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Category:Letter type:PNP
MONTHYEARPNP 2023-030, License Amendment Request to Revise Renewed Facility Operating License and Permanently Defueled Technical Specifications to Support Resumption of Power Operations2023-12-14014 December 2023 License Amendment Request to Revise Renewed Facility Operating License and Permanently Defueled Technical Specifications to Support Resumption of Power Operations PNP 2023-035, Withdrawal of License Amendment Request - Revise License Condition to Eliminate Cyber Security Plan Requirements2023-12-12012 December 2023 Withdrawal of License Amendment Request - Revise License Condition to Eliminate Cyber Security Plan Requirements PNP 2023-028, Application for Order Consenting to Transfer of Control of License and Approving Conforming License Amendments2023-12-0606 December 2023 Application for Order Consenting to Transfer of Control of License and Approving Conforming License Amendments PNP 2023-026, Pre-Submittal Meeting Presentation - Palisades Nuclear Plant License Transfer Application to Support Resumption of Power Operations2023-09-28028 September 2023 Pre-Submittal Meeting Presentation - Palisades Nuclear Plant License Transfer Application to Support Resumption of Power Operations PNP 2023-025, Request for Exemption from Certain Termination of License Requirements of 10 CFR 50.822023-09-28028 September 2023 Request for Exemption from Certain Termination of License Requirements of 10 CFR 50.82 PNP 2023-023, Special Report High Range Noble Gas Monitor Inoperable2023-08-0909 August 2023 Special Report High Range Noble Gas Monitor Inoperable PNP 2023-018, 2022 Annual Non-Radiological Environmental Operating Report2023-04-25025 April 2023 2022 Annual Non-Radiological Environmental Operating Report PNP 2023-007, and Big Rock Point, 2022 Annual Radioactive Effluent Release and Waste Disposal Reports2023-04-19019 April 2023 and Big Rock Point, 2022 Annual Radioactive Effluent Release and Waste Disposal Reports PNP 2023-008, 2022 Radiological Environmental Operating Report2023-04-18018 April 2023 2022 Radiological Environmental Operating Report PNP 2023-002, 6 to Updated Final Safety Analysis Report2023-03-31031 March 2023 6 to Updated Final Safety Analysis Report PNP 2023-006, Report of Changes to Security Plan, Revision 202023-03-29029 March 2023 Report of Changes to Security Plan, Revision 20 PNP 2023-012, Presentation on Regulatory Path to Reauthorize Power Operations2023-03-16016 March 2023 Presentation on Regulatory Path to Reauthorize Power Operations PNP 2023-001, Regulatory Path to Reauthorize Power Operations2023-03-13013 March 2023 Regulatory Path to Reauthorize Power Operations PNP 2023-004, Report of Changes to Palisades Nuclear Plant Technical Specification Bases2023-03-0808 March 2023 Report of Changes to Palisades Nuclear Plant Technical Specification Bases PNP 2023-005, Response to Palisades Nuclear Plant - Request for Additional Information Related to the Post-Shutdown Decommissioning Activities Report2023-03-0101 March 2023 Response to Palisades Nuclear Plant - Request for Additional Information Related to the Post-Shutdown Decommissioning Activities Report PNP 2022-037, Report of Changes to Security Plan, Revision 192022-12-14014 December 2022 Report of Changes to Security Plan, Revision 19 PNP 2022-036, Response to Request for Additional Information Regarding License Amendment Request for Proposed Permanently Defueled Emergency Plan and Permanently Defueled Emergency Action Level Scheme2022-11-0808 November 2022 Response to Request for Additional Information Regarding License Amendment Request for Proposed Permanently Defueled Emergency Plan and Permanently Defueled Emergency Action Level Scheme PNP 2022-035, International - Notification of Commitment Cancellations for Remaining Activities Related to Beyond-Design-Basis Seismic Hazard Reevaluations2022-11-0202 November 2022 International - Notification of Commitment Cancellations for Remaining Activities Related to Beyond-Design-Basis Seismic Hazard Reevaluations PNP 2022-026, Request for Exemption from 10 CFR 50.54(w)(1) Concerning Onsite Property Damage Insurance2022-10-26026 October 2022 Request for Exemption from 10 CFR 50.54(w)(1) Concerning Onsite Property Damage Insurance PNP 2022-024, Request for Exemption from 10 CFR 140.11(a)(4) Concerning Primary and Secondary Liability Insurance2022-10-26026 October 2022 Request for Exemption from 10 CFR 140.11(a)(4) Concerning Primary and Secondary Liability Insurance PNP 2022-031, License Amendment Request, Revise License Condition to Eliminate Cyber Security Plan Requirements2022-09-14014 September 2022 License Amendment Request, Revise License Condition to Eliminate Cyber Security Plan Requirements PNP 2022-025, Report of Changes to Palisades Nuclear Plant Security Plan, Revision 182022-09-12012 September 2022 Report of Changes to Palisades Nuclear Plant Security Plan, Revision 18 PNP 2022-032, 2022 Evacuation Time Estimate Report2022-09-0707 September 2022 2022 Evacuation Time Estimate Report PNP 2022-023, Report of Changes to Palisades Nuclear Plant