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Category:DEFICIENCY REPORTS (PER 10CFR50.55E & PART 21)
MONTHYEARML20217N3271999-10-21021 October 1999 Part 21 Rept Re non-linear Oxygen Readings with Two (2) Model 225 CMA-X Containment Monitoring Sys at Bsep.Caused by High Gain Produced by 10K Resistor Across Second Stage Amplifier.Engineering Drawings Will Be Revised ML20134L1081996-10-10010 October 1996 Part 21 Rept Re Defect in Component of Nordberg Model FS1316HSC Sdg.Nak Engineering,Inc Has Established & Adopted Procedures to Assemble Fuel Oil Lines & Climinate Possible Defective Condition ML20116H2031996-08-0505 August 1996 Part 21 Rept Re Potential Defect on Condition in Component of Nordberg Model FS1316HSC Sdg W/Fuel Injection Line Assembly Which Connects Fuel Pump to Injector.Caused by Loose Fuel Line Sleeve ML20097A5641996-01-31031 January 1996 Final Part 21 Rept Re Ball Valves Supplied by Cardinal Industrial Products Containing Suspect Pressure Boundary Bolting.Valves Containing Suspect Bolts Returned to Canadian Worcester Controls Ltd to Have Bolting Replaced ML20092H3641995-09-13013 September 1995 Part 21 Rept Re 3/4 Inch ASME Section III Class 2 Ball Valves Supplied by Canadian Worcester Controls Ltd (Cwcl) ML20059H7721994-01-17017 January 1994 Part 21 Rept Re Virginia Power Notifying Fairbands Morse Via Failure Analysis Rept NESML-Q-058 of Defective Air Start Distributor cam,16104412 ML20059F2631994-01-0707 January 1994 Part 21 Rept Re Air Start Distributor Cam Mfg by Fairbanks Morse.Mfg Suggests That Site Referenced in Encl App I Inspect Air Start Distributor Cam as Soon as Practical BSEP-93-0041, Part 21 Rept Re Mfg Defects Associated W/Westinghouse Type Hmcp & Type Hfd Breakers,Resulting in Possibility That Breaker Contacts May Not Open During Trip.Initially Reported on 930225.Functional Testing Procedures Revised1993-03-26026 March 1993 Part 21 Rept Re Mfg Defects Associated W/Westinghouse Type Hmcp & Type Hfd Breakers,Resulting in Possibility That Breaker Contacts May Not Open During Trip.Initially Reported on 930225.Functional Testing Procedures Revised BSEP-93-0030, Initial Part 21 Rept Re Possible Mfg Defects Associated W/ Westinghouse Type HMCP150 & Type Hfd Breakers Resulting in Possibility That Breaker Contacts May Not Open During Trip Conditions.Evaluation of Corrective Action Underway1993-02-25025 February 1993 Initial Part 21 Rept Re Possible Mfg Defects Associated W/ Westinghouse Type HMCP150 & Type Hfd Breakers Resulting in Possibility That Breaker Contacts May Not Open During Trip Conditions.Evaluation of Corrective Action Underway ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in ABB Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML20095J3061992-04-24024 April 1992 Initial Part 21 Rept Re Defectively Installed Bolting in Emergency Diesel Generator Bldg Internal Wall Seismic Supports.Repairs to Reestablish Seismic Qualification of Walls Continuing & Emergency Buses Declared Inoperable ML20079G8921991-08-27027 August 1991 Part 21 Rept Re Failure of Normally Energized Asco Model L206-832 Solenoid Valves Due to Gelling of Lubricant (Dow Corning 550).Initially Reported on 910826 Via Telcon.Ler 2-91-005 Re ESF Actuations Caused by Transient Encl ML20077A4041991-04-29029 April 1991 Deficiency Rept Re Possible Mfg Problems W/Certain Coils Used on Asco Nuclear Qualified Valves.Problems Discussed in NRC Info Notice 86-057.All Purchasers Will Be Notified & Replacement Product Will Be Offered If Item Still in Svc BSEP-91-0191, Part 21 Rept Re Discrepancy Noted Between Torque Indicated by motor-actuator Characterization Sys & Output Torque Measured by Limitorque Actuator Test Stand.Initially Reported on 910426.Vendor Contacted Re Software Problem1991-04-29029 April 1991 Part 21 Rept Re Discrepancy Noted Between Torque Indicated by motor-actuator Characterization Sys & Output Torque Measured by Limitorque Actuator Test Stand.Initially Reported on 910426.Vendor Contacted Re Software Problem ML20043A6091990-04-27027 April 1990 Part 21 Rept Re Defective Axial Cracks in Pump Shaft in Region Immediately Above Impeller & in Reactor Recirculation Pumps.Probably Caused by Crack Growth as Thermal Fatigue. Technical Advisory Bulletin Will