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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML19346G9701994-07-19019 July 1994 LER 94-006-00:on 940620,group 2 Isolation Occurred Due to Operator Turning Wrong Switch & Deenergizing Radiation Monitor.Operator Disciplined & Radiation Monitor Switches modified.W/940719 Ltr ML20029D7901994-05-0202 May 1994 LER 89-021-02:on 890916,crack Was Discovered on Upper Support Brace of One Jet Pump Riser.Caused by High Cycle Fatigue.Testing Has Demonstrated That Cracking Is Self limiting.W/940502 Ltr ML20029C7061994-04-22022 April 1994 LER 94-001-00:on 940323,missed Surveillance on SRV Low-Low Set Logic.Caused by Incorrect Surveillance Procedure Prerequisite.Corrective Action:Removed Incorrect Prerequisites,Trained on Procedure review.W/940422 Ltr ML20029C6921994-04-22022 April 1994 LER 94-002-00:on 940324,discovered That Breaker Tripped at Current Below Tolerance.Caused by Design of Breakers. Corrective Action:Circuit Breakers Revised for Further Classification for Testing Instantaneous trip.W/940422 Ltr ML20045G3241993-07-0606 July 1993 LER 93-007-00:on 930604,ESF Actuation Occurred Due to Loss of Reactor Protection Sys Power Supply.Replaced Failed Relay & Returned Motor Generator Set to svc.W/930706 Ltr ML20045B2601993-06-0909 June 1993 LER 93-006-01:on 930323,RPM Actuation Occurred from High Pressure Caused by Inadequate Procedure.Turbine Stop & Control Valve Tightness Test Procedures & Plant Simulator revised.W/930609 Ltr ML20044D5361993-04-14014 April 1993 LER 90-001-05:on 900313,design Deficiencies Noted in Emergency Filter Train Sys.On 930315,determined That Train B of CR Emergency Filtration Sys Could Not Provide Adequate Flow.Alternate Measuring Sys Method Implemented ML20044D5381993-04-14014 April 1993 LER 89-040-02:on 891219,secondary Containment Failed to Meet Operability Requirements During Special Test.Caused by Design Deficiencies.Operating Procedures Revised & Administrative Hold Placed on One Sys Component ML20024H2171991-05-22022 May 1991 LER 91-008-00:on 910422,cracking Discovered on Control Rod Drive Housing Flange Cap Screws.Caused by Inadequate Design of Screws.Four New,Original Equipment Cap Screws Installed & Reactor Vessel Hydro performed.W/910522 Ltr ML20028E8261983-01-21021 January 1983 LER 83-001/01T-0:on 830108,during Cold shutdown,post-LOCA Recombiner B Discharge Inboard Primary Containment Isolation Valve & Leak Test Valves Not Fully Closed.Caused by Contractor Error.Valves Closed ML20027D5031982-10-0909 October 1982 Updated LER 82-016/01T-1:on 821009,during Inservice Insp, Indication Found at 12 O'Clock Location on Recirculation safe-end to Pipe Weld E & at 3 O'Clock Location on 821020. Caused by Intergranular Stress Corrosion Cracking ML20052F9951982-05-0808 May 1982 LER 82-005/03L-0:on 820408,lead Lifted in Control Circuitry for Outboard Shutdown Cooling valve,MO-2030,rendering Valve Inoperable.Caused by Misinterpretation of Special Operating Procedure.Lead Reinstalled & Procedures Revised ML20052C2051982-04-23023 April 1982 LER 82-004/01T-0:on 820410,ASCO Inboard & Outboard Drywell Vent 3-way Solenoid Valves,Model 830064C64U,failed to Close Upon Hand Switch Activation When Coil de-energized.Probably Caused by Horizontally Mounted Solenoids.Valves Replaced ML20050B0531982-03-23023 March 1982 Updated LER 81-001/03X-1:on 810126,while Performing Surveillance Test Mo 2035,HPCI Outboard Steam Supply Isolation Valve Failed to Close.Caused by Opened Limitorque SMB-O,240-volt Dc & Torque Switches.Switches Replaced ML20042A4631982-03-12012 March 1982 LER 82-003/03L-0:on 820212,reactor Water Cleanup Primary Containment Inboard Isolation Valve MO-2397 Became Inoperable While in Full Open Position.Caused by Normally Energized Relay Coil 16A-K36 Shorting.Relay Replaced ML20040G7371982-02-0606 February 1982 LER 82-002/03L-0:on 820107,core Spray Pump 11 Start Time Delay Relay Failed to Operate.Caused by Loose Terminal Connection & Microswitch Contact Burned Open.New GE CR 2820 Relay Installed ML20040A5701982-01-15015 January 1982 LER 82-001/01T-0:on 820102,outboard Shutdown Cooling Suction Isolation Valve Found to Exceed Tech Spec Limits for Local Leak Rate Test.Caused by Valve Disc,Undersized by Extensive Lapping of Disc & Valve Body Seats,Traveling Too Far ML20039B2281981-12-10010 December 