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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20133E1681997-01-0707 January 1997 Safety Evaluation Re Third 10-yr Interval ISI Plan,Rev 1 to Relief Request R11 for Plant.Proposed Alternative to ASME Requirements Authorized ML20128L1601996-10-0303 October 1996 Safety Evaluation Accepting Third 10-yr Interval Inservice Insp Plan Request for Relief R15 ML20128F4791996-10-0101 October 1996 Safety Evaluation Accepting Rev to Inservice Testing Program Re Leakage Testing of Containment Isolation Valves ML20056H2651993-08-24024 August 1993 SE Re Inservice Testing Program Requests for Relief ML20056E0911993-08-0404 August 1993 SE Re Util 930614 Response to Bulletin 93-03, Resolution of Issues Related to Reactor Vessel Water Level Instrumentation in Bwrs. Util Justification for Not Implementing Addl Short Term Actions Acceptable ML20128P4651993-02-18018 February 1993 Safety Evaluation Accepting Util Justification for Cancelling Commitment on Five Plant Control Room Human Engineering Discrepancies Re Relocation of Shift Supervisor Ofc ML20128F1361993-02-0505 February 1993 Safety Evaluation Re Leak on Core Spray in-vessel Annulus Piping.Plant Can Be Safely Operated for One Fuel Cycle W/O Repairing Observed Leak at Listed 1/4-inch Fillet Weld ML20125C3901992-12-0707 December 1992 Safety Evaluation Re Upper Reactor Bldg & Nonsafety Architectural Components Subjected to tornado-wind Loading ML20127P2251992-11-23023 November 1992 Safety Evaluation Accepting Response to SBO Rule ML20058A7621990-10-18018 October 1990 SE Accepting Util Insp & Repairs for Igscc,Per Generic Ltr 88-01 ML20246M7561989-08-30030 August 1989 Safety Evaluation Accepting Util 890624 Response to Integrated Plant Safety Assessment Section 4.11, Seismic Design Consideration, Items 4.11(1), Piping Sys & 4.11(3), Electrical Equipment ML20247A7061989-07-17017 July 1989 Safety Evaluation Supporting Generic Ltr 83-28,Item 4.5.2 Re Periodic on-line Testing of Reactor Trip Sys ML20245C1711989-06-15015 June 1989 Safety Evaluation Re Generic Ltr 83-28,Item 4.5.3 Re Reactor Trip Sys Reliability for All Domestic Operating Reactors ML20244C8501989-06-12012 June 1989 Safety Evaluation Accepting Util Response to Generic Ltr 83-28,Item 4.5.3 Re on-line Testing for Reactor Trip Sys NUREG-1000, Safety Evaluation Accepting Util 831114 & 851023 Responses to Generic Ltr 83-28,Item 2.1 (Part 1),confirming That All Applicable Components Identified as safety-related1989-04-0303 April 1989 Safety Evaluation Accepting Util 831114 & 851023 Responses to Generic Ltr 83-28,Item 2.1 (Part 1),confirming That All Applicable Components Identified as safety-related ML20235X1281989-03-0606 March 1989 Safety Evaluation Supporting Licensee Request to Extend Second 10-yr Inservice Insp & Testing Interval Until 911014 ML20205P5291988-11-0404 November 1988 Safety Evaluation Supporting Util Submittal Re Compliance W/Atws Rule 10CFR50.62 Concerning Alternate Rod Injection & Recirculation Pump Trip Sys ML20207L0831988-10-11011 October 1988 Safety Evaluation Re Systematic Evaluation of Ipsar Topic VII-1.A, Isolation of Reactor Protection Sys from Non-Safety Sys. Issue Resolved IR 05000219/19840311988-03-0404 March 1988 Safety Evaluation Concluding Util Compliance W/Generic Ltr 83-28,Items 3.1.1,3.1.2,3.2.1,3.2.2 & 4.5.1,based on Util 831114,850809,0509,1023 & 871223 Descriptions of Planned & Completed Actions & Insp Rept 50-219/84-31 on 841126-30 ML20149L6381988-02-18018 February 1988 Safety Evaluation Supporting Proposed Standby Liquid Control Sys Operation ML20236Q5311987-11-0606 November 1987 Safety Evaluation Re Safety Limit Violation on 870911.Safety Significance Considered Low Due to Adequate Core Cooling & Low Decay Heat Levels.Basis for Conclusion Elaborated in Encl Insp Rept 50-219/87-29 ML20235E0661987-09-22022 September 1987 Safety Evaluation Re