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Category:MONTHLY OPERATING ANALYSIS REPORT
MONTHYEARML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20249A4121998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7501998-04-30030 April 1998 Rev 2 to Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit ML20247F6721998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Davis-Bess Nuclear Power Station,Unit 1 ML20249A4141998-04-30030 April 1998 Revised Monthly Operating Rept for Apr 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216B4041998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20216C5131998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20202D3721998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20198K7931997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20203A3931997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Davis-Besse Nuclear Power Plant,Unit 1 ML20198S5371997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Davis-Besse Nuclear Power Station ML20217H7701997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20216H3261997-08-31031 August 1997 Monthly Operating Rept for August 1997 for DBNPS ML20217K0241997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Davis Besse Nuclear Power Station,Unit 1 ML20140H0441997-05-31031 May 1997 Monthly Operating Rept for May 1997 for Davis-Besse Nuclear Power Station Unit 1 ML20141B9521997-04-30030 April 1997 Monthly Operating Rept for Apr 1997 for Davis-Beese Nuclear Power Station Unit 1 ML20137T5271997-03-31031 March 1997 Monthly Operating Rept for Mar 1997 for Davis-Besse Nuclear Power Station,Unit 1 ML20136G7221997-02-28028 February 1997 Monthly Operating Rept for Feb 1997 for Davis-Besse Nuclear Station Unit 1 ML20134L9831997-01-31031 January 1997 Monthly Operating Rept for Jan 1997 for Dbnps,Unit 1. W/Undated Ltr ML20133G0161996-12-31031 December 1996 Monthly Operating Rept for Dec 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20149M4071996-11-30030 November 1996 Monthly Operating Rept for Nov 1996 for Davis-Besse Nuclear Power Station Unit 1 ML20134P9821996-10-31031 October 1996 Monthly Operating Rept for Oct 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20128Q0611996-09-30030 September 1996 Monthly Operating Rept for Sept 1996 for Davis-Besse NPP, Unit 1 ML20117D5341996-07-31031 July 1996 Monthly Operating Rept for July 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20117D5411996-06-30030 June 1996 Revised MOR for June 1996 for Davis-Besse Nuclear Power Station,Unit 1 ML20116E0161996-06-30030 June 1996 Monthly Operating Rept for June 1996 for Davis-Besse Nuclear Station Unit 1 ML20113B9111996-05-31031 May 1996 Monthly Operating Rept for May 1996 for Davis-Beese Nuclear Power Station Unit 1 ML20117H7231996-04-30030 April 1996 Monthly Operating Rept for Apr 1996 for Davis-Besse Unit 1 ML20112E6061996-03-31031 March 1996 Monthly Operating Rept for Mar 1996 for David-Besse Nuclear Power Station,Unit 1 ML20101G5251996-02-29029 February 1996 Monthly Operating Rept for Feb 1996 for DBNPS Unit 1 ML20149K7711996-01-31031 January 1996 Monthly Operating Rept for Jan 1996 for Davis-Besse Nuclear Power Station.W/Undated Ltr ML20096C7971995-12-31031 December 1995 Monthly Operating Rept for Dec 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20095H3761995-11-30030 November 1995 Monthly Operating Rept for Nov 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20094L1041995-10-31031 October 1995 Monthly Operating Rept for Oct 1995 for Davis-Besse Nuclear Power Station Unit 1 ML20093J2341995-09-30030 September 1995 Monthly Operating Rept for Sept 1995 for Davis-Besse Nuclear Power Station ML20098A2651995-08-31031 August 1995 Monthly Operating Rept for Aug 1995 for Davis-Besse Nuclear Power Station,Unit 1 1999-09-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K1231999-10-14014 October 1999 Revised Positions for DBNPS & PNPP QA Program ML20217D5441999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1998-011, :on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle1999-09-0303 September 1999
- on 981014,manual Reactor Trip Occurred.Caused by Component Cooling Water Sys Leak.Breaker Being Installed Into D1 Bus cubicle.AACD1 Was Removed from Cubicle
