|
---|
Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 ML20204H7131999-03-17017 March 1999 Safety Evaluation Concluding That NNECO Provided Adequate Justification for Deviations from RG 1.97,Rev 2, Recommendations,For Instrumentation Monitoring CST Level & Containment Area Radiation at Mnps Unit 2 ML20204C9441999-03-10010 March 1999 Safety Evaluation Denying Licensee Request for License Amend to Revise Frequency of Certain SRs for Electrical Power Sys ML20207L2631999-03-0505 March 1999 Safety Evaluation Supporting Amend 104 to License DPR-21 ML20207L5961999-02-22022 February 1999 Safety Evaluation Concluding That Code Requirements,Which Require 100 Percent Volumetric Exam of RPV flange-to-shell, Impractical to Perform to Extent Required & That Alternative Provide Reasonable Assurance of Structural Integrity ML20203D7601999-02-11011 February 1999 Safety Evaluation Supporting Millstone 1 Certified Fuel Handler Training & Retraining Program ML20196B0501998-11-24024 November 1998 Safety Evaluation Re Licensee 960213 Submittal of 180-day Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant,Unit 2 ML20155K1981998-11-0909 November 1998 Safety Evaluation Re Application of leak-before-break Status to Portions of Safety Injection & Shutdown Cooling Sys ML20195B8711998-11-0909 November 1998 Safety Evaluation Approving Revised Evaluation of Primary Cold Leg Piping leak-before-break Analysis for Plant ML20155C3781998-10-30030 October 1998 SER Denying Amend to Allow Changes to Fsar.Nrc Found That NNECO Had Not Considered Diversity Provided by Switch in Control Room That Removes Power to 1 of 2 MOV in SDC Sys Flow Path in Evaluation of High Low Pressure Design ML20155C8441998-10-29029 October 1998 Safety Evaluation Accepting Licensee Proposal to Withdraw ATWS Test Commitment ML20238F2781998-08-27027 August 1998 SER Related to Proposed Rev 20 to Northeast Utilities Quality Assurance Program Topical Rept for Millstone Nuclear Power Station,Units 1,2 & 3 ML20237D5001998-08-20020 August 1998 SER Approving Code Case N-389-1, Alternative Rules for Repairs,Replacements,Or Mods,Section Xi,Div 1 ML20236U7051998-07-22022 July 1998 Safety Evaluation Granting All Requests for Relief W/Exception of Requests RR-89-17 (Authorized for Class 1 Sys Only) & RR-89-21.Requests RR-13 & RR-14 Will Be Addressed in Separate Evaluation ML20236K6971998-07-0101 July 1998 SER Accepting Third 10-year Interval Inservice Insp Program Plan,Rev 2 & Associated Request for Relief & Proposed Alternatives for Plant,Unit 2 ML20236K3531998-07-0101 July 1998 Safety Evaluation Supporting Amend 218 to License DPR-65 ML20249C2541998-06-24024 June 1998 Safety Evaluation Accepting Proposed Rev 19 to NNECO QAP Topical Rept & Amended Through 980609.Informs That NNECO Exception to Provisions in Paragraph 10.3.5 of Constitutes Temporary & Acceptable Alternative ML20248J0031998-06-0404 June 1998 Safety Evaluation Accepting Millstone Nuclear Power Station Emergency Plan ML20248M2991998-06-0202 June 1998 Safety Evaluation Approving Application Re Restructuring of Central Maine Power Co by Establishment of Holding Company ML20248C4131998-05-26026 May 1998 SER of Individual Plant Exam of External Events Submittal on Millstone Nuclear Power Station,Unit 3 ML20217M4181998-04-30030 April 1998 Suppl Safety Evaluation Accepting Licensee RCS Pressure & Heat Removal by Containment Heat Removal Sys post-accident Monitoring Instrumentation ML20216G7921998-03-13013 March 1998 Safety Evaluation Authorizing Proposed Alternative to Check Valve Obturator Movement Requirements of OM-10 for SIL Accumulator Outlet for Listed Check Valves ML20203E8521998-02-17017 February 1998 SER Accepting Request for Relief from Requirements