed for Research and Test
                  Reactor (RTR) operators to receive a medical examination.
                  The licensee was informed that failure to have an operator with an active
                  license complete a medical examination every two years and within the
                  30 month time period normally allowed for RTR operator licensees was a
                  violation of 10 CFR 55.21 (VIO 50-228/2014-201-01).
    c.    Conclusion
            Operator requalification was being conducted and completed as required by the
            Operator Requalification Program. One violation was noted for failure to have an
            operator with an active license complete a medical examination biennially as
            required.
6. Maintenance and Surveillance
    a.    Inspection Scope (IP 69001)
          To determine that maintenance and surveillance activities were being completed
          as required by TS Sections 3, 4, 5, 6, and 7, the inspector reviewed:
                  ARRR Repair Folders for various instruments
                  Operations Request Forms for 2013 and to date in 2014 which document
                  the completion of inspections, fuel movement, and instrument repair and
                  calibration
                  Monthly Alarm Check Lists for 2013 and to date in 2014
                  ARRR Pool Water Analysis sheets for 2013 and to date in 2014
                  Quarterly Maintenance Check Lists for 2013 and to date in 2014
                  Selected ARRR Startup/Shutdown Sheets for 2013 and to date in 2014
                  Section VIII of the ARRR Procedures Manual entitled, Maintenance
                  Procedures, PCN No. 2, RSC approval dated January 14, 1993
    b.    Observations and Findings
            (1)    Maintenance
                  The various Repair Folders and Operations Request Forms maintained
                  by the licensee indicated that emergent problems were addressed by
                  appropriate corrective maintenance as needed. If electrical components
                  for the nuclear instrumentation were replaced, the maintenance protocol
                  stipulated that calibrations and voltage checks occur prior to the
                  instrumentation being placed back into service. The inspector verified
                  that these tests were completed as required. Records showed that
                  routine maintenance activities were conducted at the required frequency
                  and in accordance with the TS and/or the applicable procedure.
 
                                          -7-
        (2)    Surveillance
                After suspending reactor operations in October 2010, the licensee
                continued to complete various monthly, quarterly, semiannual, and annual
                checks, tests, and calibrations as required. It was noted that the licensee
                had developed a modified checklist to ensure that appropriate oversight
                was maintained over various other items. These included such items as
                pool water temperature, air filter changeout, water conductivity, and cycling
                the pumps. These items were checked on a daily or weekly basis even
                though this was not required because the reactor was shut down and not
                operating.
  c.    Conclusion
        Maintenance was being completed in accordance with TS and procedural
        requirements. The modified program for surveillance checks, tests, verifications,
        and calibrations was being implemented in accordance with TS requirements that
        were still applicable with the reactor shutdown.
7. Fuel Handling
  a.    Inspection Scope (IP 69001)
        The inspector reviewed selected aspects of the following to verify that fuel
        movement and handling was being conducted as required by TS Section 5.1.1
        and Section 11:
                Revised Fuel Weighing Procedure
                Fuel movement and examination records
                Fuel handling equipment and reactor instrumentation
                Various records and data sheets related to fuel movement
                Selected ARRR Operational Log Sheets for 2013 and 2014
                Data Sheets for Fuel and Graphite Transfer forms for 2013 and 2014
                Letter from NRC to Licensee, Aerotest Radiography and Research
                Reactor (ARRR) Fuel Examination, letter dated July 29, 1992
                Section IV of the ARRR Procedures Manual entitled, Critical Assembly
                and Power Calibration
  b.    Observations and Findings
        (1)    Fuel Elements With Damaged Cladding
                The licensee has experienced various problems with their fuel. As
                documented in IR Nos. 50-228/2012-201 through 50-228/2012-206, the
                licensee took various measures to deal with the problems. These are
                briefly described below.
 
                          -8-
In December 2011 the licensee began an inspection of all their fuel
elements in an effort to comply with their commitment to the U.S. Nuclear
Regulatory Commission (NRC) to inspect all the fuel elements every 5
years. After removing all the elements that they could, the licensee found
that there were 27 aluminum clad fuel elements and 11 graphite elements
that were stuck in place and could not be removed through core upper
grid plate (none of the stainless steel clad elements were found to be
stuck). The licensee then used their underwater video camera to conduct
an inspection of those fuel elements. The licensee found that, of those
elements that remained in the core, four had signs of cracks in the
cladding. On January 9, 2012, the licensee notified the NRC of the
cracked fuel elements. The licensee submitted a letter documenting the
problem the same day.
The licensee subsequently made the decision to remove the stuck fuel
elements from the core and they hired a contractor to assist in the project.
A project plan was subsequently developed for removing all the elements
and submitted it to the licensee. When all the elements had been
removed from the core, it was the intention of the licensee to place the
fuel elements with cracked cladding in specially designed and fabricated
canisters. Before beginning removal of the fuel with damaged cladding,
the licensee anticipated that four to five more elements would be found
with cracks in the cladding, in addition to the ones already noted.
Therefore, a total of ten canisters were ordered and fabricated and a
storage rack was designed and fabricated to hold up to twelve canisters
in the reactor pool.
During the period of July 16-26, 2012, licensee and contractor personnel
were able to remove all the stuck fuel elements from the core and
conduct an initial examination of the elements. The licensee then
proceeded to examine all the remaining aluminum clad elements and all
of the stainless steel clad elements that were stored in the pool. Initially,
two elements with cracked cladding were placed into the specially
designed canisters (i.e., canned) and placed in the new storage rack.
However, after examining all the fuel elements, the licensee determined
that there were substantially more fuel elements with cladding problems
than had originally been anticipated. On August 10, 2012, the licensee
submitted a letter to the NRC documenting the fact that the inspection of
the fuel elements at the facility indicated that there were a total of 22 fuel
elements with cracks in the cladding. Plans were made to have
contractor personnel return to the ARRR facility on December 10, 2012,
to complete the containerization process.
The NRC staff observed as each of the elements with damaged cladding
was placed into a canister and the canister was closed, dried, tested,
backfilled with a cover gas, and weighed. The canisters were then placed
into pre-designated locations in the new storage rack on the reactor pool
floor.
 
