ML20133J811

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Units, Units 2 and 3 - Integrated Inspection Report 05000237/2020001 and 05000249/2020001
ML20133J811
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 05/11/2020
From: Kenneth Riemer
NRC/RGN-III/DRP/B1
To: Bryan Hanson
Exelon Generation Co, Exelon Nuclear
References
IR 2020001
Download: ML20133J811 (34)


See also: IR 05000237/2020001

Text

May 11, 2020

Mr. Bryan C. Hanson

Senior VP, Exelon Generation Co., LLC

President and CNO, Exelon Nuclear

4300 Winfield Road

Warrenville, IL 60555

SUBJECT:

DRESDEN NUCLEAR POWER STATION, UNITS 2 AND 3 - INTEGRATED

INSPECTION REPORT 05000237/2020001 AND 05000249/2020001

Dear Mr. Hanson:

On March 31, 2020, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection

at Dresden Nuclear Power Station, Units 2 and 3. On April 8, 2020, the NRC inspectors

discussed the results of this inspection with Mr. P. Karaba, Site Vice President, and other

members of your staff. The results of this inspection are documented in the enclosed report.

Two findings of very low safety significance (Green) are documented in this report. Two of

these findings involved violations of NRC requirements. One Severity Level IV violation without

an associated finding is documented in this report. We are treating these violations as non-cited

violations (NCVs) consistent with Section 2.3.2 of the Enforcement Policy.

If you contest the violations or the significance or severity of the violations documented in this

inspection report, you should provide a response within 30 days of the date of this inspection

report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001; with copies to the Regional

Administrator, Region III; the Director, Office of Enforcement; and the NRC Resident Inspector

at Dresden Nuclear Power Station, Units 2 and 3.

B. Hanson

2

This letter, its enclosure, and your response (if any) will be made available for public inspection

and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document

Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public

Inspections, Exemptions, Requests for Withholding.

Sincerely,

/RA/

Kenneth R. Riemer, Chief

Branch 1

Division of Reactor Projects

Docket Nos. 05000237 and 05000249

License Nos. DPR-19 and DPR-25

Enclosure:

As stated

cc w/ encl: Distribution via LISTSERV

ML20133J811

X

SUNSI Review

X

Non-Sensitive

Sensitive

X

Publicly Available

Non-Publicly Available

OFFICE RIII

NAME

CPhillips:wc

KRiemer via email

DATE

5/11/2020

5/11/2020

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

Inspection Report

Docket Numbers:

05000237 and 05000249

License Numbers:

DPR-19 and DPR-25

Report Numbers:

05000237/2020001 and 05000249/2020001

Enterprise Identifier: I-2020-001-0045

Licensee:

Exelon Generation Company, LLC

Facility:

Dresden Nuclear Power Station, Units 2 and 3

Location:

Morris, IL

Inspection Dates:

January 01, 2020 to March 31, 2020

Inspectors:

J. Corujo-Sandin, Senior Resident Inspector

G. Edwards, Health Physicist

R. Elliott, Resident Inspector

M. Garza, Emergency Preparedness Inspector

T. Go, Health Physicist

J. Park, Reactor Inspector

C. Phillips, Project Engineer

L. Rodriguez, Reactor Inspector

C. St. Peters, Reactor Engineer

Approved By:

Kenneth R. Riemer, Chief

Branch 1

Division of Reactor Projects

2

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees

performance by conducting an integrated inspection at Dresden Nuclear Power Station, Units 2

and 3, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is

the NRCs program for overseeing the safe operation of commercial nuclear power reactors.

Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

Unit 2B Low Pressure Coolant Injection Valve Damaged Due To Inadequate Inspection

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000237/2020001-01

Open/Closed

None (NPP)

71111.22

A self-revealed Green finding and associated non-cited Violation (NCV) of 10 CFR 50,

Appendix B, Criterion V, was identified on October 23, 2019. During a performance of a

surveillance test on October 23, 2019, the 2B low pressure coolant injection (LPCI) pump

suction valve 2-1501-5B failed to reopen following closure resulting in the 2B LPCI pump

being declared inoperable. The licensee's evaluation of this failure identified that an

inspection was performed in 2015 with inadequate inspection guidance that should have

identified corrosion of the valve motor limit switch that lead to the failure of the valve.

Failure to Account Instrument Uncertainties

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000237,05000249/2020001-02

Open/Closed

None (NPP)

71111.22

The inspectors identified a Green finding and associated non-cited Violation (NCV) of

10 CFR 50, Appendix B, Criterion XI, Test Control, when the licensee failed to account for

instrument uncertainty in surveillance procedures' acceptance criteria for High Pressure

Coolant Injection required flow and Ultimate Heat Sink maximum temperature.

Differential Pressure Indicating Switch Failure in Low Pressure Core Injection Loop Select

Logic

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Not Applicable

NCV 05000249/2020001-03

Open/Closed

Not Applicable

71153

A self-revealed Severity Level (SL) IV NCV of Technical Specifications (TS) 3.3.5.1,

Emergency Core Cooling System (ECCS) Instrumentation, was identified when the licensee

determined during routine surveillance testing that one of four (4) channels of the recirculation

pump high differential pressure function was inoperable for longer than the 24-hour allowed

outage time.

3

Additional Tracking Items

Type

Issue Number

Title

Report Section

Status

LER 05000249/2019-001-00

LER 2019-001-00 for

Dresden, Unit 3, Degraded

Differential Pressure

Indicating Switch in the LPCI

Loop Select Logic Caused

by Water Damage Results in

a Condition Prohibited by

Technical Specifications

71153

Closed

4

PLANT STATUS

Unit 2 began the inspection period in a forced outage (D2F59) due to an unexplained increase

in unidentified leakage. The unit was returned to full power on January 6, 2020. On

January 7, 2020, Unit 2 was down powered to 80 percent for control rod adjustment and was

returned to full power on the same day, then remained there for the rest of the inspection period.

Unit 3 began the inspection period at full power and maintained full power throughout the first

quarter.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs) in

effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with

their attached revision histories are located on the public website at

http://www.nrc.gov/readingrm/doc-collections/insp-manual/inspection-procedure/index.html.

Samples were declared complete when the IP requirements most appropriate to the inspection

activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor

Inspection Program - Operations Phase. From January 1 - March 19, 2020, the inspectors

performed plant status activities described in IMC 2515, Appendix D, Plant Status, and

conducted routine reviews using IP 71152, Problem Identification and Resolution. The

inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel to assess licensee performance and compliance with Commission rules and

regulations, license conditions, site procedures, and standards.

Starting on March 20, 2020, in response to the National Emergency declared by the President

of the United States on the public health risks of the coronavirus (COVID-19), resident

inspectors were directed to begin telework and to remotely access licensee information using

available technology. During this time the resident inspectors performed periodic site visits

each week and during that time conducted plant status activities as described in IMC 2515,

Appendix D; and observed risk significant activities when warranted. In addition, resident and

regional baseline inspections were evaluated to determine if all or portion of the objectives and

requirements stated in the IP could be performed remotely. If the inspections could be

performed remotely, they were conducted per the applicable IP. In the cases where it was

determined the objectives and requirements could not be performed remotely, management

elected to postpone and reschedule the inspection to a later date.