Security Plan, Revision 172022-08-15015 August 2022 Report of Changes to Palisades Nuclear Plant Security Plan, Revision 17 PNP 2022-014, Report of Changes to Palisades Nuclear Plant Site Emergency Plan, Revision 342022-07-13013 July 2022 Report of Changes to Palisades Nuclear Plant Site Emergency Plan, Revision 34 PNP 2022-016, License Amendment Request: Proposed Permanently Defueled Emergency Plan and Permanently Defueled Emergency Action Level Scheme2022-07-12012 July 2022 License Amendment Request: Proposed Permanently Defueled Emergency Plan and Permanently Defueled Emergency Action Level Scheme PNP 2022-017, Request for Exemptions from Certain Emergency Planning Requirements of 10 CFR 50.47(b); 10 CFR 50.47(c)(2); and 10 CFR Part 50, Appendix E2022-07-11011 July 2022 Request for Exemptions from Certain Emergency Planning Requirements of 10 CFR 50.47(b); 10 CFR 50.47(c)(2); and 10 CFR Part 50, Appendix E PNP 2022-019, & Big Rock Point - Notification of Expected Date of Transfer of Ownership of Nuclear Plants to Holtec Palisades, LLC; and Notification of Receipt of All Required Regulatory Approvals2022-06-24024 June 2022 & Big Rock Point - Notification of Expected Date of Transfer of Ownership of Nuclear Plants to Holtec Palisades, LLC; and Notification of Receipt of All Required Regulatory Approvals PNP 2022-011, Termination of the Emergency Response Data System (Eros) Link2022-06-13013 June 2022 Termination of the Emergency Response Data System (Eros) Link PNP 2022-010, Certifications of Permanent Cessation of Power Operations and Permanent Removal of Fuel from the Reactor Vessel2022-06-13013 June 2022 Certifications of Permanent Cessation of Power Operations and Permanent Removal of Fuel from the Reactor Vessel PNP 2022-004, 2021 Radiological Environmental Operating Report2022-05-12012 May 2022 2021 Radiological Environmental Operating Report PNP 2022-003, and Big Pock Point Plant - 2021 Annual Radioactive Effluent Release and Waste Disposal Report2022-04-25025 April 2022 and Big Pock Point Plant - 2021 Annual Radioactive Effluent Release and Waste Disposal Report PNP 2022-007, 2021 Annual Non-Radiological Environmental Operating Report2022-04-21021 April 2022 2021 Annual Non-Radiological Environmental Operating Report PNP 2022-012, Response to Request for Additional Information Regarding License Amendment Request to Revise Facility Operating License and Technical Specifications for a Permanently Defueled Condition2022-04-21021 April 2022 Response to Request for Additional Information Regarding License Amendment Request to Revise Facility Operating License and Technical Specifications for a Permanently Defueled Condition PNP 2022-002, Annual Report of Changes in Emergency Core Cooling System Models2022-03-24024 March 2022 Annual Report of Changes in Emergency Core Cooling System Models PNP 2021-012, Report of Changes, Tests and Experiments, and Summary of Commitment Changes2021-10-0707 October 2021 Report of Changes, Tests and Experiments, and Summary of Commitment Changes PNP 2021-029, Pre-Notice of Disbursement from Decommissioning Trust2021-09-0202 September 2021 Pre-Notice of Disbursement from Decommissioning Trust PNP 2021-013, Request for Rescission of Interim Compensatory Measure from Order EA-02-0262021-07-21021 July 2021 Request for Rescission of Interim Compensatory Measure from Order EA-02-026 PNP 2021-020, Request for Partial Exemption from Record Retention Requirements in 10 CFR 50.122021-06-15015 June 2021 Request for Partial Exemption from Record Retention Requirements in 10 CFR 50.12 PNP 2021-005, License Amendment Request to Revise Renewed Facility Operating License and Technical Specifications for Permanently Defueled Condition2021-06-0101 June 2021 License Amendment Request to Revise Renewed Facility Operating License and Technical Specifications for Permanently Defueled Condition PNP 2021-026, Pre-Notice of Disbursement from Decommissioning Trust2021-05-27027 May 2021 Pre-Notice of Disbursement from Decommissioning Trust PNP 2021-016, 2020 Radiological Environmental Operating Report2021-05-12012 May 2021 2020 Radiological Environmental Operating Report PNP 2021-022, 2020 Annual Non-Radiological Environmental Operating Report2021-04-27027 April 2021 2020 Annual Non-Radiological Environmental Operating Report PNP 2021-015, and Big Rock Point, Submittal of 2020 Annual Radioactive Effluent Release and Waste Disposal Report2021-04-21021 April 2021 and Big Rock Point, Submittal of 2020 Annual Radioactive Effluent Release and Waste Disposal Report PNP 2021-017, Schedule Change to Open Phase Condition Detection Implementation2021-04-0101 April 2021 Schedule Change to Open Phase Condition Detection Implementation PNP 2021-003, 2020 Steam Generator Tube Inspection Report2021-03-25025 March 2021 2020 Steam Generator Tube Inspection Report PNP 2021-010, Annual Report of Changes in Emergency Core Cooling System Models2021-03-19019 March 2021 Annual Report of Changes in Emergency Core Cooling System Models PNP 2021-004, Report - Changes to Palisades Nuclear Plant Technical Specifications Bases2021-03-10010 March 2021 Report - Changes to Palisades Nuclear Plant Technical Specifications Bases PNP 2021-006, Pre-Notice of Disbursement from Decommissioning Trust2021-03-0808 March 2021 Pre-Notice of Disbursement from Decommissioning Trust PNP 2021-001, ASME Section XI 90-Day Owner'S Activity Report2021-01-12012 January 2021 ASME Section XI 90-Day Owner'S Activity Report 2023-09-28