                              -9-
    During a fuel inspection conducted in July 2013, the licensee found that 8
    fuel element serial numbers from the July 2012 inspection had been
    misidentified. Many of the serial numbers were very hard to read and
    only with a different camera was the licensee able to correctly identify all
    the proper numbers. The licensee also found two more elements with
    cracks in the cladding. In addition, one element was found to have
    bubbles leaking from the cladding. The bubbles were observed to stop
    after just a few minutes. This brings the number of fuel elements with
    cracked or damaged cladding to 25.
(2) Fuel Weighing Problems
    During their fuel inspection earlier this year, the licensee attempted to
    weigh the cans containing damaged fuel, for the purpose of comparing
    2014 weights with 2012 weights. They planned to verify that none of the
    fuel cans had allowed any water to enter the canisters, which would
    allow the fuel elements inside to continue to corrode. Canisters that
    were heavier than their 2012 weights would be assumed to have had
    water leaked into them. After beginning the weighing process, the
    licensee was unable to match the previous weights of the first four
    canisters. Also, there were problems with the strain gage which showed
    fluctuating weights if the canisters were moved even one inch. When
    the licensee and the Chairman of the Reactor Safeguards Committee
    reviewed the videotape of previous weighing operations, several points
    of potential error in the weighing operation were noted, especially with
    the depth of water over the weighed element. Therefore, it was noted
    that buoyancy affected the weights observed. The licensee then halted
    the weighing operation and re-worked the Reactor Work Instruction
    (RWI) and included an appendix for the weighing procedure, which was
    not previously described in the RWI. The new RWI required the entire
    assembly to hang vertically in one line from the crane hook, instead of
    being run through an I-bolt which added frictional forces, to ensure that
    each weighing was done in the exact same manner. The licensee also
    took care to make sure that the cans were all weighed at the same depth
    of the pool, which was near the bottom so it was easily reproducible.
    The licensee re-weighed all of the canisters during the week of
    September 29, 2014. Using the new procedure, the weights were much
    more uniform. The cropped instrumented fuel element (IFE) with the new
    swage top was different than the other elements and weighed 8.1
    pounds. All of the other 21 canisters weighed 7.7 pounds, +/- 0.1 pound.
    The weighing data was sent via email to the RSC. After reviewing the
    data, the RSC was satisfied that none of the cans had any water
    intrusion.
 
                                              - 10 -
                      The inspector reviewed the RWI and the weighing data. It appeared that
                      the procedure used to weigh the canisters was appropriate and that there
                      had been no water leakage into the canisters.
      c.    Conclusion
            Following a fuel inspection in 2013, the total number of fuel elements with
            cracked or damaged cladding has been determined to be 25. Fuel movements
            and weighing of those elements in canisters were completed and documented in
            accordance with the requirements specified by procedure.
8.  Experiments
      a.    Inspection Scope (IP 69001)
            To ensure that the requirements of TS Sections 8 and 9 were being met
            concerning experimental programs, the inspector reviewed selected aspects
            and/or portions of:
                    Aerotest Experiment Type Review forms (previously designated as
                      AGNIR Operation Request Forms) documenting experiments approved
                      by the RSC
                    Section VII of the ARRR Procedures Manual entitled, Experiment Review
                      and Approval, stipulating experimental program requirements
                    The last two ARRR annual reports
    b.      Observations and Findings
            There were six basic types of experiments that had been approved to be
            conducted at the ARRR facility. The one most commonly used was No. 114 -
            neutron radiography performed in the radiography facilities. Based on records
            review, observations of the facility, and radiation surveys, the inspector verified
            that no experiments had been conducted since October 2010.
      c.    Conclusion
            No experiments had been conducted since October 2010.
10. Follow-up on Previously Identified Item
      a.    Inspection Scope (IP 92701)
            The inspector reviewed the licensee's actions taken in response to a previously
            identified Inspector Follow-up Item.
 
                                    - 11 -
b. Observation and Findings
  (1)    Inspector Follow-up Item (IFI) - 50-228/2007-201-01 - Follow-up on the
          completion of the Autoliv, Inc. divestiture and negation plans involving
          Aerotest Operations, Inc.
          During an inspection in 2007, the inspector discussed the issue of the
          apparent indirect or ultimate transfer of the license. This had occurred
          when the ownership of the Aerotest Radiography and Research Reactor
          (ARRR) was transferred in substantial part to Autoliv, Inc., through an
          indirect transfer. This issue had been under review by both the licensee
          and the NRC for several years. During the inspection it was noted that
          the pathway to a resolution had apparently been established. The
          resolution of this issue never materialized and has been the subject of
          continuing discussions between the licensee and the NRC.
          The original issue concerning foreign ownership and divestiture is closed.
  (2)    IFI - 50-228/2010-201-01 - Follow-up on the licensees corrective actions
          to instruct workers in the proper use of extremity dosimetry - finger rings.
          During an inspection in 2010, an issue was noted concerning the
          positioning of workers extremity monitoring devices, i.e., their finger
          rings. Workers at the facility are issued ring dosimeters that are used
          whenever they handle radioactive materials. The dosimeter is in the form
          of a plastic ring containing one thermoluminescent chip enclosed in a
          protective cover. The dosimeter is intended to be worn on the finger
          closest to the source of the radiation, with the TLD chip facing the palm
          side of the hand. Through Interviews with licensee personnel it was
          noted that workers were wearing their ring dosimeter during work
          activities, but that sometimes the dosimeter was worn on the thumb or
          small finger because it would not fit properly on any of the other fingers.
          The rings were also being worn with the TLD chip facing the back of the
          hand. In this configuration, the dosimeter monitored the general area
          radiation in the vicinity of the hand rather than the dose to the hand. The
          licensee was cautioned that workers should be instructed to wear their
          extremity monitors - finger rings properly in order to provide an accurate
          assessment of the dose to the hands.
          During this inspection it was noted that no work was being performed and
          no extremity monitoring was needed or being used. This issue is
          considered closed.
c. Conclusion
  Two IFIs were reviewed and closed.
 
