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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20212A7381999-09-10010 September 1999 Safety Evaluation Supporting Amend 174 to License NPF-49 ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20210U0881999-08-13013 August 1999 Safety Evaluation Supporting Amends 239 & 173 to Licenses DPR-65 & NPF-49,respectively ML20210Q1401999-08-12012 August 1999 Safety Evaluation Supporting Amend 238 to License DPR-65 ML20209G3061999-07-13013 July 1999 Safety Evaluation Supporting Amend 237 to License DPR-65 ML20209D6581999-07-0202 July 1999 Safety Evaluation Supporting Amend 172 to License NPF-49 ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20196H1621999-06-29029 June 1999 Safety Evaluation Supporting Amend 236 to License DPR-65 ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 ML20205S5341999-04-16016 April 1999 Safety Evaluation Supporting Amend 169 to License NPF-49 ML20205N3601999-04-12012 April 1999 Safety Evaluation Supporting Amend 233 to License DPR-65 ML20205G0191999-03-17017 March 1999 Safety Evaluation Supporting Amend 168 to License NPF-49 ML20204H7131999-03-17017 March 1999 Safety Evaluation Concluding That NNECO Provided Adequate Justification for Deviations from RG 1.97,Rev 2, Recommendations,For Instrumentation Monitoring CST Level & Containment Area Radiation at Mnps Unit 2 ML20205G4781999-03-12012 March 1999 Safety Evaluation Supporting Amend 231 to License DPR-65 ML20205G8671999-03-11011 March 1999 Safety Evaluation Supporting Amend 230 to License DPR-65 ML20204C9441999-03-10010 March 1999 Safety Evaluation Denying Licensee Request for License Amend to Revise Frequency of Certain SRs for Electrical Power Sys ML20205G4591999-03-10010 March 1999 Safety Evaluation Supporting Amend 229 to License DPR-65 ML20204E7581999-03-10010 March 1999 Safety Evaluation Supporting Amend 228 to License DPR-65 ML20207L2631999-03-0505 March 1999 Safety Evaluation Supporting Amend 104 to License DPR-21 ML20207L5961999-02-22022 February 1999 Safety Evaluation Concluding That Code Requirements,Which Require 100 Percent Volumetric Exam of RPV flange-to-shell, Impractical to Perform to Extent Required & That Alternative Provide Reasonable Assurance of Structural Integrity ML20203D7601999-02-11011 February 1999 Safety Evaluation Supporting Millstone 1 Certified Fuel Handler Training & Retraining Program ML20203J3191999-02-10010 February 1999 Safety Evaluation Supporting Amend 227 to License DPR-65 ML20199H9181999-01-20020 January 1999 Safety Evaluation Supporting Amend 224 to License DPR-65 ML20198S7801998-12-31031 December 1998 Safety Evaluation Supporting Amend 223 to License DPR-65 ML20198E1471998-12-18018 December 1998 Safety Evaluation Supporting Amend 222 to License DPR-65 ML20198E0571998-12-17017 December 1998 Safety Evaluation Supporting Amend 221 to License DPR-65 ML20196B0501998-11-24024 November 1998 Safety Evaluation Re Licensee 960213 Submittal of 180-day Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant,Unit 2 ML20155K1981998-11-0909 November 1998 Safety Evaluation Re Application of leak-before-break Status to Portions of Safety Injection & Shutdown Cooling Sys ML20195B8711998-11-0909 November 1998 Safety Evaluation Approving Revised Evaluation of Primary Cold Leg Piping leak-before-break Analysis for Plant ML20155C3781998-10-30030 October 1998 SER Denying Amend to Allow Changes to Fsar.Nrc Found That NNECO Had Not Considered Diversity Provided by Switch in Control Room That Removes Power to 1 of 2 MOV in SDC Sys Flow Path in Evaluation of High Low Pressure Design ML20155C8441998-10-29029 October 1998 Safety Evaluation Accepting Licensee Proposal to Withdraw ATWS Test Commitment ML20153D8921998-09-23023 September 1998 Safety Evaluation Supporting Amend 163 to License NPF-49 ML20238F2781998-08-27027 August 1998 SER Related to Proposed Rev 20 to Northeast Utilities Quality Assurance