1981 LER 81-023/03L-0:on 811110,during Cold shutdown,4 Channel a Main Steam Line High Flow Switches Found Inoperable.Caused by Heating of Switching Element Due to Relay Coil Failure, Initially Reported in LER 81-021.Elements Replaced ML20027C2371981-08-24024 August 1981 LER 81-020/03L-0:on 810724,main Steam Leak Revealed in Drain Line to Condenser.Caused by Piping Leaking Immediately Downstream of 45 Degree Elbow Due to Erosion & Impingement Resulting from Steam & Water Flow from Restricting Orifice ML20009E4141981-07-20020 July 1981 LER 81-018/03L-0:on 810620,reactor Water Cleanup Sys Was Returned to Svc Following Maint W/Discharge Isolation Valve MO2399 Open & Inoperable.Caused by Torque Switch Failure. Motor & Torque Switch Replaced & Sys Returned to Svc ML20009D5671981-07-16016 July 1981 LER 81-017/03L-0:on 810617,cracks Discovered on 4-inch & 1-inch Reactor Water Cleanup Heat Exchanger Piping,At Connection to Heat Exchanger.Caused by Poor fit-up & Welding Due to 3-inch Slag Line Near Root of Weld ML19332B3791980-09-22022 September 1980 LER 80-027/03L-0:on 80823,during Monthly surveillance,42-11 Test Control Rod Could Not Be Withdrawn After Partial Insertion.Caused by Closed Drive Withdraw Riser Isolation Valve CRD-102.Valve Opened & Rod Was Operable ML1129007601980-07-0101 July 1980 LER 80-023/03L-0:on 800601,air Ejector Offgas Radiation Monitors Dropped to About 20% Normal for About 40 Minutes. Caused by Mechanical Vacuum Pump Offgas Sample Valve Being Incorrectly Opened.Valve Now Wired Shut ML1129007541980-06-26026 June 1980 LER 80-022/03L-0:on 800529,primary Containment Oxygen Concentration Exceeded 5% by Weight Tech Spec Limit.Caused by Open Svc Air Isolation Valve to Drywell.Procedures Have Been Revised to Assure Proper Valve Positioning ML1129007511980-06-12012 June 1980 LER 80-021/03L-0:on 800515,during Normal Startup,Reactor Core Isolation Cooling Control Power Fuse Opened.Caused by Shorted Relay Coil in Circuit Due to Ac Relay Inadvertently Installed by Maint Personnel.Relay Replaced ML1129007481980-06-0202 June 1980 Updated 79-015/03L-1:on 790712,during Routine Insp,Steam Leak from 13A Intermediate Pressure Feedwater Heater Was Detected.Insulation Removal Revealed through-wall Flaw in Heater Shell.Caused by erosion-corrosion ML1129007451980-05-27027 May 1980 LER 80-020/03L-0:on 800427,during post-maint Startup of Reactor Recirculation Sys,Inaccessible Recirculation Valve Motor Failed.Cause Not Stated.Motor Is Limitorque Type SMB-2 W/Magnetic Brake ML1129007221980-05-0909 May 1980 LER 80-018/03L-0:on 800411,during Routine Operator Insp, Attachment Weld of Ripple to Level Switch Float Chamber Assembly on Moisture Separator Level Switch LS-1188 Found Cracked.Caused by Improper Weld Procedure ML1129007071980-04-11011 April 1980 LER 80-017/01T-0:on 800328,Bechtel Power Corp Notified Util That Control Rod Driveline Hydraulic Piping Frame Supports Would Not Meet OBE Stress Limits.Caused by Eds Computer Code Error.Supports Modified ML1129006851980-04-10010 April 1980 LER 80-016/01T-0:on 800327,during Refueling,Supports for SRV Pneumatic Supply Sys Would Not Meet Seismic Class I Requirements.Caused by Inadequate Design & Installation of Sys.Sys Was Upgraded to Satisfy Requirements ML1129006801980-03-27027 March 1980 LER 80-015/01T-0:on 800317,during Refueling Outage & Insp Required by IE Bulletin 79-01B,unqualified Splices Found in Power Cables for Inboard MSIV Solenoid Valves.Cause Not Stated.Splices Replaced W/Qualified Matls ML1129006781980-03-26026 March 1980 LER 80-006/03L-0:on 800226,during Refueling Outage,Seven of Main Steam Line Area Temp Switches Found to Trip Above Required Level.Caused by Setpoint Drift.Switches Recalibr ML1129006651980-03-21021 March 1980 LER 80-013/01T-0:on 800309,during Refueling Operations,Rod Withdrawn Block Not Received When Refueling Bridge Traversed Core.Caused by Actuating Arm Out of Adjustment.Components Readjusted & Interlocks Tested Prior to Refueling ML1129006681980-03-20020 March 1980 LER 80-011/01T-0:on 800306,during Refueling Outage,Repairs to Outboard MSIV Stop Valve Revealed Flow Path Between Secondary Containment & Turbine Bldg When MSIV Poppet Was Pulled.Caused by Lack of Preventive Procedure Controls ML1129006621980-03-14014 March 1980 LER 80-007/01T-0:on 800303,during Refuel Shutdown,Cable Routing for