ML20039D285

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LER 81-067/03L-0:on 811120,81-psi Control Air Header Was Out Inadvertently During Installation of NUREG-0737 Design Change,Causing Normal Letdown Isolation Valve QCR-300 to Close.Shift Supervisor Reinstructed
ML20039D285
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 12/21/1981
From: Don Krause
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20039D257 List:
References
RTR-NUREG-0737, RTR-NUREG-737 LER-81-067-03L, LER-81-67-3L, NUDOCS 8112310492
Download: ML20039D285 (1)


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NRC FORM 3G6 U. S. NUCLE AR REGUL ATORY COMMISSION (7 77)

LICENSEE EVENT REPORT

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(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI CONTROL BLOCK: l i

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l C l Cl 2 l@l 010 l -l 0101010 LICENSEE CODE 14 15 LICENSE NuveER l 0 l- l010 l@l 25 4111111 26 LICENSE TYPEl 0JOl@l 57 CAl T b8l@

CON'T LO_L' I 7 8 5fRMlLl@l 60 61 01510101013l116l@l1111210l811l@l11212111811l@

DOCKk f NUMBER 68 69 EVENT DATE 14 75 RFPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h I

I o 12 l lAN EVENT OCCURRED AS THE RESULT OF A PLANNED ENTRY INTO AN ACTION ITEM TO INSTALL A l

I O i a l l NUREG-0737 DESIGN CHANGE. THIS RE0VIRED THE ISOLATION OF THE 50 PSI CONTROL AIR iOla11 HEADER. INADVERTENTLY THE 85 PSI CONT. AIR HDR. WAS CUT. THIS CAUSED THE NORMAf I 1

iOIsi ILETDOWN ISOLATION VALVE OCR-300 TO CLOSE. VALVE WAS RLOCKED OPEN AND OPERATOR 1

I o is I l STATIONED AT THE MANUAL ISOLATION VALVE IN ORDER TO MAINTAIN NORMAL I ETDOWN FLOW.

I O I 7 I l THIS IS CONTRARY TO T.S. 3.6.1.1. I I

10181l CODE C0$e Su8 CODE COMPONENT CODE S BC D'E S E l0l9l l S l D I @ LA_J@ l A l @ l Vl Al L l V I E l X I@ [_F_j@ [.D_J @

7 8 9 10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION EVENT YE AR REPORT NO. CODE TYPE N O.

Nu,g O "LE EP R'RO [--] l 016171 l/l 1013l [L_J [-j l_0_j

_ l21 81 22 Il 23 24 26 27 28 29- 30 31 32 K N A T OP O* P NT METH HOURS S8 fi FO ib 8. SUPPLIE MAN FACTURER ll.j@llLJ@ LZ-]@ I.2J@ 10101010I 31 l!LJ@ IN l@ [Z_j@ lC161315l@

44 3J 34 35 36 40 di 42 43 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h Ii l o l l THE VALVE WAS BLOCKED WITH THE SHIFT SUPERVISORS KNOWLEDGE WITH ISOLATION CAPABILITY I I

lilil l ASSURED BY STATIONING AN OPERATOR AT MANUAL ISOL. VALVE. THE S.S. HAS BEEN REIN-I ii i2 I STRUCTED THAT AUT0. ISOLATION FEATURES CAN NOT BE DEFEATED. THIS EVENT WILL BE I

I i I a 1 i REVIEWED BY ALL LICENSED OPERATORS.

1 li14l l ST S *s POWER OTHER STATUS DIS O RY DISCOVERY DESCRIPTION 32 N/A NOTIFIED BY CONSTRUCTION PERSONNEL l 11 Is l [E_J@ l1 l 010 l@l l l l@l ACTIVITY CO RENT AMOUNT OF ACTIVITY LOCATION OF RELE ASE I 516 iRELEASE Lz_j @D OF RELEASEI.zjgl N/A l l N/A [

7 8 9 to 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION g l 0 l 0 l O l@l Z l@l N/A l PERSO~NE L imuLS NuveER oESCRiPriON@

N/A l It la 8l 9l 0101 Ol@l12 7 11 80

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