ML20064F235

From kanterella
Jump to navigation Jump to search
/01X-0 on 781108:a Field Mod Was Made to Vessel Lower Head Insulation & the Mod Was Not Seismically Analyzed IAW FSAR Due to Personnel Error.Subsequently Analyzed by Stone & Webster & by Westinghouse
ML20064F235
Person / Time
Site: North Anna Dominion icon.png
Issue date: 11/17/1978
From: Cartwright W
VIRGINIA POWER (VIRGINIA ELECTRIC & POWER CO.)
To:
Shared Package
ML20064F229 List:
References
LER-78-100-01X, LER-78-100-1X, NUDOCS 7811280325
Download: ML20064F235 (2)


Text

~ ~ * = "^" =^=u i

,CONTdOL BLOCK: l l' l l l l lh (PLEASE PRINT CR TYPE ALL REQUIRED INFCRMATION)

I 6

[Ohj l v I A l N l A lS l 1 l@!O l0 l-LICENSE 14 15 l0 l0 -l0 l0 l0 l-lOlOl@l4l1l1l1l1l@!

NUMtFER 25 26 LICENSE TYPE JO l

57 CA r 58 l@

3 8 9 LICENSEE CODE CON'T F6TTl 7 8 "f "C' l i. l@l 0 l 5 10 10 10 l 3 l 3 18 l@l il il 0181 718 @l i i i l i I 7l 7 l R @

S 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121 l A field modification was made to the rancent vaaaal inwar hand inci>1 =ri nn , which i= i O 3 l supported by the incore instrumentation nozzles. and the modification was not sein- l 0 . lmically analyzed as required by the FSAR. This event in renort abl e nn nor T 3 - l l0Isi l6.9.1.8.i. I 10161I I 10171 I I I

Lo_l a.1 1 80

.7 9 SYSTEM CAUSE CAUSE " OMP. VALVE CODE CODE SUSCODE COMPONENT CODE SUSCODE SU8 CODE j7 O 9 8

lClA 9 10 l @ (B_lh l A lh l X13l X l X l X l X l X 11 12 18 lh (Z_jh 19 (Z_j 20 h

,_ SEQUENTI AL OCCURRENCE REPORT REVISION LE R/RO EVENT YE AR REPORT NO. CODE TYPE N O.

hR g l7 l8l [--J l1l0l0l 24 26 l/l 27 l 0l Il 28 29 y

30 l-l 31 l0 l 32

_ 21 22 23 AK N AC ON PL NT M S8 IT FOR B. SU PLIE MANUF C RER yg[34FJ@ (Z lZ l@ l0 p l0 HOURS [22 [Yj@ l [ N_j@ lAl@ l44S l 4 l 2 l 047l@

35_J@

33 36 31 40 41 42 43 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l i l 0 l lThe field modification was not seismically analyzed due to personnel error. We s tinst- l~

i i [ house and Stone & Webster subsequently performed a structural analysis on the incore I g .,j l tubes. Analysis results indicated that, in the event of the worst case earthquake, as I

\

[ q 3 l lmany as 6 incore instrument tubes may yield, but the structural integrity of the tubes l lil41 ]would not be violated. A new modification is presently being developed. l 7 8 9 80 ST S  % POWER OTHER STATUS IS OV RY DISCOVERY DESCRIPTION Vendor li15l(Z)@ l0l9l7l@l_

NA l lDl@l l aC TIVI T Y CO TENT RELE ASED OF RELEASE A...OUNT OF ACTIVITY LOCATION OF RELEASE NA NA

'7 i 6 Is 9 _

(Z ]@ 10

@l 11 44 l l 45 80 l

PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION i 7 l0 l010 l@lZ J@lNA _

I

,EnSONNE L iN2unS NUvsER oESCRIPflON@

l i n

!7 8 9 l0l0l0l@l 11 12 NA 80 l

LOSS OF OR DAMAGE TO FACILtTY TYPE DESCRIPTION NA l lli 191 7 8 9 IZ l@l10 80 l2l0l ISSUEl @ DESCRIPTION NA l l l l l l l l l l l l l lg1 1

81811"80328 n ~.,3 c, ,. p , . 7, : .U. R. Ca rturich t cgg 703-894-5151 {

. Vi'rginic Electric cnd Powar Corptny North Anna Power Station, Unit #1 Atta:chment: Pago 1 of 1 Docket No. 50-338  :

Report No. LER 78-100/01X-0 1 1 Event Description  !

A field modification was made to the reactor vessel lower head insula-tion, which is supported by the incore instrumentation nozzles, and the modification was not seismically analyzed as required in the FSAR. This event is reportable as per T.S. 6.9.1.8.i.

Probable Consequences of Occurrence .

~

The FSAR requires all Class I structures to be seismically analyzed ,

to ensure the safe operation and control of the plant during a seismic  ;

event.

A detailed analysis by Westinghouse and Stone and Webster shows that the continued operation of Unit 1 is acceptable due to the fact that the structural integrity of the tubes will not be violated for the postulated i b, seismic conditio..s of the FSAR.

  • In the event of the occurrence of a seismic event prior to modification, I there would be no effect on the health and safety of the public.

Cause of Occurrence The original design of reflective type insulation would have interfered with the installation of supplementary neutron shielding. A field modification was made to the ' insulation to relieve this interference, but due to personnel error, the modification was not seismically analyzed. '

Immediate Corrective Action Westinghouse, Stone and Webster and Transco performed a structural.  !

! analysis of the insulation. ,

I (. '

It was found that, in the event of the worse case earthquake, as many as 6 in-core instrumentation tubes may yield, but the structural integrity of '

the tubes would not be violated.

Scheduled Corrective Action At the. present time, Westinghouse and Stone and Webster are developing a modification to the insulation which will be installed at the first refuel-ing on Unit #1.

Actions Taken to Prevent Recurrences No further action is required.

i 1

l

_ . _ . . _ . - ,