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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20133E1681997-01-0707 January 1997 Safety Evaluation Re Third 10-yr Interval ISI Plan,Rev 1 to Relief Request R11 for Plant.Proposed Alternative to ASME Requirements Authorized ML20128L1601996-10-0303 October 1996 Safety Evaluation Accepting Third 10-yr Interval Inservice Insp Plan Request for Relief R15 ML20128F4791996-10-0101 October 1996 Safety Evaluation Accepting Rev to Inservice Testing Program Re Leakage Testing of Containment Isolation Valves ML20056H2651993-08-24024 August 1993 SE Re Inservice Testing Program Requests for Relief ML20056E0911993-08-0404 August 1993 SE Re Util 930614 Response to Bulletin 93-03, Resolution of Issues Related to Reactor Vessel Water Level Instrumentation in Bwrs. Util Justification for Not Implementing Addl Short Term Actions Acceptable ML20128P4651993-02-18018 February 1993 Safety Evaluation Accepting Util Justification for Cancelling Commitment on Five Plant Control Room Human Engineering Discrepancies Re Relocation of Shift Supervisor Ofc ML20128F1361993-02-0505 February 1993 Safety Evaluation Re Leak on Core Spray in-vessel Annulus Piping.Plant Can Be Safely Operated for One Fuel Cycle W/O Repairing Observed Leak at Listed 1/4-inch Fillet Weld ML20125C3901992-12-0707 December 1992 Safety Evaluation Re Upper Reactor Bldg & Nonsafety Architectural Components Subjected to tornado-wind Loading ML20127P2251992-11-23023 November 1992 Safety Evaluation Accepting Response to SBO Rule ML20058A7621990-10-18018 October 1990 SE Accepting Util Insp & Repairs for Igscc,Per Generic Ltr 88-01 ML20246M7561989-08-30030 August 1989 Safety Evaluation Accepting Util 890624 Response to Integrated Plant Safety Assessment Section 4.11, Seismic Design Consideration, Items 4.11(1), Piping Sys & 4.11(3), Electrical Equipment ML20247A7061989-07-17017 July 1989 Safety Evaluation Supporting Generic Ltr 83-28,Item 4.5.2 Re Periodic on-line Testing of Reactor Trip Sys ML20245C1711989-06-15015 June 1989 Safety Evaluation Re Generic Ltr 83-28,Item 4.5.3 Re Reactor Trip Sys Reliability for All Domestic Operating Reactors ML20244C8501989-06-12012 June 1989 Safety Evaluation Accepting Util Response to Generic Ltr 83-28,Item 4.5.3 Re on-line Testing for Reactor Trip Sys NUREG-1000, Safety Evaluation Accepting Util 831114 & 851023 Responses to Generic Ltr 83-28,Item 2.1 (Part 1),confirming That All Applicable Components Identified as safety-related1989-04-0303 April 1989 Safety Evaluation Accepting Util 831114 & 851023 Responses to Generic Ltr 83-28,Item 2.1 (Part 1),confirming That All Applicable Components Identified as safety-related ML20235X1281989-03-0606 March 1989 Safety Evaluation Supporting Licensee Request to Extend Second 10-yr Inservice Insp & Testing Interval Until 911014 ML20205P5291988-11-0404 November 1988 Safety Evaluation Supporting Util Submittal Re Compliance W/Atws Rule 10CFR50.62 Concerning Alternate Rod Injection & Recirculation Pump Trip Sys ML20207L0831988-10-11011 October 1988 Safety Evaluation Re Systematic Evaluation of Ipsar Topic VII-1.A, Isolation of Reactor Protection Sys from Non-Safety Sys. Issue Resolved IR 05000219/19840311988-03-0404 March 1988 Safety Evaluation Concluding Util Compliance W/Generic Ltr 83-28,Items 3.1.1,3.1.2,3.2.1,3.2.2 & 4.5.1,based on Util 831114,850809,0509,1023 & 871223 Descriptions of Planned & Completed Actions & Insp Rept 50-219/84-31 on 841126-30 ML20149L6381988-02-18018 February 1988 Safety Evaluation Supporting Proposed Standby Liquid Control Sys Operation ML20236Q5311987-11-0606 November 1987 Safety Evaluation Re Safety Limit Violation on 870911.Safety Significance Considered Low Due to Adequate Core Cooling & Low Decay Heat Levels.Basis for Conclusion Elaborated in Encl Insp Rept 50-219/87-29 ML20235E0661987-09-22022 