Be Sent to Each Util ML20005G6831990-01-0505 January 1990 Part 21 Rept Re Installation Instructions for Grommet Use Range for Patel Conduit Seal P/N 841206.Conduit Seals in Environ Qualification Applications Inspected for Proper Wire Use Range & Grommets Replaced BSEP-89-1095, Suppl to Part 21 Rept Re Completion of Replacement of Unit 1 CR205 Series Auxiliary Contacts w/CR305 Contacts.Initially Reported on 871030.Implementation of Five of Six Auxiliary Contacts Extended Until 9001311989-12-15015 December 1989 Suppl to Part 21 Rept Re Completion of Replacement of Unit 1 CR205 Series Auxiliary Contacts w/CR305 Contacts.Initially Reported on 871030.Implementation of Five of Six Auxiliary Contacts Extended Until 900131 ML19325E4571989-10-20020 October 1989 Part 21 Rept Re Potential Inconsistencies in Mac Diagnostic Sys Software.Licensee to Review All Smb,Sb & Sbd Size 3 Mac Torque Test Data Using Mac Software Version 2.96 to Insure That Torque Switch Settings Meet Valve Design Requirements BSEP-89-0342, Part 21 Rept Re Problem in Pump Suction & Discharge Valves of Standby Liquid Control Sys.Initially Reported on 890427. Evaluation Found Defect Consisting of Casting Flaws/Surface Irregularities in Valves1989-05-0101 May 1989 Part 21 Rept Re Problem in Pump Suction & Discharge Valves of Standby Liquid Control Sys.Initially Reported on 890427. Evaluation Found Defect Consisting of Casting Flaws/Surface Irregularities in Valves BSEP-87-1205, Part 21 Rept & Deficiency Rept Re Defective GE CR205X Series Auxiliary Contacts.Initially Reported on 871027.Contacts for Loads Listed in Attachment 3 Will Be Replaced on Unit 1 by 880701 & by 881101 on Unit 21987-10-30030 October 1987 Part 21 Rept & Deficiency Rept Re Defective GE CR205X Series Auxiliary Contacts.Initially Reported on 871027.Contacts for Loads Listed in Attachment 3 Will Be Replaced on Unit 1 by 880701 & by 881101 on Unit 2 ML20203D0221986-07-14014 July 1986 Part 21 Rept Re Air Monitoring Sys Probes Exhibiting Blue Tip Rather than Normal White Tip & Insensitive to Chlorine. Caused by Improper Handling/Storage.Advisory Bulletin Encl. Item Not Reportable Per Part 21 ML20206S0841986-06-30030 June 1986 Part 21 Rept Re Possible Cut Wires in Wire Harness of Bbc Brown Boveri K600/K800 Circuit Breakers.Initially Reported on 860509.Safety Implications Listed.Gear Guard Designed to Prevent Cut Wires ML20141N8511986-03-11011 March 1986 Part 21 Rept Re Valves W/Improperly Qualified Cardinal Industrial Products Corp Stock Matl Furnished to Listed Customers.Matl Deviated from ASME Section III,NCA-3800. Results of Test Repts of Stock Valves Forthcoming ML20140A5281985-12-19019 December 1985 Part 21 Rept Forwarding Ltr Sent to Customers Re Check Valves Missing Lock Welds on Hinge Supports or Hinge Support Capscrews,Per 851121 Request.List of Customers Receiving Ltr Also Encl BSEP-85-1850, Part 21 & Deficiency Rept Re 12 of 16 Rockwell Edward Valves Exceeding Leak Rate Criteria as Specified by Procurement Documentation.Initially Reported on 850705. Valves Returned to Vendor for Cause Determination1985-10-18018 October 1985 Part 21 & Deficiency Rept Re 12 of 16 Rockwell Edward Valves Exceeding Leak Rate Criteria as Specified by Procurement Documentation.Initially Reported on 850705. Valves Returned to Vendor for Cause Determination ML20134Q1741985-08-29029 August 1985 Part 21 Rept Re Potential Maint Issues Associated w/Anker-Holth Snubbers.Owners of Anker-Holth Snubbers Will Be Informed of Problems & Sent Revs to Technical Instruction Manuals to Include Procedures for Seal & Fluid Maint ML20210G9921985-08-13013 August 1985 Part 21 Rept Re Failure of Isolated Worm Shaft Gear When Certain Critical Speeds Combined W/Repetitive Transfer of Actuator Clutch Mechanism from Manual (Handwheel) to Motor Drive Mode.Two Possible Solutions Noted ML20133N4691985-08-0505 August 1985 Part 21 Rept Re Raychem Wcsf Shrink Sleeving for Sensor/ Connecting Assembly of Safety Relief Valve Monitoring Sys. Testing & Retesting in Progress.Sensor Installation Utilizing Shrink Sleeving Recommended ML20125B1611985-06-0606 June 1985 Supplemental Part 21 Rept Re Addl Circuit Breakers,Furnished as Spares,W/Overcurrent Trip Devices That May Have Short Time Delay