ML17309A123: Difference between revisions

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| issue date = 01/28/1981
| issue date = 01/28/1981
| title = LER 81-001/03L-0:on 810105,leak Noted on Diesel Emergency Generator B Jacket Cooling Water Return Line to Expansion Tank.Caused by Broken Bushing Due to Possible Lack of Support Connection.Bushing Replaced
| title = LER 81-001/03L-0:on 810105,leak Noted on Diesel Emergency Generator B Jacket Cooling Water Return Line to Expansion Tank.Caused by Broken Bushing Due to Possible Lack of Support Connection.Bushing Replaced
| author name = MAIER J E
| author name = Maier J
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| addressee name =  
| addressee name =  
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{{#Wiki_filter:NRCFORM366(7~7(<~O78CON'T~o~LQB050002447010581B012881QB6061DOCKETNUMBER6869EVENTDATE7475REPORTDATE80EVENTDESCRIPTIONANDPROBABLECONSEQUENCESQ10During''monthlysurveillanceoperatornotedleak'on"B"Dieselemergencygenerator78U.S.NUCLEARREGULATORYCOMMISSIONO81-001/03L-0LICENSEEEVENTREPORTCONTROLBLOCK:Q1(PLEASEPRINTORTYPEALLREQUIREDINFORMATION)I6NYREG1Q900-00000-00Q941111Q4~Q99LICENSEECODE1415LICENSENUMBER2526LICENSETYPE3057CAT58(EG)jacketcooling'waterreturnlinetoexpansiontankcomingfromabrokenbushing.~O4~OS~OB(T.S.3.7.1)."A"EGwasimmediatelyplacedinservice.~O7~OB789~OB7880SYSTEMCAUSECAUSECOMP.VALVECODECODESUBCODECOMPONENTCODESUBCODESUBCODE~EEQ>>AQ(9~EQ(9>1BEX>Q4~AQ(9~ZQ(9910111213181920SEQUENTIALOCCURRENCEREPORTREVISIONLFRIROEVENTYEARREPORTNO.CODETYPENO.Q(999499>~81+'001QH~03+LQQO2122232426272829303132ACTIONFUTUREEFFECTSHUTDOWNATTACHMENTNPRDQPRIMECOMP.COMPONENTTAKENACTIONONPLANTMETHODHOURSQ22SUBMITTEDFOAMSUB.SUPPLIERMANUFACTURERQ(9~Z.Q(9~ZQ99~ZQ>>0000NQ99~NQ94AQooB130Qoo3334353637404142434447CAUSEDESCRIPTIONANDCORRECTIVEACTIONSQ27oPossiblelackofconnectionofsuortdurinoriinalconnectionorersonnelinvolvedinmodificationinstallationinareamayhavebumpedline.Bushingis3/4"plasticforatmosphericpressureservice.Replacedbushing,addedcouplingforfuturemainte-3nanceease.METHODOFOTHERSTATUS~DISCOVERYNALBJQ31444545~14789FACILITYSTATUS%POWER~EQ99~100Q29789101213ACTIVITYCONTENTRELEASEDOFRELEASEAMOUNTOFACTIVITYQ~6~ZQ3~ZQ34NA789101144PERSONNELEXPOSURESNUMBERTYPEDESCAIPTIONQ397~000Q>>ZQ39'A789111213PERSONNELINJURIESNUMBERDESCRIPTIONQ9~000Q4oNA7891112LOSSOFORDAMAGETOFACILITYQ43TYPEDESCRIPTIONzQ4.NA8910PUBLICITYISSUEDDESCAIPTIONQKZL~IONA8108D40974NAMEQFPREPARER-aryMeierDISCOVERYDESCRIPTIONQ32oeratcrobservationLOCATIONOFRELEASEQNA80808080NRCUSEONLY80686980oPDNEI315524-4446ext.369a 0''I'4~54g,",~}}
{{#Wiki_filter:NRC FORM 366                                                                                                                            U. S. NUCLEAR REGULATORY COMMISSION (7~7( <                                                                                 81-001/03L-0 O LICENSEE EVENT REPORT CONTROL BLOCK:                                                      Q1                  (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)
I                                    6
~O              N Y        R      E      G      1 14 Q90 15 0    0          0    0 LICENSE NUMBER 0      0      0        0 25 Q94 26 1      1 LICENSE TYPE 1      1Q4~Q9 30  57 CAT 58 7      8    9        LICENSEE CODE CON'T 0    5    0    0    0    2    4    4    7    0      1    0    5    8      1    B    0    1    2    8  8      1  QB
~o                             ~LQB                                                          68      69        EVENT DATE              74      75      REPORT DATE          80 7      8                        60            61              DOCKET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES                                    Q10 During''monthly surveillance operator noted leak'on "B" Diesel emergency generator (EG)     jacket cooling 'water return line to expansion tank coming from                                                                  a broken      bushing.
~O4             (T.S. 3.7.1). "A" EG was immediately placed in service.
~OS
~OB
~O7
~OB                                                                                                                                                                                      80 7      8 9 SYSTEM                CAUSE          CAUSE                                                          COMP.            VALVE CODE                  CODE        SUBCODE                  COMPONENT CODE                        SUBCODE          SUBCODE
~OB                              ~EE              Q>>           A  Q(9     ~EQ(9             >   1      B      E    X >       Q4       ~AQ(9             ~ZQ(9 12              13                                18          19              20
                                                              + '00 7      8                        9            10            11 SEQUENTIAL                            OCCURRENCE            REPORT                      REVISION EVENT YEAR                                  REPORT NO.                                 CODE                TYPE                          NO.
Q(9 LF RIRO 99499>         ~81 21          22          23            24 1
26 QH 27
                                                                                                                        ~03 28        29
                                                                                                                                                +L 30 Q
31 QO 32 ACTION FUTURE                      EFFECT            SHUTDOWN                                    ATTACHMENT            NPRDQ          PRIME COMP.             COMPONENT TAKEN ACTION                    ON PLANT            METHOD                    HOURS Q22          SUBMITTED          FOAM SUB.         SUPPLIER          MANUFACTURER Q(9   ~Z. Q(9           ~ZQ99             ~ZQ>>                 0    0    0      0            N  Q99        ~NQ94                A    Qoo      B    1  3  0    Qoo 33          34                    35                36              37                      40      41                42                43            44                47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS                              Q27 o          Possible lack of connection of su                                        ort durin ori inal connection or ersonnel involved in modification installation in area may have bumped line. Bushing is 3/4" plastic for atmospheric pressure service. Replaced bushing, added coupling for future mainte-3          nance ease.
  ~14 7      8    9 FACILITY STATUS
            ~E      Q99      ~10
                                  % POWER 0    Q29 OTHER STATUS NA
                                                                                      ~         METHOD OF DISCOVERY LBJQ31              o DISCOVERY DESCRIPTION Q32 eratcr observation 7      8    9                10                12      13                              44      45                                                                                    80 ACTIVITY CONTENT RELEASED OF RELEASE                            AMOUNT OF ACTIVITY        Q                                                    LOCATION OF RELEASE        Q
~6 7      8
            ~Z 9
Q3      ~ZQ34 10            11 NA 44            45 NA 80 PERSONNEL EXPOSURES 7      ~00 NUMBER 0 Q>>
TYPE Z    Q39            'A DESCAIPTION Q39 80 7      8    9                11      12            13 PERSONNEL INJURIES NUMBER                DESCRIPTIONQ 9      ~00            0    Q4o                            NA 80 7      8  9                11        12 LOSS OF OR DAMAGE TO FACILITY TYPE        DESCRIPTION                      Q43 z    Q4.                                         NA 8  9            10                                                                                                                                                              80 PUBLICITY                                                                                                                                        NRC USE ONLY ISSUED        DESCAIPTION        Q KZ L~IO                                                          NA 68    69                          80 o 8108 D40 974                            ary Meier                                                      PDNEI315          524-4446          ext. 369    a NAME QF PREPARER
 