Corrosion of Drywell Shell.Licensee Meets NRC Requirements as Specified in 861224 Safety Evaluation ML20207S2311987-03-13013 March 1987 Safety Evaluation Re Generic Ltr 84-09 Re Hydrogen Recombiner Capability.Licensee Should Provide Nitrogen Containment Atmosphere Dilution Sys Capable of Isolating Air from Containment Whenever Isolation Signal Occurs ML20212M3561987-03-0303 March 1987 Safety Evaluation Rejecting Util Schedule for Completion of Mark I Containment Program Re Vacuum Breaker Integrity. Required Vacuum Breaker Parts Should Be Replaced Prior to Startup from Cycle 12 Refueling Outage ML20207M2081986-12-29029 December 1986 Safety Evaluation Re Corrosion of Drywell Shell Line Break in Isolation Condenser.Operation of Plant for Cycle 12 Safe W/Drywell Steel Plates Not Fully in Conformance W/Fsar.Util Shall Provide Plans for Mitigating Problem by 870630 ML20215F3681986-12-15015 December 1986 Safety Evaluation Supporting Util Response to IE Bulletin 86-002 Re Static O-Ring Differential Pressure Switches ML20211M3911986-11-28028 November 1986 Safety Evaluation Re Deferment of NRC Required Mods from Cycle 11R Outage,Including SPDS Implementation,Isolation Condenser Makeup Pump,Intake Canal Level Instrumentation & Masonry Wall Mods.Request Acceptable ML20214A5571986-11-14014 November 1986 Safety Evaluation Re Insp & Repair of Reactor Coolant Piping Sys & Supporting Return to Operation for Next Operating Cycle ML20213G5551986-10-31031 October 1986 Safety Evaluation Supporting Util 860903 Submittal Re Insp of Core Spray Sparger Sys in Current Cycle 11 Refueling Outage.Licensee Satisfied Requirements of License Condition 2.C.(7) for Current Cycle 11 Refueling Outage NUREG-0822, Safety Evaluation Finding Integrated Plant SAR (NUREG-0822), Section 4.12 Complete W/Exception of Three Issues,Including Evaluation of Drywell for Concrete Subj to High Temps & Thermal Transients1986-10-29029 October 1986 Safety Evaluation Finding Integrated Plant SAR (NUREG-0822), Section 4.12 Complete W/Exception of Three Issues,Including Evaluation of Drywell for Concrete Subj to High Temps & Thermal Transients ML20197B8801986-10-10010 October 1986 Safety Evaluation Supporting Util 850924 Proposal Not to Replace Existing Containment Purge & Vent Isolation Valves W/New Clow Valves ML20215E7261986-10-0101 October 1986 Safety Evaluation Supporting Cancellation of Torus Pool Temp Indication & Thermal Mixing Mods ML20204F9721986-07-28028 July 1986 Corrected Page 3 to 860522 Safety Evaluation Re Integrated Plant Safety Assessment Rept,Section 4.38, Locas. Correction Concerns Licensee Maint to Repack Four MSIVs Each Refueling Outage ML20210K2481986-04-22022 April 1986 Safety Evaluation Supporting Util 831114 Response to Generic Ltr 83-28,Item 1.2, Post-Trip Review,Data & Info Capability ML20141D4261986-03-31031 March 1986 Safety Evaluation Re Generic Ltr 83-28,Items 3.1.3 & 3.2.3, Post-Maint Testing (Program Description & Procedure). Tech Specs Incorporating post-maint Testing of Reactor Protection Sys Components Should Be Proposed ML20141N0451986-02-24024 February 1986 Safety Evaluation Supporting Deferment of Feedwater Nozzle Insps Until Cycle 12R Outage Scheduled for 1988 ML20205H7981986-01-21021 January 1986 Safety Evaluation Re Venting & Purging Containment During Plant Operation.Rationale Utilized for Design & Operation of Purge/Vent Sys Acceptable ML20136A9351985-12-23023 December 1985 Safety Evaluation Accepting Licensee Response to Items 2(b) & 3 of IE Bulletin 80-11, Masonry Wall Design. Licensee 850726 Request Re Wall Mods to Be Completed During Operating Cycle 11 Not Addressed ML20137Q7621985-11-22022 November 1985 Safety Evaluation Supporting Determination That Max 150 F Drywell Temp Acceptable for Containment Safety,Drywell Steel & Concrete Structural Components & Normal Plant Operations. Tech Specs Re Limiting Factors Requested ML20128H5241985-05-28028 May 1985 Safety Evaluation Supporting Environ Qualification of Electric Equipment Important to Safety.Proposed Resolutions for Environ Qualification Deficiencies Acceptable ML20126K1221981-03-29029 March 1981 Safety Evaluation Supporting Amend 54 to License DPR-16 1998-03-23