[Table view] Category:Report
MONTHYEARPNP 2023-025, Request for Exemption from Certain Termination of License Requirements of 10 CFR 50.822023-09-28028 September 2023 Request for Exemption from Certain Termination of License Requirements of 10 CFR 50.82 ML23087A0392023-05-0202 May 2023 PSDAR Comment Resolution PNP 2023-001, Regulatory Path to Reauthorize Power Operations2023-03-13013 March 2023 Regulatory Path to Reauthorize Power Operations CNRO-2021-00023, Entergy Operations, Inc. - Supplement to CNRO-2021-00002, Basis for Concluding the Terms of Confirmatory Order EA-17-132/EA-17-153 Are Complete, Element L2021-10-0606 October 2021 Entergy Operations, Inc. - Supplement to CNRO-2021-00002, Basis for Concluding the Terms of Confirmatory Order EA-17-132/EA-17-153 Are Complete, Element L PNP 2020-039, 10 CFR 71.95 Report Involving 3-608 Cask2020-11-20020 November 2020 10 CFR 71.95 Report Involving 3-608 Cask ML20272A1662020-09-30030 September 2020 Attachment 3 - Framatome Document No. ANP-3876, Revision 1Q1NP, Response to NRC Request for Additional Information of Palisades Relief Request Number RR 5-8, Repair of Reactor Pressure Vessel Head Penetration, Inservice Inspection Program, ML20267A3912020-09-22022 September 2020 Attachment 4, Framatome Document No. 51-9292503-002, Palisades CEDM Nozzle Idtb Repair - Life Assessment Summary PNP 2019-001, Request for Deferral of Actions Related to a Beyond-Design-Basis External Seismic Event2019-03-20020 March 2019 Request for Deferral of Actions Related to a Beyond-Design-Basis External Seismic Event ML18354B1332019-01-17017 January 2019 Staff Assessment of Flood Focused Evaluation ML18330A1432018-11-26026 November 2018 Relief Request Number RR 5-7, Proposed Alternative to ASME Section Xi Code Requirements for Repair of Reactor Pressure Vessel Head Penetrations ML18330A1462018-11-24024 November 2018 Framatome, Document No. 51-9292503, Palisades CRDM & Ici Nozzle Idtb Repair - Life Assessment Summary ML18270A3232018-09-27027 September 2018 Attachment 2: Probabilistic Risk Assessment Technical Adequacy PNP 2018-036, Revised Mitigating Strategies Assessment for Flooding Pursuant to 10 CFR 50.54(f) Request for Information Regarding Recommendation 2.1: Flooding of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident2018-09-25025 September 2018 Revised Mitigating Strategies Assessment for Flooding Pursuant to 10 CFR 50.54(f) Request for Information Regarding Recommendation 2.1: Flooding of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident PNP 2018-041, Focused Evaluation Pursuant to 10 CFR 50.54(f) Request for Information Regarding Recommendation 2.1: Flooding of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident2018-09-25025 September 2018 Focused Evaluation Pursuant to 10 CFR 50.54(f) Request for Information Regarding Recommendation 2.1: Flooding of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident PNP 2016-066, Special Report for Inoperability of High Range Noble Gas Monitor2016-12-20020 December 2016 Special Report for Inoperability of High Range Noble Gas Monitor PNP 2016-042, Annual Status Notification in Response to Confirmatory Order, EA-14-0132016-06-16016 June 2016 Annual Status Notification in Response to Confirmatory Order, EA-14-013 ML16048A3442016-02-10010 February 2016 Annual Fatigue Reporting Form 2015 ML15351A3522015-12-16016 December 2015 Attachment 1, Compliance with Order EA-12-049 ML15351A3532015-12-16016 December 2015 Attachment 2, Order EA-12-049 Compliance Elements Summary ML15351A3542015-12-16016 December 2015 Attachment 3, Audit Open Item Responses ML15351A3552015-12-16016 December 2015 Attachment 4, Interim Staff Evaluation Open Item and Confirmation Item Responses ML15351A3622015-12-16016 December 2015 Attachment 6, System Operating Procedure 23, Plant Heating System, Attachment 14, Actions When Outside Temperatures Are Less than 20 Degrees Fahrenheit. ML15351A3602015-12-16016 December 2015 Attachment 5, Final Integrated Plan PNP 2015-066, Submittal of Report on the 8-120B Cask2015-08-20020 August 2015 Submittal of Report on the 8-120B Cask PNP 2015-058, Technical Specification Required Report2015-08-0404 August 2015 Technical Specification Required Report PNP 2015-037, Appendix a, Computer Files Listing, File No. 1200895.306, Revision 12015-05-22022 May 2015 Appendix a, Computer Files Listing, File No. 1200895.306, Revision 1 ML15147A6192015-05-22022 May 2015 Enclosure 2, Corrected Documentation for Relief Request Number RR 4-18 ML15147A6182015-05-22022 May 2015 Appendix a, Computer File Listing, File No. 1400669.323, Revision 0 ML15147A6172015-05-22022 May 2015 Enclosure 1, Relief Request Number RR 4-21 Proposed Alternative, in Accordance with 10 CFR 50.55a(z)(2), Hardship Without a Compensating Increase in Level of