                                          - 12 -
14. Exit Meeting Summary
    The inspector reviewed the inspection results with members of licensee management at
    the conclusion of the inspection on November 19, 2014. The licensee acknowledged the
    findings presented and did not identify as proprietary any of the material provided to or
    reviewed by the inspector during the inspection.
 
                        PARTIAL LIST OF PERSONS CONTACTED
Licensee Personnel
C. Bauman        Nuclear Engineer and Senior Reactor Operator
F. Meren          Reactor Supervisor and Reactor Operations Manager
T. Richey        Neutron Radiography Manager
S. Warren        General Manager and Radiological Safety Officer
M. Wilkinson      Quality Assurance Manager
                              INSPECTION PROCEDURE USED
IP 69001    Class II Non-Power Reactors
IP 92701    Review of Previously Identified Items
                        ITEMS OPENED, CLOSED, AND DISCUSSED
Opened
None
Closed
50-228/2007-201-01 IFI      Follow-up on the completion of the Autoliv, Inc. divestiture and
                            negation plans involving Aerotest Operations, Inc.
50-228/2010-201-01 IFI      Follow-up on the licensees corrective actions to instruct workers
                            in the proper use of extremity dosimetry - finger rings.
                                  LIST OF ACRONYMS USED
ADAMS        Agencywide Documents Access and Management System
AO          Aerotest Operations, Inc.
ARRR        Aerotest Radiography and Research Reactor
CFR          Code of Federal Regulations
E-Plan      Emergency Plan
IFI          Inspector Follow-up Item
kW          kilowatt
LOA          Letter of Agreement
N-Ray        neutron radiography
NRC          Nuclear Regulatory Commission
OEA          OEA Aerospace, Inc.
ORF          Operations Request Form
PCN          Procedure Change Notice
RSC          Reactor Safeguards Committee
SRO          Senior Reactor Operator
SRV          San Ramon Valley
TS          Technical Specification
}}

Latest revision as of 18:30, 31 October 2019

IR: 05000228/2014201 on November 17-19, 2014 at the Aerotest Operations, Inc. Facility - NRC Routine Inspection Report No. 50-228/2014-201 and Notice of Violation
ML14351A262
Person / Time
Site: Aerotest
Issue date: 12/19/2014
From: Kevin Hsueh
Division of Policy and Rulemaking
To: Warren S
Aerotest
C Bassett
References
IR 2014201
Download: ML14351A262 (13)


See also: IR 05000228/2014201

Text

December 19, 2014

Ms. Sandra Warren, General Manager

Aerotest Operations, Inc.

3455 Fostoria Way

San Ramon, CA 94583

SUBJECT: AEROTEST OPERATIONS, INC. - NRC ROUTINE INSPECTION REPORT

NO. 50-228/2014-201 AND NOTICE OF VIOLATION

Dear Ms. Warren:

On November 17-19, 2014, the U.S. Nuclear Regulatory Commission (NRC, the Commission)

completed an inspection at the Aerotest Radiography and Research Reactor facility (Inspection

Report No. 50-228/2014-201). The enclosed report documents the inspection results which

were discussed on November 19, 2014, with you and Mr. Alfredo Meren, Manager of Reactor

Operations.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspector reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, the NRC has determined that a Severity Level IV

violation of NRC requirements occurred. The violation was evaluated in accordance with the

NRC Enforcement Policy. The current Enforcement Policy is included on the NRC's Web site at

http://www.nrc.gov/about-nrc/regulatory/enforcement/enforce-pol.html. The violation is cited in

the enclosed Notice of Violation (Notice) and the circumstances surrounding it are described in

detail in the subject inspection report. The violation is being cited in the Notice because it

constitutes a failure to meet regulatory requirements that has more than minor safety

significance and the violation was identified by the NRC.

You are required to respond to this letter and should follow the instructions specified in the

enclosed Notice when preparing your response. The NRC will use your response in part, to

determine whether further enforcement action is necessary to ensure compliance with

regulatory requirements.

S. Warren -2-

In accordance with Title 10 of the Code of Federal Regulations Section 2.390 of the NRCs

Agency Rules of Practice and Procedure, a copy of this letter, its enclosure, and your

response (if any) will be available electronically for public inspection in the NRC Public

Document Room or from the NRCs document system (Agencywide Documents Access and

Management System (ADAMS)). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html. To the extent possible, your response should not

include any personal privacy or proprietary information so that it can be made available to the

public without redaction.

Should you have any questions concerning this inspection, please contact Mr. Craig Bassett at

(301) 466-4495 or by electronic mail at Craig.Bassett@nrc.gov.

Sincerely,

/RA/

Kevin Hsueh, Chief

Research and Test Reactors Oversight Branch

Division of Policy and Rulemaking

Office of Nuclear Reactor Regulation

Docket No. 50-228

License No. R-98

Enclosures:

1. Notice of Violation

2. NRC Inspection Report No. 50-228/2014-201

cc: See next page

Aerotest Operations, Inc. Docket No. 50-228

cc:

Mr. Michael Anderson, President

Aerotest Operations, Inc.

Autoliv ASP, Inc.

1320 Pacific Drive

Auburn Hills, MI 48326

Mr. Alfredo Meren, Manager of Reactor Operations

Aerotest Operations, Inc.

