ML17266A249: Difference between revisions

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| issue date = 07/24/1980
| issue date = 07/24/1980
| title = Updated LER 80-015/03L-1:on 800316,during Shutdown,Diesel Generator Loading Timers Found Out of Tolerance & Containment & Reactor Cavity Cooling Fans Failed to Start. Caused by Normal Setpoint Drift.Fans Retested
| title = Updated LER 80-015/03L-1:on 800316,during Shutdown,Diesel Generator Loading Timers Found Out of Tolerance & Containment & Reactor Cavity Cooling Fans Failed to Start. Caused by Normal Setpoint Drift.Fans Retested
| author name = PACE P L
| author name = Pace P
| author affiliation = FLORIDA POWER & LIGHT CO.
| author affiliation = FLORIDA POWER & LIGHT CO.
| addressee name =  
| addressee name =  

Revision as of 02:49, 19 June 2019

Updated LER 80-015/03L-1:on 800316,during Shutdown,Diesel Generator Loading Timers Found Out of Tolerance & Containment & Reactor Cavity Cooling Fans Failed to Start. Caused by Normal Setpoint Drift.Fans Retested
ML17266A249
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 07/24/1980
From: Pace P
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17208A925 List:
References
LER-80-015-03L, LER-80-15-3L, NUDOCS 8008220232
Download: ML17266A249 (2)


Text

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'IO PROSAS'C DISce<<U 7ICSS Q 2 2~F'QA THE 2A,E T'I ree NOT START;,AND TllE SklIELD BUILDING VENT.SYSTElf OUTSIDE COOLING AIR VALVES~e DXD NOT OPEN.SYSTEI21 CAPABILITY HAS HO'I SIOHXFXCAl'TLY DEGPADED SINCE~BOTH

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+k!~R 0 10 o ,PP.L.PaCe DIRC LS=OPDLV (305%552-3S01 20 soosoe0 9.39, REPORTA)3LE OCCURREN~35-80-15 LICENSEE EVENT REPOR~PACE Tt<0'ADDITIONAL CAUSE DESCRIPTION AND CORRECTIVE ACTIONS The diesel generator loading sequence timers were out of tolerance by the following amounts: lA HPSI pump+0.18 sec, 1B HPSI pump+0.22 sec, 1A ICH pump+0.15 sec, 1A CS pump+0.60, 1B CS pump+0.8 sec., HVE-9A+0.86 sec, HVE-13B+0.30 sec., lB CVCS HT.Trace+1.00 sec, 1A battery charger+0.20 sec;, and HVS-4A+5.00 sec.Based on a review of previous engineered safety feature tests it appears that with the exception of HVS-4A (RAB vent.), the timers exhibited normally*expected minor setpoint drift.'he HVS-4A timer relay was replaced and the other relays were readjusted to specification.

All relays retested satisfactorily.

As'a result of continued evidence of undesirable timer drift, an engineering evaluation of the feasibility of a different and more repeatable timing circuit design is in progress.If significant design changes are made as a result of this evaluation, a follow-up report will be issued.The reactor cavity cooling fan was retested for loss of power restart and functioned properly.he containment cooling fan was retested for loss of power restart and SIAS relay actuation and also functioned properly in both cases.No problems were found during fan trouble shooting.f The SBVS valves were retested satisfactorily.

It was'determined that'uring the initial test, a shield building door had been opens for refueling access, thus preventing the valves from opening on shield building differential pressure.