REACTOR SAFETY

71111.01 - Adverse Weather Protection

Impending Severe Weather Sample (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated the adequacy of the overall preparations to protect risk-

significant systems from expected snowfall and wind gusts on

February 12 and 13, 2020

5

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (3 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following

systems/trains:

(1)

Unit 2 High Pressure Coolant Injection (HPCI) Post Maintenance on March 5, 2020

(2)

2/3 Emergency Diesel Generator (EDG) with 2/3 EDG maintenance window on

March 24, 2020

(3)

Unit 3 Standby Liquid Control (SBLC) on March 28, 2020

Complete Walkdown Sample (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated system configurations during a complete walkdown of the

Unit 3 Isolation Condenser with Unit 3 HPCI maintenance window system on

February 25, 2020

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (4 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a

walkdown and performing a review to verify program compliance, equipment functionality,

material condition, and operational readiness of the following fire areas:

(1)

Fire Zone (FZ) 9.0.A, Unit 2 diesel generator elevation 517 on January 10, 2020

(2)

FZ 7.0.A.1-3 and FZ 8.2.7, Unit 2 battery room elevation 549 on January 22, 2010

(3)

FZ 8.2.8.A, Unit 3 main turbine floor elevation 561' on January 27, 2020

(4)

FZ 11.1.1, Unit 3 southwest corner room elevation 476' on January 27, 2020

Fire Brigade Drill Performance Sample (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated the onsite fire brigade training and performance during an

announced fire drill on February 13, 2020

71111.07T - Heat Sink Performance

Triennial Review (IP Section 03.02) (2 Samples 1 Partial)

The inspectors evaluated heat exchanger/sink performance on the following:

(1)

Unit 3 Diesel Generator Cooling Water Coolers (3-6669-A/B), cooled by the service

water system, Section 02.02.b

(2)

Unit 3 HPCI Room Cooler (3-5747), cooled by the service water system,

Section 02.02.b

(3)

(Partial)

Ultimate Heat Sink, Sections 02.02.d.2 and 02.02.d.6

6

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01)

(1 Sample)

(1)

The inspectors observed and evaluated licensed operator performance in the Unit 2

Control Room during forced outage D2F59 restart on January 3, 2020

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1)

The inspectors observed and evaluated 2020-OBE [out-of-the box evaluation] 03B on

January 28, 2020

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (1 Sample)

The inspectors evaluated the effectiveness of maintenance to ensure the following

structures, systems, and components (SSCs) remain capable of performing their intended

function:

(1)

Rod block monitor (A2 at risk) on February 26, 2020

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the accuracy and completeness of risk assessments for the

following planned and emergent work activities to ensure configuration changes and

appropriate work controls were addressed:

(1)

Unit 2 Station Blackout Diesel maintenance window on January 27, 2020

(2)

Unit 3 4 KV Technical Specification Undervoltage and Degraded Voltage Relay

Replacement (normally done off-line) on February 11, 2020

(3)

Unit 2 Rod Position Indication System (RPIS) Power Supply Replacement (on-line) on

February 24, 2020

(4)

Unit 3 work week risk on February 26, 2020

(5)

Unit 2 work week risk on February 26, 2020

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (5 Samples)

The inspectors evaluated the licensee's justifications and actions associated with the

following operability determinations and functionality assessments:

(1)

Functionality of station black out diesel generator batteries

(2)

Emergency Diesel Generator Unit 2 and Unit 3 Surveillance Requirement 3.3.8.1.4

possibly missed

(3)

Standby Gas Treatment due to use of chemicals in the turbine building

(4)

Unit 3 HPCI - operability of room cooling system with seam leaks in the room

7

(5)

Unit 2/3 EDG Operability with elevated Ultimate Heat Sink (UHS) Temperature

71111.18 - Plant Modifications

Temporary Modifications and/or Permanent Modifications (IP Section 03.01 and/or 03.02)

(1 Sample)

The inspectors evaluated the following temporary or permanent modifications:

(1)

Engineering Change 622852, Revision 2, Containment Cooling Service Water 16"

Pipe Replacement - DIV I Line 2-1510-16"-D Pipe Penetration on 517" Elevation of

the Turbine Building

71111.19 - Post-Maintenance Testing

Post-Maintenance Test Sample (IP Section 03.01) (5 Samples)

The inspectors evaluated the following post maintenance test activities to verify system

operability and functionality:

(1)

Unit 2 Station Blackout Diesel Generator surveillance run after scheduled

maintenance window on January 30, 2020

(2)

Unit 3 HPCI on February 27, 2020

(3)

Containment vent and purge isolation valve on February 28, 2020

(4)

Unit 2 RPIS power supply replacement on February 25, 2019

(5)

Unit 2 EDG on March 11, 2020

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated D2F59 forced outage due to generator hydrogen leak,

which began in December 2019 and ended on January 3, 2020

71111.22 - Surveillance Testing

The inspectors evaluated the following surveillance tests:

Surveillance Tests (other) (IP Section 03.01) (6 Samples)

(1)

Unit 2/3 EDG Monthly Surveillance on January 6, 2020

(2)

Unit 3 HPCI Fast Start Surveillance under Work Order (WO) 04733340-01

(3)

Unit 2/3 B Isolation Condenser Makeup Pump Quarterly Operability under

WO 04982736-01

(4)

Recirculation pump DP indication and setpoint calibration on March 20, 2020

(5)

Electromatic relief valve and Target Rock valve calibration and functional test on

March 31, 2020

(6)

Unit 2 HPCI, Core Spray and LPCI Verification systems discharge piping are full of

water, WO 05003761-01, WO 0500370-01, and 05003762-01 on February 19, 2020

8

Inservice Testing (IP Section 03.01) (1 Sample)

(1)

3A Core Spray In-service Test on February 3, 2020

71114.02 - Alert and Notification System Testing

Inspection Review (IP Section 02.01-02.04) (1 Sample)

(1)

The inspectors evaluated the following maintenance and testing of the alert and

notification system:

2018 Annual Preventive Maintenance

2019 Annual Preventive Maintenance

71114.03 - Emergency Response Organization Staffing and Augmentation System

Inspection Review (IP Section 02.01-02.02) (1 Sample)

(1)

The inspectors evaluated the readiness of the Emergency Preparedness

Organization

71114.05 - Maintenance of Emergency Preparedness

Inspection Review (IP Section 02.01 - 02.11) (1 Sample)

(1)

The inspectors evaluated the maintenance of the emergency preparedness program

71114.06 - Drill Evaluation

Drill/Training Evolution Observation (IP Section 03.02) (1 Sample)

The inspectors evaluated:

(1)

2020-Out-of-Box Evolution-03B on January 28, 2020

RADIATION SAFETY

71124.03 - In-Plant Airborne Radioactivity Control and Mitigation

Permanent Ventilation Systems (IP Section 03.01) (1 Sample)

The inspectors evaluated the configuration of the following permanently installed ventilation

systems:

(1)

Unit-2/3 Standby Gas Treatment System and Control Room Emergency Ventilation

System (CREVS) Diagram M-49

9

Temporary Ventilation Systems (IP Section 03.02) (1 Sample)

The inspectors evaluated the configuration of the following temporary ventilation systems:

(1)

Temporary portable high-efficiency particulate air (HEPA) ventilation unit located in

the Unit-3 reactor building 545' shutdown cooling heat exchanger room

Use of Respiratory Protection Devices (IP Section 03.03) (1 Sample)

(1)

The inspectors evaluated the licensees use of respiratory protection devices

Self-Contained Breathing Apparatus for Emergency Use (IP Section 03.04) (1 Sample)

(1)

The inspectors evaluated the licensees use and maintenance of self-contained

breathing apparatuses

71124.04 - Occupational Dose Assessment

Source Term Characterization (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated licensee performance as it pertains to radioactive source

term characterization

External Dosimetry (IP Section 03.02) (1 Sample)

(1)

The inspectors evaluated licensee performance as it pertains to external dosimetry

that is used to assign occupational dose

Internal Dosimetry (IP Section 03.03) (1 Sample)

The inspectors evaluated the following internal dose assessments for actual internal

exposures:

(1)

Dose assessment of individuals potentially exposed to airborne radioactivity during

the clean up and inspection of Unit 2 steam jet ejector 2-300B valve on

November 11, 2019, Doc: DR-02-19-00808

Special Dosimetric Situations (IP Section 03.04) (1 Sample)

The inspectors evaluated the following special dosimetric situations:

(1)

Dose assessment for two declared pregnant workers

10

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification

The inspectors verified licensee performance indicators submittals listed below:

EP01: Drill/Exercise Performance (IP Section 02.12) (1 Sample)

(1)

3rd quarter 2019 through 4th quarter 2019

IE01: Unplanned Scrams per 7000 Critical Hours Sample (IP Section 02.01) (2 Samples)

(1)

Unit 2 1st quarter through 4th quarter 2019

(2)

Unit 3 1st quarter through 4th quarter 2019

EP02: ERO Drill Participation (IP Section 02.13) (1 Sample)

(1)

3rd quarter 2019 through 4th quarter 2019

IE03: Unplanned Power Changes per 7000 Critical Hours Sample (IP Section 02.02)

(2 Samples)

(1)

Unit 2 1st quarter through 4th quarter 2019

(2)

Unit 3 1st quarter through 4th quarter 2019

EP03: Alert & Notification System Reliability (IP Section 02.14) (1 Sample)

(1)

3rd quarter 2019 through 4th quarter 2019

IE04: Unplanned Scrams with Complications (USwC) Sample (IP Section 02.03) (2 Samples)

(1)

Unit 2 1st quarter through 4th quarter 2019

(2)