ML20211R0811999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1999-003, :on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With1999-08-26026 August 1999
- on 990727,failure to Perform Engineering Evaluation for Pressurizer Cooldown Rate Exceeding TS Limit Was Noted.Caused by Inadequate Procedural Guidance.Provided Required Reading for Operators.With
ML20211B0271999-08-13013 August 1999 SER Accepting Second 10-year Interval Inservice Insp Requests for Relief RR-A16,RR-A17 & RR-B9 for Plant, Unit 1 ML20210Q8541999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20209E6231999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-013, :on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With1999-06-24024 June 1999
- on 981105,safety Valve Rupture Disks May Induce Excessive Eccentric Loading of Pressurizer Vessel Nozzles.Caused by Failure of RCS Pressure Boundary.Plant Mod Was Implemented in May of 1999.With
ML20212H9961999-06-22022 June 1999 Safety Evaluation Supporting Amend 233 to License NPF-3 ML20195K2871999-06-16016 June 1999 Safety Evaluation Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G6661999-06-0808 June 1999 Safety Evaluation Supporting Amend 232 to License NPF-3 ML20195F4871999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U7371999-05-19019 May 1999 Safety Evaluation Supporting Amend 231 to License NPF-3 ML20207E8011999-05-19019 May 1999 Non-proprietary Rev 2 to HI-981933, Design & Licensing Rept DBNPS Unit 1 Cask Pit Rack Installation Project ML20207F4351999-05-0404 May 1999 Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504 ML20206M6341999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Davis-Besse Nuclear Station,Unit 1.With ML20205M2931999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Davis-Besse Nuclear Power Station.With 05000346/LER-1999-002, :on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With1999-03-0505 March 1999
- on 990208,both Trains of Emergency Ventilation Sys Were Rendered Inoperable.Caused by Unattended Open Door. Door Was Immediately Closed Upon Discovery.With
ML20207J1461999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Davis-Besse Nuclear Power Station,Unit 1.With ML20206U2441999-02-0909 February 1999 Safety Evaluation Supporting Amend 229 to License NPF-3 ML20199H5931999-01-20020 January 1999 Safety Evaluation Accepting Thermo-Lag Re Ampacity Derating Issues for Plant ML20204J6751998-12-31031 December 1998 1998 Annual Rept for Dbnps,Unit 1,PNPP,Unit 1 & BVPS Units 1 & 2 ML20199E2501998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20205K5781998-12-31031 December 1998 Waterhammer Phenomena in Containment Air Cooler Swss ML20206B0101998-12-31031 December 1998 1998 Annual Rept for Firstenergy Corp, for Perry Nuclear Power Plant & Davis-Besse Nuclear Power Station.Form 10-K Annual Rept to Us Securities & Exchange Commission for Fiscal Yr Ending 981231,encl ML20197J3441998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-012, :on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With1998-11-17017 November 1998
- on 981018,reactor Trip Occurred from Approx 4% Power Due to ARTS Signal.Caused by Inadequate Design Drawing Resulting in Inadequate Procedure.Procedure Revised to Correct Deficiency.With
05000346/LER-1998-009, :on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With1998-11-13013 November 1998
- on 980909,RCS Pressurizer Spray Valve Was Not Functional with Two of Eight Body to Bonnet Nuts Missing. Caused by Less than Adequate Matl Separation Work Practices. Bonnet Nuts Replaced.With
05000346/LER-1998-011, :on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With1998-11-13013 November 1998
- on 981014,manual RT Due to Ccws Leak Was Noted.Caused by Failure of One Letdown Cooler Rupture Disk. All Letdown Cooler Rupture Disks Were Replaced Prior to Plant Restart.With
ML20195D0001998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Davis-Besse Nuclear Power Station,Unit 1.With ML20155B6781998-10-28028 October 1998 Safety Evaluation Accepting Proposed Reduction in Commitment Changes in QA Program Matl Receipt Insp Process 05000346/LER-1998-010, :on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with1998-10-26026 October 1998