Band Lever.Items Require Insp & Replacement If Link Found Incorrect ML20093M2391984-10-0303 October 1984 Supplemental Response to Part 21 Rept Re Leak or Break on Certain Piping Sys Outside Pipe Tunnel.Initially Reported in Apr 1982.Mods to Resolve Deficiency Scheduled to Be Consistent W/Resolution of Environ Qualification Issue ML20094D8761984-07-13013 July 1984 Second Interim Deficiency Rept,Item 160 Re Defective Shop Welds on Seismic Restraint Structures.Initially Reported on 840306.Next Rept Anticipated by 850331 BSEP-83-1260, Supplemental Response to Part 21 Rept Re Postulated Pipe Crack in Hpci,Rcic,Reactor Water Cleanup Sys & Main Steam Line Drains.Required Mods Will Be Installed to Meet Requirements of Environ Qualification Program1983-04-26026 April 1983 Supplemental Response to Part 21 Rept Re Postulated Pipe Crack in Hpci,Rcic,Reactor Water Cleanup Sys & Main Steam Line Drains.Required Mods Will Be Installed to Meet Requirements of Environ Qualification Program BSEP-83-1220, Part 21 Rept Re Pipe Clamps for Snubber/Struts Oriented in off-axis Direction.Initially Reported on 830224 & by IE Info Notice 83-13.Clamps Will Be Replaced by End of Fall 1983 Refueling Outage1983-04-22022 April 1983 Part 21 Rept Re Pipe Clamps for Snubber/Struts Oriented in off-axis Direction.Initially Reported on 830224 & by IE Info Notice 83-13.Clamps Will Be Replaced by End of Fall 1983 Refueling Outage ML20064L2641983-02-0101 February 1983 Interim Part 21 Rept Re Postulated Pipe Cracks.Initially Reported During Apr 1982.United Engineers & Constructors Evaluating Reactor Bldg Environ Rept & Developing Corrective Actions.Final Rept Expected by 830331 ML20069P0101982-11-30030 November 1982 Part 21 Rept Re Discrepancies Between Orientation of Snubbers as Shown on Pipe Support Details & Orientation as Used in Analysis of Record.Review of Supports,Design & Issue of Any Fixes Scheduled for Completion by 821201 for Unit 1 ML20069K4131982-10-15015 October 1982 Interim Part 21 Rept.Detailed Status of Corrective Actions Taken Will Be Sent by 821020 ML20062L6291982-08-17017 August 1982 Part 21 Rept Re Pipe Stress & Snubber Loads Exceeding Tech Spec for Main Steam & Safety Relief Valve Discharge Lines. Structural Integrity Will Be Assured by Listed Corrective Actions by 821015 ML20063C7661982-08-17017 August 1982 Potential Part 21 Rept Re Defect Concerning Pipe Stress & Support Loads Exceeding Allowable Limits.Initially Reported on 820814.Piping Sys Structural Adequacy Not Jeopardized ML20052G3601982-04-30030 April 1982 Part 21 Rept Re Leak or Break Outside Pipe Tunnel on Connections to Main Feedwater Lines Not Detected &/Or Terminated by Existing Sys.Supplemental Response Will Be Issued by 820831 ML20052A3321982-04-20020 April 1982 Part 21 Rept Re Apparent Lack of Control Over Issuance of Class II Piping,Fittings & Pressure Switches in Class I Applications,Initially Reported 820416.Task Force Organized to Classify Suspect Components.No Related Failures to Date BSEP-81-1359, Final Deficiency Rept on Potential Part 21 Concern Re Incorrect Seismic Analysis.Deficiency Found Not Reportable Under Part 21.No Loss of Safety Function Would Be Necessary to Mitigate Consequences of Accident1981-07-16016 July 1981 Final Deficiency Rept on Potential Part 21 Concern Re Incorrect Seismic Analysis.Deficiency Found Not Reportable Under Part 21.No Loss of Safety Function Would Be Necessary to Mitigate Consequences of Accident BSEP-81-1211, Part 21 Rept Re Failure of RHR Heat Exchanger Baffle Plates. Info Required Has Been Reported in LERs 1-81-32 & 2-81-491981-06-12012 June 1981 Part 21 Rept Re Failure of RHR Heat Exchanger Baffle Plates. Info Required Has Been Reported in LERs 1-81-32 & 2-81-49 ML19344F3431980-09-0303 September 1980 Part 21 Rept Re Leaks in Heat Exchanger Tubes of Calandria Type Radwaste Evaporator at Facility.Cause Attributed to Corrosive Attack.Evaporator Unit Out of Svc Pending Repair of Leaks in Tubes & Shell ML19330B8601980-07-20020 July 1980 Part 21 Rept Re Testing Failure of safety-related Pressure Switches in Toxic Gas Monitors for Chloride.Dwyer Instruments,Inc Notified of Potential Defect & Safety Analysis Requested ML19323J3271980-06-0606 June 1980 Final Part 21 Rept Re Mixed Heat of Steel Supplied by Us Steel from Which 4-inch Elbows & 2-inch Tees Were Mfg to A234WPB Requirement.Investigations Conducted & Closed at 46 Listed Facilities 1999-10-21