September 1987 Safety Evaluation Re Corrosion of Drywell Shell.Licensee Meets NRC Requirements as Specified in 861224 Safety Evaluation ML20207S2311987-03-13013 March 1987 Safety Evaluation Re Generic Ltr 84-09 Re Hydrogen Recombiner Capability.Licensee Should Provide Nitrogen Containment Atmosphere Dilution Sys Capable of Isolating Air from Containment Whenever Isolation Signal Occurs ML20212M3561987-03-0303 March 1987 Safety Evaluation Rejecting Util Schedule for Completion of Mark I Containment Program Re Vacuum Breaker Integrity. Required Vacuum Breaker Parts Should Be Replaced Prior to Startup from Cycle 12 Refueling Outage ML20207M2081986-12-29029 December 1986 Safety Evaluation Re Corrosion of Drywell Shell Line Break in Isolation Condenser.Operation of Plant for Cycle 12 Safe W/Drywell Steel Plates Not Fully in Conformance W/Fsar.Util Shall Provide Plans for Mitigating Problem by 870630 ML20215F3681986-12-15015 December 1986 Safety Evaluation Supporting Util Response to IE Bulletin 86-002 Re Static O-Ring Differential Pressure Switches ML20211M3911986-11-28028 November 1986 Safety Evaluation Re Deferment of NRC Required Mods from Cycle 11R Outage,Including SPDS Implementation,Isolation Condenser Makeup Pump,Intake Canal Level Instrumentation & Masonry Wall Mods.Request Acceptable ML20214A5571986-11-14014 November 1986 Safety Evaluation Re Insp & Repair of Reactor Coolant Piping Sys & Supporting Return to Operation for Next Operating Cycle ML20213G5551986-10-31031 October 1986 Safety Evaluation Supporting Util 860903 Submittal Re Insp of Core Spray Sparger Sys in Current Cycle 11 Refueling Outage.Licensee Satisfied Requirements of License Condition 2.C.(7) for Current Cycle 11 Refueling Outage NUREG-0822, Safety Evaluation Finding Integrated Plant SAR (NUREG-0822), Section 4.12 Complete W/Exception of Three Issues,Including Evaluation of Drywell for Concrete Subj to High Temps & Thermal Transients1986-10-29029 October 1986 Safety Evaluation Finding Integrated Plant SAR (NUREG-0822), Section 4.12 Complete W/Exception of Three Issues,Including Evaluation of Drywell for Concrete Subj to High Temps & Thermal Transients ML20197B8801986-10-10010 October 1986 Safety Evaluation Supporting Util 850924 Proposal Not to Replace Existing Containment Purge & Vent Isolation Valves W/New Clow Valves ML20215E7261986-10-0101 October 1986 Safety Evaluation Supporting Cancellation of Torus Pool Temp Indication & Thermal Mixing Mods ML20204F9721986-07-28028 July 1986 Corrected Page 3 to 860522 Safety Evaluation Re Integrated Plant Safety Assessment Rept,Section 4.38, Locas. Correction Concerns Licensee Maint to Repack Four MSIVs Each Refueling Outage ML20210K2481986-04-22022 April 1986 Safety Evaluation Supporting Util 831114 Response to Generic Ltr 83-28,Item 1.2, Post-Trip Review,Data & Info Capability ML20141D4261986-03-31031 March 1986 Safety Evaluation Re Generic Ltr 83-28,Items 3.1.3 & 3.2.3, Post-Maint Testing (Program Description & Procedure). Tech Specs Incorporating post-maint Testing of Reactor Protection Sys Components Should Be Proposed ML20141N0451986-02-24024 February 1986 Safety Evaluation Supporting Deferment of Feedwater Nozzle Insps Until Cycle 12R Outage Scheduled for 1988 ML20205H7981986-01-21021 January 1986 Safety Evaluation Re Venting & Purging Containment During Plant Operation.Rationale Utilized for Design & Operation of Purge/Vent Sys Acceptable ML20136A9351985-12-23023 December 1985 Safety Evaluation Accepting Licensee Response to Items 2(b) & 3 of IE Bulletin 80-11, Masonry Wall Design. Licensee 850726 Request Re Wall Mods to Be Completed During Operating Cycle 11 Not Addressed ML20137Q7621985-11-22022 November 1985 Safety Evaluation Supporting Determination That Max 150 F Drywell Temp Acceptable for Containment Safety,Drywell Steel & Concrete Structural Components & Normal