Program Topical Rept for Millstone Nuclear Power Station,Units 1,2 & 3 ML20237D4681998-08-21021 August 1998 Safety Evaluation Supporting Amend 219 to License DPR-65 ML20237D5001998-08-20020 August 1998 SER Approving Code Case N-389-1, Alternative Rules for Repairs,Replacements,Or Mods,Section Xi,Div 1 ML20236Y5601998-08-0707 August 1998 Safety Evaluation Supporting Amend 162 to License NPF-49 ML20236U7051998-07-22022 July 1998 Safety Evaluation Granting All Requests for Relief W/Exception of Requests RR-89-17 (Authorized for Class 1 Sys Only) & RR-89-21.Requests RR-13 & RR-14 Will Be Addressed in Separate Evaluation ML20236K3531998-07-0101 July 1998 Safety Evaluation Supporting Amend 218 to License DPR-65 ML20236K6971998-07-0101 July 1998 SER Accepting Third 10-year Interval Inservice Insp Program Plan,Rev 2 & Associated Request for Relief & Proposed Alternatives for Plant,Unit 2 ML20249C2541998-06-24024 June 1998 Safety Evaluation Accepting Proposed Rev 19 to NNECO QAP Topical Rept & Amended Through 980609.Informs That NNECO Exception to Provisions in Paragraph 10.3.5 of Constitutes Temporary & Acceptable Alternative ML20249C0491998-06-22022 June 1998 Safety Evaluation Supporting Amend 217 to License DPR-65 ML20249B0751998-06-16016 June 1998 Safety Evaluation Supporting Amend 216 to License DPR-65 ML20248K9271998-06-0505 June 1998 Safety Evaluation Supporting Amend 161 to License NPF-49 ML20248J0031998-06-0404 June 1998 Safety Evaluation Accepting Millstone Nuclear Power Station Emergency Plan ML20248M2991998-06-0202 June 1998 Safety Evaluation Approving Application Re Restructuring of Central Maine Power Co by Establishment of Holding Company ML20248A8291998-05-27027 May 1998 Safety Evaluation Supporting Amend 160 to License NPF-49 ML20248C4131998-05-26026 May 1998 SER of Individual Plant Exam of External Events Submittal on Millstone Nuclear Power Station,Unit 3 ML20248A3221998-05-26026 May 1998 Safety Evaluation Supporting Amend 215 to License DPR-65 1999-09-10
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program 05000336/LER-1999-012, :on 990917,unrecoverable CEA Misalignment Entry Into TS 3.0.3 Was Noted.Caused by Grounded Coil Wire for Lower Gripper Assembly.Leads Leading to Lower Gripper Coil Were Insulated1999-10-15015 October 1999
- on 990917,unrecoverable CEA Misalignment Entry Into TS 3.0.3 Was Noted.Caused by Grounded Coil Wire for Lower Gripper Assembly.Leads Leading to Lower Gripper Coil Were Insulated
ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 05000336/LER-1999-011, :on 990823,thermal Reactor Power Limit Was Exceeded.Caused by Lack of Conservatism in Procedures & Alarm Setpoints Used to Limit Reactor Power.Revised Operating Procedures1999-09-20020 September 1999
- on 990823,thermal Reactor Power Limit Was Exceeded.Caused by Lack of Conservatism in Procedures & Alarm Setpoints Used to Limit Reactor Power.Revised Operating Procedures
ML20212A7381999-09-10010 September 1999 Safety Evaluation Supporting Amend 174 to License NPF-49 05000245/LER-1999-001-02, :on 990810,discovered That Stack Flow Monitor Four H LCO Action Statement Had Not Been Met.Caused by Personnel Error.Frequency of LCO Action Was Increased & Personnel Involved Received Coaching.With1999-09-0808 September 1999
- on 990810,discovered That Stack Flow Monitor Four H LCO Action Statement Had Not Been Met.Caused by Personnel Error.Frequency of LCO Action Was Increased & Personnel Involved Received Coaching.With
05000336/LER-1999-010, :on 990804,noted Failure to Perform ASME Section XI IST on Pressurizer Relief Line Flow Control Sample Valve.Caused by Inadequate man-machine Interface. Planning Personnel Will Be Briefed on QC Program Indicators1999-09-0202 September 1999
- on 990804,noted Failure to Perform ASME Section XI IST on Pressurizer Relief Line Flow Control Sample Valve.Caused by Inadequate man-machine Interface. Planning Personnel Will Be Briefed on QC Program Indicators
ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20210U0881999-08-13013 August 1999 Safety Evaluation Supporting Amends 239 & 173 to Licenses DPR-65 & NPF-49,respectively ML20210Q1401999-08-12012 August 1999 Safety Evaluation Supporting Amend 238 to License DPR-65 B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr ML20209G3061999-07-13013 July 1999 Safety Evaluation Supporting Amend 237 to License DPR-65 B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D6581999-07-0202 July 1999 Safety Evaluation Supporting Amend 172 to License NPF-49 ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196H1621999-06-29029 June 1999 Safety Evaluation Supporting Amend 236 to License DPR-65 05000423/LER-1999-007-01, :on 990518,discharge Filter Associated with Crss Cubicle Sump Pump 3DAS-8A,was Determined to Be Contaminated.Caused by Back Leakage from Contaminated Drains Feeding Into ECCS Pump.Lines Modified.With1999-06-17017 June 1999
- on 990518,discharge Filter Associated with Crss Cubicle Sump Pump 3DAS-8A,was Determined to Be Contaminated.Caused by Back Leakage from Contaminated Drains Feeding Into ECCS Pump.Lines Modified.With
05000423/LER-1999-006-01, :on 990516,both Reactor Plant Aerated Drains SR Air Driven Sump Pumps Failed During TRM Surveillance.Caused by Inadequate Preventive Maint Program Design.Surveillance Procedure Sp 3635B.2 Will Be Conducted Monthly1999-06-15015 June 1999
- on 990516,both Reactor Plant Aerated Drains SR Air Driven Sump Pumps Failed During TRM Surveillance.Caused by Inadequate Preventive Maint Program Design.Surveillance Procedure Sp 3635B.2 Will Be Conducted Monthly
05000423/LER-1999-004-01, :on 990516,ESFA of Numerous Plant Components on Restoration of a Train Sequencer Occurred.Caused by Inadequate Procedure Direction.Issued Brief to Operations Describing Inadvertent Sequencer LOP Event.With1999-06-14014 June 1999
- on 990516,ESFA of Numerous Plant Components on Restoration of a Train Sequencer Occurred.Caused by Inadequate Procedure Direction.Issued Brief to Operations Describing Inadvertent Sequencer LOP Event.With
ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR 05000423/LER-1999-005-01, :on 990510,failure to Perform Surveillance on RCS Pressurizer Heater Penetration Breakers Was Noted.Caused by Lack of Mgt Support.Required Surveillance of Identified Ten Breakers Was Completed1999-06-0808 June 1999
- on 990510,failure to Perform Surveillance on RCS Pressurizer Heater Penetration Breakers Was Noted.Caused by Lack of Mgt Support.Required Surveillance of Identified Ten Breakers Was Completed
05000423/LER-1999-003-01, :on 990505,identified That 18 Month EDG Surveillance Test for LOP with ESF Start Did Not Initiate Test.Caused by Inadequate Understanding of Regulatory Guidance. a & B EDG Returned to Status.With1999-06-0404 June 1999
- on 990505,identified That 18 Month EDG Surveillance Test for LOP with ESF Start Did Not Initiate Test.Caused by Inadequate Understanding of Regulatory Guidance. a & B EDG Returned to Status.With
ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With 1999-09-08
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Text
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UNITED STATES g-g NUCLEAR REGULATORY COMMISSION
't WASHINGTON, D.C. 2056M001
,o SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT NO. im TO FACILITY OPERATING LICENSE NO. NPF-49 NORTHEAST NUCLEAR ENERGY COMPANY. ET AL, MILLSTONE NUCLEAR POWER STATION. UNIT NO. 3 DOCKET NO. 50-423
1.0 INTRODUCTION
By letter dated February 10,1999, the Northeast Nuclear Energy Company, et al. (the licensee), submitted a request for a change to the Millstone Nuclear Power Station, Unit No. 3 Technical Specifications (TS). The requested change would incorporate altemative inspection requirements into TS Surveillance Requirement 3/4.4.10, " Structural Integrity," for the reactor coolant pump (RCP) flywheel.