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217N3271999-10-21021 October 1999 Part 21 Rept Re non-linear Oxygen Readings with Two (2) Model 225 CMA-X Containment Monitoring Sys at Bsep.Caused by High Gain Produced by 10K Resistor Across Second Stage Amplifier.Engineering Drawings Will Be Revised 05000324/LER-1999-008-02, :on 990920,condenser Pressure Sensing Line Drain Activities Resulted in ESF & RPS Actuation.Caused by Inadequate Implementation of C/A to Previously Identified Condition.Procedures Were Revised.With1999-10-20020 October 1999
- on 990920,condenser Pressure Sensing Line Drain Activities Resulted in ESF & RPS Actuation.Caused by Inadequate Implementation of C/A to Previously Identified Condition.Procedures Were Revised.With
ML20217D7371999-10-0505 October 1999 Safety Evaluation Supporting Amends 206 & 236 to Licenses DPR-71 & DPR-62,respectively 05000325/LER-1999-008, :on 990809,electric Motor Driven & Diesel Driven Fire Pump Concurrent Inoperability Occurred.Caused by Human Performance Error.Diesel Fire Pump Jacket Water Temp Switch Replaced.With1999-10-0101 October 1999
- on 990809,electric Motor Driven & Diesel Driven Fire Pump Concurrent Inoperability Occurred.Caused by Human Performance Error.Diesel Fire Pump Jacket Water Temp Switch Replaced.With
BSEP-99-0168, Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Bsep,Units 1 & 2. with ML20212D0431999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Brunswick Steam Electric Plant,Units 1 & 2 05000325/LER-1999-007-01, :on 990731,CB Emergency Air Filtration Sys Actuation During Chlorine Car Replacement Was Noted.Caused by Small Amount of Residual Chlorine Gas Which Escaped. Evaluated to Determine Enhancements Needed.With1999-08-30030 August 1999
- on 990731,CB Emergency Air Filtration Sys Actuation During Chlorine Car Replacement Was Noted.Caused by Small Amount of Residual Chlorine Gas Which Escaped. Evaluated to Determine Enhancements Needed.With
05000324/LER-1999-007, :on 990714,noted That Overlapping of Safety Systems Outages Resulted in TS Prohibited Operation.Caused by Inadequate Training/Communications Re Implementation of Its.Training Will Be Provided to Operators.With1999-08-13013 August 1999
- on 990714,noted That Overlapping of Safety Systems Outages Resulted in TS Prohibited Operation.Caused by Inadequate Training/Communications Re Implementation of Its.Training Will Be Provided to Operators.With
ML20210P9441999-08-10010 August 1999 Safety Evaluation Accepting Licensee Assessment of Impact on Operation of Plant,Unit 1,with Crack Indications of 2.11, 6.36 & 1.74 Inches in Three Separate Jet Pump Risers ML20210P9181999-08-10010 August 1999 Safety Evaluation Authorizing Request for Reliefs CIP-01,02, 06,07,08,09,10 & 11 (with Certain Exceptions) & 12-18,for Second 10-year ISI Interval.Request CIP-04 & 05 Would Result in hardship,CIP-03 Not Required & CIP-11 Denied in Part ML20210N2341999-08-0505 August 1999 SER Accepting Response to NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issues (USI) A-46 ML20210R1191999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Bsep,Units 1 & 2 05000324/LER-1999-006-02, :on 990628,automatic Reactor SD Occurred.Caused by Condenser Low Vacuum Main Turbine Trip.Reviewed Operational Guidance & Development of Operational Strategy CWIP Trips.With1999-07-28028 July 1999
- on 990628,automatic Reactor SD Occurred.Caused by Condenser Low Vacuum Main Turbine Trip.Reviewed Operational Guidance & Development of Operational Strategy CWIP Trips.With
BSEP-99-0118, Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Bsep,Units 1 & 2. with ML20210R1311999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Bsep,Unit 2 05000324/LER-1999-005-02, :on 990511,determined That as-found Lift Settings for Two SRVs Exceeded TS Setpoint Limits.Cause Indeterminate.Srv Pilot Valve Assemblies Were Replaced with Certified Spares Prior to Startup of Plant.With1999-06-0707 June 1999
- on 990511,determined That as-found Lift Settings for Two SRVs Exceeded TS Setpoint Limits.Cause Indeterminate.Srv Pilot Valve Assemblies Were Replaced with Certified Spares Prior to Startup of Plant.With
