ML20214P206

From kanterella
Jump to navigation Jump to search
SER Supporting 860917 & 19 Requests for Amend to License NPF-40,changing Tech Spec Table 3.6.4-1 to Allow Inoperability of Inboard Isolation Valve MOVFO76 Through 861004
ML20214P206
Person / Time
Site: River Bend 
Issue date: 09/19/1986
From:
Office of Nuclear Reactor Regulation
To:
Shared Package
ML20214P025 List:
References
FOIA-86-687 NUDOCS 8612040113
Download: ML20214P206 (13)


Text

.

s*

w

  1. og UNITED STATES f*

NUCLEAR REGULATORY COMMISSION n

g

,I wasHINcTow,0. c. 20sss

...../

SAFETY EVALUATION REPORT BY THE OFFICE OF NUCLEAR REACTOR REGULATION AMENDING THE CONTAINMENT ISOLATION VALVE TABLE TECHNICAL SPECIFICATION RIVER BEND STATION, UNIT 1 DOCKET NO. 50-458

1.0 INTRODUCTION

In River Bend Technical Specification 3.6.4, Table 3.6.4-1. Item a.1 identifies the reactor core isolation cooling (RCIC) steam supply valve IE51*MOVF076 (MOVF076) as a primary containment automatic isolation valve. By letters dated September 17, 1986 and September 19, 1986, the Gulf States Utilities Company (GSU) requests a one-time change to the Table by adding a footnote, applicable to isolation valve MOVF076, that would exempt the operability requirements for this valve from September 22, 1986 through October 4, 1986.

While the reactor was at 100% power on September 8,1986 the MOVF076 valve was undergoing a functional test of the annunciator when the MOV76 breaker tripped due to a ground in the system. A subsequent attemp't to stroke the valve indicated the valve to be fully open. As required by the River Bend Technical Specification 3.6.4 Action Statements, the outboard isolation valve IE51*M0VF064(MOVF064)wasclosed.

Consequently, the RCIC system was rendered inoperable and by Specification 3.7.3, the plant was placed in a 14-day Action Statement tha,t requires the plant to initiate a shutdown on September 22, 1986.

The GSU_ proposed technical specification revision will exempt valve MOVF076 from~ technical specification operability requirements, thereby allowing

=

isolation valve F064 to be opened and returning the RCIC system to operable 20 3 861125 GUSTE86-687 PDR

1 s',a tus. This request would be a one-time modification to the Technical Specification effective through October 4, 1986, at which time GSU has scheduled a shutdown and will repair the inoperable isolation valve (MOVF076).

2.0 EVALUATION The RCIC steam turbine supply line is an 8-inch line that branches off the main steamline "A".

Inside the River Bend drywell the 8-inch line has a inboard isolation valve IE51*MOVF063 (MOVF063)and circumventing this valve is a 3/4 inch bypass line consisting of a manual isolation valve and the motor-operated isolation valve M0VF076. The 3/4-inch bypass line is parallel to the 8-inch inboard isolation valve; its functions during start-up are to equalize i,.he pressure around MOV63 and to warmup the RCIC steamline. The consnon outboard isolation valve (8-inch) is MOVF064.

During power operation, the normal RCIC turbine steam supply line valve lineup is MOVF076 closed and inboard and outboard isolation vlaves MOVF063 and MOVF064 open.

The RCIC is a high pressure system primarily designed to maintain 1

sufficient water in the reactor pressure vessel to cool the core and to maintain the reacter in the standby condition in the event.the vessel becomes l

1solated and feedwater is not available. During a LOCA, RCIC (which augments other core injection systems) initiates on low vessel water level and deliverers rated flow to the vessel through a connection in the vessel head.

Even though RCIC is not a part of the ECCS network, the RCIC system is designated as a safety-related system. During limiting conditions of operation (LCO) (i.e.. when HPCS is inoperable), power operation is allowed to continue for a period-of time provided RCIC is operable.

1

. Valve MOVF076 is only used for RCIC turbine steam supply line wann-up before start-up of the system and the ability to close the valve is not required for the RCIC system to perform its intended design function.

Therefore, in the open position MOVF076 will not affect system operation.