- on 980924,manual Reactor Trip Was Noted.Caused by Misdiagnosed Failure of Main FW Control Valve Solenoid Valve.Faulty Solenoid valve,SVSP6B1,was Replaced & Tested. with
05000346/LER-1998-008, :on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With1998-10-0101 October 1998
- on 981001,documented Proceduralized Guidance for Initiation of Post LOCA B Dilution Flow Path.Caused by Design Analysis Oversight.Revised Procedures to Provide Active B Dilution Flow Path Guidance.With
ML20154H5801998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Davis-Besse Nuclear Power Station,Unit 1.With 05000346/LER-1998-007, :on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With1998-09-22022 September 1998
- on 980824,CR Humidifier Ductwork Failure Caused Excessive Opening in Positive Pressure Boundary. Caused by Less than Adequate Fabrication.Evaluation of CR Humidifiers Conducted.With
ML20151W1611998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Dbnps.With 05000346/LER-1998-006, :on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources1998-08-21021 August 1998
- on 980624,loss of Offsite Power Was Noted. Caused by Tornado Damage to Switchyard.Tested & Repaired Affected Electrical & Mechanical Equipment Necessary to Restore Two Offsite Power Sources
ML20237E3171998-08-21021 August 1998 ISI Summary Rept of Eleventh Refueling Outage Activities for Davis-Besse Nuclear Power Station ML20237B1681998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236U5011998-07-23023 July 1998 Special Rept:On 980624,Unit 1 Site Damaged by Tornado & High Winds.Alert Declared by DBNPS Staff,Dbnps Emergency Response Facilities Activiated & Special Insp Team Deployed to Site by Nrc,As Result of Event ML20236R1441998-07-15015 July 1998 SER Related to Quality Assurance Program Description Changes for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-004, :on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired1998-07-13013 July 1998
- on 980601,ductwork for Number 2 Control Room Humidifier Found Disconnected from Humidifier.Caused by Less than Adequate Connection at Humidifier Blower Housing. Ductwork Repaired
05000346/LER-1998-005, :on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations1998-07-11011 July 1998
- on 980601,both Low Pressure Injection/Dhr Pumps Were Rendered Inoperable During Testing.Caused by Inadequate Self Checking,Communication & Procedure Usage Work Practices.Operations Mgt Reviewed Expectations
ML20236M9411998-07-0707 July 1998 Safety Evaluation Supporting Amend 225 to License NPF-3 ML20236K3981998-06-30030 June 1998 SER Accepting in Part & Denying in Part Relief Requests from Some of ASME Section XI Requirements as Endorsed by 10CFR50.55a for Containment Insp for Davis-Besse Nuclear Power Station,Unit 1 ML20236N7451998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Davis-Besse Nuclear Power Station,Unit 1 ML20236K4321998-06-30030 June 1998 Safety Evaluation Supporting Amend 224 to License NPF-03 ML20236K5131998-06-29029 June 1998 Safety Evaluation Accepting Proposed Alternate Emergency Operations Facility Location for Davis-Besse Nuclear Power Station,Unit 1 05000346/LER-1998-003, :on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure1998-06-18018 June 1998
- on 980519,Mode 3 Entry Without Completion of Surveillance Requirement Occurred.Caused by Failure of I&C Technicians to Perform Each Sp as Written or Adherence. Revised Procedure
1999-09-30
[Table view] |
Text
AVERAGE DAILY UNIT POWER LEVEL v
DOCKET NO.
Davis-Besse Unit 1
.lT January 8, 1980 DATE Erdal Caba COMPLETED BY 419-259-5000, Ext.
TELEPfl0NE 236 December, 1979 MONTil i
DAY AVER AGE DAILY POWER LEVEL DAY AVER AGE DAILY POWER LEVEL (MWe-Net )
(MWe Net) 0 1
0 37 0
2 0
gg 0
0 39
,3 0
0 4
20 0
0 21 5
0 0
22 6
0 0
7 23 0
0 24 8
0 0
9 25 0
10 0
26 O
0 II 27 0
0 12 28 0
0 29 13 0
0 30 14 0
0 15 31 0
16 INSTRUCTIONS On this format. list the aserage daily unit power lesel in MWe. Net for each day in the reporting month. Compute to the nearest whole megawatt.
90017282 em, N
.80u1140
'4 OPERATING DATA REPORT DOCKET NO. 50-346 DATE January B, 1980 COMPLETED BY Erdal Caba TELEPilONE 419-259-5000, Ext.