Unit 3 1st quarter through 4th quarter 2019

71153 - Followup of Events and Notices of Enforcement Discretion

Event Followup (IP Section 03.01) (1 Sample)

(1)

The inspectors evaluated Loss of Power to Non-Power Block Buildings and licensees

response on March 12, 2020

Event Report (IP Section 03.02) (1 Sample)

The inspectors evaluated the following licensee event reports (LERs):

(1)

LER 05000249/2019-001, Unit 3, Degraded Differential Pressure Indicating Switch in

the LPCI Loop Select Logic Caused by Water Damage Results in a Condition

Prohibited by Technical Specifications (ADAMS Accession No. ML19325C091). The

inspection conclusions associated with this LER are documented in this report under

Inspection Results Section 71153

11

INSPECTION RESULTS

Unit 2B Low Pressure Coolant Injection Valve Damaged Due To Inadequate Inspection

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000237/2020001-01

Open/Closed

None (NPP)

71111.22

A self-revealed Green finding and associated non-cited Violation (NCV) of 10 CFR 50,

Appendix B, Criterion V, was identified on October 23, 2019. During a performance of a

surveillance test on October 23, 2019, the 2B low pressure coolant injection (LPCI) pump

suction valve 2-1501-5B failed to reopen following closure resulting in the 2B LPCI pump

being declared inoperable. The licensee's evaluation of this failure identified that an

inspection was performed in 2015 with inadequate inspection guidance that should have

identified corrosion of the valve motor limit switch that lead to the failure of the valve.

Description:

On October 23, 2019, the 2-1501-5B was closed during a surveillance test. The valve limit

switch had corroded in position and did not remove the torque switch bypass during valve

closure resulting in the actuator over thrusting the valve by 250 percent of the rated actuator

thrust limit. The actuator springpack, limit switch, torque switch, motor, and operator bolts

were replaced. The valve stem and yoke were inspected and were found to be satisfactory.

Upon closure, the valve could not be reopened and the 2B LPCI pump was declared

inoperable.

The licensee's evaluation of the event determined that this valve had experienced historical

wetting on top of the actuator due to ground water intrusion from as early as 2006. The

ground water leakage was eventually repaired in 2009. In 2010 Exelon operating experience

required a review of risk significant components that had experienced wetting from internal

leakage. The station identified the 2-1501-5B as a component of interest even though it was

not considered a risk significant component. An inspection of the actuator was performed

during the next 6-year preventive maintenance window for the valve in 2015.

On March 3, 2015, the licensee competed Work Order (WO) 01216146 which performed a

PM inspection on the limit switch and torque switch of 2-1501-5B per MA-AA-723-301,

Periodic Inspection of Limitorque Model SMB/SB/SBD-000 Through 5 Motor Operated

Valves. During the PM, the limit switch cover and the torque switch were found degraded.

The torque switch and limit switch cover gasket were replaced, and rust found on the limit

switch cover was cleaned. Pictures taken during this inspection showed the limit switch rotor

base showed signs of corrosion. The corrosion of the limit switch base was not identified, or

at least not recorded, during the inspection. The licensee's evaluation stated that the

procedure guidence was not clear as to what should have been done about the corrosion on

the limit switch base. The inspectors reviewed the licensee's evaluation (which included

pictures of the limit switch rotor in 2015) and the 2015 completed work order. Procedure

MA-AA-723-301, Step 4.4.5 stated, "inspect limit switch compartment for moisture, corrosion,

foreign materials leaking lubricant and casting irregularities. Record inspection results on

Attachment 2." The inspectors determined that, based on the guidance given in the work

order, corrosion found during the inspection was unsatisfactory and should have been

12

addressed either by cleaning or replacement of the limit switch rotor at that time. The

licensee's corrective actions were not complete at the time of the inspection.

Corrective Actions: The licensee replaced the actuator springpack, limit switch, torque

switch, motor, and operator bolts. The valve stem and yoke were inspected and were found

to be satisfactory. The licensee planned to train electrical maintenance personnel on the

results of the equipment failure evaluation.

Corrective Action References: Action Request 04290376, 2-1501-5B Valve Failure During

DOS 1500-01

Performance Assessment:

Performance Deficiency: The failure to follow procedure MA-AA-723-301, Step 4.4.5, in part,

to inspect the limit switch compartment for moisture, corrosion . . . Record inspection results

on Attachment 2, during the inspection of the actuator for 2-1501-5B was a performance

deficiency. Valve 2-1501-5B was a safety-related valve and the inspection of the valve

actuator was an activity that affected quality. Title 10 CFR Part 50, Appendix B, Criterion V,

required that activities affecting quality shall be prescribed by documented instructions,

procedures, or drawings, of a type appropriate to the circumstances and shall be

accomplished in accordance with these instructions, procedures, or drawings.

Screening: The inspectors determined the performance deficiency was more than minor

because it was associated with the Human Performance attribute of the Mitigating Systems

cornerstone and adversely affected the cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent undesirable

consequences. The maintenance technicians that inspected that valve actuator for corrosion

in 2015 failed to identify, document, and correct corrosion that existed on the 2-1501-5B limit

switch actuator. This corrosion later resulted in the failure of the valve during surveillance

testing. The inspectors determined that this example was similiar to IMC 0612, Appendix E,

January 1, 2020, examples 4.c and 4.k.

Significance: The inspectors assessed the significance of the finding using Appendix A,

The Significance Determination Process (SDP) for Findings At-Power. The finding was

screened against the Mitigating Systems cornerstone and determined to be of very low safety

significance (Green) because the inspectors answered no all six questions in IMC 0609,

Appendix A, Exhibit 2, dated December 13, 2019.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to

this finding because the inspectors determined the finding did not reflect present licensee

performance. The cause of this valve failure was greater than three years old and not

considered present performance.

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, requires, in part, that activities affecting quality be prescribed by documented

procedures of a type appropriate to the circumstances and be accomplished in accordance

with these procedures. The licensee established MA-AA-723-301, Periodic Inspection of

Limitorque Model SMB/SB/SBD-000 Through 5 Motor Operated Valves, Revision 10, as the

implementing procedure for WO 01216146, D2 6Y MOV [motor operated valve] Diagnostic

Testing & Limitorque Surv [surveillance] 2-1501-5B, an activity affecting quality.

13

Procedure MA-AA-723-301, Step 4.4.5 states, inspect limit switch compartment for moisture,

corrosion, foreign materials leaking lubricant and casting irregularities. Record inspection

results on Attachment 2.

Contrary to the above, on March 3, 2015, licensee personnel performed an inspection of the

2-1501-5B LPCI 2B pump suction valve, an activity that affected quality, but did not

accomplish the inspection in accordance with procedures that were appropriate to the

circumstances. Specifically, licensee personnel failed to follow Step 4.4.5, of procedure

MA-AA-723-301 by inspecting the 2-1501-5B limit switch compartment with corrosion present

on the limit switch rotor base and did not mark the presence of the corrosion in Attachment 2.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Failure to Account Instrument Uncertainties

Cornerstone

Significance

Cross-Cutting

Aspect

Report

Section

Mitigating

Systems

Green

NCV 05000237,05000249/2020001-02

Open/Closed

None (NPP)

71111.22

The inspectors identified a Green finding and associated non-cited Violation (NCV) of

10 CFR 50, Appendix B, Criterion XI, Test Control, when the licensee failed to account for

instrument uncertainty in surveillance procedures' acceptance criteria for high pressure

coolant injection required flow and Ultimate Heat Sink maximum temperature.

Description:

When using an instrument to measure a quantity, the recorded value will always have an

amount of uncertainty. These uncertainties need to be accounted for to ensure that when a

quality related test is performed the results collected validate the associated SSCs remain

withing licensing and design bases values. During their review, the inspectors noted at least

two safety-related and Technical Specifications (TS) systems' surveillance tests where the

licensee failed to account for said instrument uncertainties. The systems with the deficiencies

identified were the high-pressure coolant injection (HPCI) systems and the Ultimate Heat Sink

(UHS).