The RCIC steam line isolation valves MOVF063 and MOVF064 are normally kept open and should be kept open in order to keep the steam inlet lines warmed-up and to minimize the potential for water hamer upon system startup.

Accordingly, the RCIC steam supply line does not receive the standard containment isolation signals (e.g., high drywell pressure and low reactor water level). The isolation. signals that serve the inboard and outboard isolation valve monitor conditions to reveal a break in the RCIC syrtem.

The applicant in a letter dated September 19, 1986, also submitted a radiation dose assessment.

In the event of a pipe break downstream of the outboard isolation valve (MOVF064), the leakage will be detected by the leakage detection systems. The leakage detection systems are the area temperature l

monitoring system and the RCIC steam line flow monitoring system. Either leakage detection system will provide an isolation signal to MOVF063 and MOVF064. Once a signal is received, a total of 20 seconds (a 10 second delay for diesel start plus a 10 second delay for valve closure) delay is assumed for closing of the valve. Full flow is assumed through the 8-inch line for the first 20 seconds. At the end of 20 seconds, the inboard isolation valve F063 is assumed to close, but the outboard isolation valve fails to close (single failure). With the. inoperable valve F076 in the failed open position M

and the outboard F064 assumed to be failed open, there will be an 1solated 3

1eakage path'(3/4-inch line) from the reactor to the auxiliary building.

The e

. maximum expected flow through the bypass (F076) is 30 GPM. Feedwater flow could provide make-up for this fluid loss.

If feedwater is not available, the High Pressure Core Spray (HPCS) system could be used to provide cooling water to the vessel, thereby preventing uncovering of the reactor fuel. Fuel failure would, therefore, be precluded. The only radioactivity available for release from the break is that which is present in the reactor coolant prior to the break. The bypass flow is assumed to be constant for the first 30 minutes of the transie-; and then is ramped down to zero in the next 3.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> as the reactor is brought down to a cold shutdown condition. The total mass released from the RCIC steam lin'e break is estimated to be about 50,000 lbs compared with the 140,000 lbs estimated by the staff for Main Steam Line Break' Accident Analysis.

In section 15._6.4 of River Bend SER, we concluded that the doses for Main Steam Line Break are only a small fraction of 10 CFR Part 100 Guideline values. Since the RCIC piping break with unisolated bypass flow through the F076 valve is bounded by the Main Steam Line Break analysis, the expected doses for the RCIC break also will be a small fraction of 10 CFP ""t i

100 guidelines values, and hence within our acceptance criteria.

The staff concurs with GSU's assessment that there is no significant reduction 'in the margin of safety relating to the temporary period (i.e., about 12 days) of having the MOVF076 valve in an inoperable condition. The alternative approach would require reactor shutdown in order to enter th6 drywell and subject plant personnel to exposures from the harsh drywell environment. Therefore, such an action would induce unwarranted and inherent challenges to various plant systems and to the affected plant personnel.

3.0 CONCLUSION

The staff finds the incremental risk of allowing the 3/4-inch inboard isolation valve to be inoperable through October 4, 1986 to be minimal.

Therefore, the staff approves GSU's proposed amendment to the River Bend Technical Specification as indicated in the licensee's September 17, 1986 and September 19, 1986 letters. Specifically, a footnote will be added to the Technical. Specification Table 3.6.4-1 not requiring MOVF076 to be operable through October 4, 1986.

s I

O e

m 9

FOB / DBL SALP INPUT PLANT: River Bend Station, Unit 1 LICENSEE: Gulf States Utilities Company DOCKET NO:

50-458 LICENSEE STATUS: OR SER

SUBJECT:

REVISED TECHNICAL SPECIFICATION FOR CONTAINMENT ISOLATION VALVE TABLE PERFORMANCE PARAMETERS:

(1f) Management Involvement in Assuring Quality

) Approach to Resolution of Technical of Issue From a Safety Standpoint

(, )) Staffing (Including Management)

Response to NRC Initiatives

(

q ) Reporting and Analysis of Reportable Events I

Training and Qualification Effectiveness L, J)Any Other SALP Functional Area PERFORMANCE NARRATIVE DESCRIPTION OF CATEGORY /