HPCI & Automatic Depressurization Sys Cables Identified Lack of Physical Separation Between Automatic Depressurization Sys Cables & Ones for Div of HPCI Sensors ML1129009771980-01-18018 January 1980 LER 79-024/03L-0:on 791220,during Normal Operation,Routine Operator Insp Revealed Steam Leak in 1-inch 90 Degree Elbow in Reactor Core Isolation Cooling Steam Line Drain to Condenser.Caused by Pinhole Failure of 3,000-lb Socket Weld ML1129009741980-01-14014 January 1980 Updated LER 79-023/01T-1:on 800103,one Fuel Type Noted to Exceed Max Allowable Max Average Planar Linear Heat Generation Rate Value & Another as Improperly Programmed in Plant Computer.Caused by Inadequate Review ML1129009551979-12-19019 December 1979 LER 79-021/03L-0:on 791119,during IE Bulletin 79-02 Evaluation,Snubber SS-31 Base Plate Expansion Anchor Bolt Safety Factor Found to Be Less than One.Caused by Inadequate Base Plate & Expansion Anchor Bolts ML1129009031979-08-31031 August 1979 LER 79-017/03L-0:on 790806,steam Leak Observed on Feedwater Extraction Steam Line Drain 15A.Caused by Steam Erosion Through Wall of Steam Trap on Line.Trap Isolated Pending Repair or Replacement at Next Appropriate Outage ML1129008891979-08-10010 August 1979 LER 79-015/03L-0 on 790712:discovered Steam Leak from Intermediate Pressure Feedwater Heater.Cause Undetermined. Temporary Patch Installed Pending Replacement of Heater Shell ML1129008831979-08-0707 August 1979 LER 79-013/03L-0 on 790708:motor Operator Failed,Rendering Torus Cooling Injection Valve Inoperable During Normal Operation.Caused by Failure of Motor Winding Due to Limit Switch Not de-energizing Motor.Switch Replaced ML1129008801979-08-0606 August 1979 LER 79-014/03L-0 on 790709:water Leak Discovered in 1/2 Inch Instrument Line from Reactor Water Cleanup Sys Nonregenerative Heat Exchanger.Cause Not Determined.Leaking Line Isolated & Will Be Further Investigated & Repaired ML1129008771979-08-0101 August 1979 LER 79-012/03L-0 on 790702:during Reactor Core Isolation Cooling Sys Test,Governor end-bearing Temp Alarm Received & Bearing Exhibited High Vibration.Sys Inoperative.Caused by Turbine Oil Pump Drive Gear Failure.Gears Replaced ML1129008561979-06-28028 June 1979 LER 79-011/03L-0 on 790529:no Min Flow in B Train Standby Gas Treatment Sys.Caused by Dilution Flow from Compressed Storage Not Isolated by BV-5.Replaced Positioner & Installed Filter in Cylinder Supply/Return Line ML1127801511979-03-15015 March 1979 LER 79-003/01T-0 on 790301:containment Vent & Purge Isolation Valves Would Not Close During DBA-LOCA.Cause Unknown.Fisher Continential 18 & 20 Inch,Type 9220 Butterfly Valves Opening Is Administratively Controlled ML1127601481979-02-0909 February 1979 LER 79-002/03L-0 on 790118:during Normal Operation,Weekly Average Power Range Monitor Functional Scram Test Was Not Completed within Time Allowed.Caused by Personnel Error ML1127601201979-02-0202 February 1979 LER 79-001/03L-0 on 790110:during Normal Operation,Steam Leak Found in Elbow on Turbine Main Steam Bypass Header 1 Inch Drain Line to Condenser,Due to Erosion Caused by Steam & Water Flow of Restricting orifice,RO-2569 ML1127601181979-01-29029 January 1979 LER 78-016/03X-1 on 780908:during Normal Operation,Trip of Essential MCC B33A Supply Breaker 52-304 Resulted in Operation in Degraded Mode.Caused by Low Setpoint on Trip Device & by Loss of Dash Pot Oil in Trip Device ML1127601131978-12-29029 December 1978 LER 78-030/01T-0 on 781218:during surveillance,MO-2-64A Recirculation Loop 11 Discharge Bypass Valve Would Not Close.Cause Is Unknown Due to Inaccessibility of Valve ML1127601431978-12-19019 December 1978 LER#78-028/03L-0 on 781124:during Normal Oper,Small Steam Leak Was Discovered in Weld of 45 Degree Elbow on HPCI Steam Supply Line 1 Inch Drain Line to Main Condenser Due to Corrrosion.Weld Repair Made at Leak.Awaiting Parts 1994-07-19
[Table view] Category:RO)