3455 Fostoria Way

San Ramon, CA 94583

California Energy Commission

1516 Ninth Street, MS-34

Sacramento, CA 95814

Radiological Health Branch

P.O. Box 997414, MS 7610

Sacramento, CA 95899-7414

Test, Research, and Training

Reactor Newsletter

University of Florida

202 Nuclear Sciences Center

Gainesville, FL 32611

S. Warren -2-

In accordance with Title 10 of the Code of Federal Regulations Section 2.390 of the NRCs

Agency Rules of Practice and Procedure, a copy of this letter, its enclosure, and your

response (if any) will be available electronically for public inspection in the NRC Public

Document Room or from the NRCs document system (Agencywide Documents Access and

Management System (ADAMS)). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html. To the extent possible, your response should not

include any personal privacy or proprietary information so that it can be made available to the

public without redaction.

Should you have any questions concerning this inspection, please contact Mr. Craig Bassett at

(301) 466-4495 or by electronic mail at Craig.Bassett@nrc.gov.

Sincerely,

/RA/

Kevin Hsueh, Chief

Research and Test Reactors Oversight Branch

Division of Policy and Rulemaking

Office of Nuclear Reactor Regulation

Docket No. 50-228

License No. R-98

Enclosures:

1. Notice of Violation

2. NRC Inspection Report No. 50-228/2014-201

cc: See next page

DISTRIBUTION:

PUBLIC PROB r/f RidsNrrDprPrta Resource

RidsNrrDprPrtb Resource CBassett, NRR STraiforos, NRR

MNorris, NSIR MCompton, NRR

ACCESSION NO.: ML14351A262 *concurred via e-mail NRC-002

OFFICE NRR/DPR/PROB* NRR/DPR/PROB

NAME CBassett KHsueh

DATE 12/18/2014 12/19/2014

OFFICIAL RECORD COPY

NOTICE OF VIOLATION

Aerotest Operations, Inc. Docket No. 50-228

Aerotest Radiography and Research Reactor License No. R-98

During a U.S. Nuclear Regulatory Commission (NRC) inspection conducted on

November 17-19, 2014, a violation of NRC requirements was identified. In accordance with the

NRC Enforcement Policy, the violation is listed below:

Title 10 of the Code of Federal Regulations Part 55.21, Medical Examination, states that a

licensee shall have a medical examination by a physician every two years.

Contrary to the above, a Senior Reactor Operator at the Aerotest Radiography and Research

Reactor facility had a medical examination on November 12, 2010, but did not have another

medical examination until September 18, 2013, a period greater than two years and a period

greater than 30 months which includes a grace period of 6 months typically allowed for licensed

operators at Research and Test Reactor facilities.

This has been determined to be a Severity Level IV violation (Section 6.4.d.1(c)).

Pursuant to the provisions of 10 CFR 2.201, Aerotest Operations, Inc. is hereby required to

submit a written statement or explanation to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, D.C. 20555-0001 with a copy to the responsible

inspector, within 30 days of the date of the letter transmitting this Notice of Violation (Notice).

This reply should be clearly marked as a "Reply to a Notice of Violation" and should

include: (1) the reason for the violation, or, if contested, the basis for disputing the violation or

severity level, (2) the corrective steps that have been taken and the results achieved, (3) the

corrective steps that will be taken to avoid further violations, and (4) the date when full

compliance will be achieved. Your response may reference or include previous docketed

correspondence, if the correspondence adequately addresses the required response. If an

adequate reply is not received within the time specified in this Notice, an order or Demand for

Information may be issued as to why the license should not be modified, suspended, or

revoked, or why such other action as may be proper should not be taken. Where good cause is

shown, consideration will be given to extending the response time.

If you contest this enforcement action, you should also provide a copy of your response,

with the basis for your denial, to the Director, Office of Enforcement, U.S. Nuclear Regulatory

Commission, Washington, D.C. 20555-0001.

Because your response will be made available electronically for public inspection in the NRC

Public Document Room or from the Publicly Available Records component of the NRCs

Agencywide Documents Access and Management System (ADAMS), to the extent possible, it

should not include any personal privacy, proprietary, or safeguards information so that it can be

made available to the public without redaction. ADAMS is accessible from the NRC Web site at

(the Public Electronic Reading Room) http://www.nrc.gov/reading-rm/adams.html. If personal

privacy or proprietary information is necessary to provide an acceptable response, then please

provide a bracketed copy of your response that identifies the information that should be

protected and a redacted copy of your response that deletes such information. If you request

Enclosure 1

-2-

withholding of such material, you must specifically identify the portions of your response that

you seek to have withheld and provide in detail the bases for your claim of withholding

(e.g., explain why the disclosure of information will create an unwarranted invasion of personal

privacy or provide the information required by 10 CFR 2.390(b) to support a request for

withholding confidential commercial or financial information). If safeguards information is

necessary to provide an acceptable response, please provide the level of protection described

in 10 CFR 73.21.

In accordance with 10 CFR 19.11, you may be required to post this Notice within two working

days.

Dated this 19th day of December, 2014

U.S. NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

Docket No: 50-228

License No: R-98

Report No: 50-228/2014-201

Licensee: Aerotest Operations, Inc.

Facility: Aerotest Radiography and Research Reactor

Location: 3455 Fostoria Way

San Ramon, CA 94583

Dates: November 17-19, 2014

Inspector: Craig Bassett

Accompanied by: Kevin Hsueh, Chief

Research and Test Reactors Oversight Branch

William Schuster, Project Manager

Research and Test Reactors Oversight Branch

Approved by: Kevin Hsueh, Chief

Research and Test Reactors Oversight Branch

Division of Policy and Rulemaking

Office of Nuclear Reactor Regulation

Enclosure 2

EXECUTIVE SUMMARY

Aerotest Operations, Inc.

Aerotest Radiography and Research Reactor

Report No: 50-228/2014-201

The primary focus of this routine, announced inspection was the on-site review of selected

aspects of the Aerotest Operations, Inc. (the licensees) Class II research and test reactor safety

program including: 1) organization and staffing, 2) review and audit and design change

functions, 3) facility operations, 4) procedures, 5) operator requalification, 6) maintenance and

surveillance, 7) fuel handling, and 8) experiments since the last U.S. Nuclear Regulatory

Commission (NRC) inspection of these areas.

