ML20140H044
| ML20140H044 | |
| Person / Time | |
|---|---|
| Site: | Davis Besse |
| Issue date: | 05/31/1997 |
| From: | Lash J, Matranga E TOLEDO EDISON CO. |
| To: | NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM) |
| References | |
| KB-97-0090, KB-97-90, NUDOCS 9706180021 | |
| Download: ML20140H044 (5) | |
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TOLEDO
%m EDICON A Centerior Energy Company 1
Davis-Besse Nuclear Power Staten 5501 North State Floute 2 Oak Harbor. OH 43449-9760 June 12,1997 KB-97-0090 l
Document Control Desk l
U. S. Nuclear Regulatory Commission l
' Washington, D. C. 20555 l
l Ladies and Gentlemen:
Monthly Operating Report, May 1997 l
Davis-Besse Nuclear Power Station Unit 1 l
Enclosed is a copy of the Monthly Operating Report for the Davis-Besse Nuclear Power Station for the month of May 1997.
l If you have any questions, please contact E. C. Matranga at (419) 321-8369.
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l Very truly yours, 3M.skbN f
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James II. Lash Plant Manager Davis-Besse Nuclear Power Station f/
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ECM/ljk Enclosure -
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A. B. Beack
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l NRC Reg: m III Administrator
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q A. G. Hansen i
NRC Project Manager S. Stasek
$ r' D,0 NRC Senior Residdnt Inspector 9706190021 970531 ~..
!hl PDR ADOCK 05000346' R
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AVERAGE DAILY UNIT POWER LEVEL DOCKET NO. 50-0346 i
UNIT Davis-Besse Unit 1 DATE June 2,1997 COMPLETED BY Eugene C. Matranga TELEPHONE 419/321-8369 MONTH May,199/
l AVERAGE DAILY POWER LEVEL AVERAGE DAILY POWER LEVEL l
DAY (MWe-Net)
DAY (MWe-Net) i 1
876 16 0
)
l 2
879 17 0
3 878 18 0
l 4
453 19 0
1 l
5 0
20 0
l 6
0 21 0
1 7
0 22 0
1
)
8 0
23 0
I 9
0 24 0
10 0
25 0
11 0
26 0
l l
12 0
27 0
i' 13 0
28 46 14 0
29 849 1
15 0
30 877
)
l l
OPERATING DATA REPORT DOCKET NO 50-0346 DATE June 2,1997 l
COMPLETED BY Eucene C. Matranca TELEPHONE 419/321-8369 OPERATING STATUS l
- 1. Unit Name: Davis-Besse Unit 1 Notes l
- 2. Reportina Period May,1997
- 3. Licensed Thermal Power (MWt) 2772
- 4. Nameplate Ratina (Gross MWe) 925
- 5. Desian Electrical Ratina (Net MWe) 906 i
l
- 6. Maximum Dependable Capacity (Gross MWe) 917 l
- 7. Maximum Dependable Capacity (Net MWe) 873
- 8. If Chances Occurin Capacity Ratinas i
j (Items number 3 through 7) since last report, give reasons:
- 9. Power Level To Which Restricted, If Any (Net MWe):
- 10. Reasons For Restrictions, if Any (Net MWe):
i This Month Yr-to-Date Cumulative
- 11. Hours In Reporting Period 744.00 3,623.00 165,120.00
- 12. Number Of Hours Reactor Was Critical 220.18 3,099.18 109,295.15
- 13. Reactor Reserve Shutdown Hours 0.00 0.00 5,532.00 l
- 14. Hours Generator On-Line 174.06 3,047.32 106,950.82
- 15. Unit Reserve Shutdown Hours 0.00 0.00 1,732.50
- 16. Gross Thermal Energy Generated (MWH) 467,439 8,395,202 278,974,047
- 17. Gross Electrical Energy Generated (MWH) 146,281 2,801,708 90,731,785
- 18. Net Electrical Energy Generated (MWH) 138,030 2,663,283 85,706,477
- 19. Unit Service Factor 23.40 84.11 64.77
- 20. Unit Availability Factor 23.40 84.11 65.82
- 21. Unit Capacity Factor (Using MDC Net) 21.25 84.20 59.46
- 22. Unit Capacity Factor (Using DER Net) 20.48 81.14 57.29
- 23. Unit Forced Outage Rate 76.60 15.89 17.24
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
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- 25. If Shut Down At End Of Report Period, Estimated Date of Startup:
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- 26. Units In Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICAllTY INITIAL ELECTRICITY i
COMMERCIAL OPERATION J
W
OPERATIONAL
SUMMARY
May 1997 Reactor power was maintained at approximately 100 percent full power until 0008 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> on May 4,1997, when a manual power reduction was initiated to perform turbine valve testing. Reactor power was reduced to approximately 92 percent full power by 0033 hours3.819444e-4 days <br />0.00917 hours <br />5.456349e-5 weeks <br />1.25565e-5 months <br />, and control valve and stop valve testing were conducted. At the completion of testing at 0117 hours0.00135 days <br />0.0325 hours <br />1.934524e-4 weeks <br />4.45185e-5 months <br />, power was gradually increased to approximately 100 percent full power, which was achieved at 0205 hours0.00237 days <br />0.0569 hours <br />3.38955e-4 weeks <br />7.80025e-5 months <br />.