, PARAMETER APPLICANT / LICENSEE'S PERFORMANCE RATING 1

The quality of submittals was 3

adequate 2

The understanding of the issue was 3

adequate 3

Responses were timely 3

4 No basis for assessment N/A 5

No basis for assessment N/A 6&7 No basis for assessment N/A OVERALL APPLICANT / LICENSEE PERFORMANCE RATING 3 e

M l

{

MEM0h DUM FOR: Sholly Coordinator DISTRIBitTT6 et File FROM:

Walter R. Butler Director PDf4 Reading BWR Project Directorate No. 4 M0'Brien ision of BWR Licensing SStern OGC w/ incoming

SUBJECT:

REQUES R PUBLIC IN BI-WEEKLY FR NOTICE - NOTICE OF CONSIDERAT SSUANCE OF AMENDMENT TO FACILITY OPERATING D NO SIGNIFICANT HAZARDS CONSIDERATION LICENSE AN n

DETER ION AND OP RTUNITY FOR HEARING Gulf States Utilitie's Company, Docket No. 50-458, River Bend Station, Unit 1 West Feliciana Parish, Louisiana Se 7t I'l Qi I'l Date of amendment request:

%;;;-t ' and %,;;t 15,1986.

Description of amendment request: Amend Attech.T.;.t -III er,d Technical Speci-fication S v 0.S. 4 of the River Bend Station Operating License. NPT-47 to hb.

i r_ _ W... _....i... c,A. M. v_ i, i.n eN " D, S P..,. ___ N _k _ b M._. M

,I _

M R

ivi einervenu

- ndatinn of kev % ex\\ve..s..... -

u us

' ' q I of TDI Dietalundue \\E SW LkH.Q: - Od3%u % IMi%

c%udRe.

t ix I ision 2 o tS wi' 1 imnlemon+

W % &. M 68A4 MM RtIc. tr 4Topute4.

Gruup uesign Kevtew ana quainy nevaiiuoi.aun gunyn) nevur i

^

0e r.s.. i.v.

nne.

  • hut 'tted Mr.y-1, 1^00). RRC 3 6.if... ;.. o f Giu LR R u uvuuiuen 6eu in

- L i,i ;..;c.; 3 ef the R;.cr Benu 32R.

I d

Basis for proposed no significant hazards consideration determination: The l

Comission has provided standards for determining whether a significant hazards consideration exists as stated in 10 CFR 50.92. A proposed amendment 1

to an operating license for a facility involves no significhnt hazards considerations if operation of the facility in accordance with a proposed amendment would not: (1) Involve a significant increase in the probability or consequences of an accident previously evaluated; or (2) Create the possibility of a new or different kind of accident from any accident previously evaluated; or (3) Involve a significant reduction in a margin of safety.

I.L.

e i

2-The licensee has provided an analysis of sig f aza s con iderations in

apWden n e#1G its "usud 4,1956 requestfo&A

"'"'J E#

The licensee has[9 % M lief' i

r a license amendm t.

concluded, wi.th appropriate bases, that the proposed amendment meets the three standards in 10 CFR 50.92 and, therefore, involves no significant hazards considerations.

The Commission has also provided guidance concerning the application of these standards by providing examples of amendments considered likely, and not likely, to involve a significant hazards consideration. These were published in the Federal Register on March 6,1986(51FR7744). The NRC staff has made a preliminary review of the licensee's submittal. A discussion of these examples as they relate to the proposed amendment follows.

One of the examples of actions involving no si nificant hazards considera ion u-M A R h a n tM M 60. %

yi) is a change thet ccastitutes 4r. Litienel limitatie., restriction -ee r

h hetec$ais 442bu.t ti c

m J2, to w weud-a y M udigth cl1 el

=ar: :tringent surveilience requirement. The proposed amVn nt does et involve a nificant increase in the probability or c equence an accident previo ly evaluated; or create the possi lity of a ew or rent kind of accident fr any accident previously valuated; or involv a significant reduction i a margin of saf cause the dherenc to the TDI Diesel Generator Owners Gro DRQR ort requires i pectio that ar more thorough than the manufactur econsnendations those equired y the current Technical Sp ica ons an egulato Guide.108.

