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This page provides a simple browsing interface for finding entities described by a property and a named value. Other available search interfaces include the page property search, and the ask query builder.
List of results
- ML20080E857 + (ML20080E857)
- ML20080E860 + (ML20080E860)
- ML20080E863 + (ML20080E863)
- ML20080E871 + (ML20080E871)
- ML20080E876 + (ML20080E876)
- ML20080E884 + (ML20080E884)
- NRC-94-0145, Comment Supporting Proposed Rule 10CFR50 Re Shutdown & Low Power Operations for Np Reactors.All Util Outages Currently Controlled by Defense in Depth Philosophy Implemented by Operations & Work Control Group + (ML20080E889)
- ML20080E893 + (ML20080E893)
- 05000272/LER-1984-002, :on 840107,inlet Valve 13CN27 Closed Due to Spurious High Level in Feedwater Heater 15C.Caused by Heater Bypass 1CN47 Failing to Open.Bypass Differential Setpoint Lowered & Signal Summator Module Replaced + (ML20080E912)
- ML20080E928 + (ML20080E928)
- ML20080E933 + (ML20080E933)
- NLS8400026, Responds to NRC Re Violations & Deviations Noted in IE Insp Rept 50-298/83-26.Corrective Actions:Refresher Training Administered for Design Initiation & Review of Governing Procedures for Design Changes + (ML20080E935)
- ML20080E937 + (ML20080E937)
- ML20080E940 + (ML20080E940)
- AECM-83-0578, Forwards Rev 0 to Pump & Valve Inservice Insp Program + (ML20080E948)
- ML20080E952 + (ML20080E952)
- 05000250/LER-1984-002, :on 840108,reactor Trip Occurred Due to Initiation of Safety Injection.Caused by Excessive Steam Usage in Secondary Sys & Steam Leakage Through Steam Supply Valves.Equipment Upgraded + (ML20080E956)
- 05000327/LER-1984-005, :on 840109,cold Leg Accumulator 3 Declared Inoperable Due to High Boron Concentration.Cause Not Stated. Accumulator Drained & Diluted + (ML20080E959)
- ML20080E973 + (ML20080E973)
- ML20080E979 + (ML20080E979)
- ML20080E989 + (ML20080E989)
- NRC-84-0026, Forwards Request for Relief from ASME Code,Section XI Requirements for Volumetric Preservice Insp of 18 Branch Connection Welds in Rcs.Details Supporting Request,Including Identification of Specific Welds,Encl + (ML20080F009)
- ML20080F016 + (ML20080F016)
- ML20080F018 + (ML20080F018)
- ML20080F022 + (ML20080F022)
- ML20080F024 + (ML20080F024)
- ML20080F029 + (ML20080F029)
- W3P84-0288, Forwards Description of Facility Capability for Assessing Sequence of Events & Analog Variable Time History Both pre- & post-trip,in Response to Item 1.2 in Generic Ltr 83-28 + (ML20080F034)
- B11023, Forwards Responses to Requests for Addl Info Re Loop Bypass Valves & Rcpb.Responses Will Be Included in Feb 1984 Amend 7 to FSAR + (ML20080F041)
- ML20080F044 + (ML20080F044)
- 0CAN019502, Documents Basis for Licensee Commitment Change & Current Controls for Reporting of Confirmed Positive Supervisors. Believes That Determination Process for Reporting Supervisory Drug Use,Per 10CFR26.73(a)(2)(ii),effective + (ML20080F047)
- ML20080F048 + (ML20080F048)
- W3P84-0297, Forwards Response to Generic Ltr 83-28,Item 1.1 Requesting Description of Program Ensuring That Unscheduled Reactor Shutdowns Analyzed.Util Employs post-trip Review for Diagnosing Unscheduled Reactor Trips + (ML20080F051)
- 05000275/LER-1984-001-01, :on 840106,inadvertent Safety Injection Actuation Occurred.Caused by Momentary Grounding of Ac Supply to Solid State Protection Sys Slave Relay Circuit. Operators Reinstructed on Procedures + (ML20080F057)
- JAFP-84-0149, Monthly Operating Rept for Jan 1984 + (ML20080F068)
- 05000416/LER-1983-117-03, /03L-0:on 830812,drywell Purge Compressor a auto-started.Caused by Pulled Output Relays (Per Work Authorization).Compressor Returned to Normal Following False Signal Verification + (ML20080F073)
- ML20080F076 + (ML20080F076)
- ML20080F081 + (ML20080F081)
- AECM-83-0508, Updated RO 83-052/1:on 830523,fire-rated Penetrations Opened to Implement Design Change Package Per Tech Specs. Penetrations Resealed.Last Penetration Restored on 830829 + (ML20080F086)
- 05000247/LER-1983-032-03, /03L-0:on 830806,pinhole Leak Discovered on 3/4- Inch Safety Injection Pump Test Pipe to Relief Valve 855. Cause Unknown.Leak Will Be Inspected During Biweekly Containment Insps.Correction Will Be Reported + (ML20080F092)
- 05000416/LER-1983-116-03, /03L-0:on 830809,during Mod of Div II Load Shedding Panel,Temporary Jumpers Removed Causing Partial Loca/Losp Signal to Occur.Caused by Loss of Continuity. Method to Prevent Recurrence Under Development + (ML20080F095)
- AECM-83-0542, Updated RO 83-012/1:on 830222-0316,numerous fire-rated Seals Opened to Perform Planned Maint Activities.Hourly Fire Watch Being Conducted.Estimated Completion Date Is 831015 + (ML20080F100)
- ML20080F103 + (ML20080F103)
- ML20080F106 + (ML20080F106)
- ML20080F109 + (ML20080F109)
- ML20080F123 + (ML20080F123)
- ML20080F124 + (ML20080F124)
- ML20080F130 + (ML20080F130)
- RC-95-0009, Comment Supporting Proposed Rule 10CFR21 Re inter-utility Transfer + (ML20080F133)
- U-602384, Response to NRC Re Certain RP & Physical Security Incidents at Plant.Informs That Although Some Incidents Did Occur,No Intent Made to Prevent Employees from Recording Actual Dose + (ML20080F135)
- ML20080F136 + (ML20080F136)