At 1731 hours0.02 days <br />0.481 hours <br />0.00286 weeks <br />6.586455e-4 months <br /> on May 4,1997, a spurious deluge system activation occurred on the Main Transformer resulting in an automatic reactor trip 4 i
minutes later. The plant was maintained in Mode 3 while various inspections and maintenance were performed.
1 On May 7,1997, a decision was made to replace the Main Transformer and i
preparations are made to enter Mode 5. The cooldown was completed on May 9,1997.
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A plant heatup was commenced at 0538 hours0.00623 days <br />0.149 hours <br />8.895503e-4 weeks <br />2.04709e-4 months <br /> on May 19,1997 and the reactor achieved criticality at 1324 hours0.0153 days <br />0.368 hours <br />0.00219 weeks <br />5.03782e-4 months <br /> on May 26,1997.
L At 0940 hours0.0109 days <br />0.261 hours <br />0.00155 weeks <br />3.5767e-4 months <br /> on May 28,1997, power was increased to approximately 20 percent full power and the Main Turbine was synchronized to the grid at l
1132 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.30726e-4 months <br />. Power w., increased until 0212 hours0.00245 days <br />0.0589 hours <br />3.505291e-4 weeks <br />8.0666e-5 months <br /> on May 29,1997 when power was held at approximately 80 percent full power for nuclear instrumentation calibration. Nuclear instrumentation calibration was completed at 0405 hours0.00469 days <br />0.113 hours <br />6.696429e-4 weeks <br />1.541025e-4 months <br /> and the power ascension was resumed. The power increase was stopped at 0633 hours0.00733 days <br />0.176 hours <br />0.00105 weeks <br />2.408565e-4 months <br /> at approximately 97 percent full power
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for nuclear instrumentation calibration. Nuclear instrumentation calibration was completed at 0847 hours0.0098 days <br />0.235 hours <br />0.0014 weeks <br />3.222835e-4 months <br /> and the power ascension was resumed. At 1014 hours0.0117 days <br />0.282 hours <br />0.00168 weeks <br />3.85827e-4 months <br />,100 percent full power was achieved.
. Reactor power was maintained at approximately 100 percent full power for the remainder of the month.
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UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.
50-346 UNIT NAME Davis-Besse #1
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DATE June 2,1997 Report Month May.1997 COMPLETED BY E. C. Matranga l
TELEPHONE (419) 321-8369 i
t 8g "c
E E" b Cause & Corrective b
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No Date 8.
%5 8
E k$
Action to l
f h
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Prevent Recurrence 8
2 97-05-04 F
569.9 A
3 97-010 IC T;S Plant trip occurred after receipt of a fire alarm on the Main transformer and activation of the Deluge Fire t
Protec3on System.
A temperature switch falsely indicated a high temperature condition and activated the Deluge System. 4 of 168 nozzles were not optimally aimed and may have contributed to causing a i
flashover which in tum caused the reactor trip.
The Main Transformer and its re?ated temperature sensors were replaced. Similar transformer sensors were checked. Nozzles not optimally aimed were realigned.
T i
1 2
3 4
F: Forced Reason:
Method:
Exhibit G-Instructions S: Scheduled A-Equipment Failure (Explain) 1-Manual for Preparation of Data B-Maintenance or Test 2-Manual Scram Entry Sheets for Licensee C-Refueling 3-Automatic Scram Event Report (LER) File (NUREG-D-Regulatory Restriction 4-Continuation from 0161)
E-OperatorTraining & License Examination Previous Month F-Administrative 5-Load Reduction 5
G-Operational Error (Explain) 9-Other (Explain)
Exhibit 1 - Same Source H-Other (Explain)
- Report challenges to Power Operated Relief Valves (PORVs) and Pressurizer Code Safety Valves (PCSVs) t
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