MONTHYEARML19346G9701994-07-19019 July 1994 LER 94-006-00:on 940620,group 2 Isolation Occurred Due to Operator Turning Wrong Switch & Deenergizing Radiation Monitor.Operator Disciplined & Radiation Monitor Switches modified.W/940719 Ltr ML20029D7901994-05-0202 May 1994 LER 89-021-02:on 890916,crack Was Discovered on Upper Support Brace of One Jet Pump Riser.Caused by High Cycle Fatigue.Testing Has Demonstrated That Cracking Is Self limiting.W/940502 Ltr ML20029C7061994-04-22022 April 1994 LER 94-001-00:on 940323,missed Surveillance on SRV Low-Low Set Logic.Caused by Incorrect Surveillance Procedure Prerequisite.Corrective Action:Removed Incorrect Prerequisites,Trained on Procedure review.W/940422 Ltr ML20029C6921994-04-22022 April 1994 LER 94-002-00:on 940324,discovered That Breaker Tripped at Current Below Tolerance.Caused by Design of Breakers. Corrective Action:Circuit Breakers Revised for Further Classification for Testing Instantaneous trip.W/940422 Ltr ML20045G3241993-07-0606 July 1993 LER 93-007-00:on 930604,ESF Actuation Occurred Due to Loss of Reactor Protection Sys Power Supply.Replaced Failed Relay & Returned Motor Generator Set to svc.W/930706 Ltr ML20045B2601993-06-0909 June 1993 LER 93-006-01:on 930323,RPM Actuation Occurred from High Pressure Caused by Inadequate Procedure.Turbine Stop & Control Valve Tightness Test Procedures & Plant Simulator revised.W/930609 Ltr ML20044D5361993-04-14014 April 1993 LER 90-001-05:on 900313,design Deficiencies Noted in Emergency Filter Train Sys.On 930315,determined That Train B of CR Emergency Filtration Sys Could Not Provide Adequate Flow.Alternate Measuring Sys Method Implemented ML20044D5381993-04-14014 April 1993 LER 89-040-02:on 891219,secondary Containment Failed to Meet Operability Requirements During Special Test.Caused by Design Deficiencies.Operating Procedures Revised & Administrative Hold Placed on One Sys Component ML20024H2171991-05-22022 May 1991 LER 91-008-00:on 910422,cracking Discovered on Control Rod Drive Housing Flange Cap Screws.Caused by Inadequate Design of Screws.Four New,Original Equipment Cap Screws Installed & Reactor Vessel Hydro performed.W/910522 Ltr ML20028E8261983-01-21021 January 1983 LER 83-001/01T-0:on 830108,during Cold shutdown,post-LOCA Recombiner B Discharge Inboard Primary Containment Isolation Valve & Leak Test Valves Not Fully Closed.Caused by Contractor Error.Valves Closed ML20027D5031982-10-0909 October 1982 Updated LER 82-016/01T-1:on 821009,during Inservice Insp, Indication Found at 12 O'Clock Location on Recirculation safe-end to Pipe Weld E & at 3 O'Clock Location on 821020. Caused by Intergranular Stress Corrosion Cracking ML20052F9951982-05-0808 May 1982 LER 82-005/03L-0:on 820408,lead Lifted in Control Circuitry for Outboard Shutdown Cooling valve,MO-2030,rendering Valve Inoperable.Caused by Misinterpretation of Special Operating Procedure.Lead Reinstalled & Procedures Revised ML20052C2051982-04-23023 April 1982 LER 82-004/01T-0:on 820410,ASCO Inboard & Outboard Drywell Vent 3-way Solenoid Valves,Model 830064C64U,failed to Close Upon Hand Switch Activation When Coil de-energized.Probably Caused by Horizontally Mounted Solenoids.Valves Replaced ML20050B0531982-03-23023 March 1982 Updated LER 81-001/03X-1:on 810126,while Performing Surveillance Test Mo 2035,HPCI Outboard Steam Supply Isolation Valve Failed to Close.Caused by Opened Limitorque SMB-O,240-volt Dc & Torque Switches.Switches Replaced ML20042A4631982-03-12012 March 1982 LER 82-003/03L-0:on 820212,reactor Water Cleanup Primary Containment Inboard Isolation Valve MO-2397 Became Inoperable While in Full Open Position.Caused by Normally Energized Relay Coil 16A-K36 Shorting.Relay Replaced ML20040G7371982-02-0606 February 1982 LER 82-002/03L-0:on 820107,core Spray Pump 11 Start Time Delay Relay Failed to Operate.Caused by Loose Terminal Connection & Microswitch Contact Burned Open.New GE CR 2820 Relay Installed ML20040A5701982-01-15015 January 1982 LER 82-001/01T-0:on 820102,outboard Shutdown Cooling Suction Isolation Valve Found to Exceed Tech Spec Limits for Local Leak Rate Test.Caused by Valve Disc,Undersized by Extensive Lapping of Disc & Valve Body Seats,Traveling Too Far ML20039B2281981-12-10010 December 1981 LER 81-023/03L-0:on 811110,during Cold shutdown,4 Channel a Main Steam Line High Flow Switches Found Inoperable.Caused by Heating of Switching Element Due to Relay Coil Failure, Initially Reported in LER 81-021.Elements Replaced ML20027C2371981-08-24024 August 1981 LER 81-020/03L-0:on 810724,main Steam Leak Revealed in Drain Line to Condenser.Caused by Piping Leaking Immediately Downstream of 45 Degree Elbow Due to Erosion & Impingement Resulting from Steam & Water Flow from Restricting Orifice ML20009E4141981-07-20020 