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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML19346G9701994-07-19019 July 1994 LER 94-006-00:on 940620,group 2 Isolation Occurred Due to Operator Turning Wrong Switch & Deenergizing Radiation Monitor.Operator Disciplined & Radiation Monitor Switches modified.W/940719 Ltr ML20029D7901994-05-0202 May 1994 LER 89-021-02:on 890916,crack Was Discovered on Upper Support Brace of One Jet Pump Riser.Caused by High Cycle Fatigue.Testing Has Demonstrated That Cracking Is Self limiting.W/940502 Ltr ML20029C7061994-04-22022 April 1994 LER 94-001-00:on 940323,missed Surveillance on SRV Low-Low Set Logic.Caused by Incorrect Surveillance Procedure Prerequisite.Corrective Action:Removed Incorrect Prerequisites,Trained on Procedure review.W/940422 Ltr ML20029C6921994-04-22022 April 1994 LER 94-002-00:on 940324,discovered That Breaker Tripped at Current Below Tolerance.Caused by Design of Breakers. Corrective Action:Circuit Breakers Revised for Further Classification for Testing Instantaneous trip.W/940422 Ltr ML20045G3241993-07-0606 July 1993 LER 93-007-00:on 930604,ESF Actuation Occurred Due to Loss of Reactor Protection Sys Power Supply.Replaced Failed Relay & Returned Motor Generator Set to svc.W/930706 Ltr ML20045B2601993-06-0909 June 1993 LER 93-006-01:on 930323,RPM Actuation Occurred from High Pressure Caused by Inadequate Procedure.Turbine Stop & Control Valve Tightness Test Procedures & Plant Simulator revised.W/930609 Ltr ML20044D5361993-04-14014 April 1993 LER 90-001-05:on 900313,design Deficiencies Noted in Emergency Filter Train Sys.On 930315,determined That Train B of CR Emergency Filtration Sys Could Not Provide Adequate Flow.Alternate Measuring Sys Method Implemented ML20044D5381993-04-14014 April 1993 LER 89-040-02:on 891219,secondary Containment Failed to Meet Operability Requirements During Special Test.Caused by Design Deficiencies.Operating Procedures Revised & Administrative Hold Placed on One Sys Component ML20024H2171991-05-22022 May 1991 LER 91-008-00:on 910422,cracking Discovered on Control Rod Drive Housing Flange Cap Screws.Caused by Inadequate Design of Screws.Four New,Original Equipment Cap Screws Installed & Reactor Vessel Hydro performed.W/910522 Ltr ML20028E8261983-01-21021 January 1983 LER 83-001/01T-0:on 830108,during Cold shutdown,post-LOCA Recombiner B Discharge Inboard Primary Containment Isolation Valve & Leak Test Valves Not Fully Closed.Caused by Contractor Error.Valves Closed ML20027D5031982-10-0909 October 1982 Updated LER 82-016/01T-1:on 821009,during Inservice Insp, Indication Found at 12 O'Clock Location on Recirculation safe-end to Pipe Weld E & at 3 O'Clock Location on 821020. Caused by Intergranular Stress Corrosion Cracking ML20052F9951982-05-0808 May 1982 LER 82-005/03L-0:on 820408,lead Lifted in Control Circuitry for Outboard Shutdown Cooling valve,MO-2030,rendering Valve Inoperable.Caused by Misinterpretation of Special Operating Procedure.Lead Reinstalled & Procedures Revised ML20052C2051982-04-23023 April 1982 LER 82-004/01T-0:on 820410,ASCO Inboard & Outboard Drywell Vent 3-way Solenoid Valves,Model 830064C64U,failed to Close Upon Hand Switch Activation When Coil de-energized.Probably Caused by Horizontally Mounted Solenoids.Valves Replaced ML20050B0531982-03-23023 March 1982 Updated LER 81-001/03X-1:on 810126,while Performing Surveillance Test Mo 2035,HPCI Outboard Steam Supply Isolation Valve Failed to Close.Caused by Opened Limitorque SMB-O,240-volt Dc & Torque Switches.Switches Replaced ML20042A4631982-03-12012 March 1982 LER 82-003/03L-0:on 820212,reactor Water Cleanup Primary Containment Inboard Isolation Valve MO-2397 Became Inoperable While in Full Open Position.Caused by Normally Energized Relay Coil 16A-K36 Shorting.Relay Replaced ML20040G7371982-02-0606 February 1982 LER 82-002/03L-0:on 820107,core Spray Pump 11 Start Time Delay Relay Failed to Operate.Caused by Loose Terminal Connection & Microswitch Contact Burned Open.New GE CR 2820 Relay Installed ML20040A5701982-01-15015 January 1982 LER 82-001/01T-0:on 820102,outboard Shutdown Cooling Suction Isolation Valve Found to Exceed Tech Spec Limits for Local Leak Rate Test.Caused by Valve Disc,Undersized by Extensive Lapping of Disc & Valve Body Seats,Traveling Too Far ML20039B2281981-12-10010 December 1981 LER 81-023/03L-0:on 811110,during Cold shutdown,4 Channel a Main Steam Line High Flow Switches Found Inoperable.Caused by Heating of Switching Element Due to Relay Coil Failure, Initially Reported in LER 81-021.Elements Replaced ML20027C2371981-08-24024 August 1981 LER 81-020/03L-0:on 810724,main Steam Leak Revealed in Drain Line to Condenser.Caused by Piping Leaking Immediately Downstream of 45 Degree Elbow Due to Erosion & Impingement Resulting from Steam & Water Flow from Restricting Orifice ML20009E4141981-07-20020 July 1981 LER 81-018/03L-0:on 810620,reactor Water Cleanup Sys Was Returned to Svc Following Maint W/Discharge Isolation Valve MO2399 Open & Inoperable.Caused by Torque Switch Failure. Motor & Torque Switch Replaced & Sys Returned to Svc ML20009D5671981-07-16016 July 1981 LER 81-017/03L-0:on 810617,cracks Discovered on 4-inch & 1-inch Reactor Water Cleanup Heat Exchanger Piping,At Connection to Heat Exchanger.Caused by Poor fit-up & Welding Due to 3-inch Slag Line Near Root of Weld ML19332B3791980-09-22022 September 1980 LER 80-027/03L-0:on 80823,during Monthly surveillance,42-11 Test Control Rod Could Not Be Withdrawn After Partial Insertion.Caused by Closed Drive Withdraw Riser Isolation Valve CRD-102.Valve Opened & Rod Was Operable ML1129007601980-07-0101 July 1980 LER 80-023/03L-0:on 800601,air Ejector Offgas Radiation Monitors Dropped to About 20% Normal for About 40 Minutes. Caused by Mechanical Vacuum Pump Offgas Sample Valve Being Incorrectly Opened.Valve Now Wired Shut ML1129007541980-06-26026 June 1980 LER 80-022/03L-0:on 800529,primary Containment Oxygen Concentration Exceeded 5% by Weight Tech Spec Limit.Caused by Open Svc Air Isolation Valve to Drywell.Procedures Have Been Revised to Assure Proper Valve Positioning ML1129007511980-06-12012 June 1980 LER 80-021/03L-0:on 800515,during