his adherence to the DRQR rt req res additional ins ctions which re designed to incre the. reliability of the Division I and Divi on II TDI diesel 9enerators.

g 0""'

" m a -gem 4 @c e

L w o a 4 4 t ru A t k n

  • 0 " %

1 The proposed amendment to the Technical Specificaticns would not involve a

significant increase in the probability or consequences of an accident previously evaluated because the penetration is limited to a 3/potentially unisolated 4" line discharging to a closed system that returns to the containmentf vL gesuming a break in the RCIC steam line between valves HOV64 and

.MOV45, 10CFR Part 100 limits will not be exceeded.

This conclusion is fuel failure is not expected because the make-up waterbased up fluid loss can from the Pressure Core Spray system.be provided by the Feedwater system or the High The only activity available for release from the break is that which is coolant and steam lines prior to the break.present in the reactor break LOCA Moreover, the large failure assume (Double-Ended Recirculation Line Break) with fuel s a closed loop in the RCIC system and filtration by the Standby Gas Treatment System for any valve packing leaks and meets the currant accident analysis and 10CFR Part 100 limits.

6 Additionall eq'q,sted b- ~y6uY J~ ta{WoAignificanVNatardsf -~was TopKDm y

mation Lc6'ncer ng WI 7

Q,of-dhe EvhluatichT ANtdA4 M The proposed cMnge does not create the possibility of a new or different kind of accident from any accident previously evaluated because line breaks such as may be postulated for the RCIC system have bean, considered in the analysis and design basis with many of the previous i

analysis bounding all the short-term consequences of the plant for this event.

There may,however, be longer term environmental effects which would only impact the overall lifespan of the equipment and would be evaluated if such an event should occur.

This change introduces no new mode of operation and no change in the plant design is being made.

~

r

~

O a >w{

o om A h am ch M u

.o nn w.

ON~d

/

{

J pb No k h-et.R.

T d

Mp M*

a m_ dL cm.

.-!~,.

rp c

q u ur.

. )y

[.

]

+

4 Y

g'..

)

[

l)

, '1

..,u g,

/

C(

t n*.q

, J. E

.p l

.,' E

[

t q.

.+,v___..

c.,~.

P

~."

Y,

.l

f-g

....... m.

m e.. -

i t

~~vm &1k-m s & p.

o b t h

.., ~ t s a,

i a m * ~ u e x % ryeo m

A 4 Ltc urLA wtAo A

& %Runik.

w,Ldun s. y a

% auks wu a a JALu at at afa ow S M AB,M%, d $fu.tia ma S n,' IESI*thoY Fcm.

\\

f

~

D f

-a um u

c _-, p

%" hw LU vah<

Q -O Mo V '7 0 Ja a

d PAIt Ah5k14.

.a t g u) d da enhe to e R.t_Te wu M Lb An.isue situu0 Etz y e k q &

e. v 4 x

g w L w M tu,a & L< ~ u M d b w&. we a

e a p % sex a

~

in-s uco q

A l

.?.

~

'(A tuuu ha-g10 L v%-4_

k

& van d t0at tk W s d nn dua wao k e, ww- -- -

tiwwd

(

0 ~ cy ~J-3 f O4x }g 3

R wg u a, +y W G t ATuid &

a n'a a.

-a A

o>d MA.

  • g

&pAwSa ip%, 'A 3

b uhd,1(2 fxwiu a.daupo% h 44 a ins W &

% Qtu&o mau.

w, i dc, 4 Auum W4*

u d w d At LA J meuEL,.

t 1

t daA>d opLhp

-E L~

v ua s

~ m L, en La,

& % m2e >&

cevisM J cput/gca e%

cc 9 LD L W

~

ama t $2ea o@$ Auia cJJko cuiLa'ab o

TA chj' xA Low y 7

4-m **

m m

I,

.. ?.

o

/

W.

CW 4M u

c(42q d M cj.,dt j

cu d A u g 7dt u=%t A2 JJr/m n sou %d u d a.