July 1981 LER 81-018/03L-0:on 810620,reactor Water Cleanup Sys Was Returned to Svc Following Maint W/Discharge Isolation Valve MO2399 Open & Inoperable.Caused by Torque Switch Failure. Motor & Torque Switch Replaced & Sys Returned to Svc ML20009D5671981-07-16016 July 1981 LER 81-017/03L-0:on 810617,cracks Discovered on 4-inch & 1-inch Reactor Water Cleanup Heat Exchanger Piping,At Connection to Heat Exchanger.Caused by Poor fit-up & Welding Due to 3-inch Slag Line Near Root of Weld ML19332B3791980-09-22022 September 1980 LER 80-027/03L-0:on 80823,during Monthly surveillance,42-11 Test Control Rod Could Not Be Withdrawn After Partial Insertion.Caused by Closed Drive Withdraw Riser Isolation Valve CRD-102.Valve Opened & Rod Was Operable ML1129007601980-07-0101 July 1980 LER 80-023/03L-0:on 800601,air Ejector Offgas Radiation Monitors Dropped to About 20% Normal for About 40 Minutes. Caused by Mechanical Vacuum Pump Offgas Sample Valve Being Incorrectly Opened.Valve Now Wired Shut ML1129007541980-06-26026 June 1980 LER 80-022/03L-0:on 800529,primary Containment Oxygen Concentration Exceeded 5% by Weight Tech Spec Limit.Caused by Open Svc Air Isolation Valve to Drywell.Procedures Have Been Revised to Assure Proper Valve Positioning ML1129007511980-06-12012 June 1980 LER 80-021/03L-0:on 800515,during Normal Startup,Reactor Core Isolation Cooling Control Power Fuse Opened.Caused by Shorted Relay Coil in Circuit Due to Ac Relay Inadvertently Installed by Maint Personnel.Relay Replaced ML1129007481980-06-0202 June 1980 Updated 79-015/03L-1:on 790712,during Routine Insp,Steam Leak from 13A Intermediate Pressure Feedwater Heater Was Detected.Insulation Removal Revealed through-wall Flaw in Heater Shell.Caused by erosion-corrosion ML1129007451980-05-27027 May 1980 LER 80-020/03L-0:on 800427,during post-maint Startup of Reactor Recirculation Sys,Inaccessible Recirculation Valve Motor Failed.Cause Not Stated.Motor Is Limitorque Type SMB-2 W/Magnetic Brake ML1129007221980-05-0909 May 1980 LER 80-018/03L-0:on 800411,during Routine Operator Insp, Attachment Weld of Ripple to Level Switch Float Chamber Assembly on Moisture Separator Level Switch LS-1188 Found Cracked.Caused by Improper Weld Procedure ML1129007071980-04-11011 April 1980 LER 80-017/01T-0:on 800328,Bechtel Power Corp Notified Util That Control Rod Driveline Hydraulic Piping Frame Supports Would Not Meet OBE Stress Limits.Caused by Eds Computer Code Error.Supports Modified ML1129006851980-04-10010 April 1980 LER 80-016/01T-0:on 800327,during Refueling,Supports for SRV Pneumatic Supply Sys Would Not Meet Seismic Class I Requirements.Caused by Inadequate Design & Installation of Sys.Sys Was Upgraded to Satisfy Requirements ML1129006801980-03-27027 March 1980 LER 80-015/01T-0:on 800317,during Refueling Outage & Insp Required by IE Bulletin 79-01B,unqualified Splices Found in Power Cables for Inboard MSIV Solenoid Valves.Cause Not Stated.Splices Replaced W/Qualified Matls ML1129006781980-03-26026 March 1980 LER 80-006/03L-0:on 800226,during Refueling Outage,Seven of Main Steam Line Area Temp Switches Found to Trip Above Required Level.Caused by Setpoint Drift.Switches Recalibr ML1129006651980-03-21021 March 1980 LER 80-013/01T-0:on 800309,during Refueling Operations,Rod Withdrawn Block Not Received When Refueling Bridge Traversed Core.Caused by Actuating Arm Out of Adjustment.Components Readjusted & Interlocks Tested Prior to Refueling ML1129006681980-03-20020 March 1980 LER 80-011/01T-0:on 800306,during Refueling Outage,Repairs to Outboard MSIV Stop Valve Revealed Flow Path Between Secondary Containment & Turbine Bldg When MSIV Poppet Was Pulled.Caused by Lack of Preventive Procedure Controls ML1129006621980-03-14014 March 1980 LER 80-007/01T-0:on 800303,during Refuel Shutdown,Cable Routing for HPCI & Automatic Depressurization Sys Cables Identified Lack of Physical Separation Between Automatic Depressurization Sys Cables & Ones for Div of HPCI Sensors ML1129009771980-01-18018 January 1980 LER 79-024/03L-0:on 791220,during Normal Operation,Routine Operator Insp Revealed Steam Leak in 1-inch 90 Degree Elbow in Reactor Core Isolation Cooling Steam Line Drain to Condenser.Caused by Pinhole Failure of 3,000-lb Socket Weld ML1129009741980-01-14014 January 1980 Updated LER 79-023/01T-1:on 800103,one Fuel Type Noted to Exceed