This issue was addressed in Westinghouse topical report, WCAP-14535, " Topical Report on 1
Reactor Coolant Pump Flywheel Inspection Elimination," which was approved by the Nuclear Regulatory Commission (NRC) with certain conditions. These conditions were specified in the NRC safety evaluation report (SER) dated September 12,1996, for WCAP-14535. The licensee requested to apply this topical report to Millstone Unit 3 and change their RCP flywheel inspection intervals in accordance with the conclusions of the SER related to WCAP-14535.
2.0 BACKGROUND
The function of the RCP in the reactor coolant system (RCS) of a pressurized water reactor (PWR) plant is to maintain an adequate cooling flow rate by circulating a large volume of primary coolant water at high temperature and pressure through the RCS. A concern about overspeed of the RCP and its potential for failure led to the issuance of Regulatory Guide (RG) 1.14, " Reactor Coolant Pump Flywheel Integrity,"in 1971. Since then, all licensees for PWR plants, with very few exceptions, have adopted the guidelines of RG 1.14 to conduct their RCP flywheel examinations. These requirements are normally specified in the individual plant's TS as is the case for Millstone Unit 3. These requirements are specified in Millstone Unit 3 TS 4.4.10 and state that in addition to the requirements of TS 4.0.5, each RCP flywheel shall be inspected per the recommendations of Regulatory Position C.4.b of RG 1.14, Revision 1, August 1975. The recommendations of Regulatory Position C.4.b are as follows:
9904260250 990416 PDR ADOCK 05000423 P
peg
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. Inservice inspection should be performed for each flywheel as follows:
(1) An in-place ultrasonic volumetric examination of the areas of higher stress concentration at the bore and keyway at approximately 3-year intervals, during the refueling or maintenance shutdown coinciding with the inservice inspection schedule as J
required by Section XI of the ASME Code.
(2) A surface examination of all exposed surfaces and complete ultrasonic volumetric examination at approximately 10-year intervals, during the plant shutdown coinciding with the inservice inspection schedule as required by Section XI of tne ASME Code.
(3) Examination procedures should be in accordance with the requirements of Subarticle IWA-2200 of Section XI of the ASME Code.
(4) Acceptance criteria chould conform to the recommendations of regulatory position C.2.f.
(5) If the examination and evaluation indicate an increase in flaw size or growth rate greater than predicted for the service life of the flywheel, the resuits of the examination and evaluation should be submitted to the staff for evaluation.
3.0 EVALUATION in the SER on Westinghouse topical report WCAP-14535, the staff stated that the evaluation
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methodology for RCP flywheels in WCAP-14535 is appropriate and the criteria are in 1
accordance with the design criteria of RG 1.14. In addition, the staff specified:
(1). Licensees who plan to submit a plant-specific application of this topical report for flywheels made of SA 533 8 material need to confirm that their flywheels are made of SA 533 8 material. Further, licensees having Group-15 flywheels need to demonstrate that the material properties of their A516 material are equivalent to SA 533 B material, and its reference temperature, rte, is less than 30 *F.