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Latest revision as of 09:55, 29 October 2019

LER 81-001/03L-0:on 810105,leak Noted on Diesel Emergency Generator B Jacket Cooling Water Return Line to Expansion Tank.Caused by Broken Bushing Due to Possible Lack of Support Connection.Bushing Replaced
ML17309A123
Person / Time
Site: Ginna Constellation icon.png
Issue date: 01/28/1981
From: Maier J
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17258A753 List:
References
LER-81-001-03L, LER-81-1-3L, NUDOCS 8102040475
Download: ML17309A123 (2)


Text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7~7( < 81-001/03L-0 O LICENSEE EVENT REPORT CONTROL BLOCK: Q1 (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6

~O N Y R E G 1 14 Q90 15 0 0 0 0 LICENSE NUMBER 0 0 0 0 25 Q94 26 1 1 LICENSE TYPE 1 1Q4~Q9 30 57 CAT 58 7 8 9 LICENSEE CODE CON'T 0 5 0 0 0 2 4 4 7 0 1 0 5 8 1 B 0 1 2 8 8 1 QB

~o ~LQB 68 69 EVENT DATE 74 75 REPORT DATE 80 7 8 60 61 DOCKET NUMBER EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 Duringmonthly surveillance operator noted leak'on "B" Diesel emergency generator (EG) jacket cooling 'water return line to expansion tank coming from a broken bushing.

~O4 (T.S. 3.7.1). "A" EG was immediately placed in service.

~OS

~OB

~O7

~OB 80 7 8 9 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE

~OB ~EE Q>> A Q(9 ~EQ(9 > 1 B E X > Q4 ~AQ(9 ~ZQ(9 12 13 18 19 20

+ '00 7 8 9 10 11 SEQUENTIAL OCCURRENCE REPORT REVISION EVENT YEAR REPORT NO. CODE TYPE NO.

Q(9 LF RIRO 99499> ~81 21 22 23 24 1

26 QH 27

~03 28 29

+L 30 Q

31 QO 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ PRIME COMP. COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FOAM SUB. SUPPLIER MANUFACTURER Q(9 ~Z. Q(9 ~ZQ99 ~ZQ>> 0 0 0 0 N Q99 ~NQ94 A Qoo B 1 3 0 Qoo 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o Possible lack of connection of su ort durin ori inal connection or ersonnel involved in modification installation in area may have bumped line. Bushing is 3/4" plastic for atmospheric pressure service. Replaced bushing, added coupling for future mainte-3 nance ease.

~14 7 8 9 FACILITY STATUS

~E Q99 ~10

% POWER 0 Q29 OTHER STATUS NA

~ METHOD OF DISCOVERY LBJQ31 o DISCOVERY DESCRIPTION Q32 eratcr observation 7 8 9 10 12 13 44 45 80 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY Q LOCATION OF RELEASE Q

~6 7 8

~Z 9

Q3 ~ZQ34 10 11 NA 44 45 NA 80 PERSONNEL EXPOSURES 7 ~00 NUMBER 0 Q>>

TYPE Z Q39 'A DESCAIPTION Q39 80 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ 9 ~00 0 Q4o NA 80 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY TYPE DESCRIPTION Q43 z Q4. NA 8 9 10 80 PUBLICITY NRC USE ONLY ISSUED DESCAIPTION Q KZ L~IO NA 68 69 80 o 8108 D40 974 ary Meier PDNEI315 524-4446 ext. 369 a NAME QF PREPARER

0 '

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