Max Allowable Max Average Planar Linear Heat Generation Rate Value & Another as Improperly Programmed in Plant Computer.Caused by Inadequate Review ML1129009551979-12-19019 December 1979 LER 79-021/03L-0:on 791119,during IE Bulletin 79-02 Evaluation,Snubber SS-31 Base Plate Expansion Anchor Bolt Safety Factor Found to Be Less than One.Caused by Inadequate Base Plate & Expansion Anchor Bolts ML1129009031979-08-31031 August 1979 LER 79-017/03L-0:on 790806,steam Leak Observed on Feedwater Extraction Steam Line Drain 15A.Caused by Steam Erosion Through Wall of Steam Trap on Line.Trap Isolated Pending Repair or Replacement at Next Appropriate Outage ML1129008891979-08-10010 August 1979 LER 79-015/03L-0 on 790712:discovered Steam Leak from Intermediate Pressure Feedwater Heater.Cause Undetermined. Temporary Patch Installed Pending Replacement of Heater Shell ML1129008831979-08-0707 August 1979 LER 79-013/03L-0 on 790708:motor Operator Failed,Rendering Torus Cooling Injection Valve Inoperable During Normal Operation.Caused by Failure of Motor Winding Due to Limit Switch Not de-energizing Motor.Switch Replaced ML1129008801979-08-0606 August 1979 LER 79-014/03L-0 on 790709:water Leak Discovered in 1/2 Inch Instrument Line from Reactor Water Cleanup Sys Nonregenerative Heat Exchanger.Cause Not Determined.Leaking Line Isolated & Will Be Further Investigated & Repaired ML1129008771979-08-0101 August 1979 LER 79-012/03L-0 on 790702:during Reactor Core Isolation Cooling Sys Test,Governor end-bearing Temp Alarm Received & Bearing Exhibited High Vibration.Sys Inoperative.Caused by Turbine Oil Pump Drive Gear Failure.Gears Replaced ML1129008561979-06-28028 June 1979 LER 79-011/03L-0 on 790529:no Min Flow in B Train Standby Gas Treatment Sys.Caused by Dilution Flow from Compressed Storage Not Isolated by BV-5.Replaced Positioner & Installed Filter in Cylinder Supply/Return Line ML1127801511979-03-15015 March 1979 LER 79-003/01T-0 on 790301:containment Vent & Purge Isolation Valves Would Not Close During DBA-LOCA.Cause Unknown.Fisher Continential 18 & 20 Inch,Type 9220 Butterfly Valves Opening Is Administratively Controlled ML1127601481979-02-0909 February 1979 LER 79-002/03L-0 on 790118:during Normal Operation,Weekly Average Power Range Monitor Functional Scram Test Was Not Completed within Time Allowed.Caused by Personnel Error ML1127601201979-02-0202 February 1979 LER 79-001/03L-0 on 790110:during Normal Operation,Steam Leak Found in Elbow on Turbine Main Steam Bypass Header 1 Inch Drain Line to Condenser,Due to Erosion Caused by Steam & Water Flow of Restricting orifice,RO-2569 ML1127601181979-01-29029 January 1979 LER 78-016/03X-1 on 780908:during Normal Operation,Trip of Essential MCC B33A Supply Breaker 52-304 Resulted in Operation in Degraded Mode.Caused by Low Setpoint on Trip Device & by Loss of Dash Pot Oil in Trip Device ML1127601131978-12-29029 December 1978 LER 78-030/01T-0 on 781218:during surveillance,MO-2-64A Recirculation Loop 11 Discharge Bypass Valve Would Not Close.Cause Is Unknown Due to Inaccessibility of Valve ML1127601431978-12-19019 December 1978 LER#78-028/03L-0 on 781124:during Normal Oper,Small Steam Leak Was Discovered in Weld of 45 Degree Elbow on HPCI Steam Supply Line 1 Inch Drain Line to Main Condenser Due to Corrrosion.Weld Repair Made at Leak.Awaiting Parts 1994-07-19
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217D1261999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for Monticello Nuclear Generating Plant.With ML20216E7031999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Monticello Nuclear Generating Plant.With ML20210Q0521999-08-0404 August 1999 Safety Evaluation Approving Relief Request 10 to License DPR-22 Per 10CFR50.55a(g)(6)(i).Inservice Exam for Relief Request 10,Parts A,B,C,D & E Impractical & Reasonable Assurance of Structural Integrity Provided ML20210Q6611999-07-31031 July 1999 Monthly Operating Rept for July 1999 for Monticello Nuclear Generating Plant.With ML20209F7901999-06-30030 June 1999 Monthly Operating Rept for June 1999 for Monticello Nuclear Generating Plant.With ML20195H0351999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Monticello Nuclear Generatintg Plant.With ML20206N1721999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for Monticello Nuclear Generating Plant.With ML20205N0861999-04-12012 