Normal Startup,Reactor Core Isolation Cooling Control Power Fuse Opened.Caused by Shorted Relay Coil in Circuit Due to Ac Relay Inadvertently Installed by Maint Personnel.Relay Replaced ML1129007481980-06-0202 June 1980 Updated 79-015/03L-1:on 790712,during Routine Insp,Steam Leak from 13A Intermediate Pressure Feedwater Heater Was Detected.Insulation Removal Revealed through-wall Flaw in Heater Shell.Caused by erosion-corrosion ML1129007451980-05-27027 May 1980 LER 80-020/03L-0:on 800427,during post-maint Startup of Reactor Recirculation Sys,Inaccessible Recirculation Valve Motor Failed.Cause Not Stated.Motor Is Limitorque Type SMB-2 W/Magnetic Brake ML1129007221980-05-0909 May 1980 LER 80-018/03L-0:on 800411,during Routine Operator Insp, Attachment Weld of Ripple to Level Switch Float Chamber Assembly on Moisture Separator Level Switch LS-1188 Found Cracked.Caused by Improper Weld Procedure ML1129007071980-04-11011 April 1980 LER 80-017/01T-0:on 800328,Bechtel Power Corp Notified Util That Control Rod Driveline Hydraulic Piping Frame Supports Would Not Meet OBE Stress Limits.Caused by Eds Computer Code Error.Supports Modified ML1129006851980-04-10010 April 1980 LER 80-016/01T-0:on 800327,during Refueling,Supports for SRV Pneumatic Supply Sys Would Not Meet Seismic Class I Requirements.Caused by Inadequate Design & Installation of Sys.Sys Was Upgraded to Satisfy Requirements ML1129006801980-03-27027 March 1980 LER 80-015/01T-0:on 800317,during Refueling Outage & Insp Required by IE Bulletin 79-01B,unqualified Splices Found in Power Cables for Inboard MSIV Solenoid Valves.Cause Not Stated.Splices Replaced W/Qualified Matls ML1129006781980-03-26026 March 1980 LER 80-006/03L-0:on 800226,during Refueling Outage,Seven of Main Steam Line Area Temp Switches Found to Trip Above Required Level.Caused by Setpoint Drift.Switches Recalibr ML1129006651980-03-21021 March 1980 LER 80-013/01T-0:on 800309,during Refueling Operations,Rod Withdrawn Block Not Received When Refueling Bridge Traversed Core.Caused by Actuating Arm Out of Adjustment.Components Readjusted & Interlocks Tested Prior to Refueling ML1129006681980-03-20020 March 1980 LER 80-011/01T-0:on 800306,during Refueling Outage,Repairs to Outboard MSIV Stop Valve Revealed Flow Path Between Secondary Containment & Turbine Bldg When MSIV Poppet Was Pulled.Caused by Lack of Preventive Procedure Controls ML1129006621980-03-14014 March 1980 LER 80-007/01T-0:on 800303,during Refuel Shutdown,Cable Routing for HPCI & Automatic Depressurization Sys Cables Identified Lack of Physical Separation Between Automatic Depressurization Sys Cables & Ones for Div of HPCI Sensors ML1129009771980-01-18018 January 1980 LER 79-024/03L-0:on 791220,during Normal Operation,Routine Operator Insp Revealed Steam Leak in 1-inch 90 Degree Elbow in Reactor Core Isolation Cooling Steam Line Drain to Condenser.Caused by Pinhole Failure of 3,000-lb Socket Weld ML1129009741980-01-14014 January 1980 Updated LER 79-023/01T-1:on 800103,one Fuel Type Noted to Exceed Max Allowable Max Average Planar Linear Heat Generation Rate Value & Another as Improperly Programmed in Plant Computer.Caused by Inadequate Review ML1129009551979-12-19019 December 1979 LER 79-021/03L-0:on 791119,during IE Bulletin 79-02 Evaluation,Snubber SS-31 Base Plate Expansion Anchor Bolt Safety Factor Found to Be Less than One.Caused by Inadequate Base Plate & Expansion Anchor Bolts ML1129009031979-08-31031 August 1979 LER 79-017/03L-0:on 790806,steam Leak Observed on Feedwater Extraction Steam Line Drain 15A.Caused by Steam Erosion Through Wall of Steam Trap on Line.Trap Isolated Pending Repair or Replacement at Next Appropriate Outage ML1129008891979-08-10010 August 1979 LER 79-015/03L-0 on 790712:discovered Steam Leak from Intermediate Pressure Feedwater Heater.Cause Undetermined. Temporary Patch Installed Pending Replacement of Heater Shell ML1129008831979-08-0707 August 1979 LER 79-013/03L-0 on 790708:motor Operator Failed,Rendering Torus Cooling Injection Valve Inoperable During Normal Operation.Caused by Failure of Motor Winding Due to Limit Switch Not de-energizing Motor.Switch Replaced ML1129008801979-08-0606 August 1979 LER 79-014/03L-0 on 790709:water Leak Discovered in 1/2 Inch Instrument Line from Reactor Water Cleanup Sys Nonregenerative Heat Exchanger.Cause Not Determined.Leaking Line Isolated & Will Be Further Investigated & Repaired ML1129008771979-08-0101 August 1979 LER 79-012/03L-0 on 790702:during Reactor Core Isolation Cooling Sys Test,Governor end-bearing Temp Alarm Received & Bearing Exhibited High Vibration.Sys Inoperative.Caused by Turbine Oil Pump Drive Gear Failure.Gears Replaced ML1129008561979-06-28028 June 1979 LER 79-011/03L-0 on 790529:no Min Flow in B Train Standby Gas Treatment Sys.Caused by Dilution Flow from Compressed Storage Not Isolated by BV-5.Replaced Positioner & Installed Filter in Cylinder Supply/Return Line ML1127801511979-03-15015 March 1979 LER 79-003/01T-0 on 790301:containment Vent & Purge Isolation Valves Would Not Close During DBA-LOCA.Cause Unknown.Fisher Continential 18 & 20 Inch,Type 9220 Butterfly Valves Opening Is Administratively Controlled ML1127601481979-02-0909 February 1979 LER 79-002/03L-0 on 790118:during Normal Operation,Weekly Average Power Range Monitor Functional Scram Test Was Not Completed within Time Allowed.Caused by Personnel Error ML1127601201979-02-0202 February 1979 LER 79-001/03L-0 on 790110:during Normal Operation,Steam Leak Found in Elbow on Turbine Main Steam Bypass Header 1 Inch Drain Line to Condenser,Due to Erosion Caused by Steam & Water Flow of Restricting orifice,RO-2569 ML1127601181979-01-29029 January 1979 LER 78-016/03X-1 on 780908:during Normal Operation,Trip of Essential MCC B33A Supply Breaker 52-304 Resulted in Operation in Degraded Mode.Caused by Low Setpoint on Trip Device & by Loss of Dash Pot Oil in Trip Device ML1127601131978-12-29029 December 1978 LER 78-030/01T-0 on 781218:during surveillance,MO-2-64A Recirculation Loop 11 Discharge Bypass Valve Would Not Close.Cause Is Unknown Due to Inaccessibility of Valve ML1127601431978-12-19019 December 1978 LER#78-028/03L-0 on 781124:during Normal Oper,Small Steam Leak Was Discovered in Weld of 45 Degree Elbow on HPCI Steam Supply Line 1 Inch Drain Line to Main Condenser Due to Corrrosion.Weld Repair Made at Leak.Awaiting Parts 1994-07-19
