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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20249A4121998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7501998-04-30030 April 1998 Rev 2 to Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit ML20247F6721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Davis-Bess Nuclear Power Station,Unit 1 ML20249A4141998-04-30030 April 1998 Revised Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216B4041998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216C5131998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20202D3721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20198K7931997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20203A3931997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Davis-Besse Nuclear Power Plant,Unit 1 ML20198S5371997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Davis-Besse Nuclear Power Station ML20217H7701997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20216H3261997-08-31031 August 1997 Monthly Operating Rept for August 1997 for DBNPS ML20217K0241997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Davis Besse Nuclear Power Station,Unit 1 ML20140H0441997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Davis-Besse Nuclear Power Station Unit 1 ML20141B9521997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Davis-Beese Nuclear Power Station Unit 1 ML20137T5271997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20136G7221997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Davis-Besse Nuclear Station Unit 1 ML20134L9831997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Dbnps,Unit 1. W/Undated Ltr ML20133G0161996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20149M4071996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Davis-Besse Nuclear Power Station Unit 1 ML20134P9821996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20128Q0611996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Davis-Besse NPP, Unit 1 ML20117D5341996-07-31031 July 1996 Monthly Operating Rept for July 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20117D5411996-06-30030 June 1996 Revised MOR for June 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20116E0161996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Davis-Besse Nuclear Station Unit 1 ML20113B9111996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Davis-Beese Nuclear Power Station Unit 1 ML20117H7231996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Davis-Besse Unit 1 ML20112E6061996-03-31031 March 1996 Monthly Operating Rept for Mar 1996 for David-Besse Nuclear Power Station,Unit 1 ML20101G5251996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for DBNPS Unit 1 ML20149K7711996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for Davis-Besse Nuclear Power Station.W/Undated Ltr ML20096C7971995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20095H3761995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20094L1041995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20093J2341995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for Davis-Besse Nuclear Power Station ML20098A2651995-08-31031 August 1995 Monthly Operating Rept for Aug 1995 for Davis-Besse Nuclear Power Station,Unit 1 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process 05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With 05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
1999-09-30
[Table view] |
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N Rev. 1 - 5/26/86 s
, OPERATIONAL
SUMMARY
MARCH, 1986 i
The unit remained shutdown the entire month of March following the reactor trip on June 9, 1985.
Investigation of the causes of the event and corrective actions continues. See NUREG 1154 for further details.
Below are some of the major activities performed during this month:
1)
Continued testing as part of the System Review and Test Program.
2)
Continued MOVATS testing.
t 3)
Completed rewiring of SFAS Channel 4.
4)
The ultrasonic testing for all four Reactor Coolant Pump (RCP) shafts revealed significant areas of interest. This inspection was conducted as a result of the Crystal River Power Plant inspection of the RCPs which revealed a failed shaft.
All four RCP seals have been removed, and the RCP 2-1 motor and impeller also have been removed from the pump.
Plans are to replace RCP 2-1 shaft with a spare rotating assembly and conduct hot functional tests. However, the other pump shafts will be replaced after the hot functional tests.
The RCP shaft replacements will extend the outage longer than
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V B607210461 860331
.A PDR ADOCK 05000346_
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Rsv. 1 - 5/16/86 COMPLETED FACILITY ^ CHANGE' REQUEST
- i FCR No.:
77-433 SYSTEM: RC/SP COMPONENT: Instrumentation CHANGED. TEST OR EXPERIMENT: This FCR improved instrument transmitter &
RTD's inside the containment vessel to promote hermeticity, by replacement and installation of conax wire leads and seals. This FCR also promoted the hermeticity of wire pigtail terminations inside existing Crouse Hinds outlet boxes.
Work was completed May 13, 1985.
REASON FOR CHANGE: To promote hermeticity of seals and wire terminations and instrument logic to withstand C.V. design environment.
SAIETY EVALUATION
SUMMARY
- The proposed design change promoted and improved the hermeticity of instrumentation inside the containment vessel. This change will not adversely affect the operation of the instrumentation or plant, nor the function of the safety protection system.
The proposed change does not involve a technical specification, nor an unreviewed safety question.
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Rev. 1 - 5/16/86 COMPLETED FACILITY ~ CHANGE REQUEST FCR NO.:
79-400 SYSTEM:
Reactor Coolant System COMPONENT: TE-RC3A3, TE-RC3Al and TE-RC3B1 Inconel Mounting Bosses CHANGE, TEST OR EXPERIMENT: This FCR replaced the resistance temperature detector mounting bosses, for TE-RC3A3, TE-RC3Al and TE-RC3B1 in accordance with B&W field change (FC-138).