Plant Operations. Tech Specs Re Limiting Factors Requested ML20128H5241985-05-28028 May 1985 Safety Evaluation Supporting Environ Qualification of Electric Equipment Important to Safety.Proposed Resolutions for Environ Qualification Deficiencies Acceptable ML20126K1221981-03-29029 March 1981 Safety Evaluation Supporting Amend 54 to License DPR-16 1998-03-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F1891998-05-0505 May 1998 Risk Evaluation of Post-LOCA Containment Overpressure Request ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20151Y4651998-03-31031 March 1998 Non-proprietary Version of Rev 1 to GENE-E21-00143, ECCS Suction Strainer Hydraulic Sizing Rept ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20212E2291998-03-0404 March 1998 Rev 11 to 1000-PLN-7200,01, Gpu Nuclear Operational QAP, Consisting of Revised Pages & Pages for Which Pagination Affected ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203B2781998-02-16016 February 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Systems & Procedures ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20217C7591997-12-31031 December 1997 1997 Annual Environmental Operating Rept for Oyster Creek Nuclear Generating Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20202E8511997-10-21021 October 1997 Rev 0 to Scenario 47, Gpu Nuclear Oyster Creek Nuclear Generating Station Emergency Preparedness (Nrc/Fema Evaluated) 1997 Biennial Exercise. Pages 49 & 59 of Incoming Submittal Were Not Included ML20211M9481997-10-0303 October 1997 Supplemental Part 21 Rept Re Condition Effected Emergency Svc Water Pumps Supplied by Bw/Ip Intl Inc to Gpu Nuclear, Oyster Creek Nuclear Generation Station.No Other Nuclear Generating Stations Effected by Notification ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20211B7461997-09-24024 September 1997 Part 21 Rept Re Failure of Emergency Service Water Pump Due to Threaded Flange Attaching Column to Top Series Case Failure.Caused by Dissimilar Metals.Pumps in High Ion Svc Will Be Upgraded to 316 Stainless Steel Matl ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station 1999-09-30
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UNITED STATES 8 o NUCLEAR REGULATORY COMMISSION WASHINGTON, D. C. 20555 r,; y
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SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATING TO TORUS P0OL TEMPERATURE INDICATION AND THERMAL M:XINr. MODIFICATIONS GPU NUCLEAR CORPORATION JERSEY CENTRAL POWER AND LIGHT COMPANY OYSTER CREEK NUCLEAR GENERATING STATION DOCKET NO. 50-219
1.0 INTRODUCTION
By letter dated October 31, 1985, and supplemented by letters dated June 16, July 22 and August 4, 1986, GPU Nuclear (the licenseel proposed to cancel two modifications to provide (1) local suppression (torus) pool temperature monitoring at the electromatic relief valve quenchers, or discharge headers, in the pool and (2) thermal mixing for pool near the quenchers. The licensee considers these modifications are part of the scope of work required by the 13, 1981 Order and December Confirmatory Order, " Modification19, nf 1982.
the JanuaryThis Order is related to the Mark I 29, 1981 Order",
Containment dated' Lono Term Program January (LTP) and would require the licensee to complete these modifications before the restart from the Cycle 11 Refueling (Cycle 11R) outage. This outage commenced in April 1986 and is scheduled to end in October 1986.
2.0 BACKGROUND
The primary containment for Oyster Creek is the drywell and the torus.
This is discussed in Section 6.2 of the Oyster Creek Updated Final Safety Analysis Peport (FSAR) dated December 1984 The function of this containment is to accommodate, with a minimum of leakage, the pressures and temperatures resulting from the break of any orocess piping in the containment including reactor coolant system piping.
