ML20052E705

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LER 82-028/04L-0:on 820404,flow Indicator SFR-201 for Turbine Gland Seal Leakoff Failed High.Caused by Excessive Moisture on Sensing Element.Moisture Removed,Probe Reinstalled & Indicator Returned to Svc
ML20052E705
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 04/29/1982
From: Palmer R
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20052E703 List:
References
LER-82-028-04L, LER-82-28-4L, NUDOCS 8205110367
Download: ML20052E705 (1)


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" "' l 60Ll@l 0l 5 l 0lDOCK 3o C 61 010131 ET NUM8 ER 1161@l 68 014101418121@l 63 EVENT DATE 74 014REPORT 75 l 2l 918DATE l 21@80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Oio 10 : 21 l DURING NORMAL OPERATION, THE FLOW INDICATOR (SFR-201) FOR THE TURBINE GLAND SEAL l io i,i l LEAK 0FF (GSLO) FAILED HIGH. THE INSTRUMENTATION WAS DECLARED INOPERABLE AT 1137 l i o i ., i l HOURS ON APRIL 4, 1982. CONTINUOUS FLOW MEASUREMENT IS REQUIRED BY TECHNICAL SPEC- l io is; i IFICATION, APPENDIX B, 2.4.4.b AND TABLE 2.2.4. l I

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CODE CODE SU8 CODE COMPONENT CODE SUBC D'E S E 10191 l MI Cl@ W@ l A l@ l Il NI Sl Tl Ri Ul@ [Ej@ l Z l@ 18 19 20 i 8 9 10 11 12 13 LER RO EVENT YEAR REPORT O DE Y N

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3b 36 31 40 41 42 44 CAUSE DESC RIPTION AND CORRECTIVE ACTIONS 27 l ioil THE FLOW INDICATING PROBE (SFR-201) WAS EXAMINED AND FOUND TO HAVE EXCESSIVE l 1iiil l MOISTURE ON THE SENSING ELEMENT. THE M0ISTURE WAS REMOVED, THE PROBE LAS REINSTALLED I INVESTIGATIDN i,,,i! AND THE INDICATOR RETURNED TO NORMAL AT 1000 HOURS ON APRIL 5, 1982. l i, ,,i l IS CONTINUING TO REDUCE THE M0IST!'RE IN THIS AREA. l I

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NAME OF PREPARER PHONE:

616-465-5901 2,