of 10CFR50.55a(f) for Performing Required Inservice Testing of Certain Class 2 Components IAW ASME Boiler & Pressure Vessel Code Section XI for Plant,Unit 3 ML20203E9341998-02-17017 February 1998 SER Accepting Request for Relief from Requirements of 10CFR50.55a(g) for Performing Required Exams for Certain Class 1 Components IAW ASME Boiler & Pressure Vessel Code Section XI for Plant,Unit 3 ML20203E2441998-02-0909 February 1998 Safety Evaluation Accepting Re Approval of Realistic,Median Centered Spectra Generated for Resolution of USI-A-46 ML20198R9941998-01-13013 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Millstone Nuclear Power Station,Unit 3 ML20202H7461997-12-10010 December 1997 Safety Evaluation Accepting Licensee Position That Correction of AC-11 Single Failure Vulnerability Unncessary ML20202J0911997-12-0202 December 1997 Safety Evaluation Accepting Proposed Exemption,Which Meets Special Circumstance Given in 10CFR50.12(a)(2)(ii) ML20198S2411997-10-31031 October 1997 SE Accepting Licensee Request for Deviations from Recommendations in Reg Guide 1.97,Rev 2 for Temp & Flow Monitoring Instrumentation for Cooling Water to ESF Sys Components & Containment Isolation Valve Position ML20212G5991997-10-27027 October 1997 Safety Evaluation Supporting Amend 103 to License DPR-21 ML20217K8801997-10-27027 October 1997 Correction to Safety Evaluation Supporting Amend 103 to License DPR-21.Phrase or Rod Block Protection Has Been Deleted from Listed Sentence in Staff Associated SE ML20212F1381997-10-22022 October 1997 Safety Evaluation Supporting Amend 102 to License DPR-21 ML20217M9301997-08-19019 August 1997 Safety Evaluation Accepting Continued Operation W/O High Startup Rate Trip by Nene for Millstone,Unit 2 ML20149J2661997-07-23023 July 1997 Safety Evaluation Accepting Changes & Reanalyses in ECCS Evaluation Models & Application of Models for Plant,Unit 2 ML20141L8821997-05-28028 May 1997 Safety Evaluation Supporting Amend 101 to License DPR-21 ML20138A0111997-04-23023 April 1997 Safety Evaluation Accepting Licensee Proposal,Not to Perform Type C Leakage Rate Testing on 14 Subject CIVs ML20137V5931997-04-15015 April 1997 Safety Evaluation Supporting Amend 100 to License DPR-21 ML20137U3121997-04-10010 April 1997 Safety Evaluation Supporting Amends 99,206 & 135 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20134A0331997-01-23023 January 1997 Safety Evaluation Accepting Util Proposed Alternatives to ASME Code Requirements ML20133N3401997-01-14014 January 1997 Safety Evaluation Supporting Amend 98 to License DPR-21 ML20135C4221996-12-0202 December 1996 Safety Evaluation Accepting Proposed Alternative Described in Relief Request R-1 Re Valve Inservice Testing Program at Facility ML20128P4381996-10-0909 October 1996 Safety Evaluation Accepting Review of Cracked Weld Operability Calculations & Staff Response to NRC Task Interference Agreement ML20128L7541996-10-0404 October 1996 Safety Evaluation Supporting Amend 97 to License DPR-21 ML20248C5451995-05-0202 May 1995 SER on Millstone Unit 3 Individual Plant Exam of External Events to Identify plant-specific Vulnerabilities,If Any,To Severe Accidents & Rept Results Together W/Any licensee-determined Improvements & C/A to Commission ML20248C5731994-07-19019 July 1994 SER Step 1 Review of Individual Plant Exam of External Fire Events for Millstone Unit 3 ML20059H4991994-01-24024 January 1994 Safety Evaluation Accepting Revised Responses to IEB-80-04 Re MSLB Reanalysis 1999-08-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
[Table view] |
Text
-. . _ _ .
f
- f. t UNITED STATES f M .. j NUCLEAR REGULATORY COMMISSION gk-gv [f g WASHINGTON. D.C. 20555-0001 SUPPLEMENTAL SAFETY EVALVATION 1
l H !
