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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 ML20204H7131999-03-17017 March 1999 Safety Evaluation Concluding That NNECO Provided Adequate Justification for Deviations from RG 1.97,Rev 2, Recommendations,For Instrumentation Monitoring CST Level & Containment Area Radiation at Mnps Unit 2 ML20204C9441999-03-10010 March 1999 Safety Evaluation Denying Licensee Request for License Amend to Revise Frequency of Certain SRs for Electrical Power Sys ML20207L2631999-03-0505 March 1999 Safety Evaluation Supporting Amend 104 to License DPR-21 ML20207L5961999-02-22022 February 1999 Safety Evaluation Concluding That Code Requirements,Which Require 100 Percent Volumetric Exam of RPV flange-to-shell, Impractical to Perform to Extent Required & That Alternative Provide Reasonable Assurance of Structural Integrity ML20203D7601999-02-11011 February 1999 Safety Evaluation Supporting Millstone 1 Certified Fuel Handler Training & Retraining Program ML20196B0501998-11-24024 November 1998 Safety Evaluation Re Licensee 960213 Submittal of 180-day Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Plant,Unit 2 ML20155K1981998-11-0909 November 1998 Safety Evaluation Re Application of leak-before-break Status to Portions of Safety Injection & Shutdown Cooling Sys ML20195B8711998-11-0909 November 1998 Safety Evaluation Approving Revised Evaluation of Primary Cold Leg Piping leak-before-break Analysis for Plant ML20155C3781998-10-30030 October 1998 SER Denying Amend to Allow Changes to Fsar.Nrc Found That NNECO Had Not Considered Diversity Provided by Switch in Control Room That Removes Power to 1 of 2 MOV in SDC Sys Flow Path in Evaluation of High Low Pressure Design ML20155C8441998-10-29029 October 1998 Safety Evaluation Accepting Licensee Proposal to Withdraw ATWS Test Commitment ML20238F2781998-08-27027 August 1998 SER Related to Proposed Rev 20 to Northeast Utilities Quality Assurance Program Topical Rept for Millstone Nuclear Power Station,Units 1,2 & 3 ML20237D5001998-08-20020 August 1998 SER Approving Code Case N-389-1, Alternative Rules for Repairs,Replacements,Or Mods,Section Xi,Div 1 ML20236U7051998-07-22022 July 1998 Safety Evaluation Granting All Requests for Relief W/Exception of Requests RR-89-17 (Authorized for Class 1 Sys Only) & RR-89-21.Requests RR-13 & RR-14 Will Be Addressed in Separate Evaluation ML20236K6971998-07-0101 July 1998 SER Accepting Third 10-year Interval Inservice Insp Program Plan,Rev 2 & Associated Request for Relief & Proposed Alternatives for Plant,Unit 2 ML20236K3531998-07-0101 July 1998 Safety Evaluation Supporting Amend 218 to License DPR-65 ML20249C2541998-06-24024 June 1998 Safety Evaluation Accepting Proposed Rev 19 to NNECO QAP Topical Rept & Amended Through 980609.Informs That NNECO Exception to Provisions in Paragraph 10.3.5 of Constitutes Temporary & Acceptable Alternative ML20248J0031998-06-0404 June 1998 Safety Evaluation Accepting Millstone Nuclear Power Station Emergency Plan ML20248M2991998-06-0202 June 1998 Safety Evaluation Approving Application Re Restructuring of Central Maine Power Co by Establishment of Holding Company ML20248C4131998-05-26026 May 1998 SER of Individual Plant Exam of External Events Submittal on Millstone Nuclear Power Station,Unit 3 ML20217M4181998-04-30030 April 1998 Suppl Safety Evaluation Accepting Licensee RCS Pressure & Heat Removal by Containment Heat Removal Sys post-accident Monitoring Instrumentation ML20216G7921998-03-13013 March 1998 Safety Evaluation Authorizing Proposed Alternative to Check Valve Obturator Movement Requirements of OM-10 for SIL Accumulator Outlet for Listed Check Valves ML20203E8521998-02-17017 February 1998 SER Accepting Request for Relief from Requirements of 10CFR50.55a(f) for Performing Required Inservice Testing of Certain Class 2 Components IAW ASME Boiler & Pressure Vessel Code Section XI for Plant,Unit 3 ML20203E9341998-02-17017 February 1998 SER Accepting Request for Relief from Requirements of 10CFR50.55a(g) for Performing Required Exams for Certain Class 1 Components IAW ASME Boiler & Pressure Vessel Code Section XI for Plant,Unit 3 ML20203E2441998-02-0909 February 1998 Safety Evaluation Accepting Re Approval of Realistic,Median Centered Spectra Generated for Resolution of USI-A-46 ML20198R9941998-01-13013 January 1998 SER Accepting Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves, for Millstone Nuclear Power Station,Unit 3 ML20202H7461997-12-10010 