For the HPCI systems, the TS Surveillance Requirement (SR) 3.5.1.6 required the licensee

"to verify the HPCI pump can develop a flow rate greater than or equal to 5,000 gpm against

a system head corresponding to reactor pressure." The UFSAR Table 6.3-20b described the

HPCI LOCA analysis value for the Minimum Rated Flow Over Range as 5,000 gpm. After

conversations with the licensee, it was also established that Technical Specifications pump

flows were used as inputs into the LOCA analyses without adjustments for uncertainty. This

condition was repeated as the licensee transitioned through different nuclear fuel vendors

(GE, Westinghouse, and Areva). Procedure DOS 2300-03, "High Pressure Coolant Injection

System Operability and Quarterly IST Verification Test," Revision 11, was the implementing

procedure to comply with TS SR 3.5.1.6. Step H.5.a and Data Sheet 2 to this procedure

established a HPCI flow of equal or greater than 5,000 gpm in order to meet the procedure's

acceptance criteria. Flow was measured using Flow Controller FIC 2(3)-2340-1. In

licensee's calculation NED-I-EIC-0109, Revision 6, Section 13, "Conclusions", the associated

flow instrument uncertainties were determined (these vary depending on the model of the

instrument installed and the unit it is installed). The average instrument uncertainty

14

associated with FIC 2(3)-2340-1 was +/- 255 gpm under normal plant conditions and +/- 846

gpm under accident conditions.

For the UHS, the TS Surveillance Requirement 3.7.3.2 required the licensee to verify the

average water temperature of the UHS was less than or equal to 95 degrees Fahrenheit (F).

The UFSAR Section 6.2.1.3, Table 6.2-7 and Section 9.5.5 described 95 degrees F as the

maximum inlet water temperature for the Diesel Generator Cooling Water and the

Containment Cooling Service Water systems. Both of these systems are supplied by the

UHS. A sampling review of calculations related to the UHS and supplied systems also noted

that 95 degrees F was the maximum UHS supplied water temperature assumed (Reference

calculations ATD-0400, "Unit 2/3 Diesel Generator Jacket Water Capacity", Revision 0; and

DRE98-0077, "Dresden HPCI Room Thermal Response with Reduced Room Cooler

Capability", Revision 001C). Procedure Unit 2(3) Appendix B, "Assist NSO and Common

Unit Daily Surveillance Log" Revision 90, was the implemented procedure to comply with TS

SR 3.7.3.2. Attachment A to this procedure established an acceptance criteria for the UHS

average water temperature of less than or equal to 95 degrees F as measure by instrument

TR 2/3-4441-16. The licensee informed the inspectors that instrument TR 2/3-4441-16

had an uncertainty of +/- 1 degree F when measuring temperatures between 90 and

100 degrees F.

Based on the above, the inspectors were concerned that failure to account for said

uncertainties could result in a situation where a surveillance test was declared satisfactory

when in reality the structure system or component (SSC) could be within the unacceptable

results range once uncertainties were considered. Since these were safety-related and TS

SSCs a failed TS Surveillance would result in the SSC becoming inoperable and the

associated LCO action statement must be entered. A review of the results from the last time

the affected surveillances were performed showed results which were satisfactory even when

accounting for uncertainties.

In addition, based on the licensee's initial understanding of this issue, the inspectors believed

an extent of condition would reveal additional surveillance tests which fail to account for

instrument uncertainties. This concern was shared with the licensee. The licensee was

evaluating if an extent of condition review was needed.

Corrective Actions: The licensee has validated, currently, there are no challenges to meeting

Technical Specifications Surveillance Requirements, and the affected equipment remains

operable and able to perform their function. In addition, the licensee was recommending:

1) to revise procedures for HPCI (DOS 2300-03) and UHS (Daily Surveillance Log

Appendix B) to account for instrument uncertainty; 2) revise setpoint calculations output

listings to designate the associated surveillance procedure; and 3) perform extent of condition

review.

Corrective Action References: AR 04315614, NRC Question on DOS 2300-03 Acceptance

Criteria

AR 04317369, NRC Ultimate Heat Sink (UHS) Inspection Question

AR 04318639, NRC UHS Open Question 011-2

AR 04331189, NRC Procedures and Instrument Uncertainty

15

Performance Assessment:

Performance Deficiency: The licensee surveillance procedures' acceptance criteria for HPCI

required flow and UHS maximum temperature failed to account for instrument uncertainty.

This was contrary to Title 10 CFR Part 50, Appendix B, Criterion XI, Test Control, and was a

performance deficiency.

Screening: The inspectors determined the performance deficiency was more than minor

because if left uncorrected, it would have the potential to lead to a more significant safety

concern. Specifically, implementing the acceptance criteria as written, without accounting for

the associated instruments' uncertainty, could result in a satisfactory test result, when in

actuality the SSCs had failed the surveillance test. Since the acceptance criteria values used

in the procedure are the same as those used in Technical Specifications and their associated

analysis, this would have resulted in the licensee failing to declare the associated equipment

inoperable, entering the required TS Limiting Condition of Operation (LCO) action and

potentially place the plant in an unanalyzed configuration. This is consistent with the

guidance provided in IMC 0612, Appendix E, Example 3.g.

Significance: The inspectors assessed the significance of the finding using Appendix A, The

Significance Determination Process (SDP) for Findings At-Power. Specifically, the

inspectors determined this finding is of very low safety significance (Green) because: the

performance deficiency was not a design or qualification issue; it did not represent a loss of

the system function; the associated trains were neither inoperable for greater than its allowed

outage time nor was it inoperable for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />; and were not part of an external

event mitigating system. The inspector was unable to find an example where the deficient

procedures resulted in an actual failed surveillance test.

Cross-Cutting Aspect: Not Present Performance. No cross-cutting aspect was assigned to

this finding because the inspectors determined the finding did not reflect present licensee

performance.

Enforcement:

Violation: Title 10 CFR Part 50, Appendix B, Criterion XI, Test Control, requires, in part, that

a test program be established to assure that all testing required to demonstrate that

structures, systems, and components will perform satisfactorily in service is identified and

performed in accordance with written test procedures which incorporate the requirements and

acceptance limits contained in applicable design documents.

For high pressure coolant injection, a safety-related SSC:

Procedure DOS 2300-03, "High Pressure Coolant Injection System Operability and Quarterly

IST Verification Test," Revision 11, is the implementing procedure to comply with applicable

design documents. Section H of this procedure, "Acceptance Criteria", include step H.5.a

which states "The HPCI pump develops a flow of greater than or equal to 5000 gpm against a

system head corresponding to reactor pressure head with reactor pressure greater than or

equal to 920 psig and less than or equal to 1005 psig. (Tech Spec SR 3.5.1.6)."

For the Ultimate Heat Sink, a safety-related SSC:

Procedure Unit 2(3) Appendix B, "Assist NSO and Common Unit Daily Surveillance Log,"

Revision 90, is the implemented procedure to comply with applicable design documents.

Attachment A to this procedure was a table which included the established acceptance

16

criteria for the UHS average water temperature of less than or equal to 95 degrees F as

required by TS SR 3.7.3.2.

Contrary to the above, as of March 11, 2020, the licensee failed to assure that the testing

required to demonstrate that the HPCI and UHS systems would perform satisfactorily in

service was identified and performed in accordance with written test procedures which

incorporated the requirements and acceptance limits contained in applicable design

documents, as evidenced by the following examples:

1) Specifically, for the HPCI systems' procedure DOS 2300-03, Revision 117, the licensee

failed to account for instrument uncertainties when establishing the acceptance criteria to

ensure successful completion of these tests would ensure the associated SSCs would remain

operable and within the acceptable limits as determined by applicable design documents.

2) Specifically, for the UHS system's procedure Appendix B, Revision 90, the licensee failed

to account for instrument uncertainties when establishing the acceptance criteria to ensure

successful completion of these tests would ensure the associated SSCs would remain

operable and within the acceptable limits as determined by applicable design documents.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

Differential Pressure Indicating Switch Failure in Low Pressure Coolant Injection Loop Select

Logic

Cornerstone

Severity

Cross-Cutting

Aspect

Report

Section

Not

Applicable

Severity Level IV

NCV 05000249/2020001-03

Open/Closed

Not

Applicable

71153

A self-revealed Severity Level (SL) IV NCV of Technical Specifications (TS) 3.3.5.1,

Emergency Core Cooling System (ECCS) Instrumentation, was identified when the licensee

determined during routine surveillance testing that one of four (4) channels of the recirculation

pump high differential pressure function was inoperable for longer than the 24-hour allowed

outage time.