Quality and Safety PNP 2015-018, Areva, Inc., 51-9226987-000, Palisades Nuclear Plant Flooding Hazard Re-Evaluation Report.2015-02-25025 February 2015 Areva, Inc., 51-9226987-000, Palisades Nuclear Plant Flooding Hazard Re-Evaluation Report. PNP 2014-108, Expedited Seismic Evaluation Process Report (CEUS Sites), Response to NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima.2014-12-18018 December 2014 Expedited Seismic Evaluation Process Report (CEUS Sites), Response to NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima. PNP 2014-051, Response to May 1, 2014 Request for Additional Information for License Amendment Request to Revise Emergency Response Organization Staff Augmentation Response Times2014-07-16016 July 2014 Response to May 1, 2014 Request for Additional Information for License Amendment Request to Revise Emergency Response Organization Staff Augmentation Response Times PNP 2014-038, Special Report for Inoperability of High Range Noble Gas Monitor2014-04-14014 April 2014 Special Report for Inoperability of High Range Noble Gas Monitor PNP 2014-033, Seismic Hazard and Screening Report (CEUS Sites), Response to NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding the Seismic Aspects of Recommendation 2.1 of the Near-Term Task Force Review of Insights from The.2014-03-31031 March 2014 Seismic Hazard and Screening Report (CEUS Sites), Response to NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding the Seismic Aspects of Recommendation 2.1 of the Near-Term Task Force Review of Insights from The. ML13365A2642014-02-10010 February 2014 Interim Staff Evaluation Regarding Overall Integrated Plan in Response to Order EA-12-049 (Mitigation Strategies) ML14030A2072014-02-0606 February 2014 Mega-Tech Services, LLC, Technical Evaluation Report Regarding the Overall Integrated Plan for Palisades Nuclear Plant, TAC No.: MF0768 PNP 2013-072, Report of Changes, Tests and Experiments and Summary of Commitment Changes2013-10-14014 October 2013 Report of Changes, Tests and Experiments and Summary of Commitment Changes PNP 2013-063, Unsatisfactory Laboratory Testing Report2013-09-18018 September 2013 Unsatisfactory Laboratory Testing Report ML13242A1592013-08-29029 August 2013 Addendum to the Results of Independent Samples Collected by the NRC at Palisades Nuclear Plant Storm Drain Outfall ML13295A4502013-07-31031 July 2013 WCAP-15353-Supplement 2-NP, Rev. 0, Palisades Reactor Pressure Vessel Fluence Evaluation. PNP 2013-046, Updated Palisades Nuclear Plant Reactor Vessel Fluence Evaluation2013-06-25025 June 2013 Updated Palisades Nuclear Plant Reactor Vessel Fluence Evaluation PNP 2013-027, National Pollutant Discharge Elimination System (NPDES) Permit Renewal Application2013-04-10010 April 2013 National Pollutant Discharge Elimination System (NPDES) Permit Renewal Application ML14316A2082013-02-28028 February 2013 Attachment 5 - Westinghouse WCAP-17651-NP, Revision 0, Palisades Nuclear Power Plant Reactor Vessel Equivalent Margins Analysis ML13295A4512013-02-28028 February 2013 WCAP-17651-NP, Rev. 0, Palisades Nuclear Power Plant Reactor Vessel Equivalent Margins Analysis. ML13038A4402013-02-0707 February 2013 BADGER Test Campaign at Palisades Nuclear Plant ML13295A4492013-01-31031 January 2013 WCAP-17403-NP, Rev. 1, Palisades Nuclear Power Plant Extended Beltline Reactor Vessel Integrity Evaluation. ML14316A1992013-01-31031 January 2013 Attachment 3 - Westinghouse WCAP-17403-NP, Revision 1, Palisades Nuclear Power Plant Extended Beltline Reactor Vessel Integrity Evaluation ML12334A0962012-11-27027 November 2012 PLP-RPT-12-00141, Rev. 0, Palisades Seismic Walkdown Report for Resolution of Fukushima Near-Term Task Force Recommendation 2.3: Seismic, Part 1 of 3 PNP 2012-101, Flooding Walkdown Report - Response to NRC Request for Information Pursuant to 10CFR50.54(f) the Flooding Aspects of Recommendation 2.3 of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident2012-11-27027 November 2012 Flooding Walkdown Report - Response to NRC Request for Information Pursuant to 10CFR50.54(f) the Flooding Aspects of Recommendation 2.3 of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident ML12334A0972012-11-27027 November 2012 PLP-RPT-12-0041, Rev. 0, Palisades Seismic Walkdown Report for Resolution of Fukushima Near-Term Task Force Recommendation 2.3: Seismic, Part 2 of 3 2023-09-28
[Table view] Category:Miscellaneous