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K4451999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Oyster Creek Nuclear Generating Station.With ML20211P6731999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Oyster Creek Nuclear Generating Station.With ML20211A7051999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Oyster Creek Nuclear Station.With ML20209G0631999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Oyster Creek Nuclear Generating Station.With ML20212H5491999-06-18018 June 1999 Non-proprietary Rev 4 to HI-981983, Licensing Rept for Storage Capacity Expansion of Oyster Creek Spent Fuel Pool ML20195E7961999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Oyster Creek Nuclear Generating Station.With ML20206N7431999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Oyster Creek Nuclear Generating Station.With ML20205P5401999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Oyster Creek Nuclear Generating Station.With ML20204C8201999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Oyster Creek Nuclear Generating Station.With ML20199E4671998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Oyster Creek Nuclear Generating Station.With ML20195E8321998-12-31031 December 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Sys & Procedures, for Period of June 1997 to Dec 1998.With ML20198D2091998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Oyster Creek Nuclear Generating Station.With ML20195J8591998-11-12012 November 1998 Rev 11 to 1000-PLN-7200.01, Gpu Nuclear Operational QA Plan ML20195C4271998-11-0606 November 1998 Safety Evaluation Supporting Proposed Ocnpp Mod to Install Core Support Plate Wedges to Structurally Replace Lateral Resistance Provided by Rim Hold Down Bolts for One Operating Cycle ML20155J3021998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Oyster Creek Nuclear Generating Station.With ML20154R4981998-10-20020 October 1998 Core Spray Sys Insp Program - 17R ML20154L3051998-10-14014 October 1998 Safety Evaluation Accepting Licensee Request to Defer Insp of 79 Welds from One Fuel Cycle at 17R Outage ML20154Q3371998-09-30030 September 1998 Rev 8 to Oyster Creek Cycle 17,COLR ML20154L5571998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Oyster Creek Nuclear Generating Station.With ML20151V6311998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Oyster Creek Nuclear Generating Station.With ML20237D5691998-08-31031 August 1998 Rev 0 to MPR-1957, Design Submittal for Oyster Creek Core Plate Wedge Modification ML20237D5711998-08-18018 August 1998 Rev 0 to SE-000222-002, Core Plate Wedge Installation ML20237B0131998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Oyster Creek Nuclear Generating Station ML20236R0511998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Oyster Creek Nuclear Generating Station ML20249B2981998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Oyster Creek Nuclear Station ML20248F3531998-05-21021 May 1998 Part 21 Rept Re Electronic Equipment Repaired or Reworked by Integrated Resources,Inc from Approx 930101-980501.Caused by 1 Capacitor in Each Unit Being Installed W/Reverse Polarity. Policy of Second Checking All Capacitors Is Being Adopted ML20247F1891998-05-0505 May 1998 Risk Evaluation of Post-LOCA Containment Overpressure Request ML20247G0581998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Oyster Creek Nuclear Generating Station ML20216K0341998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Oyster Creek Nuclear Generating Station ML20151Y4651998-03-31031 March 1998 Non-proprietary Version of Rev 1 to GENE-E21-00143, ECCS