Description:

This LER is associated with a Differential Pressure Indicating Switch (DPIS) failure in the Low

Pressure Coolant Injection (LPCI) Loop Select Logic that was inoperable for greater than the

TS LCO 3.3.5.1. On September 20, 2019, while performing LPCI reactor recirculating pump

A and B Differential Pressure Indication switch channel calibration and channel functional test

(DIS 1500-09), it was determined that DPIS 3-0261-35C was inoperable. The licensee

entered TS LCO 3.3.5.1 condition C, replaced DPIS 3-0261-35C and restored operability

within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Licensee operations staff requested a past operability evaluation of the Unit

3 LPCI Loop selection design function.

On June 20, 2019, water from the Unit 3 East LPCI corner room cooler was leaking (AR

04258407) onto the instrument rack that contained the DPIS 3-0262-35C. The licensee

installed a deflector to prevent water from dripping onto the instrument rack. On July 6, 2019,

a ground was identified (AR 04262209) on the Unit 3 125 VDC battery. The licensee entered

17

DOP 6900-07 (125 VDC Ground Detection) to try and locate and eliminate the ground. The

ground alarm cleared and it was determined that the ground did not affect operability of the

125 VDC system. Two subsequent grounds were identified. The first on July 28, 2019,

(AR 04267550) and the second on August 15, 2019, (AR 04272156) on the Unit 3 125 VDC

battery system which were determined not to affect the operability of the 125 VDC system.

The 125 VDC battery ground issue was resolved when DPIS 3-0262-35C, which was not

qualified for spray or submergence, was replaced on September 20, 2019.

On July 30, 2019, during the reactor recirculation pump running differential pressure switch

functional test, the results for all DPISs were satisfactory, therefore it was reasonable to

conclude that DPIS 3-0262-35C failed and was inoperable between July 30, 2019, and

September 20, 2019. Failure of DPIS 3-0262-35C did not impact the ability of the LPCI

system to perform its safety function in the event of an accident. Failure of one DPIS impacts

one division of LPCI Loop Select Logic, however the unaffected division remains capable of

performing the designed safety function.

Corrective Actions: The DPIS 3-0262-35C was replaced, tested, and the channel of

recirculation pump high differential pressure function was restored to an operable status. The

licensee performed a past operability evaluation for all DPISs that were used to support LPCI

system Loop selection design function and all remained functional with the exception of

DPIS 3-0262-35C. The licensee also performed a corrective action program evaluation to

identify programmatic factors. Service water was isolated to the Unit 3 East LPCI room

cooler until the leak was repaired.

Corrective Action References: AR 04290427, Historical Operability Review for

DPIS 3-0261-35C and AR04280928, DPIS Will Not Trip

Performance Assessment:

The NRC determined this violation was not reasonably foreseeable and preventable by the

licensee and therefore is not a performance deficiency. The inspectors determined that

because the licensee initially took actions to protect the DPIS from the leaking water and

successfully completed the surveillance requirement that specifically tested the DPIS post

leakage, the failure was not reasonably foreseeable and preventable.

Enforcement:

The ROPs significance determination process does not specifically consider the regulatory

process impact in its assessment of licensee performance. Therefore, it is necessary to

address this violation which impedes the NRCs ability to regulate using traditional

enforcement to adequately deter non-compliance. Traditional Enforcement is being used

because a violation existed, however, there was no performance deficiency. The inspectors

used the Interim Guidance for Dispositioning Severity Level IV Violations with No Associated

Performance Deficiencies, issued June 15, 2018 (ML18158A220).

Severity: This violation is characterized as a Severity Level IV NCV based on its similarity to

SL IV example 6.1.d.1 in the Enforcement Policy.

Violation: Dresden Nuclear Power Station, Unit 3 TS 3.3.5.1, "Emergency Core Cooling

System Instrumentation," Condition C requires, in part, that if one or more channels are

inoperable, the channel must be restored to operable status within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

18

Contrary to the above, from July 30, 2019, to September 20, 2019, one or more channels

associated with TS 3.3.5.1, Condition C, was inoperable and was not restored to an operable

status within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Specifically, the 3A reactor recirculation pump DPIS 3-0261-35C was

inoperable due to water intrusion on June 20, 2019, which eventually caused the DPIS to fail.

Enforcement Action: This violation is being treated as a non-cited violation, consistent with

Section 2.3.2 of the Enforcement Policy.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

On April 8, 2020, the inspectors presented the integrated inspection results to

Mr. P. Karaba, Site Vice President, and other members of the licensee staff.

On February 28, 2020, the inspectors presented the Radiation Protection inspection

results to Mr. P. Boyle, Plant Manager, and other members of the licensee staff.

On March 12, 2020, the inspectors presented the Triennial Heat Sink inspection results

to Mr. P. Boyle, Plant Manager, and other members of the licensee staff.

On March 27, 2020, the inspectors presented the Emergency Preparedness Program

inspection results to Mr. P. Karaba, Site Vice President, and other members of the

licensee staff.

19

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

71111.01

Procedures

OP-DR-108-111-

1004

Cold Weather Strategy

00

71111.04

Corrective Action

Documents

04190166

3-1105-B 3B SBLC Pmp Relief Valve did not Lift at Set Point

10/31/2018

04296647

2A SBLC Heat Trace Not Working Properly

11/12/2019

04304584

3B SBLC RV Failed Testing

12/17/2019

04313364

Evaluate Ops SBLC Tank Level Surv Acceptance Criteria

01/28/2020

2693730

2/3-5748-2B Indicating Short

07/18/2016

4272885

2/3 B ISO Cond M/U Pump Failed to Start Initially

08/19/2019

4318748

2-1301-607 Has a 1 Drop per 10 Second Packing Leak

02/17/2020

4319355

Fuel Leak on 2/3 B ISO Cond Make Up Pump

02/19/2020

4321473

NRC Question

02/25/2020

4321772

Loose Handlewheel Found

02/26/2020

Drawings

20600-001

High Pressure Coolant Injection (HPCI) System and

Instrumentation

05

20700LN001-001

Unit 2 Isolation Condenser System

03

DOP 1300-M1/E1

Unit 3 Isolation Condenser System Checklist

26

Miscellaneous

Dresden UFSAR

13

Procedures

DOP 1100-M1/E1

Unit 3 Standby Liquid Control (SBLC) System Checklist

16

DOP 1300-M2

Isolation Condenser Makeup Pump Fuel Oil System

03

DOP 2300-01

High Pressure Coolant Injection (HPCI) System Standby

Operation

59

DOP 2300-M1/E

Unit 2 HPCI System Checklist

39

DOP 2300-MI/E1

Unit 2 HPCI System Checklist

39

DOP 2300-MI/E1

Unit 2 HPCI System Checklist

39

DOP 6600-01

Diesel Generator 2(3) Preparation for Standby Operation

34

DOP 6600-E1

Unit 3 Standby Diesel Generator

06

DOP 6600-E1

Unit 2 Standby Diesel Generator

04

DOS 1100-02

Standby Liquid Control Tank Heater Surveillance Test

17

71111.05

Corrective Action

Documents

4290524

Fire Door #67 on 545' Elevation Degraded but Functional

10/23/2019

4290768

Fire Door 67 Inoperable

10/24/2019

4318345

Operations 4.0 Critique for Fire Drill (Crew 4, 2-15-2020)