MONTHYEARML23087A0392023-05-0202 May 2023 PSDAR Comment Resolution PNP 2023-001, Regulatory Path to Reauthorize Power Operations2023-03-13013 March 2023 Regulatory Path to Reauthorize Power Operations CNRO-2021-00023, Entergy Operations, Inc. - Supplement to CNRO-2021-00002, Basis for Concluding the Terms of Confirmatory Order EA-17-132/EA-17-153 Are Complete, Element L2021-10-0606 October 2021 Entergy Operations, Inc. - Supplement to CNRO-2021-00002, Basis for Concluding the Terms of Confirmatory Order EA-17-132/EA-17-153 Are Complete, Element L PNP 2019-001, Request for Deferral of Actions Related to a Beyond-Design-Basis External Seismic Event2019-03-20020 March 2019 Request for Deferral of Actions Related to a Beyond-Design-Basis External Seismic Event ML18354B1332019-01-17017 January 2019 Staff Assessment of Flood Focused Evaluation PNP 2016-066, Special Report for Inoperability of High Range Noble Gas Monitor2016-12-20020 December 2016 Special Report for Inoperability of High Range Noble Gas Monitor PNP 2016-042, Annual Status Notification in Response to Confirmatory Order, EA-14-0132016-06-16016 June 2016 Annual Status Notification in Response to Confirmatory Order, EA-14-013 ML16048A3442016-02-10010 February 2016 Annual Fatigue Reporting Form 2015 ML15351A3542015-12-16016 December 2015 Attachment 3, Audit Open Item Responses ML15351A3622015-12-16016 December 2015 Attachment 6, System Operating Procedure 23, Plant Heating System, Attachment 14, Actions When Outside Temperatures Are Less than 20 Degrees Fahrenheit. ML15351A3602015-12-16016 December 2015 Attachment 5, Final Integrated Plan ML15351A3552015-12-16016 December 2015 Attachment 4, Interim Staff Evaluation Open Item and Confirmation Item Responses ML15351A3522015-12-16016 December 2015 Attachment 1, Compliance with Order EA-12-049 ML15351A3532015-12-16016 December 2015 Attachment 2, Order EA-12-049 Compliance Elements Summary PNP 2015-066, Submittal of Report on the 8-120B Cask2015-08-20020 August 2015 Submittal of Report on the 8-120B Cask ML15147A6192015-05-22022 May 2015 Enclosure 2, Corrected Documentation for Relief Request Number RR 4-18 ML15147A6182015-05-22022 May 2015 Appendix a, Computer File Listing, File No. 1400669.323, Revision 0 ML15147A6172015-05-22022 May 2015 Enclosure 1, Relief Request Number RR 4-21 Proposed Alternative, in Accordance with 10 CFR 50.55a(z)(2), Hardship Without a Compensating Increase in Level of Quality and Safety PNP 2015-037, Appendix a, Computer Files Listing, File No. 1200895.306, Revision 12015-05-22022 May 2015 Appendix a, Computer Files Listing, File No. 1200895.306, Revision 1 PNP 2014-033, Seismic Hazard and Screening Report (CEUS Sites), Response to NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding the Seismic Aspects of Recommendation 2.1 of the Near-Term Task Force Review of Insights from The.2014-03-31031 March 2014 Seismic Hazard and Screening Report (CEUS Sites), Response to NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding the Seismic Aspects of Recommendation 2.1 of the Near-Term Task Force Review of Insights from The. PNP 2013-072, Report of Changes, Tests and Experiments and Summary of Commitment Changes2013-10-14014 October 2013 Report of Changes, Tests and Experiments and Summary of Commitment Changes PNP 2013-063, Unsatisfactory Laboratory Testing Report2013-09-18018 September 2013 Unsatisfactory Laboratory Testing Report PNP 2013-046, Updated Palisades Nuclear Plant Reactor Vessel Fluence Evaluation2013-06-25025 June 2013 Updated Palisades Nuclear Plant Reactor Vessel Fluence Evaluation PNP 2013-027, National Pollutant Discharge Elimination System (NPDES) Permit Renewal Application2013-04-10010 April 2013 National Pollutant Discharge Elimination System (NPDES) Permit Renewal Application PNP 2012-101, Flooding Walkdown Report - Response to NRC Request for Information Pursuant to 10CFR50.54(f) the Flooding Aspects of Recommendation 2.3 of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident2012-11-27027 November 2012 Flooding Walkdown Report - Response to NRC Request for Information Pursuant to 10CFR50.54(f) the Flooding Aspects of Recommendation 2.3 of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident ML12334A0962012-11-27027 November 2012 PLP-RPT-12-00141, Rev. 0, Palisades Seismic Walkdown Report for Resolution of Fukushima Near-Term Task Force Recommendation 2.3: Seismic, Part 1 of 3 ML12334A0972012-11-27027 November 2012 PLP-RPT-12-0041, Rev. 0, Palisades Seismic Walkdown Report for Resolution of Fukushima Near-Term Task Force Recommendation 2.3: Seismic, Part 2 of 3 PNP 2012-102, PLP-RPT-12-0041, Rev. 0, Palisades Seismic Walkdown Report for Resolution of Fukushima Near-Term Task Force Recommendation 2.3: Seismic, Part 3 of 32012-11-27027 November 2012 PLP-RPT-12-0041, Rev. 0, Palisades Seismic Walkdown Report for Resolution of Fukushima Near-Term Task Force Recommendation 2.3: Seismic, Part 3 of 3 PNP 2012-094, 2012 Steam Generator Tube Inspection Report2012-11-0101 November 2012 2012 Steam Generator Tube Inspection Report PNP 2012-059, 60-Day Reports Per Bulletin 2004-01 and CAL No NRR-07-023 Pressurizer Inspection Results for the 2012 Refueling Outage2012-07-11011 July 2012 60-Day Reports Per Bulletin 2004-01 and CAL No NRR-07-023 Pressurizer Inspection Results for the 2012 Refueling Outage IR 05000255/20110192012-02-14014 February 2012 Final Significance Determination of Yellow and White Findings with Assessment Followup and Notice of Violation NRC Inspection Report Nos. 05000255-11-019 and 05000255-11-020 Palisades Nuclear Plant ML12023A1872012-01-17017 January 2012 EA-PSA-SDP-D11-2-11-07, Rev. 2, SDP Assessment of DC Panel D11-2 Fault, Cover Through Appendix a ML12023A1882012-01-17017 January 2012 EA-PSA-SDP-D11-2-11-07, Rev. 2, SDP Assessment of DC Panel D11-2 Fault, Appendix B Through End