[Table view] Category:RO)
MONTHYEARML19346G9701994-07-19019 July 1994 LER 94-006-00:on 940620,group 2 Isolation Occurred Due to Operator Turning Wrong Switch & Deenergizing Radiation Monitor.Operator Disciplined & Radiation Monitor Switches modified.W/940719 Ltr ML20029D7901994-05-0202 May 1994 LER 89-021-02:on 890916,crack Was Discovered on Upper Support Brace of One Jet Pump Riser.Caused by High Cycle Fatigue.Testing Has Demonstrated That Cracking Is Self limiting.W/940502 Ltr ML20029C7061994-04-22022 April 1994 LER 94-001-00:on 940323,missed Surveillance on SRV Low-Low Set Logic.Caused by Incorrect Surveillance Procedure Prerequisite.Corrective Action:Removed Incorrect Prerequisites,Trained on Procedure review.W/940422 Ltr ML20029C6921994-04-22022 April 1994 LER 94-002-00:on 940324,discovered That Breaker Tripped at Current Below Tolerance.Caused by Design of Breakers. Corrective Action:Circuit Breakers Revised for Further Classification for Testing Instantaneous trip.W/940422 Ltr ML20045G3241993-07-0606 July 1993 LER 93-007-00:on 930604,ESF Actuation Occurred Due to Loss of Reactor Protection Sys Power Supply.Replaced Failed Relay & Returned Motor Generator Set to svc.W/930706 Ltr ML20045B2601993-06-0909 June 1993 LER 93-006-01:on 930323,RPM Actuation Occurred from High Pressure Caused by Inadequate Procedure.Turbine Stop & Control Valve Tightness Test Procedures & Plant Simulator revised.W/930609 Ltr ML20044D5361993-04-14014 April 1993 LER 90-001-05:on 900313,design Deficiencies Noted in Emergency Filter Train Sys.On 930315,determined That Train B of CR Emergency Filtration Sys Could Not Provide Adequate Flow.Alternate Measuring Sys Method Implemented ML20044D5381993-04-14014 April 1993 LER 89-040-02:on 891219,secondary Containment Failed to Meet Operability Requirements During Special Test.Caused by Design Deficiencies.Operating Procedures Revised & Administrative Hold Placed on One Sys Component ML20024H2171991-05-22022 May 1991 LER 91-008-00:on 910422,cracking Discovered on Control Rod Drive Housing Flange Cap Screws.Caused by Inadequate Design of Screws.Four New,Original Equipment Cap Screws Installed & Reactor Vessel Hydro performed.W/910522 Ltr ML20028E8261983-01-21021 January 1983 LER 83-001/01T-0:on 830108,during Cold shutdown,post-LOCA Recombiner B Discharge Inboard Primary Containment Isolation Valve & Leak Test Valves Not Fully Closed.Caused by Contractor Error.Valves Closed ML20027D5031982-10-0909 October 1982 Updated LER 82-016/01T-1:on 821009,during Inservice Insp, Indication Found at 12 O'Clock Location on Recirculation safe-end to Pipe Weld E & at 3 O'Clock Location on 821020. Caused by Intergranular Stress Corrosion Cracking ML20052F9951982-05-0808 May 1982 LER 82-005/03L-0:on 820408,lead Lifted in Control Circuitry for Outboard Shutdown Cooling valve,MO-2030,rendering Valve Inoperable.Caused by Misinterpretation of Special Operating Procedure.Lead Reinstalled & Procedures Revised ML20052C2051982-04-23023 April 1982 LER 82-004/01T-0:on 820410,ASCO Inboard & Outboard Drywell Vent 3-way Solenoid Valves,Model 830064C64U,failed to Close Upon Hand Switch Activation When Coil de-energized.Probably Caused by Horizontally Mounted Solenoids.Valves Replaced ML20050B0531982-03-23023 March 1982 Updated LER 81-001/03X-1:on 810126,while Performing Surveillance Test Mo 2035,HPCI Outboard Steam Supply Isolation Valve Failed to Close.Caused by Opened Limitorque SMB-O,240-volt Dc & Torque Switches.Switches Replaced ML20042A4631982-03-12012 March 1982 LER 82-003/03L-0:on 820212,reactor Water Cleanup Primary Containment Inboard Isolation Valve MO-2397 Became Inoperable While in Full Open Position.Caused by Normally Energized Relay Coil 16A-K36 Shorting.Relay Replaced ML20040G7371982-02-0606 February 1982 LER 82-002/03L-0:on 820107,core Spray Pump 11 Start Time Delay Relay Failed to Operate.Caused by Loose Terminal Connection & Microswitch Contact Burned Open.New GE CR 2820 Relay Installed ML20040A5701982-01-15015 January 1982 LER 82-001/01T-0:on 820102,outboard Shutdown Cooling Suction Isolation Valve Found to Exceed Tech Spec Limits for Local Leak Rate Test.Caused by Valve Disc,Undersized by Extensive Lapping of Disc & Valve Body Seats,Traveling Too Far ML20039B2281981-12-10010 December 1981 LER 81-023/03L-0:on 811110,during Cold shutdown,4 Channel a Main Steam Line High Flow Switches Found Inoperable.Caused by Heating of Switching Element Due to Relay Coil Failure, Initially Reported in LER 81-021.Elements Replaced ML20027C2371981-08-24024 August 1981 LER 81-020/03L-0:on 810724,main Steam Leak Revealed in Drain Line to Condenser.Caused by Piping Leaking Immediately Downstream of 45 Degree Elbow Due to Erosion & Impingement Resulting from Steam & Water Flow from Restricting Orifice ML20009E4141981-07-20020 July 1981 LER 81-018/03L-0:on 810620,reactor Water Cleanup Sys Was Returned to Svc Following Maint W/Discharge Isolation Valve MO2399 Open & Inoperable.Caused by Torque Switch Failure. Motor & Torque Switch Replaced & Sys Returned to Svc ML20009D5671981-07-16016 July 1981 LER 81-017/03L-0:on 810617,cracks Discovered on 4-inch & 1-inch Reactor Water Cleanup Heat Exchanger Piping,At Connection to Heat Exchanger.Caused by Poor fit-up & Welding Due to 3-inch Slag Line Near Root of Weld ML19332B3791980-09-22022 September 1980 LER 80-027/03L-0:on 80823,during Monthly surveillance,42-11 Test Control Rod Could Not Be Withdrawn After Partial Insertion.Caused by Closed Drive Withdraw Riser Isolation Valve CRD-102.Valve Opened & Rod Was Operable ML1129007601980-07-0101 July 1980 LER 80-023/03L-0:on 800601,air Ejector Offgas Radiation Monitors Dropped to About 20% Normal for About 40 Minutes. Caused by Mechanical Vacuum Pump Offgas Sample Valve Being Incorrectly Opened.Valve Now Wired Shut ML1129007541980-06-26026 June 1980 LER 80-022/03L-0:on 800529,primary Containment Oxygen Concentration Exceeded 5% by Weight Tech Spec Limit.Caused by Open Svc Air Isolation Valve to Drywell.Procedures Have Been