02/15/2020

20

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Corrective Action

Documents

Resulting from

Inspection

4309021

U2 EDG Fire Door 17A Inoperable

01/09/2020

4309433

NRC Questions Regarding EDG Fire Doors & U2 DW O2

Analyzer

01/10/2020

4311928

NRC Question Regarding EDG Fire Door Failure Mechanism 01/22/2020

4313138

NRC Identified Issues

01/27/2020

Drawings

12-2350B

Schematic Diagram Diesel Generator 2 Auxiliaries and Start

Relays

AP

12E-2311

Key Diagram Turbine Building 480V Motor Control Centers

28-2 and 29-2

AV

12E-2595

Schematic Diagram Fire Protection Co2 System Part 2

W

M-974

Diagram of Diesel Generator Room Ventilation

L

Fire Plans

117 U3RB-20

Dresden Generation Station Pre-Fire Plan FZ 11.1.1

3

173 U3TB-84

Dresden Generation Station Pre-Fire Plan FZ 8.2.8A

4

Miscellaneous

D1620

Kinnear (Division of HARSCO Corporation) Automatic

Closing Atler Doors

000

TRM

Gaseous Suppression System B 3.7.k

65

Procedures

88-4-26

Checklist No. 1; Acceptance Criteria

0

DFPP 4175-01

Fire Barrier

24

DFPS 4145-01

Cardox System Operability Test

35

OP-AA-201-003

Fire Drill Performance

17

OP-AA-201-003,

Attachment 1

"Sample" - Fire Drill Record

17

71111.07T

Calculations

87-0870/915

Unit 3 Diesel Cooling Water Pump NPSH, Fuel Oil Line

Pressure Head and Air Start Receiver Valve Pressure

Rating Evaluation

1C

ATD-0400

Unit 2/3 Diesel-Generator Jacket Water Cooler Capacity

0D

ATD-0400

Unit 2/3 Diesel-Generator Jacket Water Cooler Capacity

0

ATD-0400

Unit 2/3 Diesel-Generator Jacket Water Cooler Capacity

0B

CMED-057604

Evaluation of the Functional Capability of Components

Located in Dresden Unit 3 EQ Zones 4, 5, 6, for Elevated

Temperature due to Loss of Room Coolers

1

DRE03-0026

Analysis of the Intake Canal, CCSW Heat Exchanger, and

Temporary Pumps Following a Dam Failure and 1 Inch

LOCA

1

21

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

DRE16-0011

Required Ultimate Heat Sink (UHS) Capacity

0A

DRE16-0011

Required Ultimate Heat Sink (UHS) Capacity

0

DRE98-0077

Dresden HPCI Room Thermal Response With Reduced

Room Cooler Capability

1C

RSA-D-92-06

HPCI Room Thermal Response With Loss of HPCI Room

Cooler at Dresden Station

0

Corrective Action

Documents

0770694

Enhance Accuracy for Intake Temperature Monitoring

05/01/2008

1021725

U3 DGCW Flanges Less Than B16.5 Minimum Thickness

01/26/2010

1084166

DTP 09: Small Steam Leak

06/24/2010

2532555

UHS Insp. - Calc for DGCW Pumps Based at 501 Elevation

07/24/2015

2532734

UHS NRC Insp. - Basis for UHS Vol. (2 Million Gallons)

07/25/2015

2533713

Further Information for IR 02532555

07/28/2015

3949714

U3 HPCI Room Cooler Fan Degraded

12/06/2016

3984974

Unit 3 HPCI Room Cooler Eddy Current Results

03/14/2017

4058405

DTP 09: Small Steam Leak on HPCI Turbine Poppet Valves

10/02/2017

4093842

Small U3 HPCI Room Cooler Leak Identified by NLO on

Rounds

01/16/2018

4109028

HPCI Room Cooler Tube Plugging

02/27/2018

4110057

Unit 3 HPCI Turbine-CV Rack Steam Leak at Flange Mating

Surf.

03/01/2018

4204847

Leak Identified During VT-2 Inspection of CREVS Cooling

12/20/2018

4206201

Bathymetric Survey Results for 2018

12/27/2018

4206210

U2 HPCI Room Cooler Leak Identified

12/27/2018

4206439

UFSAR Update Required to Address UHS Related Issue

12/28/2018

4227793

Strategic Engineering Review of 2018 UHS Survey Results

03/08/2019

4297362

Bolted Connection 20 DPM Leak on 2B LPCI Room Cooler

11/14/2019

4309911

DTP 09 - Steam Leak on HPCI Turbine

01/13/2020

Corrective Action

Documents

Resulting from

Inspection

4316968

U3 Diesel Generator Cooling Water Pump

02/11/2020

4316989

NRC - Scaffolding Left Past due Date Near 3D CCSW Pump

02/11/2020

4317210

NRC Identified Corrosion on SW Elbow in U3 HPCI Room

02/12/2020

4317369

NRC Ultimate Heat Sink (UHS) Inspection Question

02/12/2020

4317374

NRC Question on U3 EDG CWP Motor Cooler Inspection

02/12/2020

4317695

DOS 6600-08 Opportunity to Improve Writers References

02/13/2020

22

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4318541

NRC UHS Inspection - Basis for HPCI Operability in UFSAR

02/17/2020

4318639

NRC UHS Open Question 011-2

02/17/2020

4318708

NRC Question of 50.59 Screening

02/17/2020

4322212

2020 UHS Inspection: DRE16-0011 UFSAR Timely Update

02/28/2020

4322375

2020 NRC UHS Inspection: UFSAR Revision UHS Volume

02/28/2020

4322395

2020 UHS Inspection - NRC Calculation Question

02/28/2020

4323025

2020 UHS Inspection - IR 2533713 Action not Complete

03/02/2020

4325402

Timber Mat Contact

03/10/2020

Engineering

Changes

363202

ENGR Review Material Change and EDG Thermal Report

for EDG Heat Exchangers

0

382082

Licensing Basis of the Ultimate Heat Sink (UHS) and the

Impact of Silting

0

403120

Computation of DGCW Pumps NPSHA During Dam Failure

0

629625

Licensing Basis of the Ultimate Heat Sink (UHS) Credited

Volume and UFSAR Update

0

Engineering

Evaluations

2020-02-001

Update to UFSAR Description of the Ultimate Heat Sink

(UHS) Credited Volume

0

Miscellaneous

23218036.00

2018 Bathymetric/Volume Survey of the Intake/UHS Canal

10/25/2018

23219026.00

2019 Bathymetric/Volume Survey of the 2/3 Intake/UHS

Canal

10/23/2019

50384

BEM Condition Assessment of 24" Carbon Steel Piping

CCSW Unit 2 - 2-1505-24"

12/03/2019

AH1406-

40656587

Long Range Guided Wave Ultrasonic Pipe Screening

Results

06/18/2019

AH1406-

40656587PIMS

Long Range Guided Wave Ultrasonic Pipe Screening

Results

06/24/2019

EA Project No.

1500411

2017 Bathymetric Survey of the Intake Canal at Exelon

Generation Company's Dresden Generating Station

1

SL-013900

Field Surveillance Report Annual Lake Monitoring and

Examination of Circulating Water Canals August 2017

0

SL-014493

Field Surveillance Report Annual Lake Monitoring and

Examination of Circulating Water Canals June 2018

0

SL-015035

Field Surveillance Report Annual Lake Monitoring and

Examination of Circulating Water Canals June 2019

0

23

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Operability

Evaluations08-005

U3 EDG Cooling Water (DGCW) Heat Exchanger (HX) Flex

Hoses

2 10-006

U3 EDG Jacket Water Inlet Temperature Running Higher

Than Normal

2

Procedures

DIP 3900-01

Diesel Generator Cooling Water Flow Indicator and Pump

Suction and Discharge Gauge Preparation for In-Service

Testing

9

DIS 3900-03

Diesel Generator Cooling Water Pump Suction and

Discharge Pressure Indicator Calibration

13

DOA 0010-01

Dresden Lock and Dam Failure

36

DOA 0010-01

Dresden Lock and Dam Failure

35

DOA 0010-S1

Key Phone Numbers for DOA 0010 Block Procedures

16

DOS 0010-01

Dresden Dam Failure Equipment Test

23

DOS 6600-08

Diesel Generator Cooling Water Pump Quarterly and

Comprehensive/Preservice Test for Operational Readiness

and In-Service Test (IST) Program

65

ER-AA-2002

System and Equipment Health Monitoring

22

ER-AA-340-1002

Service Water Heat Exchanger Inspection Guide

8

ER-AA-700-1003

Screening and Evaluation of Potential Aging Issues

4

Work Orders

01102337

D3 2Y PM Standby Diesel Generator Inspection

01/27/2010

01545660

D3 6Y PM Standby Diesel Generator Inspection

02/23/2018

01592255

D3 8Y PM Replace HPCI Room Cooler Cooling Coil

05/03/2019

01640181

D3 2Y TS D/G CLG WTR PMP Comprehensive Test for IST

Program

07/29/2015

01709946

D3 6Y PM D/G Conduct Eddy Current Test 3-6669-A

02/26/2016

01709947

D3 6Y PM D/G Conduct Eddy Current Test 3-6669-B

02/26/2016

01711473

D3 2Y PM Standby Diesel Generator Inspection

02/25/2016

01711473(SUP)

Supplemental - 00006645-10, PMSR, D3 2Y PM Standby

Diesel Generator Inspection, E: 3-6601, DGNA, E15

02/22/2016

01837703

D3 4Y PM D/G CLG WTR Pump Press. Gauge CAL

09/18/2019

04706728

D3 2Y TS D/G CLG WTR PMP Comprehensive Test for IST

Program

09/16/2019

04797971

U3 HPCI Room Cooler Degrading

05/03/2019

24

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

04799354

D3 AN COM Inspections of Buried Piping

05/29/2019

04799356

D2/3 AN COM Inspections of Buried Piping

05/29/2019

04870742

D1/2/3 AN PM River Temp Recorder Cal.