236 OPERATING STATUS Davis-Besse Unit 1 Notes
- 1. Unit Name:
December, 1979
- 2. Reporting Period:
2772
- 3. Licensed Thermal Power (MWt):
925
- 4. Nameplate Rating (Gross MWe):
906
- 5. Design Electrical Rating (Net NWe):
p; s'
- 6. MEimum Dependable Capacity (Gross MWe): to be deterrained
'~
t be determined l
- 7. Masimum Dependable Capacity (Net MWe):
(/
- 8. Il Changes Occur in Capacity Ratings (items Number 3 Through 7) Since Last Report. Give Reasons:
~
i None
- 9. Power Level To Which Restricted,if Any (Net MWe):
- 10. Reasons For Restrictions,if Any:
This Month Yr. to Date Cumulative i
744 8,760 20,525
- 11. Ilours In Reporting Period 29.1 4,332.4 10,964.2
- 12. Number Of flours Reactor Was Critical 0
2,085.5 2,875.8
- 13. Reactor Reserve Shutdown Hours 0
4,141.6 9,874.8
- 14. Hours Generator On Line 0
1.728.2 1.728.2
- 15. Unit Resene Shutdown ilours 806 10,011,937 20,199,507
- 16. Gross Thermal Energy Generated (MWil) 0 3,339,756 6,723,511 j
- 17. Gross Electrical Energy Generated (MWil) 0 3,129,118 6,170,578
- 18. Net Electrical Energy Generated (MWil) 0 47.3 49.5
- 19. Unit Service Factor 0
67.0 58.8
- 20. Unit Availability Factor to be determined
- 21. Unit Capacity Factor iUsing MDC Net) 0
,_39.4 36.2 J
22; Unit Capacity Factor (U>ing DER Net) 100 28.5 27.6 l
- 23. Unit Forced Outage Rate
- 24. Shutdowns Scheduled Oser Next 6 Months (Type.Date.and Duration of Eacht:
Refueling Outage, March 1980 12 weeks January 5, 1980
- 25. If Shut Down At End Of Report Period. Estimated Date of Startup:
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achiesed
. INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCI A L OPERATION 90017283 m72)
O
OPERATIONAL SUFD!ARY
~
DECEMBER, 1979 The unit-shutdown which' was initiated on November 30, 1979 to investigate the motor lower bearing oil level alarm on Reactor Coolant Pump (RCP) 1-2; to fix.
Group 7 Rod 5 and Group 5 Rod 11 APIS was still in. progress throughout the month of December. The following is a list of-the major work items performed during the outage:
1.
The RCP 1-2 motor lower bearings oil leak was thoroughly investigated.
' j No. concrete reason for the low IcVel was found.- It was possibly due to filling the motor.when it was running which caused a syphon effect.
2.
Group 7 Rod 5 and Group 5 Rod'11 APIS were fixed.
3.
Shortly after the shutdown, RTD RC3A3 failed, and it was though~t that there was a primary leak through the RTD.
It was later determined that the leakage was through the furmanited gasket and into the thermocouple extension piece. The furmanite box had come into contact with a Reactor Coolant System (RCS) piping whip restraint bending the RTD boss and RTD, j
cracking the extension piece. This in turn allowed water to leak into
~
the RTD head and short out_the signal.
Subsequently, it was found that
~
the two furmanited RTDs on Loop 2 were both damaged by the furmanite boxes contacting whip restraints. On Loop 1 there was a slight dent in the bosses due to the whip restraints contacting the pipe. _ Three of the J
bosses were replaced and new well type RTDs were also installed. The 1
repairs to the bosses _ were completed on December 26, 1979.
4.
Due to the extended outage several eighteen month' surveillance tests were completed.
90017284 4
I
]
9 E
S q
g y -
.y
~
2 b
50-346' DOCKET NO.
Davis-Fesse Unit l' UNIT SHUTDOWNS AND FOWER REL" '.TIONS UNIT NAME January 8. 1930 DATE COMPLETED BY Erdal Caba REPORT MONTil December, 1979 TELEPi!ONE 419 M9-5000 Ext. 236 Cause & Corrective Eg 3
Y Licensee Eg o
No.
Date g
5=
jis Event gg 9's Action to Prevent Recurrence yU mv H
f:
j ;7, -
Report e 6
20 79 11 30 S
11.4 B
1 NA NA NA Maintenance outage due to a low (Continued) bearing oil level alarm on Reactor F
732.6 Coolant Pump 1-2.,
see Operational Summary for further details.
e 3
CD C3 m
N 3
4
- N I 2
Method:
Exhibit G-Instructions W
F: Forced Reason:
1-Manual for Preparation of Data W
5: Schedu!ed A-Equipment Failure (Explain) 2 Manual Scram.
Entry Sheets for Licensee B-Maintenance of Test Event Report (LER) File (NUREG-3-Automatic Scram.