April 1999 Safety Evaluation Re Licensee Response to GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20205P5701999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for Monticello Nuclear Generating Plant.With ML20204H4951999-03-18018 March 1999 SER Concluding That Licensee Established Acceptable Program to Verify Periodically design-basis Capability of safety-related MOVs at Monticello.Therefore Staff Concludes Licensee Adequately Addressed Action Required in GL 96-05 ML20205G7391999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for Monticello Nuclear Generating Plant.With ML20202F7901999-01-25025 January 1999 1999 Four Year Simulator Certification Rept for MNGP Simulation Facility ML20199E4871999-01-0606 January 1999 SER Accepting Licensee 951116,960214 & 0524 Responses to NRC Bulletin 95-002, Unexpected Clogging of Residual Heat Removal Pump Strainer While Operating in Suppression Pool Cooling Mode ML20199F6211998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for Mngp.With ML20205H0561998-12-31031 December 1998 Northern States Power Co 1998 Annual Rept. with ML20198P0691998-12-28028 December 1998 Safety Evaluation Concluding That NSP Proposed Alternative to Paragraph III-3411 of App III to 1986 Edition of Section XI of ASME Code Provides Acceptable Level of Quality & Safety.Alternative Authorized ML20198D0751998-12-10010 December 1998 Safety Evaluation Supporting NSP Proposed Change to EOPs to Use 2/3 Core Height as Potential Entry Condition Into Containment Flooding ML20198B2531998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for Monticello Nuclear Generating Plant.With ML20195E3691998-11-12012 November 1998 Safety Evaluation Concluding That Licensee USI A-46 Implementation Has Met Purpose & Intent of Criteria in GIP-2 & Staff Sser 2 for Resolution of USI A-46 ML20195D2381998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for Monticello Nuclear Generating Plant.With ML20198J4451998-10-22022 October 1998 Rev 2 to SIR-97-003, Review of Test Results of Two Surveillance Capsules & Recommendations for Matls Properties & Pressure-Temp Curves to Be Used for Monticello Rpv ML20154L3471998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for Monticello Nuclear Generating Plant.With ML20153F0511998-09-21021 September 1998 Rev 2 to MNGP Colr,Cycle 19 ML20153E9361998-09-0808 September 1998 Rev 1 to MNGP Colr,Cycle 19 ML20153B0861998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for Monticello Nuclear Generating Plant.With ML20237B8461998-07-31031 July 1998 Monthly Operating Rept for July 1998 for Monticello Nuclear Generating Plant ML20236W5041998-07-21021 July 1998 ISI Exam Summary Rept - Refueling Outage 19 ML20236R1941998-06-30030 June 1998 Monthly Operating Rept for June 1998 for Monticello Nuclear Generating Plant ML20249A5861998-05-31031 May 1998 Monthly Operating Rept for May 1998 for Monticello Nuclear Generating Plant ML20247K3971998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for Monticello Nuclear Generating Plant ML20217D8731998-04-13013 April 1998 Rev 0 to MNGP Colr,Cycle 19 ML20217F6431998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for Monticello Nuclear Generating Plant ML20216D1041998-03-0505 March 1998 Rev 21 to Operational QA Plan ML20216H6481998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for Monticello Nuclear Generating Plant ML20203G1431998-02-10010 February 1998 Rev 2 to Inservice Insp Exam Plan,Third Interval,920601- 020531 ML20203B2821998-01-31031 January 1998 Monthly Operating Rept for Jan 1998 for Monticello Nuclear Generating Station ML20202F9161998-01-29029 January 1998 Special Rept:On 980128,two of Three Fire Protection Pumps Were Removed from Svc as Result of Sys Configuration Necessary to Support Planned Maintenance.Fire Pumps Were Returned to Svc on 980128 ML20216D2071997-12-31031 December 1997 1997 Annual Rept for Northern States Power Co ML20197J8131997-12-31031 December 1997 Revised Evacuation Time Estimates for Plume Exposure Pathway Emergency Planning Zone at Monticello Nuclear Power Plant. W/One Oversize Drawing ML20198P2201997-12-31031 December 1997 Monthly Operating Rept for Dec 1997 for Monticello Nuclear Generating Plant ML20203J7131997-11-30030 November 1997 Monthly Operating Rept for Nov 1997 for Monticello Nuclear Generating Plant ML20199G7051997-11-19019 