01/09/2020

04962726

D3 QTR TS (IST) EDG CLG WTR PMP Test for IST

Program Surviel.

12/19/2019

99207934

D3 6Y PM Standby Diesel Generator Inspection

11/13/2006

71111.11Q Miscellaneous

2020-OBE-03B

LORT OBE

Jan 2020

71111.12

Corrective Action

Documents

4323125

U3 RBM 7 Iprm Input Downscale Trip Ref out of Tolerance

03/02/2020

Miscellaneous

Maintenance Rule

System Basis

Document

Dresden, Unit 3, Rod Block Monitor (RBM)

02/26/2020

Maintenance Rule

System Basis

Document

Dresden, Unit 3, Reactor Protection System (RPS)

02/26/2020

MR Function

Evaluation

Dresden, Unit 3, Reactor Protection System

01/03/2020

MR Function

Evaluation

Dresden, Unit 3, U3 0708-2-N

01/03/2020

Procedures

Inspection

Procedure

71111.12

Maintenance Effectiveness

01/01/2020

71111.13

Corrective Action

Documents

4318369

Momentary Loss of Half the Core RPIS Indications

02/16/2020

Drawings

274LN001-001

Turbine Building Closed Cooling Water (TBCCW)

1

Miscellaneous

Protected Equipment Lists for Unit 2 and Unit 3 Risk

Significant Systems

ER-AA-600-1042

On-Line Risk Management

11

OP-AA-108-117

Protected Equipment List - ADS

02/23/2020

Procedures

DOP 6400-13

Electrical Yard Switching

55

DOP 6400-13

Electrical Yard Switching

55

DOS 1100-04

Standby Liquid Control System Quarterly/Comprehensive

Pump Test for the Inservice Test (IST) Program

53

DOS 1100-04

Standby Liquid Control System Quaterly/Comprehensive

53

25

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Pump Test for the Inservice Testing (IST) Program

DOS 5750-04

Control Room Train B HVAC and Air Filtration Unit

Surveillance

55

DOS 5750-04

Control Room Train B HVAC and Air Filtration Unit

Surveillance

55

MA-DR-771-403

Unit 3 - 4 KV Tech Spec Undervoltage and Degraded

Voltage Relay Routines

15

OP-AA-108-117

Protected Equipment Program

5

Work Orders

04982736-01

D2/3 Qtr Com 'B' Iso Cond Make-up Pump Operability

02/19/2020

050008840

IMD TS&R RPIS Power Supply (PSX6)

02/17/2020

71111.15

Calculations

ATD-0400

Unit 2/3 DG Jacket Water Cooler Capacity

0

ATD-0400

Unit 2/3 Diesel Generator Jacket Water Cooler Capacity

000A

Calibration

Records

127-1-B33-1

Relay Routine for 4 KV Buss 33-1 Undervoltage Relays

02/10/2020

127-2-B33-1

Relay Routine for 4 KV Buss 33-1 Undervoltage Relays

02/10/2020

Corrective Action

Documents

347338

DG Ventilation Calculation Weaknesses

06/24/2005

4162726

High Vibes on U3 HPCI Room Cooler

08/08/2018

4244414

Unexptected Alarm 903-4 C-22 Due to 3-2301 Opening

04/29/2019

4262603

IEMA Question Related to IR 4244414 3-2301-14 Valve

Opening

07/08/2019

4312803

Integrated Risk Mitigation

01/26/2020

4315913

NRC Question Regarding DOP 7500-01 Limitations and

Actions

02/06/2020

4315913

NRC Question Regarding DOP 7500-01 Limitations and

Actions

02/06/2020

4316185

NRC SRI Question on Procedural Guidance

02/07/2020

4316185

NRC SRI Question on Procedural Guidance

02/07/2020

4316185-02

NRC SRI Question on Procerdural Guidance

02/25/2020

4316326

Review of STI-16-011

02/08/2020

Corrective Action

Documents

Resulting from

Inspection

04329174

NRC DOP 7500-01 Limitations

03/24/2020

26

71111.15

Drawings

12E-3530

Schematic Diagram High Pressure Coolant Injection

Auxiliary Valves

X

12E-3684D

Wiring Diagram Reactor Building 250V DC Motor Control

Center 3 Part 1 (3-83250-3B)

V

13524-DGI-N102

Environmental Zone Map (Basement Floor Plan) Elev.

476'6" Figure 1

5

277LN001-001

CCSW Subsystem 1

05

M-374

Diagram of High Pressure Coolant Injection Piping

CX

Miscellaneous

Dresden UFAR

4

Operations Log

01/22/2020 -

01/29/2020

Design

Engineering

0006216498

Dresden Unit 2, HPCI Room Cooler Operability System

Code 1500, 2300, 3900

07/07/2000

Dresden Internal

Flood Evaluation

Summary and

Notebook

Table 3.3.1 Isolation of Standby Systems

4

Letter from

Commonwealth

Edison to A.

Giambusso, U.S.