THE OFFICE OF NUCLEAR REACTOR REGULATION REVISED RESPONSE TO IE BULLETIN 80-04 l
l MAIN STEAM LINE BREAK WITH CONTINVED FEEDWATER ADDITION MILLSTONE NUCLEAR POWER STATION. UNIT NO. 2 l
DOCKET NO. 50-336 j l
1.0 INTRODUCTION
l On October 7, 1982, the staff issued its safety evaluation (SE) of the Northeast Nuclear Energy Company's (the licensee) response to IE Bulletin No.
80-04, " Analysis of a PWR Main Steam Line Break with Continued Feedwater Addition," for the Millstone Nuclear Power Station, Unit No. 2. The SE j l concluded that; (1) there is no potential for containment overpressurization '
! resulting from a main steam line break (MSLB) with continued feedwater I
addition, (2) no damage would be incurred by the auxiliary feedwater (AFW) pumps due to runout, (3) all potential water sources were identified and there '
I would be no violation of specified acceptable fuel design limits, and (4) no further action regarding IE Bulletin 80-04 is required.
The staff evaluation was based on review of a MSLB analysis prepared by the licensee in 1979 and submitted to the staff on January 25, 1980. In 1991, the licensee discovered errors in the 1979 MSLB analysis which indicated that the peak containment pressure and temperature resulting from a MSLB would exceed containment design conditions and the qualification temperature of safety related equipment. The MSLB event containment response has been reanalyzed and corrective plant modifications have been implemented. On January 13, 1993, the licensee submitted a description of the revised MSLB analysis.
l The staff's findings and conclusions regarding the revised MSLB analysis are presented below.
2.0 EVALUATION OF CONTAINMENT RESPONSE Previous MSLB Analysis: In 1979, a MSLB reanalysis was prepared as a result of implementation of TMI Short-Term Recommendation 2.1.7.a to provide l automatic initiation of auxiliary feedwater upon loss of main feedwater flow.
l 9401280080 940124 PDR ADOCK 05000336 O PDR
l l
1 l
l It was also used for the purpose of responding to IE Bulletin 80-04. The 1979 analysis assumed the following scenario: l (a) Initial conditions of hot zero power, end-of-cycle, and two-loop operation, (b) A 3 minute delay from the start of the event until the start of AFW flow, l
(c) No credit for isolation of the main feedwater (MFW) system, thereby resulting in a rampdown to continuous MFW flow of 772 gpm (5% flow) to the affected steam generator (S/G),
(d) Two single-failure cases were considered - (1) AFW control valve failure with loss of offsite power and (2) loss of one train of l safeguards equipment due to a diesel generator failure, (e) The highest worth control rod sticks in the fully withdrawn position, (f) AFW flow is 2800 gpm which is 35% higher than the maximum runout flow. (With the 772 gpm MFW flow, the total FW flow is 3572 gpm), and (g) The MSLB occurs at the vessel nozzle (i.e., upstream of the flow venturi for the affected main steam line (MSL).
The licensee did not reanalyze for a spectrum of break sizes, but only the original limiting Final Safety Analysis Report (FSAR) case for the nozzle break location. The results of the analysis indicated a peak containment pressure of 47 psig and a peak containment temperature of 274*F. These conditions are bounded by the containment design conditions of 54 psig and 289'F.
The staff reviewed the 1979 MSLB reanalysis, and in a Safety Evaluation dated October 7,1982, concluded that the analysis was acceptable.
