ML17309A149: Difference between revisions

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| issue date = 04/22/1981
| issue date = 04/22/1981
| title = LER 81-006/03L-0:on 810323,immediate Borate Valve Outlet Piping Found Leaking.Probably Caused by Stress Corrosion Cracking.Investigation Underway
| title = LER 81-006/03L-0:on 810323,immediate Borate Valve Outlet Piping Found Leaking.Probably Caused by Stress Corrosion Cracking.Investigation Underway
| author name = SPECTOR S M
| author name = Spector S
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| author affiliation = ROCHESTER GAS & ELECTRIC CORP.
| addressee name =  
| addressee name =  

Revision as of 19:47, 18 June 2019

LER 81-006/03L-0:on 810323,immediate Borate Valve Outlet Piping Found Leaking.Probably Caused by Stress Corrosion Cracking.Investigation Underway
ML17309A149
Person / Time
Site: Ginna Constellation icon.png
Issue date: 04/22/1981
From: Spector S
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17258A983 List:
References
CAR-1296, LER-81-006-03L, LER-81-6-3L, NUDOCS 8104280509
Download: ML17309A149 (2)


Text

NRC WIVL3Isee (7.77)U.S.NUCLEAR REGULATORY COMMISSION

~01 7 8 CON'T~01 7 8 8 1-00 6/0 3L-0 ICENSEE EVENT REPORT (CAR 1296)CONTROL BLOCK: Qi tPLEASE PRINT OR TYPE ALL REQUIRED INFORMATION)

I 6 NYREG1Qso0-00000-00041111Q~Qs 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58~LQB 0 5 0 0 0 2 4 4 Q7 0 3 2 3 8 60 61 DOCKET NUMBER 68 69 EVENT DATE EVENT DESCRIPTION AND PROBABL,E CONSEQUENCES Q10 Durin o erator tour leaka e was seen at immediate borate valve outlet i in 1 QB 0 4 2 2 8 1 QB 74 75 REPORT DATE 80~Q3{T.S.6.9.2.b{4).

Line was immediately isolated for repair.Two flow paths from boric acid tanks remained opera'ole.

~06~os 7 8 9 80 7 8 SYSTEM CAUSE CAUSE COMP.VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE~OB~PC Q>>~EQts~DQ>>P I P E X X Q4~AQs~ZQs 9 10 11 12 13 18 19 20 SEOUENTIAL OCCURRENCE REPORT REVISION LER/RO EVENT YEAR REPORT NO.CODE TYPE NO.Q17 Rsposr~81 I={~00 6~~~03~L 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD 4 PRIME COMP.COMPONENT TAKEN ACTION ON PLANT METHOD HOURS+22 SUBMITTED FORM SUB.SUPPLIER MANUFACTURER

~O>>~Os~Oso~ZOs~0 0 N On MNQ24 HNQn B 1 3 0 Qto 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o Possible stress corrosion crackin.Examination showed famil of cracks on exterior surface, some thru-wall.

Pipe section was removed for metallurgical analysis to confirm cause.With unit in AE60 all similar areas of piping will be inspected.

Pipe 3 is 150 psi sch 10 304 SS containing 12%boric acid.METHOD OF DISCOVERY CO 0~O ACTIVITY CONTENT RELEASED OF RELEASE AMOUNT OF ACTIVITY 6~Z Q33 Z Q34 NA 7 8 9 10 11 PERSONNEL EXPOSURES NUI'ABER TYPE DESCRIPTION Q39~l7~00 0 Qot~ZQss NA 7 8 9 11 12 13 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41 s~oo o Qo NA 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY Q43 TYPE DESCRIPTION B~ZQ42 NA 7 8 9 10 PUBLICITY ISSUED DESCRIPTION Q~20~NQ44 NA 7 8 9 10 L~JQ>>44 45 46 Q35 44 45 7 8 9 FACILITY STATUS%POWER OTHER STATUS Q30 1 5 E 28 1 0 0 29 NA DISCOVERY DESCRIPTION Q32 Operator tour LOCATION OF RELEASE Q NA NRC USE ONLY 80 80 80 80 80 80 NAME oF PRFPARER S~M~Spector 68 69 80 PHDNE.315-524-4446, ext.214

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