December 1997 Safety Evaluation Accepting Licensee Position That Correction of AC-11 Single Failure Vulnerability Unncessary ML20202J0911997-12-0202 December 1997 Safety Evaluation Accepting Proposed Exemption,Which Meets Special Circumstance Given in 10CFR50.12(a)(2)(ii) ML20198S2411997-10-31031 October 1997 SE Accepting Licensee Request for Deviations from Recommendations in Reg Guide 1.97,Rev 2 for Temp & Flow Monitoring Instrumentation for Cooling Water to ESF Sys Components & Containment Isolation Valve Position ML20212G5991997-10-27027 October 1997 Safety Evaluation Supporting Amend 103 to License DPR-21 ML20217K8801997-10-27027 October 1997 Correction to Safety Evaluation Supporting Amend 103 to License DPR-21.Phrase or Rod Block Protection Has Been Deleted from Listed Sentence in Staff Associated SE ML20212F1381997-10-22022 October 1997 Safety Evaluation Supporting Amend 102 to License DPR-21 ML20217M9301997-08-19019 August 1997 Safety Evaluation Accepting Continued Operation W/O High Startup Rate Trip by Nene for Millstone,Unit 2 ML20149J2661997-07-23023 July 1997 Safety Evaluation Accepting Changes & Reanalyses in ECCS Evaluation Models & Application of Models for Plant,Unit 2 ML20141L8821997-05-28028 May 1997 Safety Evaluation Supporting Amend 101 to License DPR-21 ML20138A0111997-04-23023 April 1997 Safety Evaluation Accepting Licensee Proposal,Not to Perform Type C Leakage Rate Testing on 14 Subject CIVs ML20137V5931997-04-15015 April 1997 Safety Evaluation Supporting Amend 100 to License DPR-21 ML20137U3121997-04-10010 April 1997 Safety Evaluation Supporting Amends 99,206 & 135 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20134A0331997-01-23023 January 1997 Safety Evaluation Accepting Util Proposed Alternatives to ASME Code Requirements ML20133N3401997-01-14014 January 1997 Safety Evaluation Supporting Amend 98 to License DPR-21 ML20135C4221996-12-0202 December 1996 Safety Evaluation Accepting Proposed Alternative Described in Relief Request R-1 Re Valve Inservice Testing Program at Facility ML20128P4381996-10-0909 October 1996 Safety Evaluation Accepting Review of Cracked Weld Operability Calculations & Staff Response to NRC Task Interference Agreement ML20128L7541996-10-0404 October 1996 Safety Evaluation Supporting Amend 97 to License DPR-21 ML20248C5451995-05-0202 May 1995 SER on Millstone Unit 3 Individual Plant Exam of External Events to Identify plant-specific Vulnerabilities,If Any,To Severe Accidents & Rept Results Together W/Any licensee-determined Improvements & C/A to Commission ML20248C5731994-07-19019 July 1994 SER Step 1 Review of Individual Plant Exam of External Fire Events for Millstone Unit 3 ML20059H4991994-01-24024 January 1994 Safety Evaluation Accepting Revised Responses to IEB-80-04 Re MSLB Reanalysis 1999-08-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217P5391999-10-25025 October 1999 Rev 0,Change 1 to Millstone Unit 1 Northeast Utils QA Program ML20217C8721999-10-0606 October 1999 Rev 21,change 3 to MP-02-OST-BAP01, Nuqap Topical Rept, App F & G Only B17896, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 1.With B17894, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 2.With B17898, Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With1999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216J4341999-09-24024 September 1999 Mnps Unit 3 ISI Summary Rept,Cycle 6 ML20211N8401999-09-0202 September 1999 Rev 21,change 1 to Northeast Utils QA TR, Including Changes Incorporated Into Rev 20,changes 9 & 10 B17878, Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Mnps,Unit 1.With B17874, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 3.With ML20216F5141999-08-31031 August 1999 Rept on Status of Public Petitions Under 10CFR2.206 B17879, Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With1999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Millstone Nuclear Power Station,Unit 2.With ML20211G9631999-08-30030 August 1999 SER Accepting Licensee Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Motor-Operated Valves ML20211A6561999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 2 B17858, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 3.With B17856, Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With1999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Millstone Nuclear Power Station,Unit 1.With ML20210J0311999-07-21021 July 1999 Rev 20,Change 10 to QAP 1.0, Organization ML20210E5931999-07-19019 July 1999 Revised