Revised to Assure Proper Valve Positioning ML1129007511980-06-12012 June 1980 LER 80-021/03L-0:on 800515,during Normal Startup,Reactor Core Isolation Cooling Control Power Fuse Opened.Caused by Shorted Relay Coil in Circuit Due to Ac Relay Inadvertently Installed by Maint Personnel.Relay Replaced ML1129007481980-06-0202 June 1980 Updated 79-015/03L-1:on 790712,during Routine Insp,Steam Leak from 13A Intermediate Pressure Feedwater Heater Was Detected.Insulation Removal Revealed through-wall Flaw in Heater Shell.Caused by erosion-corrosion ML1129007451980-05-27027 May 1980 LER 80-020/03L-0:on 800427,during post-maint Startup of Reactor Recirculation Sys,Inaccessible Recirculation Valve Motor Failed.Cause Not Stated.Motor Is Limitorque Type SMB-2 W/Magnetic Brake ML1129007221980-05-0909 May 1980 LER 80-018/03L-0:on 800411,during Routine Operator Insp, Attachment Weld of Ripple to Level Switch Float Chamber Assembly on Moisture Separator Level Switch LS-1188 Found Cracked.Caused by Improper Weld Procedure ML1129007071980-04-11011 April 1980 LER 80-017/01T-0:on 800328,Bechtel Power Corp Notified Util That Control Rod Driveline Hydraulic Piping Frame Supports Would Not Meet OBE Stress Limits.Caused by Eds Computer Code Error.Supports Modified ML1129006851980-04-10010 April 1980 LER 80-016/01T-0:on 800327,during Refueling,Supports for SRV Pneumatic Supply Sys Would Not Meet Seismic Class I Requirements.Caused by Inadequate Design & Installation of Sys.Sys Was Upgraded to Satisfy Requirements ML1129006801980-03-27027 March 1980 LER 80-015/01T-0:on 800317,during Refueling Outage & Insp Required by IE Bulletin 79-01B,unqualified Splices Found in Power Cables for Inboard MSIV Solenoid Valves.Cause Not Stated.Splices Replaced W/Qualified Matls ML1129006781980-03-26026 March 1980 LER 80-006/03L-0:on 800226,during Refueling Outage,Seven of Main Steam Line Area Temp Switches Found to Trip Above Required Level.Caused by Setpoint Drift.Switches Recalibr ML1129006651980-03-21021 March 1980 LER 80-013/01T-0:on 800309,during Refueling Operations,Rod Withdrawn Block Not Received When Refueling Bridge Traversed Core.Caused by Actuating Arm Out of Adjustment.Components Readjusted & Interlocks Tested Prior to Refueling ML1129006681980-03-20020 March 1980 LER 80-011/01T-0:on 800306,during Refueling Outage,Repairs to Outboard MSIV Stop Valve Revealed Flow Path Between Secondary Containment & Turbine Bldg When MSIV Poppet Was Pulled.Caused by Lack of Preventive Procedure Controls ML1129006621980-03-14014 March 1980 LER 80-007/01T-0:on 800303,during Refuel Shutdown,Cable Routing for HPCI & Automatic Depressurization Sys Cables Identified Lack of Physical Separation Between Automatic Depressurization Sys Cables & Ones for Div of HPCI Sensors ML1129009771980-01-18018 January 1980 LER 79-024/03L-0:on 791220,during Normal Operation,Routine Operator Insp Revealed Steam Leak in 1-inch 90 Degree Elbow in Reactor Core Isolation Cooling Steam Line Drain to Condenser.Caused by Pinhole Failure of 3,000-lb Socket Weld ML1129009741980-01-14014 January 1980 Updated LER 79-023/01T-1:on 800103,one Fuel Type Noted to Exceed Max Allowable Max Average Planar Linear Heat Generation Rate Value & Another as Improperly Programmed in Plant Computer.Caused by Inadequate Review ML1129009551979-12-19019 December 1979 LER 79-021/03L-0:on 791119,during IE Bulletin 79-02 Evaluation,Snubber SS-31 Base Plate Expansion Anchor Bolt Safety Factor Found to Be Less than One.Caused by Inadequate Base Plate & Expansion Anchor Bolts ML1129009031979-08-31031 August 1979 LER 79-017/03L-0:on 790806,steam Leak Observed on Feedwater Extraction Steam Line Drain 15A.Caused by Steam Erosion Through Wall of Steam Trap on Line.Trap Isolated Pending Repair or Replacement at Next Appropriate Outage ML1129008891979-08-10010 August 1979 LER 79-015/03L-0 on 790712:discovered Steam Leak from Intermediate Pressure Feedwater Heater.Cause Undetermined. Temporary Patch Installed Pending Replacement of Heater Shell ML1129008831979-08-0707 August 1979 LER 79-013/03L-0 on 790708:motor Operator Failed,Rendering Torus Cooling Injection Valve Inoperable During Normal Operation.Caused by Failure of Motor Winding Due to Limit Switch Not de-energizing Motor.Switch Replaced ML1129008801979-08-0606 August 1979 LER 79-014/03L-0 on 790709:water Leak Discovered in 1/2 Inch Instrument Line from Reactor Water Cleanup Sys Nonregenerative Heat Exchanger.Cause Not Determined.Leaking Line Isolated & Will Be Further Investigated & Repaired ML1129008771979-08-0101 August 1979 LER 79-012/03L-0 on 790702:during Reactor Core Isolation Cooling Sys Test,Governor end-bearing Temp Alarm Received & Bearing Exhibited High Vibration.Sys Inoperative.Caused by Turbine Oil Pump Drive Gear Failure.Gears Replaced ML1129008561979-06-28028 June 1979 LER 79-011/03L-0 on 790529:no Min Flow in B Train Standby Gas Treatment Sys.Caused by Dilution Flow from Compressed Storage Not Isolated by BV-5.Replaced Positioner & Installed Filter in Cylinder Supply/Return Line ML1127801511979-03-15015 March 1979 LER 79-003/01T-0 on 790301:containment Vent & Purge Isolation Valves Would Not Close During DBA-LOCA.Cause Unknown.Fisher Continential 18 & 20 Inch,Type 9220 Butterfly Valves Opening Is Administratively Controlled ML1127601481979-02-0909 February 1979 LER 79-002/03L-0 on 790118:during Normal Operation,Weekly Average Power Range Monitor Functional Scram Test Was Not Completed within Time Allowed.Caused by Personnel Error ML1127601201979-02-0202 February 1979 LER 79-001/03L-0 on 790110:during Normal Operation,Steam Leak Found in Elbow on Turbine Main Steam Bypass Header 1 Inch Drain Line to Condenser,Due to Erosion Caused by Steam & Water Flow of Restricting orifice,RO-2569 ML1127601181979-01-29029 January 1979 LER 78-016/03X-1 on 780908:during Normal Operation,Trip of Essential MCC B33A Supply Breaker 52-304 Resulted in Operation in Degraded Mode.Caused by Low Setpoint on Trip Device & by Loss of Dash Pot Oil in Trip Device ML1127601131978-12-29029 December 1978 LER 78-030/01T-0 on 781218:during surveillance,MO-2-64A Recirculation Loop 11 Discharge Bypass Valve Would Not Close.Cause Is Unknown Due to Inaccessibility of Valve ML1127601431978-12-19019 December 1978 LER#78-028/03L-0 on 781124:during Normal Oper,Small Steam Leak Was Discovered in Weld of 45 Degree Elbow on HPCI Steam Supply Line 1 Inch Drain Line to Main Condenser Due to Corrrosion.Weld Repair Made at Leak.Awaiting Parts 1994-07-19