ML12006A0712012-01-0505 January 2012 SDP Assessment of DC Panel D-11-2 Fault Palisades ML1134205122011-12-19019 December 2011 Review of the 2010 Steam Generator Tube Inspections During Refueling Outage 21 ML12006A0722011-10-17017 October 2011 Plant Trip During D-11-2 Maintenance Root Cause ML1128705702011-10-14014 October 2011 Report of Changes, Tests and Experiments and Summary of Commitment Changes ML12006A0672011-09-28028 September 2011 SDP Assessment of Service Water Pump P-7C Coupling Failures Part 3 ML1031603372010-11-0909 November 2010 Unsatisfactory Laboratory Testing Report ML1012704392010-05-0505 May 2010 Y020100187 - List of Historical Leaks and Spills at U.S. Commercial Nuclear Power Plants ML1020301642010-04-28028 April 2010 E-Mail. from Dotson to Cassidy, GZA 2007 Report ML0929505252009-10-22022 October 2009 Generator Tube Inspection Report ML0928903362009-10-15015 October 2009 Report of Facility Changes, Tests and Experiments and Summary of Commitment Changes ML0901402872008-07-16016 July 2008 E-mail from Ellegood to M. Chawla Et Al. Palisades SFP Racks with Attachment: Report on Resolution of Outstanding Concerns on Spent Fuel Pit Rack Localized Swelling Palisades Nuclear Plant ML0810000792008-04-0808 April 2008 Request for Enforcement Discretion - Technical Specification 3.8.1 Required Actions F.1 and F.2 ML0717802162007-06-19019 June 2007 Revised Steam Generator Tube Integrity Assessment from the 2006 Refueling Outage ML0719400912006-09-15015 September 2006 Request for Relief from ASME Section Xl Code Requirements for Repair of Pressurizer Nozzle Penetrations (Non-Proprietary) ML0619803382006-07-20020 July 2006 Review of the 2004 Steam Generator Tube Inspection Reports ML0617301112006-06-21021 June 2006 Day Report Per First Revised Order EA-03-009 ML0608203512006-03-20020 March 2006 License Amendment Request: Removal of TSP from Palisades Containment 2023-05-02
[Table view] |
Text
Entergy Nuclear Operations, Inc.
Palisades Nuclear Plant er 27780 Blue Star Memorial Highway Covert, Ml 49043 Tel 269 764 2000 Anthony J Vita Ic Site Vice President PNP 2012-059 July 11,2012 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001
SUBJECT:
60-Day Reports per Bulletin 2004-01 and CAL No. NRR-07-023 Pressurizer Inspection Results for the 2012 Refueling Outage Palisades Nuclear Plant Docket 50-255 License No. DPR-20
References:
- 1. NRC Bulletin 2004-01: Inspection of Alloy 82/182/600 Materials Used in the Fabrication of Pressurizer Penetrations and Steam Space Piping Connections at Pressurized-Water Reactors, dated May 28, 2004 (ADAMS Accession N umber MLO4 1480034)
- 2. Nuclear Management Company, LLC letter to the NRC, 60-Day Response to Bulletin 2004-01, Inspection of Alloy 82/182/600 Materials Used in the Fabrication of Pressurizer Penetrations and Steam Space Piping Connections at Pressurized-Water Reactors, dated July 26, 2004 (ADAMS Accession Number ML042100242)
- 3. Nuclear Management Company, LLC letter to the NRC, Supplement to Inspection and Mitigation of Alloy 600/82/182 Pressurizer Butt- Welds, dated February 27, 2007 (ADAMS Accession Number ML070590333)
- 4. CAL No. NRR-07-023: ConfirmatoiyAction Letter Palisades Nuclear Plant (TAC No. MD4 168), dated March 29, 2007 (ADAMS Accession Number ML070800449)
Dear Sir or Madam:
On May 28, 2004, the Nuclear Regulatory Commission (NRC) issued Bulletin 2004-01 (Reference 1). In a 60-day bulletin response letter (Reference 2), the Nuclear Management Company, LLC (NMC), former holder of the Palisades Nuclear Plant (PNP) operating license, made a series of commitments related to inspection of pressurizer penetrations.
On March 29, 2007, the NRC issued Confirmatory Action Letter, CAL No. NRR-07-023 (Reference 4), confirming the commitments made in Reference 3. The commitments
PNP 2012-059 Page 2 addressed actions that would be taken regarding pressurizer dissimilar metal butt-welds containing Alloy 82/182/600 material.
In June 2011, the NRC issued a revision to 10 CFR 50.55a, which required licensees to implement ASME Code Cases N-722-1, N-729-1, and N-770-1, with conditions.
N-722-1 and N-770-1 encompass the earlier pressurizer inspection commitments made for PNP, except for the 60-day reporting requirement.
Entergy Nuclear Operations, Inc. (ENO) has assumed the commitments made by NMC for the refueling outage inspections of the pressurizer piping connections. During the 2012 refueling outage that ended on May 12, 2012, END inspected pressurizer heater sleeves, dissimilar metal butt-welds, and dissimilar metal pad welds containing Alloy 82/182/600 material in accordance with the commitments, qualified procedures, and 10 CFR 50.55a requirements. A total of 146 welds were examined: 120 heater sleeves, 14 butt-weld piping connections containing 24 Alloy 82/182/600 butt-welds requiring examination, and two pad repair welds. Based on the results of the examinations performed, END has concluded that all pressurizer heater sleeves, Alloy 82/182/600 pressurizer butt-welds, and pressurizer pad repair welds that were returned to service in 2012 were not degraded, and no wastage of the pressurizer occurred.