This work was completed May 13, 1985.
REASON FOR CHANGE: The change was necessary due to damage on the Inconel Mounting Bosses. Loop #1 had developed galled threads on TE-RC3Bl. Loop #2 (TE-RC3A3 and TE-RC3A1) bosses were bent and also had galled threads.
SAFETY EVALUATION
SUMMARY
- The repairs meet the requirements of the applicable specifications for the reactor coolant piping. Field changes 138 and'139 include a verified statement that an appropriate analysis was made and the repairs would be acceptable.
Included in field changes 138 and 139 are the required changes to the equipment specification for reactor coolant piping to allow the reapirs, with applicable codes and standards. Original design of this piping was 1968 draft of ANSI B31-7.
The repaired bosses have the same dimensions as the original bosses.
This is not an unreviewed safety question.
i
Rev. 1 - 5/16/86 COMPLETED' FACILITY' CHANGE ~ REQUEST FCR No.:
82-018 SYSTEM:
Containment Vessel COMPONENT: Technical Specifications CHANGE, TEST OR EXPERIMENT: This FCR revised tables 3.3.10-and 4.3.10 of the Technical Specification.
This work was completed March 4, 1986.
REASON FOR CHANGE: The revision to Technical Specification Tables 3.3.10 and 4.3.10 was required per NRC requirement NUREG 0737 Item IIF-1-4 containment wide range pressure (FCR-79-425), IIF-1-5 containment normal sump level (FCR-79-408), and containment wide range level (FCR-79-409).
SAFETY EVALUATION
SUMMARY
- The safety function of the containment pressure normal sump level and wide range level is to monitor the containment pressure and containment level and to inform the operator of post accident condition.
Technical Specification Tables 3.3.10 for post accident monitoring instrumen-tation and Technical Specification Surveillance 4.3.10 requirements are adequate to verify that these systems are available during post accident conditions, and the operability is maintained in the applicable mode.
It is concluded.that the proposed Technical Specification changes do not involve an unreviewed safety question.
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Rev. 1 - 5/16/86' i
COMPLETED' FACILITY ~ CHANGE REQUEST 1
FCR NO: 82-127 3
i
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SYSTEM: 480V Essential MCC i
j COMPONENT: Breakers BF 1223 and BF 1217 i
CHANGE. TEST OR EXPERIMENT: This FCR will replace existing 200 amp trip units on essential heaters BF 1223 and BF 1217 with 250 amp trip units.
i i
This work was completed January 14, 1983.
REASON FOR CHANGE: Breakers were causing spurious losses of pressurizer heaters. Current through these breakers is 160 amps, which is normal for a full heater bank. FCR 78-430 replaced the trip units on the non-essential breakers with 250 amp units. These breakers supply 126 KV loads also.
SAFETY EVALUATION
SUMMARY
- This FCR will not compromise the integrity of the existing pressurizer essential heater banks or their power supplies.
All modifications are internal to the breaker units and will not prevent
{
the safe shutdown of the plant. Increasing the current rating of the j
thermal magnetic trip units from 200 amps to 250 amps will improve the
~
reliability of the power supply to the pressurizer essential heater banks j
by decreasing the susceptibility of these two breakers'to current surges, which had been resulting in loss of pressurizer heaters.
I Therefore, the work authorized by this FCR does not create any new adverse j
environment and does not constitute an unreviewed safety question.
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Rev. 1 - 5/16/86 COMPLETED FACILITY CHANGE REQUEST FCR No: 83-067 SYSTEM: Various COMPONENTS: MVO-5990, MVO-06010, MVO-6080, MV0-6120, MV-15170, MV-15180, MVRC-020 CHANGES, TEST OR EXPERDfENT: This FCR replaced the motor and brake with identical motor and qualified brakes, complete with special radiation resistant coils for the following motor operated valves:
MV-15170 MV-5990 MV-15180 MV-6080 4
MV-06010 MV-020 MV-6120 This work was completed February 19, 1986.
REASON FOR CHANGE: NRC IE Bulletin 79-01B required a review of environmental qualification of Class IE Electrical Equipment. The above equipment must be replaced to meet the requirements of NRC IE Bulletin 79-01B.
SAFETY EVALUATION
SUMMARY
- The above equipment is being replaced because it does not meet environmental qualification requirements.
Since this FCR calls for replacing the motor with identical motor and brake and coil with qualified brake and coil, the operators on these valves will still perform their intended safety function. This replacement will increase reliability of these actuators during accident conditions. The work authorized by this FCR does-not create any new adverse environment and does not constitute an unreviewed safety question.