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D1261999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Monticello Nuclear Generating Plant.With ML20216E7031999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Monticello Nuclear Generating Plant.With ML20210Q0521999-08-0404 August 1999 Safety Evaluation Approving Relief Request 10 to License DPR-22 Per 10CFR50.55a(g)(6)(i).Inservice Exam for Relief Request 10,Parts A,B,C,D & E Impractical & Reasonable Assurance of Structural Integrity Provided ML20210Q6611999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Monticello Nuclear Generating Plant.With ML20209F7901999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Monticello Nuclear Generating Plant.With ML20195H0351999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Monticello Nuclear Generatintg Plant.With ML20206N1721999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Monticello Nuclear Generating Plant.With ML20205N0861999-04-12012 April 1999 Safety Evaluation Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20205P5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Monticello Nuclear Generating Plant.With ML20204H4951999-03-18018 March 1999 SER Concluding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Monticello.Therefore Staff Concludes Licensee Adequately Addressed Action Required in GL 96-05 ML20205G7391999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Monticello Nuclear Generating Plant.With ML20202F7901999-01-25025 January 1999 1999 Four Year Simulator Certification Rept for MNGP Simulation Facility ML20199E4871999-01-0606 January 1999 SER Accepting Licensee 951116,960214 & 0524 Responses to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode ML20199F6211998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Mngp.With ML20205H0561998-12-31031 December 1998 Northern States Power Co 1998 Annual Rept. with ML20198P0691998-12-28028 December 1998 Safety Evaluation Concluding That NSP Proposed Alternative to Paragraph III-3411 of App III to 1986 Edition of Section XI of ASME Code Provides Acceptable Level of Quality & Safety.Alternative Authorized ML20198D0751998-12-10010 December 1998 Safety Evaluation Supporting NSP Proposed Change to EOPs to Use 2/3 Core Height as Potential Entry Condition Into Containment Flooding ML20198B2531998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Monticello Nuclear Generating Plant.With ML20195E3691998-11-12012 November 1998 Safety Evaluation Concluding That Licensee USI A-46 Implementation Has Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20195D2381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Monticello Nuclear Generating Plant.With ML20198J4451998-10-22022 October 1998 Rev 2 to SIR-97-003, Review of Test Results of Two Surveillance Capsules & Recommendations for Matls Properties & Pressure-Temp Curves to Be Used for Monticello Rpv ML20154L3471998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Monticello Nuclear Generating Plant.With ML20153F0511998-09-21021 September 1998 Rev 2 to MNGP Colr,Cycle 19 ML20153E9361998-09-0808 September 1998 Rev 1 to MNGP Colr,Cycle 19 ML20153B0861998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Monticello Nuclear Generating Plant.With ML20237B8461998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Monticello Nuclear Generating Plant ML20236W5041998-07-21021 July 1998 ISI Exam Summary Rept - Refueling Outage 19 ML20236R1941998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Monticello Nuclear Generating Plant ML20249A5861998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Monticello Nuclear Generating Plant ML20247K3971998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Monticello Nuclear Generating Plant ML20217D8731998-04-13013 April 1998 Rev 0 to MNGP Colr,Cycle 19 ML20217F6431998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Monticello Nuclear Generating Plant ML20216D1041998-03-0505 March 1998 Rev 21 to Operational QA Plan ML20216H6481998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Monticello Nuclear Generating Plant ML20203G1431998-02-10010 February 1998 Rev 2 to Inservice Insp Exam Plan,Third Interval,920601- 020531 ML20203B2821998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Monticello Nuclear Generating Station ML20202F9161998-01-29029 January 1998 Special Rept:On 980128,two of Three Fire Protection Pumps Were Removed from Svc as Result of Sys Configuration Necessary to Support Planned Maintenance.Fire Pumps Were Returned to Svc on 980128 ML20216D2071997-12-31031 December 1997 1997 Annual Rept for Northern States Power Co ML20197J8131997-12-31031 December 1997 Revised Evacuation Time Estimates for Plume Exposure Pathway Emergency Planning Zone at Monticello Nuclear Power Plant. W/One Oversize Drawing ML20198P2201997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Monticello Nuclear Generating Plant ML20203J7131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Monticello Nuclear Generating Plant ML20199G7051997-11-19019 November 1997 Safety Evaluation Authorizing Relief Request 8 of Third 10 Yr Inservice Insp Interval ML20199H8181997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Monticello Nuclear Generating Plant ML20217K2081997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Monticello Nuclear Generating Plant ML20216H7771997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Monticello Nuclear Generating Plant ML20217K2741997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Monticello Nuclear Generating Plant ML20196H1081997-07-0808 July 1997 Rev 20 to Operational QA Plan ML20141B9271997-06-30030 June 1997 LOCA Containment Analyses for Use in Evaluation of NPSH for RHR & Core Spray Pumps ML20149E2921997-06-30030 June 1997 Monthly Operating Rept for June 1997 for MNGP ML20148S6341997-06-23023 June 1997 NPSH - Rept of Sulzer Bingham Pump 1999-09-30
[Table view] |
Text
, !