05000324/LER-1999-004-02, :on 990502,noted That Reactor Recirculation Sys Pump Discharge Bypass Valve 2-B32-F032B Was Inoperable. Caused by Valve Internal Component Tolerances & Missing Wedge Spring.Subject Valve Was Rebuilt.With1999-06-0101 June 1999
- on 990502,noted That Reactor Recirculation Sys Pump Discharge Bypass Valve 2-B32-F032B Was Inoperable. Caused by Valve Internal Component Tolerances & Missing Wedge Spring.Subject Valve Was Rebuilt.With
BSEP-99-0095, Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With 05000325/LER-1999-006, :on 990423,operation Prohibited by TS Was Noted Due to Missed Srs.Caused by Ineffective Change Mgt During Procedure Development.Revised Procedure OPT-01.14b.With1999-05-24024 May 1999
- on 990423,operation Prohibited by TS Was Noted Due to Missed Srs.Caused by Ineffective Change Mgt During Procedure Development.Revised Procedure OPT-01.14b.With
05000324/LER-1999-003-02, :on 990418,inadequate Augmented Inservice Weld Insps Were Noted.Caused by Incorrect Assumptions by Personnel.Inspected Affected Weld During Current Unit 2 Ro. with1999-05-18018 May 1999
- on 990418,inadequate Augmented Inservice Weld Insps Were Noted.Caused by Incorrect Assumptions by Personnel.Inspected Affected Weld During Current Unit 2 Ro. with
ML20210M8581999-05-14014 May 1999 B214R1 RPV Hydrotest Bolted Connection Corrective Action Evaluation, Rev 0 ML20211L3711999-05-10010 May 1999 Rev 0 to ESR 98-00333, Unit 2 Invessel Feedwater Sparger Evaluation 05000325/LER-1999-005-01, :on 990408,CR Emergency Ventilation Sys Surveillance Inadequacy Was Noted.Caused by Human Performance Error.Revised Surveillance Procedure & Tested Standby Train Time Delay Start Function.With1999-05-10010 May 1999
- on 990408,CR Emergency Ventilation Sys Surveillance Inadequacy Was Noted.Caused by Human Performance Error.Revised Surveillance Procedure & Tested Standby Train Time Delay Start Function.With
ML20206G1871999-05-0404 May 1999 Safety Evaluation Approving Third 10-year ISI Program Requests for Relief (RR) RR-08,RR-15 & RR-17 BSEP-99-0075, Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Brunswick Steam Electric Plant,Unit 1 & 2.With 05000324/LER-1999-002-02, :on 990329,reactor Tripped.Caused by Failed Electrical Connections on Vibration Detector for Number 9 Main Turbine Bearing.Vibration Detectors for Main Turbine Number 9 Bearing Replaced.With1999-04-28028 April 1999
- on 990329,reactor Tripped.Caused by Failed Electrical Connections on Vibration Detector for Number 9 Main Turbine Bearing.Vibration Detectors for Main Turbine Number 9 Bearing Replaced.With
05000325/LER-1999-004-01, On 990325,drywell Pressure Instrumentation Sensing Line Deficiency,Was Determined.Caused by Incorrect Design & Installation of Instrument Sensing Lines.Associated Sensing Lines Were Purged.With1999-04-26026 April 1999 On 990325,drywell Pressure Instrumentation Sensing Line Deficiency,Was Determined.Caused by Incorrect Design & Installation of Instrument Sensing Lines.Associated Sensing Lines Were Purged.With ML20206N1791999-04-23023 April 1999 Rev 0 to 2B21-0554, Brunswick Unit 2,Cycle 14 Colr 05000324/LER-1999-001-02, :on 990317,RCIC Sys Declared Inoperable.Caused by Inadequate Packing Compression on live-load Packing.Valve 2-E51-F008 Repacked & Tested in Accordance with Plant Procedures.With1999-04-16016 April 1999
- on 990317,RCIC Sys Declared Inoperable.Caused by Inadequate Packing Compression on live-load Packing.Valve 2-E51-F008 Repacked & Tested in Accordance with Plant Procedures.With
BSEP-99-0059, Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20205F9031999-03-30030 March 1999 Safety Evaluation Supporting Proposed Rev to BSEP RERP to Licenses DPR-62 & DPR-71,respectively 05000325/LER-1999-003-01, :on 970724,chlorinator Flange Leak Resulted in Cb Emergency Air Filtration Sys Actuation.Caused by Inadequately Manufactured Gas Inlet Line Spool Piece. Chlorinator Flange Inlet Line Spool Piece 2 Was Replaced1999-03-10010 March 1999
- on 970724,chlorinator Flange Leak Resulted in Cb Emergency Air Filtration Sys Actuation.Caused by Inadequately Manufactured Gas Inlet Line Spool Piece. Chlorinator Flange Inlet Line Spool Piece 2 Was Replaced