Organization and Staffing

The licensee's organization and staffing were in compliance with the requirements

specified in Section 12 of the facility Technical Specifications.

Review and Audit and Design Change Functions

Review and oversight functions required by Technical Specifications Section 12.1.3 were

acceptably completed by the Reactor Safeguards Committee.

No changes had been made at the facility since the last NRC inspection but a process

for design change was in place and would be followed if changes were initiated.

Reactor Operations

Reactor operations had ceased in 2010.

Procedures

Facility procedures were being reviewed by the licensee and reviewed and approved by

the Reactor Safeguards Committee as required by Technical Specifications and

administrative procedures.

Operator Requalification

Operator requalification was being conducted and completed as required by the

Operator Requalification Program.

One violation was noted for failure to have an operator with an active license complete a

medical examination biennially as required.

-2-

Maintenance and Surveillance

Maintenance was being completed in accordance with Technical Specifications and

procedural requirements.

The program for completing surveillance checks, tests, verifications, and calibrations

was being implemented in accordance with Technical Specifications requirements.

Fuel Handling

Following a fuel inspection in 2013, the total number of fuel elements with cracked or

damaged cladding has been determined.

Fuel movements and weighing of those elements in canisters were completed and

documented in accordance with the requirements specified by procedure.

Experiments

No experiments or irradiations have been conducted since October 15, 2010.

REPORT DETAILS

Summary of Facility Status

Aerotest Operations, Inc. (Aerotest, the licensee) 250 kilowatt (kW) TRIGA conversion research

reactor, known as the Aerotest Radiography and Research Reactor (ARRR), had been operated

in the past in support of neutron radiography experiments and reactor operator training.

However, the licensee had voluntarily ceased to operate the research reactor on October 15,

2010, because of foreign ownership issues. During this inspection, the reactor remained shut

down and was not operated.

1. Organization and Staffing

a. Inspection Scope (Inspection Procedure [IP] 69001)

The inspector reviewed the following regarding the licensee's organization and

staffing to ensure that the requirements of Technical Specifications (TS) Sections

10.1 and 12.1 were being met:

Current staffing of the ARRR

Management responsibilities and organizational structure indicated in

Section 12 of the TS, as implemented through the latest revision to the

Facility License Number (No.) 98, Amendment No. 4, dated January 28,

1981

Section II of the ARRR Procedures Manual entitled, Operating

Procedures, Procedure Change Notice (PCN) No. 2, RSC approval

dated June 28, 1990

Annual Summary of Changes, Tests, and Experiments at Aerotest

Radiography and Research Reactor (ARRR) for the period from July 1,

2012, to June 30, 2013, issued July 30, 2013, and for the period from

July 1, 2013, to June 30, 2014, issued July 8, 2014 (the facility annual

reports)

b. Observations and Findings

Through discussions with licensee representatives, the inspector determined that

management responsibilities at the facility had not changed since the previous

routine NRC inspection conducted in December 2012 (NRC Inspection Report

No. 50-228/2012-206). The inspector noted that the General Manager remained

the local official in charge of day-to-day activities at the facility. The Reactor

Supervisor (who was also assigned the duties of the Reactor Operations

Manager) retained direct control over, and overall responsibility for, management

of the reactor as specified in the TS. The General Manager and the Reactor

Supervisor reported to the President, Aerotest Operations, Inc.

Through review of records and discussions with licensee personnel, the inspector

determined that the staffing at the facility had been cut in 2010 due to issues

involving foreign ownership. The current staffing at the ARRR consisted of the

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General Manager (who was also the Security Officer, the Radiation Safety

Officer, and a Senior Reactor Operator), the Reactor Supervisor (who was also

the Manager of Reactor Operations and a Senior Reactor Operator), a Nuclear

Engineer (who was also a Senior Reactor Operator), the Manager of Nuclear

Radiography, and the Manager of Quality Assurance. The employees were

monitoring the facility and conducting maintenance and surveillance duties as

required by the TS.

c. Conclusion

The licensee's organization was as specified in the TS. The employees were

monitoring the facility and conducting maintenance and surveillance duties as

required by the TS.

2. Review and Audit and Design Change Functions

a. Inspection Scope (IP 69001)

In order to ensure that the audits and reviews were being completed as required

by TS Section 12.1.3 and to verify that any modifications to the facility were

consistent with 10 CFR 50.59, the inspector reviewed the following:

Completed audits for 2013 and 2014

Changes made under the licensees 10 CFR 50.59 change process

Reactor Safeguards Committee meeting minutes for 2013 and 2014

Duties of the Reactor Safeguards Committee detailed in TS Section 12

Charter of the Reactor Safeguards Committee outlined in Section I of the

ARRR Procedures Manual entitled, Administrative Procedures, PCN

No. 2, RSC approval dated June 28, 1990

The last two ARRR annual reports

b. Observations and Findings

(1) Review and Audits Functions

The Reactor Safeguards Committee (RSC) met at least once per year in

accordance with TS requirements with the last two meetings held on

November 19, 2013, and on November 5, 2014. The inspector reviewed

the RSC's meeting minutes for these meetings. The meeting minutes

showed that the RSC had considered the types of topics stipulated by the

TS. It was noted that the meetings were attended by all members of the

committee. Review of the minutes also indicated that the committee

provided guidance and direction to ensure suitable oversight of the

facility.

The inspector verified that the periodic audits specified by TS Section

12.1.3 were being completed as required. The RSC minutes and audit

records indicated that the Chair of the RSC and generally another RSC

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member conducted unannounced audits of facility operations annually

and submitted the results to the President, Aerotest Operations, Inc. The

inspector noted that current issues and the facility status were reviewed

and that the licensee took appropriate corrective actions in response to

those audit findings or recommendations as needed.