In its letter dateo October 31, 1985, the licensee statedreport, that the BWR
" Elimination Owner's Group (BWROG) General Electric (GE) NE00-30832 of Limit on BWR Suporession Pool Temperature on SRV (Safety Relief Valve)
Discharge with Quenchers" dated December 1984, concluded that unstable steam condensation is not a concern where quencher devices are used on SRV discharge piping. The licensee stated that quenchers have been installed The at Oyster Creek and the NEDO-30832 report is applicable to Oyster Creek.
above two modifications were for the operators to be able to monitor the local
' pool temperatures in the vicinity of the quenchers and provide additional themal mixing at the quenchers to prevent the onset of unstable steam condensation at the quenchers during SRV discharges to the torus and the resulting dynamic load
. 8610150475 861001 PDR ADOCK 05000219 P PDR i
~
The NED0-30832 and possible damaqe to the SRV discharge piping and torus.
report concludes that significant unstable steam condensation and dynamic loads will not occur with quenchers.
The staff has not started its detailed review of the NED0-3083? report.
3.0 EVALUATION The licensee reouested to cancel two mndifications for suppression pool thermal mixino based on BWROG's NED0-30832.
20, 1986, Progress Review Meeting The licensee explained in the Februarythat the two modifications are (1) adding (summary dated March 14,1986) temperature monitoring in the vicinity of the two Electromatic Relief Valves (EMRV) discharge headers in the torus and (P.) rercuting a containment spray dynamic test return line. They are part of the torus attached piping modifications in the licensee's letter dated June 29, 1981. The purpose of the modifications is the following:
(1) To give the control room operators indications that the temperature of the water in the vicinity of the EMRV headers is reaching the point where unstable condensation would occur and result in dynamic loads on the suppression pool shell during blowdown from a stuck coen EMRV. This would read out in the control room.
(2) The operators would know, by the local pool water In Germany, temperature, a stuck open EMRV that they had a stuck open EMRV.
with a straight open header resulted in unstable condensation of Tnere was steam 'n the pool and localized dynamic The loading.
work by General rocking of the torus and local damage.showed that unstable steam condensatio Electric in NE00-3083?
not a concern when quencher devices are used on EMRV discharge pipina as exists at Oyster Creek.
(3) The test line is used for testing the operability of Containment Spray, Presently it is routed into a torus /drywell vacuum breaker The rerouting was to and drains into the torus suppression pool.
allow means to cause some recirculation in the pool to aid in thermal mixing in the vicinity of the EPRV discharoe headers and lower local pool temperatures. There was no safety problem The new with the test line in its present design and location.
design would be used, in coniunction with the temperature monitoring and knowledge with the operators that they were at the temperature for the onset of unstable condensation, to (1) cause better thermal mixing in the vicinity of the headers and (?)
prevent unstable condensation conditions.
The temperature monitoring in itself would not prevent any unstable conditions and there are other safety grade and redundant indications to These indications are in th TS and identify when an EMRV is stuck open.There is clso torus bulk water temperature read out in the control room. The operators have Emergency Operatino indication in the control room.
Procedures (E0P) addressing a stuck open EMRV. This was verified and 21, 1986, in a tour of the discussed briefly with the operators on FebruaryThe location for and size of the control room by the NRC Pro,iect Manager.
rerouted test line does not indicate it would be effective in causing torus pool circulation in the vicinity of the headers.
These modifications were to prevent unstable steam condensation from EMRV discharges into the pool by (1) temperature monitoring to see onset of temperatures which will cause unstable steam condensation at the header and (2) discharges from the rerouted test line to causing As showncirculation of the in Figure T-1 in pool and reduced temperatures at the header.
NEDO-30837, a straight pipe discharge into the pool will cause large dynamic loads which resonate or peak with respect to the pool water tercerature.
The Figure 3-2 in NE00-3083F shows that for discharoes through quenchers, which is the situation at Oyster Creek, the dynamic loads are significantly reduced.
The above modifications are not part of the licensee's modification to monitor the torus bulk water temperature in accordance with NUREG-0661.
The latter modification for torus bulk water temperature is part of the staff's Long-tern Mark 1 Containment Review and Confirmatory Order dated January 19, 1982. The licensee reauested in its letter dated July 26, 1985, to defer this latter modification (Item 6 of its letter) from the Cycle 11R outace to Cycle 12P outaoe. This decision will be the sub.iect of a separate letter to the licensee on its July 26, 1985, request.
4.0
SUMMARY
Based on the above, the staff concludes that the two modifications presented above are of insufficient safety significance In to fact, warrant the having thereviewed steff has licensee ite de the modifications in the Cycle 11R outage.