This letter identifies no new commitments and no revisions to existing commitments.
I declare under penalty of perjury that the foregoing is true and correct. Executed on July 11,2012.
Since rely,
Attachment:
- 1. 60-Day Reports Per Bulletin 2004-01 and CAL No. NRR-07-023 Palisades Nuclear Plant Pressurizer Inspection Results for the 2012 Refueling Outage cc: Administrator, Region Ill, USNRC Project Manager, Palisades, USNRC Resident Inspector, Palisades, USNRC
ATTACHMENT 1 60-DAY REPORTS PER BULLETIN 2004-01 AND CAL NO. NRR-07-023 PALISADES NUCLEAR PLANT PRESSURIZER INSPECTION RESULTS FOR THE 2012 REFUELING OUTAGE
1.0 INTRODUCTION
On May 28, 2004, the Nuclear Regulatory Commission (NRC) issued Bulletin (BL) 2004-01, Inspection of Alloy 82/182/600 Materials Used in the Fabrication of Pressurizer Penetrations and Steam Space Piping Connections at Pressurized-Water Reactors. In a 60-day response letter dated July 26, 2004, the Nuclear Management Company. LLC (NMC), former holder of the Palisades Nuclear Plant (PNP) operating license, made a series of commitments related to inspection of pressurizer penetrations.
On March 29, 2007, the NRC issued CAL No. NRR-07-023, Confirmatory Action Letter -
Palisades Nuclear Plant (TAC No. MD4 168), confirming commitments made in a February 27, 2007, NMC letter, Supplement to Inspection and Mitigation of Alloy 600/82/182 Pressurizer Butt-Welds. The commitments addressed actions that would be taken regarding pressurizer dissimilar metal butt-welds containing Alloy 82/182/600 material.
In June 2011, the NRC issued a revision to 10 CFR 50.55a, which required licensees to implement ASME Code Cases N-722-1, N-729-1, and N-770-1, with conditions.
N-722-1 and N-770-1 encompass the earlier pressurizer inspection commitments made for PNP, except for the 60-day reporting requirement.
Entergy Nuclear Operations, Inc. (ENO), as the PNP license holder, has assumed the commitments made by NMC for the refueling outage inspections of the pressurizer piping connections. In the 2012 refueling outage that ended on May 12, 2012, ENO inspected pressurizer heater sleeves and dissimilar metal butt-welds containing Alloy 82/182/600 material in accordance with commitments and qualified procedures. A total of 146 welds were examined: 120 heater sleeves, 14 butt-weld piping connections containing 24 Alloy 82/182/600 butt-welds requiring examination, and two pad repair welds.
2.0 DESCRIPTION
OF INSPECTION METHODS Performance Demonstration Initiative (PDI)-qualified phased array ultrasonic examinations were performed by qualified non-destructive examination (NDE) personnel using qualified procedures, to inspect one power operated relief valve (PORV) pipe to nozzle butt-weld, and two surge line safe end butt-welds to elbow and nozzle. Examinations were performed in accordance with ASME Code Case N-770-1 with conditions imposed by 10 CFR 50.55a. Code Case N-770-1 supersedes Page 1 of 5
examination requirements of MRP-139 and satisfies PNP commitments for volumetric examination of Alloy 600/82/182 pressurizer butt-welds.
Qualified NDE personnel performed bare metal direct visual examinations of 100% of all 120 unmitigated Alloy 82/182/600 pressurizer heater sleeves, 16 unmitigated one-inch level tap safe end butt-welds to piping and nozzles, three unmitigated safety valve flange to nozzle butt-welds, and two unmitigated spray line safe end butt-welds to piping and nozzle. Bare metal, direct visual NDE was also performed on two temperature element nozzle pad repair welds that had been repaired in 1993.
Examinations were performed in accordance with ASME Code Cases N-722-1 and N-770-1 with conditions imposed by 10 CFR 50.55a. Code Cases N-722-1 and N-770-1 satisfy PNP commitments for visual examination of Alloy 600/82/182 pressurizer butt-welds.
3.0 COMMITMENTS AND RESULTS In 2004, four commitments for PNP were made in response to Bulletin 2004-01. Three of the commitments remain open in 2012. ENO actions and results during the 2012 PNP refueling outage are described below for heater sleeve commitments one, two, and three. Commitment four was completed in 2006.
Additionally, in February 2007, six new and two revised commitments were made for PNP, in regard to Alloy 82/182/600 pressurizer butt-welds that were confirmed in CAL No. NRR-07-023. Of these eight commitments, commitments one through four do not apply to outage activities. Commitments five and six were completed during and following the 2007 PNP refueling outage. ENO actions and results during the 2012 PNP refueling outage are described below for commitments seven and eight.
Heater Commitment 1:
NMC [ENO] will perform a bare metal visual inspection of 100 percent of all pressurizer heater sleeve locations, in a manner that visual access to the bare metal 360 degrees around each sleeve can be attained during each outage at Palisades Nuclear Plant.
Results for Commitment 1:
During the 2012 refueling outage, bare metal visual examinations of all 120 pressurizer heater sleeves (J-groove welds) were performed. This examination included 360 degrees around each sleeve. There was no accumulation of boric acid in the vicinity of the penetrations. All visual examinations of the penetrations had acceptable results.