(2) Licensees who plan to submit a plant-specific application of this topical report for their flywheels not made of SA 533 8 or A516 material need to either demonstrate that their flywheel material properties are bounded by those of SA 533 8 material, or provide the minimum specified ultimate tensile stress, Su; the fracture toughness, Km; i
and the reference temperature, rte, for that material. For the latter, the licensees should employ these material-specific properties, and use the methodology in the topical report, as extended in the two responses to the staff's request for additional information (RAI). to provide an assessment to justify a change in inspection schedules for their plants.
(3) Licensees meeting either (1) or (2) above should either conduct a qualified in-place ultrasonic testing (UT) examination of the volume from the inner bore of the flywheel to the circle of one-half the outer radius, or conduct a surface examination (MT and/or PT) of exposed surfaces defined by the volume of the disassembled flywheels once every 10 years. The staff considers this 10-year inspection requirement not
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3-burdensome when the flywheel inspection is conducted during scheduled ISI inspection or RCP motor maintenance. This would provide an appropriate level of defense in depth.
Further, the staff required:
Licensees with Group-10 flywheels need to confirm in the near term that their flywheels have an adequate shrink fit of the flywheel at the maximum overspeed.
M its submittal, the licensee confirmed that the RCP flywheels for Millstone Unit 3 are made of SA 533 B material. Hence, only (1) and (3) apply. The staff further verified that the flywheels for Millstone Unit 3 do not belong to either Group 10 or Group 15 flywheels, for which additional analyses need to be performed. Therefore, the plant-specific applicability of WCAP-
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14535 to Millstone Unit 3 has been established.
4.0 TS CHANGE in its submittal dated February 10,1999, the licensee requested changes to TS 4.4.10, specifically, TS 4,4.10 would read:
In addition to the requirements of Specification 4.0.5, each reactor coolant pump flywheel shall be inspected by either qualified in-place UT examination over the volume from the inner bore of the flywheel to the circle of one-half the outer radius or a surface examination (magnetic particle testing and/or penetrant testing) of exposed surfaces defined by the volume of the disassembled flywheels at least once every 10 years.
The staff has determined that the analysis in the Westinghouse topical report WCAP-14535 is applicable to Millstone Unit 3 and the licensee's proposed change to TS 4.4.10 is consistent with the guidance contained in the SER related to WCAP-14535. Therefore, the staff has determined that the change to TS 4.4.10 is acceptable.
5.0 STATE CONSULTATION
in accordance with the Commission's regulations, the Connecticut State official was notified of the proposed issuance of the amendment. The State official had no comments.
6.0 ENVIRONMENTAL CONSIDERATION
The amendment changes a requirement with respect to installation or use of a facility component located within the restricted aree as defined in 10 CFR Part 20 and changes surveillance requirements. The NRC staff has determined that the amendment involves no j
significant increase in the amounts, and no significant change in the types, of any effluents J
that may be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously issued a proposed finding that the amendment involves no significant hazards consideration, and there has been no public comment on such finding (64 FR 11964). Accordingly, the amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22(c)(9). Pursuant to 10 CFR 1
L
V.
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4 51.22(b) no environmental impact statement or environmental assessment need be prepared in connection with the issuance of the amendment.
7.0 CONCLUSION
The Commission has concluded, based on the considerations discussed above, that: (1) there is reasonable assurance that the health and safety of the public will not be endangered by
- operation in the proposed manner, (2) such activities will be conducted in compliance with the Commission's regulations, and (3) the issuance of the amendment will not be inimical to the common defense and security or to the health and safety of the public.
Principal Contributor J. Andersen P.
Date: April 16, 1999