Suction Strainer Hydraulic Sizing Rept ML20217A4631998-03-23023 March 1998 Safety Evaluation Accepting Use of Three Heats/Lots of Hot Rolled XM-19 Matl in Core Shroud Repair Assemblies Re Licenses DPR-16 & DPR-59,respectively ML20212E2291998-03-0404 March 1998 Rev 11 to 1000-PLN-7200,01, Gpu Nuclear Operational QAP, Consisting of Revised Pages & Pages for Which Pagination Affected ML20216J0841998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Oyster Creek Nuclear Generating Station ML20203B2781998-02-16016 February 1998 10CFR50.59(b) Rept of Changes to Oyster Creek Systems & Procedures ML20203A3801998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Oyster Creek Nuclear Generation Station ML20198P1791997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Oyster Creek Nuclear Station ML20217C7591997-12-31031 December 1997 1997 Annual Environmental Operating Rept for Oyster Creek Nuclear Generating Station ML20197E9131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Oyster Creek Nuclear Station ML20199E4561997-11-13013 November 1997 Safety Evaluation Accepting Ampacity Derating Analysis in Response to NRC RAI Re GL-92-08, Thermo-Lag 330-1 Fire Barriers, for Plant ML20199D4381997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Oyster Creek Nuclear Station ML20202E8511997-10-21021 October 1997 Rev 0 to Scenario 47, Gpu Nuclear Oyster Creek Nuclear Generating Station Emergency Preparedness (Nrc/Fema Evaluated) 1997 Biennial Exercise. Pages 49 & 59 of Incoming Submittal Were Not Included ML20211M9481997-10-0303 October 1997 Supplemental Part 21 Rept Re Condition Effected Emergency Svc Water Pumps Supplied by Bw/Ip Intl Inc to Gpu Nuclear, Oyster Creek Nuclear Generation Station.No Other Nuclear Generating Stations Effected by Notification ML20198J7361997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Oyster Creek Nuclear Generating Station ML20211B7461997-09-24024 September 1997 Part 21 Rept Re Failure of Emergency Service Water Pump Due to Threaded Flange Attaching Column to Top Series Case Failure.Caused by Dissimilar Metals.Pumps in High Ion Svc Will Be Upgraded to 316 Stainless Steel Matl ML20210V0181997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Oyster Creek Nuclear Generating Station ML20210L2961997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Oyster Creek Nuclear Station ML20149F9961997-07-18018 July 1997 Safety Evaluation Re Gpu Nuclear Operational Quality Assurance Plan,Rev 10 for Three Mile Island Nuclear Generating Station,Unit 1 & Oyster Creek Nuclear Generating Station ML20196H0111997-07-11011 July 1997 Special Rept 97-001:on 970620,removed High Range Radioactive Noble Gas Effluent Monitor (Stack Ragems) from Service to Allow Secondary Calibr IAW Master Surveillance Schedule. Completed Calibr on 970628 & Returned Stack Ragems to Svc ML20210L3081997-06-30030 June 1997 Corrected Page to MOR for June 1997 for Oyster Creek Nuclear Generating Station ML20141H2051997-06-30030 June 1997 Monthly Operating Rept for June 1997 for Oyster Creek Nuclear Station 1999-09-30
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, g a WASHINGTON, D. C 20565 SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATIM RElf, TING TO A LEAK ON THE CQM SPRAY IN-VESSEL AtMILUS PIPING GPU NUCLEAR CORPORATION OYSfER CREEK NUCLEAR GENERATING STATION DOCKET NO. 50-212
1.0 INTRODUCTION