ML20206N1831999-02-28028 February 1999 Rev 0 to Suppl Reload Licensing Rept for Bsep,Unit 2 Reload 13 Cycle 14 BSEP-99-0043, Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Brunswick Steam Electric Plant,Units 1 & 2.With ML20203D7061999-02-0909 February 1999 SER Accepting Proposed Alternatives Contained in Relief Requests PRR-04,VRR-04,VRR-13,PRR-01,PRR-03,VRR-01.VRR-07, VRR-08 & VRR-09 Denied 05000324/LER-1998-004-03, :on 981216,HPCI Sys Was Rendered Inoperable to Support Scheduled Maint Activity.Caused by Deficiencies in Scheduling & Planning of 2-E41-F079 Valve Work Activity. Personnel Have Been Briefed on Event.With1999-01-15015 January 1999
- on 981216,HPCI Sys Was Rendered Inoperable to Support Scheduled Maint Activity.Caused by Deficiencies in Scheduling & Planning of 2-E41-F079 Valve Work Activity. Personnel Have Been Briefed on Event.With
BSEP-99-0005, Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With 05000324/LER-1998-005-02, :on 981123,chlorine Leak Results in CREVS & Suspended Fire Watches,Occurred.Caused by through-wall Perforation in Cast steel/neoprene-lined Piping T Section. Event Review Team Formed to Investigate.With1998-12-22022 December 1998
- on 981123,chlorine Leak Results in CREVS & Suspended Fire Watches,Occurred.Caused by through-wall Perforation in Cast steel/neoprene-lined Piping T Section. Event Review Team Formed to Investigate.With
05000324/LER-1998-002-01, :on 980708,excessive FW Temp Reduction Was Noted as Result of Loss of Stator Cw with Main Turbine. Caused by Failure to Analyze Worst Case Lfwh Transient. Process Computer Databank Was Updated.With1998-12-0404 December 1998
- on 980708,excessive FW Temp Reduction Was Noted as Result of Loss of Stator Cw with Main Turbine. Caused by Failure to Analyze Worst Case Lfwh Transient. Process Computer Databank Was Updated.With
BSEP-98-0228, :on 980708,excessive Feedwater Temperature Reduction as Result of Loss of Stator Cooling Water with Main Turbine,Was Determined.Caused by Failure to Analyze Worst Case Lfwh Transient.Databank Updated.With1998-12-0404 December 1998
- on 980708,excessive Feedwater Temperature Reduction as Result of Loss of Stator Cooling Water with Main Turbine,Was Determined.Caused by Failure to Analyze Worst Case Lfwh Transient.Databank Updated.With
BSEP-98-0231, Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With BSEP-98-0218, Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Bsep,Units 1 & 2. with BSEP-98-0210, Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired1998-10-30030 October 1998 Special Rept:On 980824,temp Element 2-CAC-TE-1258-22 Failed. Cause of Failed Temp Element Cannot Be Conclusively Determined.Temp Element Will Be Replaced & Cable Connections Repaired ML20154P8591998-10-16016 October 1998 SER Accepting Equivalent Margins Analysis for N-16A/B Instrument Nozzles for Plant,Units 1 & 2 ML20154P8151998-10-16016 October 1998 SER Accepting Revised Safety Analysis of Operational Transient of 920117,for Plant,Unit 1 BSEP-98-0202, Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Brunswick Steam Electric Plant,Units 1 & 2.With 05000324/LER-1998-003-03, :on 980829,MSIV Closures Were Noted.Caused by Procedure Deficiency.Reviewed Lessons Learned from Occurrence with Operations Personnel & Revised Affected Operating Procedures1998-09-28028 September 1998
- on 980829,MSIV Closures Were Noted.Caused by Procedure Deficiency.Reviewed Lessons Learned from Occurrence with Operations Personnel & Revised Affected Operating Procedures
ML20151Y6371998-09-14014 September 1998 Changes to QA Program, for Bsep,Units 1 & 2 ML20151Y6211998-09-14014 September 1998 BSEP Rept Describing Changes,Tests & Experiments, for Bsep,Units 1 & 2 05000325/LER-1998-006-01, :on 980815,ESF Actuations Due to Main Stack Wide Range Gas Monitor Failure Was Noted.Caused by end-of- Life Failure of Low Range Detector.Vendor Tested Components Removed from Wrgm.With1998-09-14014 September 1998
- on 980815,ESF Actuations Due to Main Stack Wide Range Gas Monitor Failure Was Noted.Caused by end-of- Life Failure of Low Range Detector.Vendor Tested Components Removed from Wrgm.With
1999-09-30
[Table view] |
Text
.
g_ mited engineeheme1_s,ec.