In 1991, while performing S/G replacement studies using new S/G and containment models with revised moisture carryover assumptions, and ,
considering that different single-failures are limiting for different assumed ;
power levels, the licensee determined that the 1979 assumptions regarding ,
power level, break location, break size and single-failure were non- !
conservative. In 1992, two new postulated single-failures were identified i that could result in MSLB conditions exceeding the containment design !
parameters. These events, and the licensee's corrective modifications, were !
discussed in the staff's Safety Evaluation for Amendment 167 issued on December 23, 1992.
January 13. 1993. Changes to Millstone-2 MSLB Containment Analysis:
The licensee has: (a) performed extensive reanalysis, (b) implemented plant modifications, (c) implemented revised technical specifications, and (d) revised its response to IE Bulletin 80-04. Attachment 1 of the licensee's January 13, 1993, submittal provided a description of the licensee's new IE Bulletin 80-04 response for both the core and containment.
The new MSLB analysis was performed by the NSSS vendor using the SGN-III code.
SGN-III, which is referenced for use by the Standard Review Plan, is comprised of two interdependent programs, SGN and CONTRANS. SGN calculates the transient response of the reactor coolant system and S/Gs to develop mass-energy releases for use in the containment analysis. The model consists of fluid flow and heat transfer representations of the core, hot leg plena and piping, pressurizer, S/Gs, cold leg piping and plena, and S/G secondary side.
Reverse heat transfer from the intact S/Gs to the primary coolant is included.
A two-region core fuel model is used together with a >oint-kinetics representation and non-linear moderator, Doppler, boron and control rod reactivity effects. The secondary side of each S/G is represented by a finite two-node quasi-static balance of energy flux ud secondary fluid thermodynamics. The steam lines to the turbne are included in the secondary side representation.
CONTRANS is the containment response portion of the SGN-III code. CONTRANS receives mass and energy inputs from SGN and performs mass, energy, and momentum balances on the containment volumes and flow paths. CONTRANS includes active heat sinks such as containment sprays and heat exchangers, as well as passive heat sinks such as walls.
Major assumptions utilized in the new analysis were as follows:
- 1. Offsite power was assumed to be available for most cases. This is conservative in that it results in increased heat transfer due to ;
forced flow at maximum RCS flow rate. j l
Confirmatory analyses with loss-of-offsite power were run for verification that the most conservative assumption was selected.
- 2. For purposes of determining peak containment pressure, the initial containment conditions were assumed to be at the technical specifications limit of 16.8 psig and 120*F. This results in later (than in the standard atmosphere case) spray initiation and higher containment temperature. Relative humidity was assumed at 30% except for the EQ analyses cases where it was set to 100% to provide conservatism in the containment temperature response calculation. 1
- 3. Moisture carryover was as determined by the SGN-III code.
I 1
i i
i I
i 4_
l
- 4. Feedwater spiking due to pressure imbalance between the ruptured !
and intact S/G was accounted for by doubling the initial feedwater flow rate for each analysis.
- 5. Credit was taken for the main steam nonreturn valves to prevent blowdown of the intact S/G.
- 6. As with the earlier analyses, AFW initiation was delayed 3 l minutes. )
- 7. RCP heat was included, l l
- 8. Actuation signals are redundant and safety grade. Consistent with !
the original licensing basis, credit is taken in some cases for ,
nonsafety grade components initiated by safety grade signals. l
- 9. The maximum RCS flow rate was conservatively assumed. This ;
maximizes the heat transfer from the primary to secondary side.
To determine the limiting cases for containment pressure and temperature responses, the licensee analyzed a spectrum of cases for sensitivity to power level and break size and location, feedwater, electrical, and containmant heat 1
removal equipment single failures, and safety-related equipment temperature ;
response.
The licensee has used previously accepted analytical methodology for calculation of mass-energy releases and associated containment pressure-temperature responses.
Results of new MSLB analyses:
\
The results show that for all cases, the peak containment pressure is less than the containment design pressure. The highest containment pressure was for the 50% power case in which the feedwater regulating bypass valve fails-open; the calculated peak pressure was 53.7 psig. For all the cases, the peak temperature exceeded the containment design temperature for a short time period, the maximum being for the case of failure of vital bus transfer, where the peak temperature was found to be 426*F. This peak temperature is essentially identical to that of the previous MSLB analysis, discussed in the Amendment 167 safety evaluation and accepted by the staff based on supporting information provided in a licensee letter dated December 4,1992.
