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| issue date = 01/28/1981
| issue date = 01/28/1981
| title = LER 81-001/03L-0:on 810105,leak Noted on Diesel Emergency Generator B Jacket Cooling Water Return Line to Expansion Tank.Caused by Broken Bushing Due to Possible Lack of Support Connection.Bushing Replaced
| title = LER 81-001/03L-0:on 810105,leak Noted on Diesel Emergency Generator B Jacket Cooling Water Return Line to Expansion Tank.Caused by Broken Bushing Due to Possible Lack of Support Connection.Bushing Replaced
| author name = MAIER J E
| author name = Maier J
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| addressee name =  
| addressee name =  
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=Text=
=Text=
{{#Wiki_filter:NRC FORM 366 (7~7(<~O 7 8 CON'T~o~LQB 0 5 0 0 0 2 4 4 7 0 1 0 5 8 1 B 0 1 2 8 8 1 QB 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 During''monthly surveillance operator noted leak'on"B" Diesel emergency generator 7 8 U.S.NUCLEAR REGULATORY COMMISSION O 81-001/03L-0 LICENSEE EVENT REPORT CONTROL BLOCK: Q1 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
{{#Wiki_filter:NRC FORM 366                                                                                                                           U. S. NUCLEAR REGULATORY COMMISSION (7~7( <                                                                                 81-001/03L-0 O LICENSEE EVENT REPORT CONTROL BLOCK:                                                      Q1                  (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
I 6 N Y R E G 1 Q90 0-0 0 0 0 0-0 0 Q94 1 1 1 1Q4~Q9 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 (EG)jacket cooling'water return line to expansion tank coming from a broken bushing.~O4~OS~OB (T.S.3.7.1)."A" EG was immediately placed in service.~O7~OB 7 8 9~OB 7 8 80 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~EE Q>>A Q(9~EQ(9>1 B E X>Q4~AQ(9~ZQ(9 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LF RIRO EVENT YEAR REPORT NO.CODE TYPE NO.Q(9 99499>~81+'00 1 QH~03+L Q QO 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FOAM SUB.SUPPLIER MANUFACTURER Q(9~Z.Q(9~ZQ99~ZQ>>0 0 0 0 N Q99~NQ94 A Qoo B 1 3 0 Qoo 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o Possible lack of connection of su ort durin ori inal connection or ersonnel involved in modification installation in area may have bumped line.Bushing is 3/4" plastic for atmospheric pressure service.Replaced bushing, added coupling for future mainte-3 nance ease.METHOD OF OTHER STATUS~DISCOVERY NA LBJQ31 44 45 45~14 7 8 9 FACILITY STATUS%POWER~E Q99~10 0 Q29 7 8 9 10 12 13 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q~6~Z Q3~ZQ34 NA 7 8 9 10 11 44 PERSONNEL EXPOSURES NUMBER TYPE DESCAIPTION Q39 7~00 0 Q>>Z Q39'A 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ 9~00 0 Q4o NA 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43 TYPE DESCRIPTION z Q4.NA 8 9 10 PUBLICITY ISSUED DESCAIPTION Q KZ L~IO NA 8108 D40 974 NAME QF PREPARER-ary Meier DISCOVERY DESCRIPTION Q32 o eratcr observation LOCATION OF RELEASE Q NA 80 80 80 80 NRC USE ONLY 80 68 69 80 o PDNEI315 524-4446 ext.369 a 0''I'4~54g,",~}}
I                                    6
~O             N Y        R      E      G      1 14 Q90 15 0    0          0    0 LICENSE NUMBER 0      0      0        0 25 Q94 26 1      1 LICENSE TYPE 1      1Q4~Q9 30  57 CAT 58 7       8   9        LICENSEE CODE CON'T 0     5     0     0     0     2   4     4     7     0     1     0     5     8     1     B     0     1   2     8   8     1   QB
~o                              ~LQB                                                          68     69         EVENT DATE             74       75       REPORT DATE           80 7      8                        60            61              DOCKET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                                   Q10 During''monthly surveillance operator noted leak'on "B" Diesel emergency generator (EG)     jacket cooling 'water return line to expansion tank coming from                                                                   a broken       bushing.
~O4             (T.S. 3.7.1). "A" EG was immediately placed in service.
~OS
~OB
~O7
~OB                                                                                                                                                                                       80 7       8 9 SYSTEM               CAUSE           CAUSE                                                           COMP.           VALVE CODE                 CODE       SUBCODE                   COMPONENT CODE                       SUBCODE           SUBCODE
~OB                              ~EE             Q>>           A   Q(9     ~EQ(9             >   1     B     E     X >       Q4       ~AQ(9             ~ZQ(9 12             13                                 18           19               20
                                                              + '00 7      8                        9            10            11 SEQUENTIAL                             OCCURRENCE             REPORT                     REVISION EVENT YEAR                                   REPORT NO.                                 CODE                 TYPE                         NO.
Q(9 LF RIRO 99499>         ~81 21           22         23             24 1
26 QH 27
                                                                                                                        ~03 28         29
                                                                                                                                                +L 30 Q
31 QO 32 ACTION FUTURE                       EFFECT           SHUTDOWN                                     ATTACHMENT             NPRDQ         PRIME COMP.             COMPONENT TAKEN ACTION                     ON PLANT             METHOD                   HOURS Q22           SUBMITTED         FOAM SUB.         SUPPLIER           MANUFACTURER Q(9   ~Z. Q(9           ~ZQ99             ~ZQ>>                 0   0   0     0           N   Q99       ~NQ94               A     Qoo       B     1   3   0   Qoo 33         34                   35                 36             37                     40     41               42                 43             44               47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS                               Q27 o         Possible lack of connection of su                                       ort durin ori inal connection or ersonnel involved in modification installation in area may have bumped line. Bushing is 3/4" plastic for atmospheric pressure service. Replaced bushing, added coupling for future mainte-3           nance ease.
  ~14 7       8   9 FACILITY STATUS
            ~E     Q99     ~10
                                  % POWER 0     Q29 OTHER STATUS NA
                                                                                      ~        METHOD OF DISCOVERY LBJQ31              o DISCOVERY DESCRIPTION Q32 eratcr observation 7     8   9               10                 12       13                               44      45                                                                                    80 ACTIVITY CONTENT RELEASED OF RELEASE                             AMOUNT OF ACTIVITY       Q                                                   LOCATION OF RELEASE        Q
~6 7      8
            ~Z 9
Q3     ~ZQ34 10             11 NA 44             45 NA 80 PERSONNEL EXPOSURES 7     ~00 NUMBER 0 Q>>
TYPE Z     Q39           'A DESCAIPTION Q39 80 7       8   9               11       12             13 PERSONNEL INJURIES NUMBER               DESCRIPTIONQ 9     ~00             0   Q4o                             NA 80 7       8   9                 11       12 LOSS OF OR DAMAGE TO FACILITY TYPE       DESCRIPTION                       Q43 z   Q4.                                         NA 8   9           10                                                                                                                                                             80 PUBLICITY                                                                                                                                         NRC USE ONLY ISSUED       DESCAIPTION         Q KZ L~IO                                                         NA 68    69                          80 o 8108 D40 974                             ary Meier                                                     PDNEI315           524-4446         ext. 369     a NAME QF PREPARER
 