During the in-service inspection of the core spray spargers and piping in the current Oyster Creek refueling outage (14R), a leak was discovered at the inlet downcomer piping (6 inches schedule 40 st inless steel) in the core saray system I (lower sparger). The subject d ncomer alping was located in tie annulus between the vessel wall and core shroud. lie leak was found on a 1/4-inch fillet weld (L-3A) of a downcomer piping coupling. The accessibility to the area of the leak was very limited because the leak location was very_'I close to the vessel wall with a clearance of only about three inches. In examining the leak the licensee (GPUN) employed a very small camera (1 inch in diameter), which was mounted on a special fixture, and positioned the camera directly above the weld with additional lighting provided by General Electric's " Firefly", a remotely operated vehicle (R.0.V.). The-licensee reported that the leak was coming from a 1/8-inch round hole in the fillet weld. No other cracking indications were observed around the hole or at other areas of the fillet weld, The licensee also examined the fillet weld (U-3A) at the same relative location in the core spray system 11 (upper sparger).
There was no leak at weld U-3A; however, there were two linear indications.
The licen.ee concluded that these indications were most likely to be construction defects such as splits or tears between weld passes.
There are two independent core spray sparger assemblies in the Oyster Creek reactor vessel. Each sparger contains 56 nozzles and is fed from an independent penetration through the reactor vessel. The piping from the vessel penetration to the shroud penetration is known as the annulus piping.
A couplingewas c used in the installation of the annulus pi)ing with a 1/4-inch fillet weldfis the final fit up weld to be performed in tie field. The leak was observedrin this field fit up fillet weld (L-3A) of core spray system 1.
Early in 1978 a through wall crack was found in System II (upper) sparger, _ and in 1980, additional ;urface indications were observed in System I and 11 sparger:. The leak observed in 1978 was believed to be resulting frc.a intergranular stress corrosion cracking (IGSCC). A total of 10 mechanical clamps were applied at those locations to ensure structural integrity of the spargers. Air tests and/or visual inspections of core spray spargers and piping were performed during each refueling outage. No additional leaks or indications were found until the current refueling outage (14R).
93.)2110263 930205 PDR ADOCK 05000219 p PDR -
- 2. DISCUSS 10Mi i
The licensee has determined that the most probable cause for the observed leak in the subject fillet weld would be the opening up of weld defects such as slag and/or lack of fusion after approximately 20 years of service with normal cyclic stresses. This was supported by the following observations: !
(1) The surface appearance of the subject fillet weld was very rough especially in the area with limited accessibility, indicating poor quality of the weld, which would most likely contain some weld defects.
(2) The observed air bubbling rate was high which indicated that the crack path leading to the leak was not tight. If the cracking was caused by fatigue or intergranular stress corrosion cracking (IGSCC), the bubbling rate should be much less than observed.
(3) The calculated cyclic service loads were small and the cracking by fatigue would not be likely to occur. Even if it did occur, its giowth would not be significant.
(4) Intergranular stress corrosion cracking (IGSCC) was not a plausible mechanism because the observed cracking occurred at the weld metalt and not in the areas of heat affected zones.
However, the staff believes that IGSCC could be a potential dominating mechanism for continued crack growth in the subject fillet weld in view of a through wall IGSCC crack was reported in the core spray sparger piping in 1978. The licensee's 1GSCC crack growth calculations showed that the growth of the crack in the circumferential direction would be approximately 3 inche, in a period of 2 years. This calculation assumed the presence of a residual stresses of 20 ksi and an initial 1/2-inch through wall crack. The licensee estimated the leak rate for a 3-inch through wall crack would be less than 1 gpm, which is much less than the margins that are available in the core spray sparger systems.