Page 16 of 21,to App F of Northeast Util QA Program Plan ML20210C5911999-07-15015 July 1999 Revised Rev 20,change 10 to Northeast Util QA Program TR, Replacing Summary of Changes ML20210A0411999-07-15015 July 1999 Rev 20,change 10 to Northeast Util QA Program Tr B17814, Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start1999-07-12012 July 1999 Special Rept:On 990612 B Train EDG Failed to Restart within 5 Minutes Following Completion of 18 Month 24 H Endurance Run Required by TS 4.8.1.1.2.g.7.Caused by Procedural inadequacy.Re-performed Hot Restart Via Manual Start ML20209D1881999-07-0101 July 1999 Rev 20,change 9 to Northeast Util QA Program Tr ML20196J2191999-06-30030 June 1999 SER Concluding That Licensee USI A-46 Implementation Program,In General,Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20211A6751999-06-30030 June 1999 Revised Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level & Operating Data Rept ML20196A8451999-06-30030 June 1999 Post Shutdown Decommissioning Activities Rept ML20209J0541999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Unit 2 B17830, Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Nuclear Power Station,Unit 3.With ML20196K1791999-06-30030 June 1999 Addendum 6 to Millstone Unit 2 Annual Rept, ML20196J1821999-06-30030 June 1999 Rev 21,Change 0 to Northeast Utilities QAP (Nuqap) Tr B17833, Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With1999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Millstone Power Station,Unit 1.With ML20195H1011999-06-11011 June 1999 Rev 20,change 8 to Northeast Utilities QAP (Nuqap) TR ML20207G6411999-06-0303 June 1999 Safety Evaluation Supporting Amends 105,235 & 171 to Licenses DPR-21,DPR-65 & NPF-49,respectively ML20211A6631999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 2,providing Revised Average Daily Unit Power Level,Operating Data Rept & Unit Shutdowns & Power Reductions B17808, Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Millstone Nuclear Power Station,Unit 3.With ML20211B7351999-05-31031 May 1999 Cycle 7 Colr B17804, Monthly Operating Rept for May 1999 for Mnps,Unit 2.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 2.With B17807, Monthly Operating Rept for May 1999 for Mnps,Unit 1.With1999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Mnps,Unit 1.With ML20209J0661999-05-31031 May 1999 Revised Monthly Operating Rept for May 1999 for Millstone Unit 2 ML20206M4631999-05-11011 May 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Perform Ultrasonic Exam on Inner Surface of Nozzle to safe-end Weld ML20206J8351999-05-0707 May 1999 Rev 20,Change 7 to QAP-1.0, Northeast Utls QA Program (Nuqap) Tr ML20206G6221999-05-0404 May 1999 SER Accepting Util Request to Apply leak-before-break Status to Pressurizer Surge Line Piping for Millstone Nuclear Power Station,Unit 2 B17782, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station,Unit 1.With ML20205R3531999-04-30030 April 1999 Addendum 4 to Annual Rept, B17775, Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Nuclear Power Station Unit 3.With ML20205K6141999-04-30030 April 1999 Non-proprietary Version of Rev 2 to Holtec Rept HI-971843, Licensing Rept for Reclassification of Discharge in Millstone Unit 3 Spent Fuel Pool ML20206E2971999-04-30030 April 1999 Rev 1 to Millstone Nuclear Power Station,Unit 2 COLR - Cycle 13 B17777, Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with1999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Millstone Unit 2. with ML20205Q5891999-04-0909 April 1999 Rev 20,change 6 to QAP-1.0,Northeast Utils QA Program TR ML20205R8751999-04-0909 April 1999 Provides Commission with Staff Assessment of Issues Related to Restart of Millstone Unit 2 & Staff Recommendations Re Restart Authorization for Millstone Unit 2 ML20206T3991999-03-31031 March 1999 First Quarter 1999 Performance Rept, Dtd May 1999 B17747, Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With1999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Millstone Nuclear Power Station,Unit 1.With 1999-09-30
[Table view] |
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., O Mo u p 4 UNITED STATES 1 NUCLEAR REGULATORY COMMISSION l" wAsHlNGTON, D.C. 2006&4001
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SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION j i
EMERGENCY CORE COOLING SYSTEM LOCA ANALYSES l 4
l MILLSTONE NUCLEAR POWER STATION. UNIT 2
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DOCKET NO. 50-336 .