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Rev. 1 - 5/16/86 COMPLETED ~ FACILITY' CHANGE REQUEST FCR No.:
83-075 SYSTEM:
Decay Heat COMPONENT: DH-13A CHANGE, TEST OR EXPERIMENT: This FCR repaired and replaced valve'DH-13A to its original condition.
(Refer to FCR 82-130 for present pinned condition).
This work was completed February 21, 1986.
REASON FOR CHANGE: This valve (DH-13A) had been placed in a pinned position.
This FCR will repair and replace valve DH-13A to its original condition so that it can be operated.
SAFETY EVALUATION
SUMMARY
- The safety function of valve DH-13A is to maintain the pressure boundary of the decay heat system and to fail close upon SFAS actuation to prevent 'ypass of the decay heat cooler.
This FCR will restore valve DH-13A to its original design condition, which will enable it to perform its safety function.
i This FCR based on the above analysis does not constitute an unreviewed safety question.
1 t
Rev. 1 - 5/16/86 COMPLETED' FACILITY CHANGE' REQUEST FCR NO.:
84-160 SYSTEM:
Main Feedwater COMPONENT: FW-601 and FW-612 4
CHANGE, TEST OR EXPERIMENT: FCR 84-160 changed the open torque switch settings for the Main Feedwater Isolation Valves, FW-601 and FW-612, from 1.5 to 1.0.
Work was completed Januarv 9, 1985.
REASON FOR CHANGES: The new torque switch settings are to improve valve reliability. The basis for the new settings is by recommendation from the Torrey Pines Technology Report on Limitorque motor-operated valves.
SAFETY EVALUATION
SUMMARY
- The safety function of the torque switch settings is to close the valve tight enough to prevent any leakage and to break the circuit in case of high mechanical force to prevent overtraveling of the valve stem. The new torque switch settings do not affect the safety function of the torque switch. Therefore, an unreviewed safety question does not exist.
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Rev. 1 - 5/16/86 COMPLETED FACILITY CHANGE REQUEST FCR No.: 84-201 SYSTEM:
HPI/MU Systems COMPONENT: HPI and MU valves (HP-2A, B, C, & D; HP-22 & 23; MU-169, 196 and 197)
CHANGE, TEST OR EXPERIMENT: This FCR leak tested the HPI and MU valves using both liquid measuring devices (LMD) at pipe drains or vents, and acoustic emission (AE) inspection equipment for locating any leaks.
This work was completed February 21, 1986.
REASON FOR CHANGE: This information will be used as I.S.I. documentation for ASME Section XI alternative inspection requirements.
SAFETY EVALUATION
SUMMARY
- The change to both the HPI and MU systems is a temporary test committed to the NRC that will be conducted by providing a measurable leakage path through drain valves in various locations during Modes 5 and 6.
As long as a flowpath from the BWST via a decay heat removal pump to RCS is available, the Makeup System does not need to be operable.
The test pressure of 1900 psig will not exceed either the preservice hydro of 2500 psig, nor the required mill test of 2500 psig for each length of pipe per ASTM-1530.
The conduct of this test will not affect the~ integrity of the system tested; therefore, the testing proposed does not constitute an unreviewed safety question.
Y O
TOLEDO
%s EDISON May 16, 1986 Log No. KB86-0510 File:
RR 2 (P-6-86-03)
Docket No. 50-346 License No. NPF-3 Mr. Norman Haller, Director Office of Management and Program Analysis U. S. Nuclear Regulatory Commission Washington, D.C.
20555
Dear Mr. Haller:
Enclosed are ten copies of Revision 1 to the Monthly Operating Report for Davis-Besse Nuclear Power Station Unit 1 for the month of March 1986.
Please remove and destroy the Operational Summary and the Completed FCR Summaries for FCRs77-433, 79-400,82-018, 82-127,83-067, 83-075,84-160, and 84-201, and replace with the attached revised sheets.
If you have any questions, please feel free to contact Morteza Khazrai at (419) 249-5000, Extension 7290.
Yours truly, p> WeO,!
W i
7 Louis F. Storz Plant Manager Davis-Besse Nuclear Power Station LFS/MK/lj k Enclosures cc:
Mr. James G. Keppler, w/l Regional Administrator, Region III Mr. James M. Taylor, Director, w/2 Office of Inspection and Enforcement Mr. Paul Byron, w/1 i
NRC Resident Inspector CiiAlit2A:!-:iLC D JK/002 M
\\l\\
THE TOLEDO EDISON COMPANY EDISON PLAZA 300 MADISON AVENUE TOLEDO, OHIO 43652
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