30 South 17th Street.
Post Office Box 8223 Philadelphia, Pa.19101 August 17, 1982 Director Office of Inspection and Enforcement U. S. Nuclear Regulatory Conmission Washington, DC 20555
Dear Sir:
Subject:
10CFR21 Report of a Potential Defect Related to Carolina Power and Light Company - Brunswick Station - Units 1 and 2 This confirms a telephone report of a potential 10CFR21 reported to the NRC at 11:01 a.m. on August 14, 1982. This report describen a condition found during analysJs performed on a Main Steam and Attached Safety Relief Valve Discharge lines to incorporate transient loads developed from the Mark I Torus program. A review of the analysis input data indicated that a discrepancy existed in the orientation of a number of pipe support (snubbers) details and their representation in the analysic of record. This discrepancy resulted in pipe stress and cupport loads which did not jeopardize the structural adequacy of the piping system but exceeded the allowable limits.
Applicable details as required by 10CFR21, paragraph 21.21(b) (3) are contained in the attached report. This condition has been reported to Carolina Power and Light Company.
Very truly yours,
- s
~,
d'S 1
c-G. E. Sarsten Vice President - Power Attachment copy:
Regional Director USNRC - Region 1 Regional Director USNRC - Region 2 8208190177 820917
( A Raytheon Company PDR ADOCK 05000324 PDR S
NAME AFD ADDRESS OF Tile INDIVIDUAL OR INDIVIDUALS INFORMING Tile CO G. E. Sarsten, Vice President - Power United Engineers & Constructors Inc.
30 South 17th Street Philadelphia, Pa. 19101 IDENTIFICATION OF THE FACILITYcTHE ACTIVITY, OR THE BASIC COMPONENT SUPPLIED FOR SUCll FACILITY OR SUCll ACTIVITY WITilIN Ti1E UNITED STATES WHICH F COMPLY OR CONTAINS A DEFECT Brunswick Steam Electric Plant Units 1 and 2 of Carolina Power and Light Company 124 and loads Stress in the Safety Relief Valve Discharge Line No.
for the attached snubbers at data point Nos. 1073, 1037 and 1057.
Pipe stress and snubber loads exceed the allowable limits although within structural integrity limits.
IDENTIFICATION OF Tile FIRM CONSTRUCTING THF FACILITY OR SUPPLYING COMPONENT WHICH FAILS TO COMPLY OR CONTAINS A DEFECT United Engineers & Constructors Inc., architect engineer NATURE OF THE DEFECT OR FAILURE TO COMPLY AND THE SAFETY HAZ OR COULD BE CREATED BY SUCil DEFECT OR FAILURE TO COMPLY The orientation of a number of snubbers for the above mentioned main steam and attached safety relief valve discharge lines were found to deviate from the orientation considered for the pipe stress analysis.
loads and pipe stress when This deviation results in increased support The the proper orientation was accounted for in the pipe analysis.
loads and pipe stress level exceeded those permitted corrected support by the associated allowable limits; however, this condition was analyzed to not affect the structural integrity of the piping system.
Tile DATE ON WHICH THE INFORMATION OF SUCH DEFECT OR FAILURE August 12, 1982 IN Tile CASE OF A BASIC COMPONENT WilICll CONTAINS A DEFECT OR FAILS TO COMPLY, NUMBER AND LOCATION OF ALL SUCH COMPONENTS IN USE AT, SUPPLIED FOR, OR BEING SUPPLIED FOR ONE OR MORE FACILITIES OR ACTIVITIES SUBJECT TO TH IN THIS PART This defect applies to only the Brunswick Steam Electric Plant Units 1 and 2.
THE CORRECTIVE ACTION WilICil HAS BEEN, IS BEING, OR WILL BE TAKEN:
THE NAME OF THE INDIVIDUAL OR ORCANIZATION RESPONSIBLE FOR Tile ACTION: AND Tile LENGTH OF TIME THAT HAS BEEN OR WILL BE TAKEN TO COMPLETE Tile ACTION Corrective Actions 1.
llave assured that the line and the snubbers subject of the reported deficiency were within limits which assure structural integrity.
2.
Have evaluated the extent of the snubber misorientation conditions and identified the additional systems which may have the potential to be affected by similar problems.
3.
llave performed a preliminary evaluation of the additional systems identified in (2) above and estimated that if deficient conditions will be identified, they will be within structural integrity limits.
4.
Will reanalyze the systems identified in (2) above and evaluate the adequacy of the piping and associated support designs.
5.
Will develop the appropriate support modifications if required.
Further details on the corrective actions taken to date are contLined in Enclosure 1.