Exda;w J

/m U

Al%W AllM &

ost

_)j(

c)&

ge a,Qtsug s, & iwa m

.L 9

k bb 0

)

m-%

Le wealf h w geaq w Q yge & c g

w f.= = % % >

9 ogg n aa.

rl.

/

y 7 q t6

~

l i

~

4 i

.t 4

l I

ouzr erarse verzirzas couraws-aw aeenoerano=

poet omes som see er.mancema.miom 4=eA co06eos e8600es Seteset September 19, 1986 RBC-24405 File No. G9.5 t

Mr. Barold R. Denton, Director Office of Nuclear Reactor Rapistion U.S. Nuclear Regulatory Commission Washington, D.C. 20555 Dear Mr. Denton River Bend Station - Unit 1 Docket No. 50-458 As requested by 'your

Staff, Gulf States Utilities (G80) is providing below supplemental information to our application for amendment to the River Bend Station Unit 1

Technical specifications, Appendix A to facility Operating License NPF-47 detailed in a

letter (J.

C.

Doddens to R. R. Denton) dated September 17, 1986 (RBG-24405).

The River Bend Station Operations staff performed a

functional test on the 1E51*MOVF076 September.8, 1986 when the MOV76 breakerannunciator at approximately 1415 on tripped.

The initial investigation determined a

ground in the system.

During the following two

days, Electrical Maintenance investigated the grounding source and indicated that the motor was apparently wet.

An attempt was made to dry-out the valve motor.

The operator then attempted to stroke the valve and indications revealed that the valve was fully opened.

An attempt was made to.reclose the valve back to its normal position at which time the McV76 breaker tripped.

During the next few days, several other attempts were made to reclose Mov76 and to establish valve operability.

On September 15, 1986 Electrical Maintenance indicated that it had exhausted all means of fixing 'the grounding problem and CSU proceded to investigata a request for Technical Specification i

change.

Between September 15 and September 17 G8U confirmed, by calculations and

analysis, the safety significance of the proposed change.

A hand-drawn schematic that features'the main com ents which are discussed in this request is proivded as Atta nt, 8 for your use.

The Remotor Core Isolation Cooling (RCIC) s small instrument lines ( 3/4") and drain lines (ystem has several 1")

contained in rooms that have been analysed for large line* breaks.

We have

..,,__,..,__,-_,m_-...__.-

w,

.v

_m._n,g,-,-..y

I examined the RCIC line and have identified seven 3/4" lines each with instrument normally opened valve located in the RCIC room.normally opened valves 8 team Tunnel and RCIC cubicle areas.these lines include a Hig The analyses for n

The RCIC line is common to the Residual Heat Removal in the main steam tunnel.

(RNR) line steam condensing mode of operation which is not presently used River Bend Station.

the RER Equipment Removal cubicle.This RHR line is isolated by two valves in with normally opened valves located in the RHR room.The lines each Break analysis have been performed in this area including a

Moderate and High Energy Line Crack analysis.

Line Breaks.line between MOV64 and Mov45 has been analysed The remaining R for High Energy Assuming a break in the RCIC steam line between valves MOV64 a

MOV45, 10CFR Part,100 limits will not be exceeded.

This conclusion is Fuel failure is not expected because the make-up water ~ base fluid loss can from the Pressure Core Spray system.be provided by the Feedwater System or the High The only release from the break is that which isactivity available for coolant and steam lines prior to the break.present in the reactor break Moreover, the large LOCA Double-Ended Recirculation Line Break) with fuel failure assume (s a closed loop in the RCIC system by the Standby Gas Treatment System for any valve packing leaks and filtration Ond meets the current accident analysis and 10CFR Part 100 limits.

Additionally requested by your Staff mation was supplemental infor-1 concerning Item 2

of the

'No Significant Hazards Evaluation":

The proposed change does not create the possibility of a new or different kind of accident from any accident previously postulated for the RCIC system have baanevaluated because lin the considered in analysis h unding all the short-term consequences of t plant for this event.

There may,however, be longer term environmental effects which would only impact the if such an event should occur.overall lifespan of the equipment and i

This change introduces no new mode of operation design is being made.

and no change in the plant W

--,,,,-,,-,-n-,n---n-----

,--,-n-

--e

Therefore, there is no new or different kind of accident from any accident previously evaluated.