Safety Evaluation (SE), " Mark I Containment long Term Program - Pool Dynamic Loads" dated January 13, 1984 and the January 19, 1982 Confirmatory Order and concludes that the modifications are not part of the Mark I Containment modifications required to be completed in the Cycle 11R outage.
The Mark I Containnent Confirmatory Order requires only plant modifications needed to comply with the Acceptance Criteria in Appendix TheA applicable of NUREG-0661, Mark I Containment long-term Program, dated July 1980.
Acceptance Criteria for these torus modifications is the local suppression pool temperature limit for safety relief valve discharge loads in SectionB 2.13.8, page A 41, of Appendix A.
to bulk suppression pool temperature is 43*F (i.e., the Monticello test withnut the residual heat removal system on page 125 of NUREG-0661) and the maximum allowed bulk temperature is 95*F (i.e., Technical Specification 3.5 A.1.7 for reactor operation as explained in the licensee's letter dated August 4, 1986), the maximum local temperature is less than the 200"F Acceptance Criteria
_4-in Appendix A, page A 41. It is also less than the 160 F criteria in the Bases of Section 3.5, Containment, of the Technical Specifications, for relief valve operation with sonic conditions at the discharge exit to avoid the regime ofThe potentially high suppression chamber loading.that these torus modificat Acceptance Criteria of NUREG-0661 and, therefore, are not part of the modifica-tions reauired by Confirmatory Order dated January 19, 1982.
In the meeting of April 10, 1986, the staff presented a Request for Additional Information (RAI) to the licensee on this sub,iect. The RAI had ouestions on (1) the applicability of the request to cancel these torus modifications to the Acceptance Criteria in NUREG-0661, Mark 1 Containment Long-Term Program, dated July 1980 and (2) the relationship between the initial suopression pool temperature for the design bases Loss-of-Coolant Accident (LOCA) analysis and the pool temperature limits in the Oyster Creek Technical Specifications (TSl. The RAI were sent to the licensee in the staff's letter of May 5, 1986.
The licensee responded to the staff's PAI in its letters dated June 16, In these responses, the licensee stated July 22 and August 4, 1986.that without thest tool modifications the local pool exceed the limits dictated by the Acceptance Criteria of NUREG-0661 during the most severe relief valve transients of interest and that the initial suppression pool temperature is consistent with the tempe core spray system pump which draws suction on the suppression pool during the LOCA. The resolution of the staff's concerns on the initial suppression cool temperature was addressed in the staff's letter to the licensee dated
5.0 CONCLUSION
Based on the above, the staff concludes that these modifications are not required as part of the Mark I Long-term Program Confirmatory Order to Therefore, these address safety relief valve discharge loads on the torus.
torus modifications are not required for the safe operation of Oyster Creek and the staff concludes The staff is,that the licensee therefore, does with in agreement not have to do the the licensee on modifications.
cancelling its comitment to install these modifications.
6.0 REFERENCES
- 1. Letter from P.R. Fiedler (GPUN) to John A. Zwolinski (NRC) with attachment, dated October 31, 1985,
- 2. Letter froa Dennis M. Crutchfield (NRC) to P.B. Fiedler (GPUN) with attachment, dated January 13, 1984.
- 3. Letter from Dennis M. Crutchfield to I. R. Finfrock, Jr. (GPUN) with attachment, dated January 19, 1982.
A. General Electric, NED0-30832, Elimination of limit on PWR Suppression Pool Temperature on SRV Discharae with Quenchers," dated December 1984.
- 5. February 20, 1986, Proaress Review Meetino on Licensina Actions, summary dated March la, 1986.
- 6. Letter from J. Zwolinski (NRC) to P.R. Fiedler (GPUN), Meetino of April 10, 1986, on Requested Cancellation of Nitrocen Purce/ Vent System, May 5, 1986.
- 7. Letter from R.F. Wilson (GPUN) to John A. Zwolinski (NRC), Combustible Gas Control and Supnression Pool Te-oerature Linits, dated June 16, 1986
- 8. Letter frem R.F. Wilson (GPUN) to John A. Zwolinski (NRC), Peouest for Additional Information Concernino Safety Relief Valve Discharges to the Suppression Pool, dated July 22, 1986.
- 9. Letter from R.i. Wilson (GPUNI to John A. Zwolinski (NRC), Core Spray NPSH Calculations, dated August 4, 1986.
Principal Contributor: J. Donohew Dated: October 1, 1986.
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