The licensee reported that because of the weld size and diameter, a 3/16-inch fillet weld at the lower end of the subject coupling joint would be the '
limiting struct. ural weld. Therefore, the subject leaking 1/4-inch fillet weld could loose approximately 31% of its circumference (about 7 inches) and still maintain th9;r'eqbired axial loading capacity of the coupling. The licensee performed finite < element stress analyses of the subject annulus piping un_ der the conditi'ons.of, n'ormal operation and core spray injection. The combined load consisted of deadweight of the pipe including the water, drag loads due to recirculation flow in the annulus, thermal loads, pressure load during core spray injection and an assumed seismic load of 59 acting simultaneously in the three orthogonal directions. The largest shear stress was calculated to be 5.8 ksi which is much lower than the ASME Code allowable of 19 ksi at 550*F for the subject fillet weld.
With an assumption of a complete failure of the subject 1/4-inch fillet weld, the licensee performed an estimation of the relative axial displacement at the
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3 coupling jointJresulting from the blowdown loads due to a LOCA at the recirculation pising system. The calculated displacement was 0.5 inch which is well within tie designed nominal engagement of 1 inch for the coupling.
Based on the-installation drawing and measurements from the field video tapes, the licensee reported that the actual engagement was estimated to be about 0.9-inch. This evaluation concluded that the inlet downcomer piping would not be separated under the postulated LOCA condition even if the subject fillet weld was completely failed.
The licensee performed hydraulic analyses to determine the performance of the core spray system. For the bounding case of assuming a complete failure of the 1/4-inch fillet weld with a 0.015-inch gap around the pipe, the calculated flow loss through the assumed defect is small (46 gpm) in comparison to the available margin of about 500 gpm for the core spray System 1. Therefore, the flow loss due to a complete failure of the subject fillet weld would not affect the intended performance of the core spray system.
During a site visit on January 27, 1993, the staff reviewed video tapes regarding the visual examinations performed at this and previous outages to confirm the licensee's reported observations. The staff also requested some additional.information regarding their evaluation submitted on January 19, '
1993. The additional information verbally provided by the licensee was i summarized below: ;-
(1) Among all the design basis loading conditions considered, the loading condition of core spray injection and seismic would provide the limiting combined load on the annulus piping.
(2) The design basis seismic load is only 2.09 Based on this seismic load, the required length of the 1/4-inch fillet weld for the limiting load condition (core spray injection and seismic) is 9.5 inches.
(3) With an assumption of a complete f ailure of the subject fillet weld, the axial displacement of the coupling due to a combined load of recirculation piping LOCA and seismic (2.0g) was estimated to be 0.52-inch, which is within the nominal 1-inch engagement of the coupling.
(4) The;11'censee brief.ly described how the reported actual engagement (0'.Sijntli the coupling was derived. It was calculated by subtdctfh)(j of4the' length (3.6 inches) of the upper coupling sleeve, which was mqsured on'the video tape, from the dimension (4.5 inches) specipedeoptheGeneralElectric'sinstallationdra91ng.
The licensee should submit to NRC the above adoittonal information in more detail no later than 60 days after plant restart.
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. 3,0 QNCLUSIS ^
y Based on our reYiew of the licensee's submittals and the additional information as well as the viewing of the video tapes, the staff concludes that Oyster Creek can be safely operated for at least one fuel cycle without repairing the observed leak at the subject 1/4-inch fillet weld. The intended function of the core spray system would be maintained under the worst design basis condition even if the subject weld is assumed to be completely failed.
The licensee should perform detailed visual examinations and air tests of the core spray spargers and annulus piping during the next refueling _ outage to ensure there is no further degradation of the piping system. When nec9ssary, appropriate surface or volumetric examinations should also be performed to -
investigate the extent of alping degradation. A long-term mitigation program of the core spray system siould be consicered if further degradation of the core spray system is observed.
Principal Contributor: W. Koo Dated: February 5, 1993 e 1,
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