Sincero y,

.:= -

U. C. Deddene Vice President River Band Nuclear Group JCD/JEP/je Attachments e

e e

=

O

~

ATTACEMENT 1 Assumptions For RCIC Steam Line Break 1

Leakage will be picked up by high temperature leak detection based on 125 gym leakage which provides an isolation signal to F063 and F064.

Also high steam flow indication will isolate the RCIC System.

2.

Once a signal is received to close the isolation valves, a 10 second delay for diesels to start plus a 10 second delay for valve closure will be assumed.

total of 20 seconde delay is used.

A 3

Assume full flow through the 8" line for 20 seconds.

At the end of 20 seconds the isolation valve F063 is assumed'to glose and the F064 valve fails to close (single Failure).

l second closure time for the valve will actuallThis is conse t

flow from full flow to the 30 gpm bypass flow.y ramp the l

4.

Moody critical flow of 2100 lb/sec-ft 2 is used for steam flow at 1000 psia will be used to calculate the flow rates.

5 The bypass flow will be held constant (30 gpm) for the first 30 minutes of the transient and then will be ramp to 0.0 in the next 3.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> at which time the reactor will be in cold shutdown.

Calculations Mass released for

~

first 20 seconds of the transient 13,400 lba

=

Mass released for

.I next 30 minutes of the transient 7,787 lba

=

Mass released for next 3.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> of the transient 27,254 1ha

=

======,

T4tal mass from the RCIC Break 48,441 1ha

From River integrated mass leaving the RPV thBend Station (RBS) FSA 80 562 lb is, based on c.

on 15.6.4.4 The radiological analysis for through the steam line, brea onservative assumptions considered t to the NRC is for e steam line break Basis Accident" for RBS as id meeting 10CFR100 guidelines and is th o be Therefore, acceptable as can be entified in FSAR case piping break with unisolated bseen from the cacula Se e " Design valve is bounded b<

15.6.4 margin.

ypass flow As previous'r the Main Steam Line break by a co through the F076 st the exclusion area from the D i.y stated, the current FSAR thy Table 15.6-7).

nsiderable conservative Comparing the massesesign Basis Accident is 29 R roid dose for corrolation Ram for the RCI given for to the dose would be approximately 17 allowable dose.C event which is each

event, a

below the 30 Rem regulatory i

a k

0 N

a e

i W

m.-

- - - - - - " ~ ~

\\

~

p gogTAWMeg lM8ml N ?C. A

  • ... 7 y h

[El.

[::~*l % [ w-ow 1

em T

Vss nov naze

\\

gggg.Wt I E" RME D 8G vessst.

Auxsts g y

  1. 0 DRYWEu.

4 E

cumm B

/i FIGURE i RCIQ STEAM PlPING SCHEMATIC

,7

.,tp i

f i

o s

/

~

EMERGENCY LICENSE AUTHORIZATION

_ CHECK LIST q

e

. I.

Complete submittal (Section III, Item I)

[

2.

Prepare and sign handwritten SER. EA final NSHC and

[

Technical Specifications (Section III, Items)

.ORAB-cr technicah branch input X

a.

b.

Resident or regi'onal personnel input

{

7 4/

.li c am c o T) effort" b obtain state coments (Section III Item 6)-

N 3.

  • Bes's

.Wb MWs Muermo P (EP b m D u W.d m ae @a.,t%pt ( b eco q d3 j

Uet 9

4.

. Assistant Director concurrence (Section III, Item 7)

N g

pg, 5.

Assistent Director oral authorization to licensee k

(Section III. Item 8)-

6.

Telecopy Technical

  • Specifications (Section III. Item 8)

/

/a/fc,

~

7.

Forward final two day'. license ' amendment with post notice and g Y#

FNSHC (Section III. Item'9) (Prepare OLOp 220. Attachment 4)

,c Project Mana r

/

Branch Chief ORAB Branch Chief / Tech. Review' Branch Chief

/. Tech. Review Eranch AD*

.y*

f q

To the exter,t practicabl,e.

- --