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Heater Commitment 2:
NMC [ENO] will perform non-destructive examination (NDE) capable of characterizing crack orientation of all sleeves for which visual inspection shows evidence of leakage at Palisades Nuclear Plant. The NDE will be performed prior to any repairs.
Results for Commitment 2:
No action was required, because the visual examination did not show any evidence of leakage.
Heater Commitment 3:
NMC [ENO] will notify the NRC immediately if the NDE defines the flaw as potential circumferential primary water stress corrosion cracking (PWSCC) in either the pressure boundary or non-pressure boundary portions of any locations covered under the scope of BL 2004-01 for the PNP. An appropriate inspection plan will be developed, which will define additional sleeves to be inspected by NDE, sufficient to determine the extent of condition commensurate with the characterization of the flaw.
Results for Commitment 3:
No action was required, because the examinations did not show any evidence of leakage.
Butt-Weld Commitment 7:
NMC [ENO] will inspect the Alloy 82/182/600 pressurizer butt-welds per MRP-139, (Materials Reliability Program: Primary System Piping Butt Weld Inspection and Evaluation Guideilnes) on a frequency of at least every four years, until the Alloy 82/182/600 pressurizer butt-welds are mitigated or removed at PNP. NMC [ENO] will notify the NRC in writing, prior to making any changes to this commitment.
Results for Commitment 7:
All existing Alloy 82/182/600 pressurizer butt-welds were examined in accordance with MRP-1 39 within the last four years, during the spring 2009, fall 2010 and spring 2012 refueling outages.
Code Case N-770-1 imposes more stringent examination requirements than MRP-139.
Essentially 100% of the required examination volume must be examined in both the axial and circumferential directions, and essentially 100% of susceptible material must be examined. Mitigated welds must be approved by the NRC before being placed into mitigated inspection categories. Additionally, susceptible material must be examined Page 3 of 5
even if it is not exposed to primary water conditions, if it is relied upon for structural integrity. The second condition brought the mitigated surge line safe-end to elbow weld into the population of welds requiring inspection every other refueling outage. The second and third conditions brought the PORV nozzle into the population of required inspections, because it includes Alloy 82/182 weld butter that is isolated from the primary water environment but is relied upon for structural integrity.
During the 2012 refueling outage, PDI-qualified phased array ultrasonic examinations were performed to inspect a PORV nozzle weld, unmitigated surge line safe end to nozzle butt-weld, and surge line safe end butt-weld to the piping elbow mitigated in 1995 by the Mechanical Stress Improvement Process (MSIP). Also, the welds were dye penetrant examined. The 2012 examination results indicated these butt-welds were not degraded.
- The PORV nozzle, which had not required inspection under MRP-139, was last volumetrically examined in 2004. Essentially 100% volumetric coverage could not be attained, and a Relief Request was granted during the outage to defer baseline N-770-1 inspection until the faIl 2013 refueling outage.
- The surge line safe-end to nozzle butt-weld and the surge line safe end to the piping elbow butt-weld had previously received MRP-139 ultrasonic examinations during the 2009 PNP refueling outage. The surge line safe-end to nozzle butt-weld also had MRP-1 39 Category J visual examination during the 2007 and 2010 PNP refueling outages.
During the 2012 refueling outage, Code Case N-722-1 direct visual examinations were performed to inspect two unmitigated spray line safe end welds to nozzle and elbow, and three unmitigated welds attaching Alloy 600 safety valve flanges to pressurizer nozzles. The examination results indicated these welds were not degraded. These welds had previously received PDI-qualified ultrasonic examinations during the 2007 and 2010 PNP refueling outages, and MRP-139 CategoryJ visual examinations during the 2009 PNP refueling outage. Code Case N-722-1 examinations also meet the MRP-139 and Code Case N-770-1 visual examination requirements.
There has been no change to the commitment.
Butt-Weld Commitment 8:
NMC [ENO] will provide results of future inspections, including inspections on unmitigated welds and any corrective or mitigative actions taken on the pressurizer surge, spray, safety, or relief nozzle and safe end welds containing Alloy 82/182/600 material, within 60 days of the end of the station refueling outage during which the inspection was performed, until the Alloy 82/182/600 pressurizer butt-welds are mitigated or removed at PNP. NMC [ENO] will notify the NRC in writing, prior to making any changes to this commitment.
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Results for Commitment 8:
During the 2012 refueling outage, other Alloy 82/182/600 pressurizer welds were examined as required by ASME Section Xl Code Case N-722. Bare metal, direct visual examinations were performed on 16 unmitigated one-inch level tap safe end butt-welds to piping and nozzles, and on two temperature element nozzle pad repair welds that had been repaired in 1993. The examination results indicated the 16 butt-welds and two pad repair welds were not degraded. Similar examinations were performed during the 2007, 2009, and 2010 refueling outages.
There has been no change to the commitment.
4.0 CONCLUSION
S PNP returned to operation from its most recent refueling outage on May 12, 2012. This 60-day report describes inspection results for the pressurizer surge, spray, safety and relief nozzle, safe end, heater sleeve, and temperature element nozzle repair welds containing Alloy 82/182/600 material.
ENO has complied with commitments described in Bulletin 2004-01 and CAL No. NRR-07-023, for the PNP 2012 refueling outage. Based on the results of the examinations performed, ENO has concluded that all pressurizer heater sleeves, Alloy 82/182/600 pressurizer butt-welds, and pressurizer pad repair welds that were returned to service in 2012 were not degraded, and no wastage of the pressurizer occurred.
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