2 Northem States Power Company l
414 Nicollet Mall l Minneapolis, Minnesota 55401 1927 l Telephone (612) 330-5500 l l
May 2, 1994 j Report Required by )
10 CFR Part 50, Section 50.73 US Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 l
MONTICELLO NUCLEAR GENERATING PIANT Docket No. 50-263 License No. DPR-22 l
Crack on Jet Punm Riser Brace Due to Fatinue A revised Licensee Event Report for this occurrence is attached. This report j modifies corrective actions identified in the original LER submitted on October 16, 1989 and in revision 1 to LER 89-021 submitted on December 12, l 1989. This letter contains no new NRC commitments. '
Please contact Marv Engen, Sr Licensing Engineer, at (612) 295-1291 if you require further information.
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4crRoger0 Anderson Director Licensing and Management Issues 1
l c: Regional Administrator - III, NRC NRR Project Manager, NRC Sr Resident Inspector, NRC State of Minnesota Attn: Kris Sanda Attachment 9405100102 940502 PDR ADOCK 05000263 pi S PDR , l
NRC FORM 366 tS 9a U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES 5/31/95 EST1MATEO BURDEN PER RESPONSE TO CCMPLY WITH This LICENSEE EVENT REPORT (LER) !NCO A MA T'ON COLLECT:CN AE'JUES7 50 0 HHS FCRWARO CcMMENTs neGAaOsG eunOn EsT1MA rE To THe NNFOnMATic AND RECOACS MANAGEMENT BRANCH (MN6B 7714i, U S. NUCLE A A AEQULATOAV COMMrS90N AASHINGTON. CC 20555 0001, AND TO (See reverse for required number of digits / Characters for each DIOCk) THE PAPERWOAK AEOUCTICN PROJECT (3150 0104). OFF'CE O MANAGE. MENT AND BUDGET. WASHWGTON OC 00503 F ACIUTY NAME (1)
DOCKET NUMBER (2)
MONTICELLO NUCLEAR GENERATING PLANT 'PAGE(3)
TITLE 14; 05000 - 263 1 OF 10 Crack on Jet Pump Riser Brace Due to Fatigue EVENT oATE (5)
LER NUMBER (6)
REPORT NuMDER (7) uosm cAv vEAn vEAn SEQUENDA- PW:StON OTHER FACILITIES INVOLVED (8)
,ygg "# # N#"E wygg MONTH CAY YEAA DE I NN 05000
" ncoryNAME 09 16 89 94 89-21 DOCGT NvV98 02 05 02 94 OPERATING 05000 MODE (9) N THIS REPORT IS SUBMITTED
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' 20 405tc) PURSUANT TO THE REQUIREMENT 3 OF 10 50 73 fan 2)ov)
POWER l 20 4C5faH 110) 73 71tbl 50.36icH 1)
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50 73(aH2)(x) Update Report vvi LICENSEE CONTACT FOR THIS LER (12) sp%Ne Nwua oncsc. A<.a cm Pete Kissinger, System Engineer (612) 295-1081 cats; sy s'E V COMPLETE COMPONEN7 UAN #
ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS R cecaTretE TO NPSOS cAusE sv3 ssi couvCNEv ven Ts.se MANuncvP TO Nen:s X AD SPT G080 No VES SUPPLEMENTAL REPORT EXPECTED (14)
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DATE (15)
ABSTRACT IL,m t to 100 spaces, i e , apprcomately 15 s ngte-spaced(16) tycewntten bries) l A crack was discovered on the upper support brace of one jet pump riser by use of an underwater of the upper support brace on the riser forjet pumps 7 and 8. camera The crack loca This event is being reported because of its potential safety significance and generic nature.
Visualinspection of all other riser braces in the vessel were completed. There are no other crack indications on the other leaves of this riser or any other riser in th e vessel.
The crack is believed to be the result of high cycle fatigue due to excitation of the resonance of t brace leaf due to recirculation pump vane passing frequency. Originally, a finite element analysis concluded that vane passing frequencies at pump speeds greater than 94% were the most probable cause of the cracking. Experimental confirmation of the analytical results in the forrn of a pressure pulsation test, with an appropriate full scale mockup of the Monticello jet pump and riser brace assemblies, was performed by General Electric Company. Based upon data from this experimental program, we have modified our corrective actions. A safety evaluation was completed to show that this crack has no effect on plant safety.
NAC COAM 366 M21
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NRC FORM 366A U.S. NUCLEAR REGULATORY CoMMisSloN APPROVED BY OMB NO. 3150 0104 u2; EXPlRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY MTM TMS LICENSEE EVENT REPORT (LER) %C'Es ka'ARElURc#NEIE O QiNSUr'iOf TEXT CONTINUATION QSu"$8"
, 'c"^u",^l37.8%C"r$"'e' o 7c'l3iu e e,s jCyR THE PAPERWOAK AEDUCTION PROJECT p1504104), OFFICE OF MANAGEMENT AND BUDGET. WASHINGTOA OC 20503 FACIUTY NAME (1) DOCKET NUMBER (2) LER NUMBER (tl paQg g3;
$(QUENTA, ROW $;ON NUMBER NUMBER 05000 - 263 OF Monticello Nuclear Generating Plant 94 21 -
02 2 10 TEXT pr more space as requued, use acannone coores at NRC form 366A) (17)
DESCRIPTION:
On September 16,1989, with the plant in cold shutdown and the core unloaded, in-Service Inspection (ISI) personnel, during routine inspection, discovered a crack on the upper support brace (SPT) of one jet pump riser (See Figures 1 through 5). Northem States Power and General Electric personnel were performing the ISI.