C Refueling 4-Other (Explain) 0161)
D Regulatory Restrictiim E Operatur Trainin;& License Examination 5
F-Administ rative
' Exhibit I - Same Source G-Operation.il Enor (Explain)
(9/77)
I1.Other (INplain) p-
4 w
~'
S 9
DATE:
Decenher, 1979
\\
REFUELING INFORMATIO.1 Davis-Besse Nuclear Power Station Unit 1 1.
Name of f acility:
March, 1980 Scheduled date for next refueling shutdown:
2.
June. 1980 Scheduled date for restart following refueling:
3.
Will refueling or resumption of operation thereaf ter require a technical If answer is yes, whar, 4.
specification change or other license amendment?If answer is no, has the reload f in general, will those be?
r Plant Safety Review Committee and core configuration been reviewed by you' to determine whether.any unreviewed safety questions are associated with the core reload (Ref.10 CFR Section 50.59)?
Yes, see attached Scheduled date(s) for submitting proposed licensing action and supporting 5.
information.
December, 1979 Important licensing considerations associated with refueling, e.g., new or
~ ifferent fuel design or supplier, unreviewed design or performance analysis 6.
methods, significant changes in fuci design, new operating procedures.
d The spent fuci pool capacity expansion program was approved by the NRC 1, 1979.
in Amendment 19 to the operating license received August The number of fuel assemblics (a) in the core and (b) in the spent fuel 7.
storage pool.
0 (zero) 177' (b).
(a)
The present licensed spent fuel pool storage capacity and the size of any increase in licensed storage capacity that has been requested or is planned, 8.
in number of fuel assemblies.
0 (zero)
Present 735 Increase size by The projected date of the last refueling that can be discharged to.the spent 9
fuel pool assuming the present licensed capacity.
j 1989 (assuming ability to unload the entire core into the spent fuel pool is maintained and the unit goes to an 16 monta retueling cycle)
Date-9.0017286
~
g
i REFUELING INFORMATION Continued Page 2 of 2 December, 1979 4.
The following Technical Specifications (Part A) will require revision:
2.1.1 & 2.1.2 - Reactor Core Safety Limits (and Bases) 2.2.1 - Reactor Protection System Instrumentation Setpoints (and Bases) 3.1.3.6 - Regulating Rod Insertion Limits 3.1.3.7 - Rod Program 3.2.1 - Axial Power Imbalance (and Bases)
The following Technical Specifications (Part A) may also require revision:
3.1.2.8 & 3.1.2.9 - Borated Water Sources (and Bases) 3.2.4 - Quadrant Power Tilt (and Bases) 3.2.5 - DNB Parameters (and Bases) 90017287 f
9 e
g-COMPLETED FACILITY CHANGE REQUESTS i
FCR NO:
79-378 (including Supplements 1 through 4)
SYSTEM: Various Class 1E Systems COMPONENT:
125 VDC Control Relays CHANGE, TEST, OR EXPERIMENT:
On November 19, 1979, the installation and testing associated with the implementation of FCR 79-378 and its four supplements was com-
?
plcted. As requested by the FCR, arc suppression diodes were installed in various saf ety related and non-saf ety related circuits where the contacts of Couch relays are controlling highly inductive loads (generally the coils of other relays). A total of 26 safety related circuits was involved including 4 control relays in the auxiliary feedwater pump controls, 18 in switchgear controls, and 4 in emergency diesel generator controls.
l REASON FOR THE FCR:
It was found that failures of Couch relays which occurred in the reactor coolant pump interlock circuitry (see Licensee Event Report NP-33-7 9-126) had been caused by the high transient voltage which occurs when the Couch relay contacts interrupt the current flow through a highly inductive load.
The high voltage arcs across the contacts of the Couch relays resulting in a short circuit. The diodes added under this FCR preclude this from occurring by shunting out the transient voltages through a path separate of the relay contacts.
SAFETY EVALUATION: This change will not adversely affect the function of the relays.
It will improve the reliability of the circuits by providing a path for the discharge of the energy in the coil through the diode, rather than through the contacts of the interrupting relay. This is not an unreviewed safety gyestion.
f 90017288 1
e k.
COMPLETED FACILITY CHANGE REQUESTS FCR NO: 79-405 SYSTEM: Reactor Protection System (RPS)
COMPONENT: Power Range Nuclear Instrument (NI) 5 CHANGE, TEST, OR EXPERIMENT: On November 15, 1979, the physical work and testing associated with the implementation of FCR 79-405 was completed.