1.0 INTRODUCTION
[ By letter dated January 29, 1997, Northeast Nuclear Energy Company (NNECO),
the licensee for the Millstone Nuclear Power Station, Unit 2, identified "I i
errors and reported changes to the Emergency Core Cooling System evaluation models and the application of the models-for Millstone, Unit 2, as required by 10 CFR-50.46(a)(3)(ii). The submittal included changes and identified errors in both the large break loss-of-coolant accident (LBLOCA) and small break loss-of-coolant accident (SBLOCA) analyses performed for Millstone, Unit 2, since March 22, 1996.
2.0 BACKGROUND
The Millstone, Unit 2, LOCA analyses uses the Siemens Power Corporation (SPC)
LOCA evaluation models, which include the T00DEE2 computer code. The models were approved by the Nuclear Regulatory Commission (NRC) staff to meet the requirements of 10 CFR 50.46 in a letter dated July 8, 1986, from.
D.M. Crutchfield (NRC) to G. Ward (Exxon Nuclear).
The NRC staff met with SPC, formerly Exxon Nuclear, during August 1995 in regard to the SPC LBLOCA evaluation model. As a result of that meeting, the staff sent a letter to SPC, dated November 13, 1995, which identified problems relating to changes in the T00DEE2 computer code, which, as noted, is part of the evaluation models used by SPC for pressurized water reactors.
By letter dated November 13, 1995, the staff stated that SPC had made c hnges in 1991 to the NRC-approved Fuel Cooling Test Facility (FCTF) reflood heat transfer coefficient correlation used in the T000EE2 code and did not properly assess the significance of the code changes. The following two major changes were made to the FCTF correlation in the T00DEE2 code: (1) nonphysical non-monotonic behavior of the FCTF heat transfer coefficient correlation with respect to the reflood rate was eliminated; and (2) the quench time calculation used in-the model, using data from Cylindrical Core Test Facility (CCTF) experiments, was modified. By letter dated March 13, 1996, the staff requested that-SPC submit to the NRC, for review and approval, all model revisions and corrections in the T00DEE2 code implemented since the staff's approval of the code in July 1986.
On June 2, 1996, SPC submitted Topical Report XN-NF-82-20, "EXEM/PWR Large Break LOCA ECCS T00DEE2 Updates Revision 1, .0.mplement 5," which described 9707280139 970723 #
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I the updates made to the T000EE2 code between 1986 and 1991. The staff has l completed its review of this report and has concluded that the proposed 1991 j model LBLOCA-ECCS model is not acceptable and the previously approved 1986 i model has an unacceptable error. The staff issued its Safety Evaluation by letter dated November 29, 1996.
! SPC then )roposed new code changes to correct the error in the ?986 model and j to meet tie requirements of 10 CFR 50.46. The corrected model employs linear
. interpolation of reflood heat transfer coefficients used between effective
- reflood rates of 1.0 and 1.77 inches /sec to eliminate the nonphysical
! behavior. These changes are an interim step, pending completion of the staff's review of the revised LBLOCA evaluation model submitted in SPC Topical i Report XN-NF-82-20 (P), Revision 1, Supplement 6, "EXEM/PWR Large Break LOCA
{ ECCS Model Updates," December 1996.
l The proposed SPC interim model changes restricts the reflood heat transfer coefficient to increase linearly between the values calculated by the FCTF i
reflood heat transfer correlations for reflood rates of 1.0 in/sec and
- 1.77 in/sec. The interim model is used for the Millstone Unit 2 reanalysis.