This event is being reported because of its potential safety significance and generic nature.
The crack is located on the lower leaf on the right side (facing out from the vessel centerline) of the upper support brace on the riser forjet pumps #7 and #8. The crack indication runs about 3/4 of the way across the top of the leaf about 1/2" from the point where it is welded to the vessel wall.
The risers are supported by an upper brace which consists of two leaves on each side of the riser and a lower brace which consists of one thicker leaf. All remaining leaves on this riser and the 9 other risers in the vessel were examined during the 1989 refueling outage with no other indications found. Subsequent re-examinations during the 1991 and 1993 refueling outages revealed no additional cracking of these components of the subject jet pump or any otherjet pump.
CAUSE:
A study was originally performed in 1989 to determine the cause of the cracking. The results of that study indicated that the most likely cause of this crack was high cycle fatigue. The natural frequency of the riser brace in its uncracked state coincided with the vane passing frequency of the reactor recirculation pumps (AD) at a speed in the range of 92% to 98% (127 Hz to 135 Hz). The subsequent )
experimental program carried out at the General Electric facilities in San Jose, Califomia confirmed cycle fatigue as the most plausible cause of the observed cracking. The resonant frequency of the riser brace was determined by this program to be 116.4 Hz based on nominal dimensions of the riser brace leaves and that the actual riser brace frequency varies as a strong function of the riser brace leaf as-built dimensions (thickness and length) and axial loading of the brace. Based on just the allowed thickness tolerance of the riser brace leaf, the most important resonant frequency could actually lie anywhere within a wide range of 108.5 to 152.20 Hz (78% to 109% recirculation pump speed).
Visual inspections indicate that the cracked lower leaf has some cross-sectional reduction (thinning) which may have been caused by grinding performed during weld fit-up. This thinning is unique to this riser brace leaf and appears to have reduced the cross-sectional area by about 30% It also appears that there is some lack of fusion in the weld at the point on the leaf where the crack initiated. These factors, thinning, work hardening from grinding and lack of weld fusion, may have contributed to the cracking of this riser leaf by making it more susceptible to any of the possible crack initiating mechanisms (i.e.
resonance, IGSCC, ductile tearing).
NRC FOAM 366A ;5-921
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4 MC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 ts42' EXPIRES 5/31/95 EST: MATED BURDEN PEA nESPON$E TO COMPLY WITH THis LICENSEE EVENT REPORT (LER) 22" E s'E S $' E nO # $M J ic Q u su"?Ts N
TEXT CONTINUATION g "yrg85^y,^3'yN',ZNC"ryN8d 3 sa ",d'l;g,Nyc8 7 THE PAPEAWORK REDUCTION PRC;ECT (3150 0104. OFFICE OF MANAGEMENT AND BUDGET. WASMiNGTON. DC 20503 FACIUTY NAME (t) DOCKET NUMBER 12) Lf R NUMBER (4) PAGE(3)
YE,A A N N NUMBEA NUMBEA 05000 - 263 OF Monticello Nuclear Generating Plant 94 21 - 02 3 10 mT w ma, soece .vowea a sum no.es ac ram am <m ANALYSIS:
The lower riser brace leaf (Leaf #3 in Figure 1) has a calculated natural frequency of 358 Hz, which is well removed from resonant conditions. Therefore resonance is not expected to occur at the lower l
brace. Evaluation of normal and accident Jet pump loading indicates that stresses with only the lower brace in place are within acceptable limits. This shows that the loss of the entire upper brace would not affect the operability of the risers or the associated jet pumps.
All of the riser brace leaves have been visually inspected by inservice inspection personnel during the 1989,1991 and 1993 refueling outages with no other crack indications or thinning found. The 1992 test l
l program performed at GE facilities shows that adequate operational strategies are in place that minimize i the concem for additional fatigue cracks. Operation of the Hydrogen Water Chemistry system reduces the possibility of IGSCC occurring in other riser brace leaves.
The operational strategies that are in place are based on the combined analytical and test program results and understanding. The first mode of resonance (out of phase motion) occurs in these riser brace leaves at recirculation pump speeds in the range of 70% to 80%; but, the stresses during this mode of j resonance are not large enough to be a fatigue concem. The second mode of resonance (in phase
! motion), which was originally calculated to occur in the 92% to 98% pump speed range, is the only mode l which is capable of producing stresses with an amplitude high enough to produce fatigue cracking.
Insights from the 1992 test program, however, have shown that no benefit is derived from placing upper limits on the allowable recirculation pump speeds. The sensitivity of the second modal resonance frequency to the as-built riser brace leaf thickness indicates that a prohibitively broad range of pump speeds would have to be proscribed to ensure that no potentially resonant frequencies would be encountered. The test program also indicated that prolonged resonance of the riser brace leaf is self-limiting. As a crack proceeds and grows afterinitiation, the frequency of the second mode resonance and the amplitude of vibration decreases as the crack increases in length. The test program also i indicated that resonant frequencies have a narrow width of only a few Hz. Thus, sudden and rapid crack l growth is unlikely since the initiation and/or growth of a crack alters the natural resonance of the riser brace leaf. If the rirer brace leaf should completely break off on one end, its subsequent resonant frequency is significantly different due to the altered geometry and complete severance of the riser brace leaf is improbable.
The as-clad weld sur' ace of the vessel has an additional weld pad buildup at these locations and riser braces are then welded to the pad. The crack is entirely within the base-metal of the brace, follows the toe of the weld and has no indications of branching. This is indicative of fatigue cracking and not IGSCC, Crack propagation into the weld metal by fatigue is highly unlikely because of geometry and the nature of the stress loading. Propagation into the weld metal by IGSCC is unlikely because of the greater weld metal resistance to IGSCC.
