ML20198F823

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Notice of Violation from Insp on 970314-0501.Violation Noted:Grates Covering Floor Drains Leading to Containment Floor Drain Leak Detection Sys Were Not Installed
ML20198F823
Person / Time
Site: Byron  Constellation icon.png
Issue date: 07/22/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20198F705 List:
References
50-454-97-05, 50-454-97-5, 50-455-97-05, 50-455-97-5, EA-97-200, NUDOCS 9708130151
Download: ML20198F823 (2)


Text

i NOTICE OF VIOLATION Commonwealth Edison Company Docket Nos. 50-454:50 455 Byron Generating Station Licenses No. NPF 37: NPF 60 EA 97 200 During an NRC inspection conducted on March 14,1997, through May 1,1997, a violation of NRC requirements was identified, in accordance with the " General Statement of Policy and Procedure for NRC Enforcement Actions," NUREG 1600, the violation is listed below:

10 CFR 50.59, " Changes, tests and experiments," permits the licensee to make changes to the facility and procedures as described in the safety analysis report and conduct tests or experiments not described in the safety analysis report without.

prior Commission approval provided the change does not involve a change in the technical specifications or an Unteviewed Safety Question (USO). The licensee shall maintain records of changes in the facility and these records must include a written safety evaluation which provides the bases for the determination that the change does not involve a USQ.

10 CFR 50.9(a) requires, in part, that information provided to the NRC by a licer'see or information required by regulation to be maintained by a licensee shall be complete and accurate in all material respects.-

UFSAR Section 5.2.5.1, " Reactor Cavity and Containment Floor Drain Sumps,"

Figure 5.2 3 specified that a vendor bar grate of approximately 5 inches was to be installed over each of the containment floor drains.

Contrary to the above, as of March 14,1997, the facility was not as described in the UFSAR in that the grates described in UFSAR Figure 5.2 3 covering the containment floor drains leading to the containment floor drain leak detection system were not installed. The drains were either covered with a different grate or screen, or were not covered at all resulting in the potential that foreign material could enter the drain system and adversely affect the leak detection system. A written safety evaluation was not performed to make a determination that the change did not involve an unroviewed safety question in addition, the updated FSAR was not complete and accurate in all material respects in that it did not reflect this change.

This is a Severity Level IV violation (Supplement 1).

Pursuant to the provisions of 10 CFR 2.201; Commonwealth Edison Company (Licensee) is hereby required to submit a written statement or explanation tn the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, D.C. 20555 with a copy to the Regional Administrator, Region Ill, and a copy to the NRC Resident inspector at

' the facility that is the subject of this Notice, within 30 days of the date of the letter transmitting this Notice of Violation (Notice). This reply should be clearly marked as a

=9708130151=970722 - - -

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i PDR ADOCK 05000454 0 PM 4

C Notico of Violation 2-

, " Reply to a Notico of Violation" and should include for each violation: (1) the reason for the violation, or, if contested, the basis for disputing the violation, (2) the correctivo stops that have been taken and the results schloved, (3) the corrective steps that will be taken to avoid further violations, and (4) the date when full compliance will be achloved. Your response may reference or include previous docketed correspondonce, if the correspondence adequately addressos the required responso, if an adoquate reply is not received within the time specified in this Notico, an order or a Domand for Information may bo issued as to why the licenso should not be modified, suspended, or revoked, or why such other action as may be proper should not be taken. Where good cause is shown, consideration will be given to extending the response time.

Because your responso will be placed in the NRC Public Document Room (PDR), to the extent possible, it should not includo any personal privacy, proprietary, or sofoguards information so that it can be placed in the PDR without redaction, if personal privacy or proprietary information is necessary to provido an acceptablo responso, then please provido a bracketed copy of your response that identifies the information that should be protected and a redacted copy of your response that dolotos such information, if you request withholding of such material, you mpfd specifically identify the portions of your response that you sock to have withhold and provido in detail the bases for your claim of withhold-ing (o.g., explain why the disclosure of information will create an unwarranted invasion of personal privacy or provido the information required by 10 CFR 2.790(b) to support a request for withholding confidentini commercial or financial information), if safoguards in8ormation is necessary to provido an acceptable response, please provido the lovel of prrrection described in 10 CFR 73.21.

Dated at Listo, il this 22 day of July 1997

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