This FCR moved cables 2LRPSA01C and 2LRPSA01X, which are the leads for the bottom ion chamber signals of NI-5, from penetration cable GW3 to penetration cable DW3 both located in penetration P2L4EX/P2L4GI.
REASON FOR THE FCR: During the performance of IC 2002.03, NI Detector Post Installa-tion Test, it was found that the inner and outer shields on penetration cable GW3 were shorted together.
SAFETY EXPLANATION: The change outlined was reviewed on Bechtel Drawing E-530 and determined to have no adverse impact on safety. The change of modules within This penetration P2L4G will utilize a spare which was provided for this purpose.
is not an unreviewed safety question.
i l
l 90017289 i
4 e
OPERATIONAL
SUMMARY
NOVEMBER, 1979
.The unit shutdown which was initiated on October 25, 1979, when Reactor Coolant Pump (RCP) 2-2 tripped from a blown fuse, continued until 1811 hours0.021 days <br />0.503 hours <br />0.00299 weeks <br />6.890855e-4 months <br /> on November 20, 1979, when the turbine-generator was synchronized.
Below is a list of the major work items performed during the outage:
1.
All four RCP seals were replaced.
2.
A new expansion joint for 1-4-2 heater extraction was rewelded.
3.
A design change to the Couch relays in the RCP starting interlock circuits was made. This initiated a similar change in sixteen safety related cir-cuits.
4.
NI-3 was pulled and a new detector was installed. A new section of cable between the containment penetration and the NI-l pre-amp was installed.
1 5.
Several pir restraints were modified as a result of IE Bulletin 79-14 findings.
11/20/79 - 11/21/79 The unit returned on line at 1811 hours0.021 days <br />0.503 hours <br />0.00299 weeks <br />6.890855e-4 months <br /> on November 20, 1979, and reactor power was increased to 81% of full power with generator gross load at 760 MWe on November 21, 1979.
11/22/79 Reactor Coolant System (RCS) flow inidcation was determined to be less than required by Technical Specification 3.2.5 at 0300 hours0.00347 days <br />0.0833 hours <br />4.960317e-4 weeks <br />1.1415e-4 months <br />.
Reactor power was decreased to 73% at which point RCS flow indication was back within allowable limits. At 0400 hours0.00463 days <br />0.111 hours <br />6.613757e-4 weeks <br />1.522e-4 months <br /> generator gross load was 684 MWe.
11/23/79 - 11/25/79 Reactor power was maintained at approximately 73% until 0620 hours0.00718 days <br />0.172 hours <br />0.00103 weeks <br />2.3591e-4 months <br /> on November 25, 1979, when RCS flow indication was again determined to be less than that required by Technical Specifi-cations.
Reactor power was decreased to 67% at which point the RCS flow indication was again back within tolerance. The cause of the low flow indication is still being investigated.
11/26/79 Reactor power was maintained at approximately 69% of full power.
At 2145 hours0.0248 days <br />0.596 hours <br />0.00355 weeks <br />8.161725e-4 months <br /> on November 26, 1979, RCP 1-2 was manu-ally tripped due to a lower motor bearing low oil level alarm.
11/27/79 - 11/28/79 The unit remained at approximately 68% of full power with generator gross load of 635 MWe until 0645 hours0.00747 days <br />0.179 hours <br />0.00107 weeks <br />2.454225e-4 months <br /> on November 28, 1979, when it was determined that the power range nuclear instrumentation (NIs) were reading slightly greater than 2%
below the calculated heat balance.
Reactor power was reduced to 507-to bring the NIs in tolerance and to run another heat balance to get the NIs in tolerance.
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,. NOVEMBER, 1979 PAGE 2 0F'2 11/29/79 Group 7, Rod 5 was declared inoperahle at 0640 hours0.00741 days <br />0.178 hours <br />0.00106 weeks <br />2.4352e-4 months <br />.initiat-1 ing.a reduction in reactor power to approximately 42% and reset-ting the high flux trip-setpoint 'to 54%.
11/30/79
- Reactor power was reduced and.the turbine-generator taken off line at.1910 hours0.0221 days <br />0.531 hours <br />0.00316 weeks <br />7.26755e-4 months <br /> to investigate the lower motor bearing oil level alarm on RCP 1-2; to fix Group 7,- Rod 5 and Group 5, Rod 11 API.
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