The potential effect of loose parts has also been evaluated. If the cracked riser brace leaf becomes detached from its current position on the jet pump riser, the part would fall to the bottom of the shroud annulus region and rest undisturbed on the top of the jet pump support plate. This is based on the fact
.___ al NAC FCAV 366A l5 92:
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NRC FORM 366A u.s. NUCLEAR REGULATORY Commission APPROVED BY oMB No. 3150-0104 is42; EXPIRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH MS LICENSEE EVENT REPORT (LER) 20% E S%E S E' S " roe M fu "To E d u" %
TEXT CONTINUATION QE 3 8" 8*^fu c
C T 'M "No"rR *o8 "'lEdS,,N gEp THE PAPEAWORd REDUCTn0N PROJECT AISO 0104 OFFICE OF MANAGEMENT AND SUDGET.WASMiNGTON, DC 20501 FACIUTY NAME m DOCKET NUMBER (2) L1R NUMBER (el PAGEpl SEAENTA, REviS#ON NUMBER NUMBER 05000 - 263 OF l bionticello Nuclear Generating Plant 94 21 -
02 4 10 l rw m. u,.e. v.w.a a. .mm coe,.mc m, o n that the riser brace leaf is shielded from the recirculation inlet nozzle by jet pumps #8, #9 and #10 (See Figure 6) making it unlikely that it could be entrained by the recirculation suction flow during its fall to the bottom of tne snroud annulus region. As the part is not expected to migrate to the core region via the recirculation loop flow, there is a negligible potential for fuel bundle flow blockage and subsequent fuel damage. For the same reason, there is virtually no potential for interference with control rod drive I operation. However, if the jet pump riser brace directly above the recirculation loop suction nozzle is assumed to fail, the riser brace leaf may be carried into the recirculation piping due to suction flow. The following paragraphs describe the potential consequences of a loose part migrating to other portions of the recirculation system and reactor vessel.
Considering the size of the part, it is possible that it may cause some damage to the recirculation pump intemals. However, there is no safety implication with respect to the plant's operation since this l postulated recirculation system failure is bounded by the recirculation pump seizure event previously ;
analyzed for and documented in Chapter 14 of the Updated Safety Analysis Report (USAR). The impact j energy of this loose part exiting through the pump impellers will not be sufficient to damage the pump casing and degrade the pressure boundary integrity.
l To cause flow blockage at a fuel bundle, the part must migrate to the vessel lower. plenum and then be carried by flow towards the core region. Since the jet pump nozzle diameter is 3 inches, any part less than 3 inches in any one dimension is capable of exiting the jet pump nozzle and being discharged into the lower plenum of the reactor vessel. Based on the flow velocity regime at the vessellower plenum, it is estimated that any part 2.4 inches or less in diameter could be lifted by the flow and canied toward the core region.
l Parts of this size are expected to go through the fuel support inlet orifice but will be trapped at the lower j tie plate grid. To initiate boiling transition in a fuel bundle, the part would have to cause a fuel bundle flow blockage of 59% or more, which corresponds to an 86% blockage at the lower tie plate. To achieve 86% flow blockage at the lower tie plate grid would require at least 4 pieces of 2.4 inches by 2.4 inches migrating to the same fuel bundle (out of 484 bundles in the core). The probability for such an event is about 9E-9 and is therefore considered negligible.
To cause potential interference with control rod operation, the part must migrate through the spacers located along the length of the fuel bundle and exit at the top of the core. It must then reverse direction against the flow to drop into a control rod guide tube via the bypass region. To complete this tortuous path, the part must be very small (less than 0.1 inches) and for such a small part, the control rod drive hydraulic forces are more than adequate to overcome any potential mechanical friction. Therefore, there is no potential for interference with control rod operation.
Since the riser leaf is made from stainless steel, an approved material for in-reactor use, there is no concem for corrosion or chemical reaction with other reactor materials.
i
! ARO FORM 366A ($-92:
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NRC FORM 366A U.S. NUCLEAR REGULATORY COMMisslON APPROVED BY OMB NO. 3150-0104 4 '2l EXPlRES 5/31/95 ESTIMATED BUACEN PE A AESPONSE TO COMPLY WA TH!S LICENSEE EVENT REPORT (LER) 2e$Es koSES'AeNiE'uATE' c 1 ,0 u E TEXT CONTINUATION ^" "E " ****^ " '***C" (MNes nui. u s NuCLEAA AEGJLATCAY COMMrss'io'N' N WASMINGTON. DC 20S$5 0001. AND TO THE PAPEAWOAd AEDUC'iCN PAC.JEC' (31SJ c1041. CF8tCE OF MANAGEMEVT AND BUDGET, WA$MINGTON. OC 20503
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4 FACILITY N AME 0) DOCKET NUMBER (2) LER NUMBER (4) PAGE (3)
SE E TiA Hews.CN YEAA NUMBEA NUMBTA Monticello Nuclear Generating Plant 05000 - 263 CF 94 21 02 5 10 rExT vi n w.c. ,v.w.a a. .aua., coo ., or Nnc 10- as o n CORRECTIVE ACTION:
Initially, recirculation pump speed was limited to 94% as calculations indicated that the resonant frequency was greater than 94%. Additional information is available at this time:
The General Electric full scale test has shown that the resonant frequency may be lower than 94% and varies considerably with actual physical dimensions.
The testing has demonstrated that the cracking is self-limiting, Two re-examinations during refueling outages have found no additional deterioration in the subject brace leaf or in others.
4 The plant safety evaluation concluded that if a brace leaf separated from the vessel and the jet pump, it l would not cause a safety problem.
Considering that the recirculation pump speed cannot practically be limited to avoid resonant frequencies, and the conclusions of the test program, the limitation on recirculation pump speed has been removed.
These riser brace leaves will continue to be inspected during refueling outages in accordance with the Monticello inservice Inspection Program.
A Nuclear Network transmittal was initially made to alert other utilities.
ADDITIONAL INFORMATION: j
- 1. Failed Component Identification: GE Designed Jet Pump Riser Brace 1
- 2. Previous Similar Events: NONE I
- 3. Attached Figures.
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l NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 15 921 EXPlRES 5/31/95 ESTIMATED BURDEN PER RESPONSE TO COMPLY WITH TH:S INFORMATON COLLECTON REQUEIT: 50 0 HRS. FORWARD LICENSEE EVENT REPORT (LER) Cowms RtGAno:~a sueEN ESTiuATE TO THE i~FOnuATON AN RECORDS MANAGEMN BRANCH (MN80 M14), U S NUM TEXT CONTINUATlON REGULATORY COMMIS$ON WASHINGTON. DC 2055S-0001, AND TO THE PAPERWORK REDUCTON PRCVECT (31504104h OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON,0C 20503 F ACW NAME p) DOCKET NUMBER (2) LER NUMBER (6) pAgg g3g ygAn SEQUENTIAL REV15 ION 05000 - 263 op MOnticello Nuclear Generating Plant 94 -
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EXPIRES 5/31/95 EST: MATED BUROEN PER FtESPONSE TO COMPLY WITH THIS INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARO LICENSEE EVENT REPORT (LER) COMMENTS REoAnciNo BunOEN EST,uATE TO TsE ,ORMAToN AN RECOROS MANAGEMENT BRANCH (MNBB MH), U.S. NUCLEAR TEXT CONTINUATION REGULATORY COMM:SSION, WASHINGTON, OC 2055SW1. AND TO THE PAPERWORK REOUCTION PROJECT p150-0104), OFF6CE OF MANAGEMENT AND BUOGET,WASHihGTON, OC 20503.
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