1 By letter dated December 3, 1996, the staff requested that NNEC0 provide i
additional information to verify that Millstone, Unit 2, is in compliance with
' the requirements of 10 CFR 50 46. NNEC0 provided the requested information by letter dated January 29, 1997.
) 3.0 EVALUATION 4
3.1 LBLOCA 4
i NNEC0 provided a LBLCcA reanalysis for Millstone, Unit 2, using the SPC
! interim evaluation model. The interim model uses linear interpolation of heat j transfer coefficients with respect to reflood rate between reflood rates of ,
1.0 and 1.77 in/sec. A break spectrum that ranged from 0.4 to 1.0 for a double-ended cold leg guillotine (DECLG) break was analyzed for Millstone, Unit 2. The limiting break was found to be a 0.6 DECLG break. 'The limiting break calculation included the following information:
- 1. Maximum linear heat generation rate
- 2. Reflood rate as a function of time
- 3. Core collapsed level as a function of time
- 4. Quench time as a function of core height
- 5. Core pressure as a function of time
- 6. Core.subcooling as a function of time
- 7. Heat-transfer coefficient at the. peak clad temperature (PCT) location as a function of time
- 8. Clad temperature for PCT location as a function of time The staff has reviewed the information and determined that the SPC interim moc 1 has been shown to be conservative when compared with the SPC FCTF reflood data. Therefore, the LBLOCA reanalysis using the interim SPC evaluation model for Millstone, Unit, 2, is acceptable.
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l NNECO also provided the impact of an error in the Z-equivalent model, input 1 for a hydraulic diameter, and nonphysical trend in the reflood heat transfer correlations. The impact of the Z-equivalent error was previously analyzed by
- SPC and resulted in a 15-degree F increase in the PCT, which was reported to ,
" the NRC in 1994. The-impact of the error for the limiting PCT case in the reanalysis is a decrease of about 2 degrees F for which NNECO conservatively
- took no credit for. The impact of the hydraulic diameter input error is an 4 increase in the PCT of 111 degrees F and the error in the reflood heat i transfer correlations is an increase in the _ PCT of 189 degrees F.
t 2
The revised Millstone, Unit 2, LBLOCA analysis using the SPC interim evaluation model, including the errors, results in a PCT of 2111 degrees F.
This PCT is lower than the 2200_ degrees F acceptance criterion specified in 10 CFR 50.46 and is, therefore, acceptable, f 3.2 SBLOCA i
i NNECO also provided the impact of errors in the previously approved SPC SBLOCA model, ANF-RELAP, T000EE2, and RODEX2. Millstone, Unit 2, SBLOCA was i
reanalyzed with the approved SPC SBLOCA model including the impact of the identified errors. The previous analysis of record resulted in a PCT of 1707 degrees F. The following errors were identified and accounted for in the
( reanalysis:
~
! 1. A steady-state steam generator pressure control system was used instead
- of the transient pressure control system.
1
- 2. An uncertainty in the main steam safety valve set points of 1 percent
, was used in place of the Technical Specification value of 3 percent.
1 3. The time of scram for the decay heat models was incorrect in the T00DEE2
_ heatup calculation.
{
! Millstone, Unit 2, was analyzed with a peak linear heat generation rate (LHGR) j of 15.1 kw/ft. The limiting break size is P.1 square feet. The cortaction r for the errors increased the PCT by 303 degrees F. The reanalyzed PCT for the ,
L limiting SBLOCA, including the error corrections, is 2010 degrees F. This is also lower than the 2200 degrees F acceptance criterion specified in 10 CFR 50.46 and is, therefore, acceptable. 4 4.0. CONCLUSION Based.on the above, the NRC staff has concluded that the reanalysis for both the LSLOCA and SBLOCA are acceptable for the restart of Millstone, Unit 2.
The staff is still in the process of reviewing the revised LBLOCA evaluation model submitted in SPC Topical Report XN-NF-82-20 (P), Revision 1,
. i
1 i
.. l Supplement 6 "EXEM/PWR Large Break LOCA ECCS Model Updates," December 1996.
A plant-specific analysis using the SPC modified final LBLOCA model will be required before startup after the next refueling outage for the unit. ,
l l
Principal Contributors: G. Thomas J. Staudenmeir i
Date: July 23, 1997 '
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