0             '
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Latest revision as of 09:55, 29 October 2019

LER 81-001/03L-0:on 810105,leak Noted on Diesel Emergency Generator B Jacket Cooling Water Return Line to Expansion Tank.Caused by Broken Bushing Due to Possible Lack of Support Connection.Bushing Replaced
ML17309A123
Person / Time
Site: Ginna Constellation icon.png
Issue date: 01/28/1981
From: Maier J
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17258A753 List:
References
LER-81-001-03L, LER-81-1-3L, NUDOCS 8102040475
Download: ML17309A123 (2)


Text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7~7( < 81-001/03L-0 O LICENSEE EVENT REPORT CONTROL BLOCK: Q1 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6

~O N Y R E G 1 14 Q90 15 0 0 0 0 LICENSE NUMBER 0 0 0 0 25 Q94 26 1 1 LICENSE TYPE 1 1Q4~Q9 30 57 CAT 58 7 8 9 LICENSEE CODE CON'T 0 5 0 0 0 2 4 4 7 0 1 0 5 8 1 B 0 1 2 8 8 1 QB

~o ~LQB 68 69 EVENT DATE 74 75 REPORT DATE 80 7 8 60 61 DOCKET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 Duringmonthly surveillance operator noted leak'on "B" Diesel emergency generator (EG) jacket cooling 'water return line to expansion tank coming from a broken bushing.

~O4 (T.S. 3.7.1). "A" EG was immediately placed in service.

~OS

~OB

~O7

~OB 80 7 8 9 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~OB ~EE Q>> A Q(9 ~EQ(9 > 1 B E X > Q4 ~AQ(9 ~ZQ(9 12 13 18 19 20

+ '00 7 8 9 10 11 SEQUENTIAL OCCURRENCE REPORT REVISION EVENT YEAR REPORT NO. CODE TYPE NO.

Q(9 LF RIRO 99499> ~81 21 22 23 24 1

26 QH 27

~03 28 29

+L 30 Q

31 QO 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FOAM SUB. SUPPLIER MANUFACTURER Q(9 ~Z. Q(9 ~ZQ99 ~ZQ>> 0 0 0 0 N Q99 ~NQ94 A Qoo B 1 3 0 Qoo 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o Possible lack of connection of su ort durin ori inal connection or ersonnel involved in modification installation in area may have bumped line. Bushing is 3/4" plastic for atmospheric pressure service. Replaced bushing, added coupling for future mainte-3 nance ease.

~14 7 8 9 FACILITY STATUS

~E Q99 ~10

% POWER 0 Q29 OTHER STATUS NA

~ METHOD OF DISCOVERY LBJQ31 o DISCOVERY DESCRIPTION Q32 eratcr observation 7 8 9 10 12 13 44 45 80 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q LOCATION OF RELEASE Q

~6 7 8

~Z 9

Q3 ~ZQ34 10 11 NA 44 45 NA 80 PERSONNEL EXPOSURES 7 ~00 NUMBER 0 Q>>

TYPE Z Q39 'A DESCAIPTION Q39 80 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ 9 ~00 0 Q4o NA 80 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Q43 z Q4. NA 8 9 10 80 PUBLICITY NRC USE ONLY ISSUED DESCAIPTION Q KZ L~IO NA 68 69 80 o 8108 D40 974 ary Meier PDNEI315 524-4446 ext. 369 a NAME QF PREPARER

0 '

'I

'4~ 54g,", ~