(2) Design Change Functions

Through review of applicable records and interviews with licensee

personnel, the inspector determined that some design changes had been

considered at the facility but that none had actually been initiated or

completed since the last NRC inspection. It was noted that TS and

procedural requirements were in place to ensure that changes, if

proposed, would be reviewed by the RSC and in accordance with 10 CFR

50.59 as required.

c. Conclusion

Review and oversight functions required by TS Section 12.1.3 were acceptably

completed by the RSC. No changes had been made at the facility since the last

NRC inspection but a process for design change was in place and would be

followed if changes were initiated.

3. Operations

a. Inspection Scope (IP 69001)

The inspector reviewed selected portions and/or aspects of the following to

ensure compliance with TS Sections 10 and 12:

ARRR Operational Log Sheets and ARRR Startup/Shutdown Sheets for

2013 and to date in 2014

Section II of the ARRR Procedures Manual entitled, Operating

Procedures, PCN No. 2, RSC approval dated June 28, 1990

The last two ARRR annual reports

b. Observations and Findings

The inspector reviewed ARRR Startup/Shutdown Sheets and Operational Log

Sheets for reactor-related checks and activities dating from January 2013

through October 2014. Since October 2010, the reactor had not been operated

but Startup/Shutdown Sheets and Operational Log Sheets had been filled out to

document the completion of various activities including quarterly maintenance,

control rod inspection, fuel handling, and other checks and calibrations.

The operating logs appeared to be complete and provided an acceptable

indication of facility activities. The Annual Summaries of Changes, Tests, and

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Experiments (the licensees annual reports to the NRC) documented the fact that

no operations had occurred during the past two years.

c. Conclusions

Reactor operations had ceased in 2010. The operating logs appeared to be

complete and provided an acceptable indication of facility activities.

4. Procedures

a. Inspection Scope (IP 69001)

The inspector reviewed the following to ensure that the requirements of TS

Section 12.2 were being met concerning written procedures:

Varioius ARRR procedures

Procedure Approval Sheets

Procedure Change Notice forms

ARRR procedure review sign-off forms

Section I of the ARRR Procedures Manual entitled, Administrative

Procedures, which detailed the process used to review, revise, and

approve all facility procedures

b. Observations and Findings

The inspector noted that procedures had been developed for reactor operations

and safety as required by the TS. The licensees procedures were found to be

acceptable even though no operations were currently in progress. The inspector

noted that the administrative procedure specified the responsibilities of the RSC.

The inspector verified that a designated member of the RSC had completed

biennial reviews of the facility procedures as required. It was noted that the last

review of all procedures had occurred on May 15, 2013. The licensee verified

that any substantive revisions to procedures would be presented to the RSC for

review and approval as required by TS.

c. Conclusion

Facility procedures satisfied TS and administrative procedure requirements

which included being reviewed by the licensee and reviewed and approved by

the RSC.

5. Operator Requalification Program

a. Inspection Scope (IP 69001)

To verify compliance with the Operator Requalification Program for the ARRR,

which was submitted to the NRC on July 13, 2000, the inspector reviewed:

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Status of all qualified operators licenses

Operator physical examination records for 2012 and 2014

Selected ARRR Operational Log Sheets documenting reactivity

manipulations for 2013 and 2014

SRO Licensed Activities Log documenting active operator supervisory

and related functions for 2013 and 2014

2014 Senior Reactor Operator Biennial Written Examinations and related

records

2013 and 2014 Senior Reactor Operator Annual Operating test results

and related records

b. Observations and Findings

(1) Active Duty Status

There were three people who maintained an SRO license at the facility.

The inspector verified that the SROs licenses were current. It was noted

that the paperwork for one individual had been submitted in a timely

manner for a license renewal. Records showed that operators were given

biennial requalification examinations and annual operations tests as

required. Logs indicated that operators maintained active duty status as

required by performing the required maintenance and inspections of

reactor components or by completing supervisory and related licensed

operator duties. The Operator Requalification Program was being

maintained up to date. The inspector also verified that the operators were

reviewing the contents of all abnormal and emergency procedures on a

regularly scheduled basis as indicated by a sign off sheet located in the

emergency procedures folder.

(2) Medical Examinations

10 CFR Part 55.21 states that a licensee shall have a medical

examination by a physician every two years.

The inspector examined medical records to verify that each operator had

received a biennial physical examination as required. It was noted that

two of the Senior Reactor Operators had received a medical examination

every two years as required by 10 CFR 55.21. The third SRO had had an

examination on November 12, 2010, but had not had another examination

until September 18, 2013.

The inspector noted that the third SRO and the other two SROs had been

actively engaged in completing maintenance and surveillance activities

associated with the reactor, conducting periodic security tests, and

performing SRO-related functions such as supervising others during the

entire period from November 2010 through September 2013. This

included the period from May 2013 to September 2013 which was the

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time period in excess of the 30 months allowed for Research and Test

Reactor (RTR) operators to receive a medical examination.

The licensee was informed that failure to have an operator with an active

license complete a medical examination every two years and within the

30 month time period normally allowed for RTR operator licensees was a

violation of 10 CFR 55.21 (VIO 50-228/2014-201-01).

c. Conclusion

Operator requalification was being conducted and completed as required by the

Operator Requalification Program. One violation was noted for failure to have an

operator with an active license complete a medical examination biennially as

required.

6. Maintenance and Surveillance

a. Inspection Scope (IP 69001)

To determine that maintenance and surveillance activities were being completed

as required by TS Sections 3, 4, 5, 6, and 7, the inspector reviewed:

ARRR Repair Folders for various instruments

Operations Request Forms for 2013 and to date in 2014 which document

the completion of inspections, fuel movement, and instrument repair and

calibration

Monthly Alarm Check Lists for 2013 and to date in 2014

ARRR Pool Water Analysis sheets for 2013 and to date in 2014

Quarterly Maintenance Check Lists for 2013 and to date in 2014

Selected ARRR Startup/Shutdown Sheets for 2013 and to date in 2014

Section VIII of the ARRR Procedures Manual entitled, Maintenance

Procedures, PCN No. 2, RSC approval dated January 14, 1993

b. Observations and Findings

(1) Maintenance

The various Repair Folders and Operations Request Forms maintained

by the licensee indicated that emergent problems were addressed by

appropriate corrective maintenance as needed. If electrical components

for the nuclear instrumentation were replaced, the maintenance protocol

stipulated that calibrations and voltage checks occur prior to the

instrumentation being placed back into service. The inspector verified

that these tests were completed as required. Records showed that

routine maintenance activities were conducted at the required frequency

and in accordance with the TS and/or the applicable procedure.