Name of the Organization Responsible for Corrective Action Power Division of the United Engineers 6 Constructors Inc.
Length of Time that Will Be Taken To Complete the Action By October 15, 1982 i
ANY ADVICE RELATED TO THE DEFECT OR FAILURE TO COMPLY ABOUT THE FACILITY, ACTIVITY, OR BASIC COMPONENT TilAT HAS BEEN, IS BEING, OR WILL BE GIVEN TO PURCilASERS OR LICENSEES Carolina Power and Light Company was advised by UE6C on August 13, 1982.
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ENCLOSURE 1 10CFR21 Report of a Potential Defect Related to Snubber Misorientations in the Brunswick Station Units 1 and 2 - Carolina Power and Light Company Corrective Actions Taken To Date a) The system affected by the subject deficiency has been reanalyzed with the corrected snubber crientations. The analysis of the Safety / Relief Valve Discharge (SRV) Sheet 124 included the attached SRV Sheet 126, the Main Steam (!!S) Sheet 14 and the High Pressure Core Injection (HPIC)
Line. The results indicated that the maximum stress level and loads in some snubbers (at data point Nos. 1073, 1037 and 1057) in the SRV Sheet 124 exceeded the allowable limits but were within levels which assure the system's structural integrity. The other attached lines were all within the allowable stress limits, b) An evaluation to determine the extent of the snubber misorientation was performed.
o In the drywell, 16 additional sheets (representing worst and random conditions) were selected.
Including the systems identified in (a) above, these systems contained 190 snubbers (approximately 70% of the snubbers in the drywell).
Of these 190 snubbers, 29 snubbers were found with orientations exceeding the allowed tolerance and improperly represented in the piping analysis. Of these 29 snubbers, 8 have already been addressed in the reanalysis of the 3 sheets noted in a) above and the RilR Sheet 25 (see d below).
Of the remaining 21 only 2 snubbers had misorientations of the magnitude which caused the deficiency described in (a) above.
(The sheets containing these snubbers 1
are MS Sheets ISB and 15C.)
o In the reactor building, 9 sheets have been reviewed. These sheets included 150 snubbers (approximately 40% of the snubbers outside the drywell).
Of these snubbers only 5 snubbers were for:nd with minor misorientations.
i c) An evaluation of the effect due to the finding in (b) above has been performed and it has been determined that the following additional sheets have the potential for being affected by the snubber misorientations and will be reanalyzed.
These sheets are:
- Main Steam (MS) Sheet 14A (and attached Safety / Relief Valve Discharge 1
(SRV) Sheets 119 and 127).
l
- Main Steam (MS) Sheet ISB (and attached Safety / Relief Valve Discharge (SRV) Sheets 121, 122, 125 and 237).
- Main Steam (MS) Sheet 15C (and attached Safety / Relief Valve Discharge (SRV) Sheets 120,123 and 187).
- Feedwater (FW) Sheets 16 and 160.
The above sheets account for the remaining 21 snubbers which were found to have angular deviations.
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l ENCLOSURE 1 (Cont'd.)
d)
It is evaluated that the reanalysis that will be performed on the above 14 sheets plus that already performed on the 4 sheets previously noted will adequately address the generic aspects of the reported deficiency.
[
The following factors were considered to arrive at this conclusion.
[
I The severe case of misorientation which resulted in the subject reported deficiency was caused by Snubber 1073 in the SRV Sheet 124.
l That case appears to be an error.
No similar cases were found in the other 10 SRV sheets which include 81 snubbers.
- The other cases with sizable misorientation were detected in lines routed horizontally and parallel to the drywell wall, therefore, with long radius of curvature (such as portions of MS and FN sheets).
In these cases, apparently some problem was encountered in reconci-liating transverse and parallel (to pipe) snubber installations with the N-S, E-W coordinate system used in the analysis.
- Only a few cases with minor misorientations were found in systems inside the drywell which do not have the layout condition mentioned above (RHR Sheet 25, SLC Sheet 36, SRV Sheets 119, 120, 121, 122, 123, 125, 126, 127, 237 and 187).
The same applied to the sheets reviewed outside containment (Sheets 37, 63, 4, 10, 18, 23, 38, 62 and 82).
RHR Sheet 25 was selected for reanalysis as a typical line with minor deviations on the basis that none of the lines reviewed.
from outside the containment had greater snubber angular deviations.
This reanalysis did not result in any conditions exceeding allowable limits.
Therefore no further reanalysis will be performed on the lines outside the containment.
e) A preliminary evaluation of the systems identified in (c and d above) has been conducted including a preliminary reanalysis of Sheets ISB and 15C which contained the larger snubber misorientations.
Based on the results of these analyses and on knowledge of existing design margin and conservatisms inherent in the present analyses, it has been estimated that no conditions exceeding structural integrity limits will be found.