In an attachment to the licensee's December 4, 1992 submittal, entitled,
" Evaluation of EQ Equipment Thermal Response to the Postulated MSLB and LOCA in the Millstone Unit 2 Containment," the licensee summarized its environmental qualification analysis. The analysis resulted in conditions I exceeding containment design temperature for a short period of time. The l licensee determined that a condensate layer would form on the surface of equipment that would act as a thermal barrier. The analysis showed that the temperature peak represents a short duration at superheated conditions and the l
I
surface temperature of safety related equipment will not exceed the saturated temperature of the steam pressure in containment during the event. The licensee concluded that equipment surface temperature would not exceed qualification temperature during a MSLB although the containment atmosphere temperature rises to a maximum of 426*F. The surface temperature of qualified equipment would not exceed its qualification temperature of 289'F. This method of analysis is described in NUREG-0588, Section 1.2(5)(b) as being acceptable when the containment atmosphere exceeds the qualification temperature. Therefore, the staff agrees that qualified equipment can be expected to perform its safety function during and after a MSLB.
3.0 EVALUATION OF CORE RESPONSE Item 2 of IE Bulletin 80-04 requested that the licensee review the core reactivity analysis for a main steamline break (MSLB) regarding runout from the auxiliary feedwater system or continuation of feedwater or condensate flow to the affected steam generator following isolation of the main steam system.
The original response to IE Bulletin 80-04 for Millstone 2 did not consider all potential water sources. The revised responses are discussed below.
- a. The licensee reviewed the bounding conditions for the analysis and found that the existing analysis bounds the consequences of continued feedwater flow to the break.
- b. The single failure assumed in the analysis of record is the loss of one of two HPSI pumps. The effect of this decreased delivery of high concentration boric acid solution to the reactor coolant system is that return-to-power is exacerbated. During the review the licensee identified an additional single failure that could impact core response. The failure of electrical bus 24G during the fast transfer from the normal to the reserve station service transformer. The licensee determined that this event is bounded by the analysis of record.
- c. The licensee identified the primary effect of extended water supply to the affected steam generator as an increase in the duration of the event with a higher potential for return-to-power.
During the 1992 refueling outage, changes were made to the feedline isolation system to ensure redundant valve alignment, and also to the power supply to the feedwater regulating valves. The analysis of record includes the effect of runout flow for a duration of 180 seconds. The implemented changes would result in a less severe reactivity transient compared to the bounding case for the analysis of record.
- d. The analysis of record indicates that the hot channel factors corresponding to the most reactive rod in the fully withdrawn position and Minimum Departure from Nucleate Boiling Ratio (MDNBR) values for the analyzed events bound the MSLB analysis for core response. The analysis predicts a slight return to power with no fuel failure.
em-v
The licensee evaluated the MSLB analysis and found that it bounds the core '
reactivity response in the event of an extended feedwater supply. The plant modifications during the 1991 refueling outage, resulted in the additional single active failure being less limiting than the analysis of record.
The staff has reviewed the licensee's evaluation and finds that the revised response to IE Bulletin 80-04 adequately demonstrates that the January 13, >
1993 MSLB analysis of record bounds the case of continued feedwater flow.
4.0 CONCLUSION
The licensee has provided a revised response to IE Bulletin 80-04. The '
updated response indicates that; (1) acceptable methodology has been used for :
the revised MSLB analysis and that the results of the analysis indicate that :'
plant systems, structures and components in containment will not be exposed to unacceptable pressure or temperature conditions resulting from a design basis MSLB, and (2) the core response to the reanalyzed MSLB is no more severe than shown by previous analysis and is also acceptable. ;
Principal contributors: W. Long S. Brewer A. Dummer Dated: January 24, 1994 I
I e
t k
h
- - , - . .