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(2) Surveillance

After suspending reactor operations in October 2010, the licensee

continued to complete various monthly, quarterly, semiannual, and annual

checks, tests, and calibrations as required. It was noted that the licensee

had developed a modified checklist to ensure that appropriate oversight

was maintained over various other items. These included such items as

pool water temperature, air filter changeout, water conductivity, and cycling

the pumps. These items were checked on a daily or weekly basis even

though this was not required because the reactor was shut down and not

operating.

c. Conclusion

Maintenance was being completed in accordance with TS and procedural

requirements. The modified program for surveillance checks, tests, verifications,

and calibrations was being implemented in accordance with TS requirements that

were still applicable with the reactor shutdown.

7. Fuel Handling

a. Inspection Scope (IP 69001)

The inspector reviewed selected aspects of the following to verify that fuel

movement and handling was being conducted as required by TS Section 5.1.1

and Section 11:

Revised Fuel Weighing Procedure

Fuel movement and examination records

Fuel handling equipment and reactor instrumentation

Various records and data sheets related to fuel movement

Selected ARRR Operational Log Sheets for 2013 and 2014

Data Sheets for Fuel and Graphite Transfer forms for 2013 and 2014

Letter from NRC to Licensee, Aerotest Radiography and Research

Reactor (ARRR) Fuel Examination, letter dated July 29, 1992

Section IV of the ARRR Procedures Manual entitled, Critical Assembly

and Power Calibration

b. Observations and Findings

(1) Fuel Elements With Damaged Cladding

The licensee has experienced various problems with their fuel. As

documented in IR Nos. 50-228/2012-201 through 50-228/2012-206, the

licensee took various measures to deal with the problems. These are

briefly described below.

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In December 2011 the licensee began an inspection of all their fuel

elements in an effort to comply with their commitment to the U.S. Nuclear

Regulatory Commission (NRC) to inspect all the fuel elements every 5

years. After removing all the elements that they could, the licensee found

that there were 27 aluminum clad fuel elements and 11 graphite elements

that were stuck in place and could not be removed through core upper

grid plate (none of the stainless steel clad elements were found to be

stuck). The licensee then used their underwater video camera to conduct

an inspection of those fuel elements. The licensee found that, of those

elements that remained in the core, four had signs of cracks in the

cladding. On January 9, 2012, the licensee notified the NRC of the

cracked fuel elements. The licensee submitted a letter documenting the

problem the same day.

The licensee subsequently made the decision to remove the stuck fuel

elements from the core and they hired a contractor to assist in the project.

A project plan was subsequently developed for removing all the elements

and submitted it to the licensee. When all the elements had been

removed from the core, it was the intention of the licensee to place the

fuel elements with cracked cladding in specially designed and fabricated

canisters. Before beginning removal of the fuel with damaged cladding,

the licensee anticipated that four to five more elements would be found

with cracks in the cladding, in addition to the ones already noted.

Therefore, a total of ten canisters were ordered and fabricated and a

storage rack was designed and fabricated to hold up to twelve canisters

in the reactor pool.

During the period of July 16-26, 2012, licensee and contractor personnel

were able to remove all the stuck fuel elements from the core and

conduct an initial examination of the elements. The licensee then

proceeded to examine all the remaining aluminum clad elements and all

of the stainless steel clad elements that were stored in the pool. Initially,

two elements with cracked cladding were placed into the specially

designed canisters (i.e., canned) and placed in the new storage rack.

However, after examining all the fuel elements, the licensee determined

that there were substantially more fuel elements with cladding problems

than had originally been anticipated. On August 10, 2012, the licensee

submitted a letter to the NRC documenting the fact that the inspection of

the fuel elements at the facility indicated that there were a total of 22 fuel

elements with cracks in the cladding. Plans were made to have

contractor personnel return to the ARRR facility on December 10, 2012,

to complete the containerization process.

The NRC staff observed as each of the elements with damaged cladding

was placed into a canister and the canister was closed, dried, tested,

backfilled with a cover gas, and weighed. The canisters were then placed

into pre-designated locations in the new storage rack on the reactor pool

floor.

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During a fuel inspection conducted in July 2013, the licensee found that 8

fuel element serial numbers from the July 2012 inspection had been

misidentified. Many of the serial numbers were very hard to read and

only with a different camera was the licensee able to correctly identify all

the proper numbers. The licensee also found two more elements with

cracks in the cladding. In addition, one element was found to have

bubbles leaking from the cladding. The bubbles were observed to stop

after just a few minutes. This brings the number of fuel elements with

cracked or damaged cladding to 25.

(2) Fuel Weighing Problems

During their fuel inspection earlier this year, the licensee attempted to

weigh the cans containing damaged fuel, for the purpose of comparing

2014 weights with 2012 weights. They planned to verify that none of the

fuel cans had allowed any water to enter the canisters, which would

allow the fuel elements inside to continue to corrode. Canisters that

were heavier than their 2012 weights would be assumed to have had

water leaked into them. After beginning the weighing process, the

licensee was unable to match the previous weights of the first four

canisters. Also, there were problems with the strain gage which showed

fluctuating weights if the canisters were moved even one inch. When

the licensee and the Chairman of the Reactor Safeguards Committee

reviewed the videotape of previous weighing operations, several points

of potential error in the weighing operation were noted, especially with

the depth of water over the weighed element. Therefore, it was noted

that buoyancy affected the weights observed. The licensee then halted

the weighing operation and re-worked the Reactor Work Instruction

(RWI) and included an appendix for the weighing procedure, which was

not previously described in the RWI. The new RWI required the entire

assembly to hang vertically in one line from the crane hook, instead of

being run through an I-bolt which added frictional forces, to ensure that

each weighing was done in the exact same manner. The licensee also

took care to make sure that the cans were all weighed at the same depth

of the pool, which was near the bottom so it was easily reproducible.