Atomic Energy

Commissioin

Dresden Station Units 2 and 3 - Special Report No. 37 -

Analysis of Pipe Breaks Outside Containment - AEC

Dockets 50-237 and 50-249

01/23/1974

Procedures

DES 8300-14

Security UPS, Computer UPS, Lake Lift Station, Unit 1,

HCVS SBO 125VDC, 345KV Switchyard, 138KV Switchyard

and 34.5KV Switchyard Batteries Maintenance

32

DIS 2300-06

Unit 3 HPCI Room Temperature Switch Layout

18

DOP 1500-02

Torus Water Cooling Mode of Low Pressure Coolant

Injection System

70

DOP 1500-02

LPCI/CCSW Operation During Transient Situations

70

DOP 6600-05

Diesel Generator 2/3 Startup

42

DOP-1500-03

Containment Spray Cooling Mode of Low Pressure Coolant

Injection System

37

DOS 8300-14

Non-Safety Related 125 VDC and 250 VDC Battery

Surveillance

30

27

ER-AA-425-1001

Surveillance Test Interval (STI) Change Request

DRE-16-011

0

WC-AA-101

Dedicated Operator - Proprietary

29

71111.19

Corrective Action

Documents

4313545

Air Leak on 2A SBO Eng Start Air LB Supply AOV Iso Vlv

01/29/2020

4313609

U2 SBO 'A' Engine Low Oil Temp

01/29/2020

4313832

U2 SBO D/G Lube Oil Temp Proc Enhancement to DOP

6620-16

01/30/2020

4313837

Ops U2 SBO 'A' Diesel Low Jacket Water and Lube Oil T/S

01/30/2020

Drawings

12E-6870A

Schematic Diagram Engine A/B 125V DC Starting/Auxiliary

Equipment Station Blackout

A

20600-001

High Pressure Coolant Injection (HPCI) System and

Instrumentation

05

M-4308A

Diesel Generator Starting Air Piping and Instrument Diagram

Station Blackout

B

Miscellaneous

Operations Log

01/29/2020

Dresden 7 Day Schedule

01/27/2020

Procedures

DOS 2300-03

Initial HPCI Standby Lineup

117

DOS 2300-03

High Pressure Coolant Injection System Operability and

Quarterly IST Verification Test

117

DOS 6600-01

Diesel Generator Surveillance Tests

143

DOS 6600-08

Diesel Generator Cooling Water Pump Quarterly and

Comprehensive/Preservice Test for Operation Readiness

and In-Service Test (IST) Program

66

DOS 6620-07

SBO 2 (3) Diesel Generator Surveillance Tests

48

DOS 6620-07

SBO 2(3) Diesel Generator Surveillance Tests

48

ER-AA-321

Administrative Requirements for Inservice Testing

13

MA-DR-MM-5-

66001

Diesel Generator Post Maintenance Testing Run

19

Work Orders

01002305

D2 12Y PM Diesel Cooling Water Pump Motor Replacement

02/03/2020

01573090

D2 8Y EQ Replace ASCO SOL on DW Purge Valve 1601-56

01/21/2020

04774873

D2 AN COM Replacement Air Start Regulating Valve on

EDG

02/03/2020

04829226

Proactive Replacement of U2 EDG Potential Transformer

03/10/2020

04987753

Proactive Replacement of 2-6699-114 Swing Check Valve

03/10/2020

28

71111.19

Work Orders

05001931

D3 QTR TS (IST) HPCI Pump Operability Test and IST

Surveillance

02/07/2020

05008145

D2 1M TS (IST) Unit Diesel Generator Operability

03/01/2020

71111.20

Corrective Action

Documents

4308111

DOA 6100-01 Entry for TR2 Cooling

01/05/2020

4308854

4.0 Critique for D2F59 Startup

01/05/2020

Procedures

DOA 5600-01

Turbine Trip

35

DOA 6100-01

Main Transformer Trouble

37

DOS 1600-10

Drywell Closeout Inspection Plan

51

OP-AA-108-108

Start-Up Checklist

20

71111.22

Calculations

NED-I-EIC-0109

HPCI Pump Discharge Flow Loop Accuracy and Minimum

Flow Setpoints Essential Calc

6

NED-I-EIC-0109

Instrument Uncertainty Calculation for FIC-2(3)-2340-I

6

Corrective Action

Documents

04290376-09

2-1501-5B Valve Failure During DOS 1500-01

12/12/2019

4310164

4.0 Critique U3 HPCI Fast Start Surveillance

01/13/2020

4319355

Fuel Leak on 2/3 B ISO Cond Makeup Pump

02/19/2020

Drawings

M-4203

Flow Diagram Isolation Condenser Make Up System

G

Procedures

DIS 0202-05

Recirc Pump dP Indication and Setpoint Calibration

06

DOS 1300-03

2/3A(B) Isolation Condenser Makeup Pump Quarterly

Operability

26

DOS 2300-03

High Pressure Coolant Injection System Operability and

Quarterly IST Verification Test

117

DOS 2300-07

High Pressure Coolant Injection Fast Initiation Test

45

Unit 2(3)

Appendix B

Assist NSO and Common Unit Daily Surveillance Log

90

Work Orders

01216146

D2 6Y MOV [Motor Operated Valve] Diagnostic Testing &

Limitorque Surv [Surveillance] 2-1501-5B, an Activity

Affecting Quality.

03/03/2015

04795477

D3 8Y PM Recirc Pump DP Indication & Setpoint Cal

03/20/2020

04966573-01

OP D3 QTR TS HPCI Pump Oper Test and IST Surv

01/13/2020

04966573-01

D3 Qtr TS (IST) HPCI Pump Oper Test and IST Surv

01/13/2020

71111.22

Work Orders

04983344-01

D3 QTR [quarterly] TS [Technical Specification] CS [Core

Spray] Pump Test with Torus Available for IST [In-Service

Test] Data Surv [Surveillance]

02/03/2020

04985748-01

D2/3 1 M TS Unit Diesel Generator Operability

01/06/2020

71114.02

Corrective Action

04116367

EP-Siren Failure (DR02)

03/19/2018

29

Documents

04145905

EP-Siren Failure (BD10)

06/11/2018

04154129

Siren Failures (DR01, DR06)

07/09/2018

04167408

EP-Siren Failure (BD02)

08/27/2018

04208595

EP- Siren Failure (DR27)

01/07/2019

04223376

EP-Siren Failure (DR09)

02/25/2019

04229307

EP-Siren Failure (BD18)

03/14/2019

04269606

EP-Siren Failure (BD05)

08/05/2019

04292284

Inadvertent Siren Activation Of Will County Sirens

10/29/2019

04294339

EP-Siren Failure (DR01)

11/04/2019

04295174

EP-Will County Siren Controller Failure

11/05/2019

04300920

EP- Siren Failure BD11

12/02/2019

04309736

EP-Siren Failure (DR15,DR22)

02/20/2020

Miscellaneous

Braidwood/Dresden 2018 Warning System Maintenance and

Operational Reports

Braidwood/Dresden 2019 Warning System Maintenance and

Operational Reports

Dresden Generating Station Alert and Notification System

(ANS) Design Report

71114.03

Corrective Action

Documents

04176439

EP . Drive-In Drill / Off Hours Drill Program Administration

09/24/2018

04176441

EP. Drive-In Drill / Off Hours Drill Facilities and Equipment

09/24/2018

04176442

EP . Drive-In Drill / Off Hours Drill Combined FAC

Comments

09/24/2018

04198974

Individual's ERO FMT Qualification Expiring

11/29/2018

04270502

3rd Quarter TSC inventory Issues

08/08/2019

04271572

3rd Quarter EP Mazon Relocation Center Inventory Issues

08/09/2019

04327348

Field Team Inventory 1Q2020 Items

03/17/2020

Miscellaneous

4th Quarter 2019 Call-In Augmentation Drill Results

12/17/2019

3rd Quarter 2019 Call-In Augmentation Drill Results

09/16/2019

4th Quarter 2018 Call-In Augmentation Drill Results

12/03/2018

Dresden 2018 Drive-In and Off Hours Drill Evaluation Report

08/29/2018

EP-AA-112

Emergency Response Organization (ERO) - Emergency

Response Facility (ERF) Activation and Operation

22

71114.05

Corrective Action

Documents

AR04263019

DR-EP-2019-PEX-MCR-FAILED-DCS

06/25/2019

AR04263022

DR-EP-2019-PEX-TSC-FAILED-DCS

06/25/2019

AR04263026

DR-EP-2019-PEX-OSC-FAILED-DCS

06/25/2019

30

AR04268534

DR-EP-2019-NRC-MCR-FAILED-DCS

07/30/2019

AR04268535

DR-EP-2019-NRC-TSC-FAILED-DCS

07/30/2019

AR04268537

DR-EP-2019-NRC-OSC-FAILED-DCS

07/30/2019

AR04316875

Documentation of Completing hh2/155b Requirement

02/11/2020

Miscellaneous

Dresden Letters of Agreement Annual Review List 2019

EP-AA-1000

Standardized Radiological Emergency Plan

33

EP-AA-1004

Radiologicaly Emergency Plan Annex For Dresden Station

38

Self-Assessments NOSA-DRE-18-

03

Emergency Preparedness Audit Report for Dresden Station

04/18/2018

NOSA-DRE-19-

03

Emergency Preparedness Audit Report for Dresden Station

04/24/2019

71124.03

Calibration

Records

DTS-7500-07

Standby Gas Treatment System Air Filter Unit Performance

Requirements (Methyl Iodide Removal and Charcoal Leak

Test

04/23/2018

MSA Posi3

  1. L04480

Posi3 USB Test Results; Facepiece/Airline Apparatus Test

06/062019

RP-AA-825-101

MSA SCBA FireHawk Monthly Inspection list

11/06/2019

Corrective Action

Documents

AR-04219788

Unexpected Condition during SCBA Air Compressor

Preventive Maintenance

02/13/2019

AR-04245762

Precautionary Measure for SCBA Bottle from Surveillance

05/02/2019

Drawings

M-49 Critical

Control Room

Drawing

Diagram of Standby Gas Treatment (SBGT)

12

Miscellaneous

NCS Corporation

  1. 0040599

Radioiodine Penetration/Efficiency Test Records SBGT

03/20/2019

PSI #00473572

Quarterly Service Air and Self-Contained Breathing

Apparatus

10/25/2019

RP-AA-825

Respiratory Inspection and Certification Log (Monthly

Inspection)

12/04/2019

71124.04

Calculations

RP-AA-220

Intake Investigation Form #4513

11/07/2019

RP-AA-220

Intake Investigation Form #9316

01/09/2019

RP-AA-220

Intake Investigation Form #023119

01/09/2019

RP-AA-220

Intake Investigation Form # 040479

01/09/2019

Calibration

Records

NVLAP Lab

Code: 100518

NVLAP Certificate of Accreditation; Landauer, Inc

01/01/2020

Miscellaneous

RP-AA-270

Declaration of Pregnancy Form #SEGAT6114

09/17/2019

31

RP-AA-270

Declaration of Pregnancy Form #027354

03/27/2019

71152

Corrective Action

Documents

Resulting from

Inspection

4317754

NRC ID: Cables Running Into Plant by U3 Trackway

02/13/2020

71153

Corrective Action

Documents

04280928

CAPE DPIS Will Not Trip

02/20/2020

04290427

Historical Operability Review for DPIS 3-0261-35C

10/23/2019

04326046

Security - Loss of Power Affects EWS Zones/Cameras

03/12/2020

Corrective Action

Documents

Resulting from

Inspection

04319675

The NRC Resident Question of LER -2019-001-00

03/21/2020

Procedures

DOA 0040-03

Loss of Power to Non-Power Block Buildings

18