The licensee re-weighed all of the canisters during the week of

September 29, 2014. Using the new procedure, the weights were much

more uniform. The cropped instrumented fuel element (IFE) with the new

swage top was different than the other elements and weighed 8.1

pounds. All of the other 21 canisters weighed 7.7 pounds, +/- 0.1 pound.

The weighing data was sent via email to the RSC. After reviewing the

data, the RSC was satisfied that none of the cans had any water

intrusion.

- 10 -

The inspector reviewed the RWI and the weighing data. It appeared that

the procedure used to weigh the canisters was appropriate and that there

had been no water leakage into the canisters.

c. Conclusion

Following a fuel inspection in 2013, the total number of fuel elements with

cracked or damaged cladding has been determined to be 25. Fuel movements

and weighing of those elements in canisters were completed and documented in

accordance with the requirements specified by procedure.

8. Experiments

a. Inspection Scope (IP 69001)

To ensure that the requirements of TS Sections 8 and 9 were being met

concerning experimental programs, the inspector reviewed selected aspects

and/or portions of:

Aerotest Experiment Type Review forms (previously designated as

AGNIR Operation Request Forms) documenting experiments approved

by the RSC

Section VII of the ARRR Procedures Manual entitled, Experiment Review

and Approval, stipulating experimental program requirements

The last two ARRR annual reports

b. Observations and Findings

There were six basic types of experiments that had been approved to be

conducted at the ARRR facility. The one most commonly used was No. 114 -

neutron radiography performed in the radiography facilities. Based on records

review, observations of the facility, and radiation surveys, the inspector verified

that no experiments had been conducted since October 2010.

c. Conclusion

No experiments had been conducted since October 2010.

10. Follow-up on Previously Identified Item

a. Inspection Scope (IP 92701)

The inspector reviewed the licensee's actions taken in response to a previously

identified Inspector Follow-up Item.

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b. Observation and Findings

(1) Inspector Follow-up Item (IFI) - 50-228/2007-201-01 - Follow-up on the

completion of the Autoliv, Inc. divestiture and negation plans involving

Aerotest Operations, Inc.

During an inspection in 2007, the inspector discussed the issue of the

apparent indirect or ultimate transfer of the license. This had occurred

when the ownership of the Aerotest Radiography and Research Reactor

(ARRR) was transferred in substantial part to Autoliv, Inc., through an

indirect transfer. This issue had been under review by both the licensee

and the NRC for several years. During the inspection it was noted that

the pathway to a resolution had apparently been established. The

resolution of this issue never materialized and has been the subject of

continuing discussions between the licensee and the NRC.

The original issue concerning foreign ownership and divestiture is closed.

(2) IFI - 50-228/2010-201-01 - Follow-up on the licensees corrective actions

to instruct workers in the proper use of extremity dosimetry - finger rings.

During an inspection in 2010, an issue was noted concerning the

positioning of workers extremity monitoring devices, i.e., their finger

rings. Workers at the facility are issued ring dosimeters that are used

whenever they handle radioactive materials. The dosimeter is in the form

of a plastic ring containing one thermoluminescent chip enclosed in a

protective cover. The dosimeter is intended to be worn on the finger

closest to the source of the radiation, with the TLD chip facing the palm

side of the hand. Through Interviews with licensee personnel it was

noted that workers were wearing their ring dosimeter during work

activities, but that sometimes the dosimeter was worn on the thumb or

small finger because it would not fit properly on any of the other fingers.

The rings were also being worn with the TLD chip facing the back of the

hand. In this configuration, the dosimeter monitored the general area

radiation in the vicinity of the hand rather than the dose to the hand. The

licensee was cautioned that workers should be instructed to wear their

extremity monitors - finger rings properly in order to provide an accurate

assessment of the dose to the hands.

During this inspection it was noted that no work was being performed and

no extremity monitoring was needed or being used. This issue is

considered closed.

c. Conclusion

Two IFIs were reviewed and closed.

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14. Exit Meeting Summary

The inspector reviewed the inspection results with members of licensee management at

the conclusion of the inspection on November 19, 2014. The licensee acknowledged the

findings presented and did not identify as proprietary any of the material provided to or

reviewed by the inspector during the inspection.

PARTIAL LIST OF PERSONS CONTACTED

Licensee Personnel

C. Bauman Nuclear Engineer and Senior Reactor Operator

F. Meren Reactor Supervisor and Reactor Operations Manager

T. Richey Neutron Radiography Manager

S. Warren General Manager and Radiological Safety Officer

M. Wilkinson Quality Assurance Manager

INSPECTION PROCEDURE USED

IP 69001 Class II Non-Power Reactors

IP 92701 Review of Previously Identified Items

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None

Closed

50-228/2007-201-01 IFI Follow-up on the completion of the Autoliv, Inc. divestiture and

negation plans involving Aerotest Operations, Inc.

50-228/2010-201-01 IFI Follow-up on the licensees corrective actions to instruct workers

in the proper use of extremity dosimetry - finger rings.

LIST OF ACRONYMS USED

ADAMS Agencywide Documents Access and Management System

AO Aerotest Operations, Inc.

ARRR Aerotest Radiography and Research Reactor

CFR Code of Federal Regulations

E-Plan Emergency Plan

IFI Inspector Follow-up Item

kW kilowatt

LOA Letter of Agreement

N-Ray neutron radiography

NRC Nuclear Regulatory Commission

OEA OEA Aerospace, Inc.

ORF Operations Request Form

PCN Procedure Change Notice

RSC Reactor Safeguards Committee

SRO Senior Reactor Operator

SRV San Ramon Valley

TS Technical Specification