November 1997 Safety Evaluation Authorizing Relief Request 8 of Third 10 Yr Inservice Insp Interval ML20199H8181997-10-31031 October 1997 Monthly Operating Rept for Oct 1997 for Monticello Nuclear Generating Plant ML20217K2081997-09-30030 September 1997 Monthly Operating Rept for Sept 1997 for Monticello Nuclear Generating Plant ML20216H7771997-08-31031 August 1997 Monthly Operating Rept for Aug 1997 for Monticello Nuclear Generating Plant ML20217K2741997-07-31031 July 1997 Monthly Operating Rept for Jul 1997 for Monticello Nuclear Generating Plant ML20196H1081997-07-0808 July 1997 Rev 20 to Operational QA Plan ML20141B9271997-06-30030 June 1997 LOCA Containment Analyses for Use in Evaluation of NPSH for RHR & Core Spray Pumps ML20149E2921997-06-30030 June 1997 Monthly Operating Rept for June 1997 for MNGP ML20148S6341997-06-23023 June 1997 NPSH - Rept of Sulzer Bingham Pump 1999-09-30
[Table view] |
Text
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EGG DNSP-11401 j July 1994 j
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~ Idaho l T EVALUATION OF UTILITY RESPONSE T0 1? .: National. :
. SUPPLEMENT 1 TO NRC BULLETIN 90-01:
i .Eng..meenny wgp.2 j Laboratory. '
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4 Managed-by the U.S.:
' Department 4
- ' Alan C. Udy i
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No. DE-AC07-26tD01570 i
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EGG-DNSP-11401 1
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2 TECHNICAL EVALUATION REPORT l
Evaluation of Utility Response to Supplement I to NRC Bulletin 90-01: WNP-2 ,
Docket No. 50-397 i
Alan C. Udy Published July 1994 e
i EG&G Idaho, Inc.
l Idaho National Engineering Laboratory Idaho Falls, Idaho 83415 l
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Prepared for the l U.S. Nuclear Regulatory Commission l Washington, D.C. 20555 ,
i Under DDE Contract No. DE-AC07-761D01570 'l FIN No. Ll695, Task No. 11 l TAC No. MB5462 l
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SUMMARY
This report documents the EG&G Idaho, Inc., review of the Washington Public Power Supply System submittals that respond to Supplement I to NRC i Bulletin 90-01 for WNP-2. This NRC Bulletin provides information regarding l the loss of fill-oil in certain pressure and differential pressure transmitters manufactured by Rosemount, Inc. This report finds the licensee conforms to the requested actions and the reporting requirements of the l Supplement.
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FIN No. Ll695, Task No. 11 B&R No. 320-19-15-05-0 Docket No. 50-397 TAC No. M85462 ii
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. i PREFACE
, This report is supplied as part of the " Technical Assistance in Support I
of the Instrumentation and Controls Systems Branch." It is being conducted for the U.S. Nuclear Regulatory Commission, Office of Nuclear Reactor Regulation, Division of Reactor Controls and Human Factors, by EG&G Idaho, .
- Inc., DOE /NRC Support Programs Unit. l l
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l CONTENTS
SUMMARY
.............................................................. ii PREFACE .............................................................. iii j i
. 1. INTRODUCTION .................................................... 1 4 :
- 2. NRC SPECIFIED REQUESTED ACTIONS ................................. ,
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- 3. EVALUATION ...................................................... ,
3.1 Evaluation of Licensee Response to .leporting Requirements . 7 3.2 Evaluation of Licensee Response to Requested Actions ...... 7 ,
! 4. CONCLUSIONS ..................................................... 11 l l 5. REFERENCES ...................................................... 12- l l l l
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4 Evaluatian of Utility Response to Supolement I to NRC Bulletin 90-01: WNP-2
- 1. INTRODUCTION The NRC issued Bulletin 90-01 on March 9, 1990 (Reference 1). That l Bulletin discussed certain Rosemount pressure and differential pressure
! transmitter models identified by the manufacturer as prone to fill-oil j' leakage. The bulletin requested licensees to identify whether these l transmitters were or may later be installed in safety-related systems.
l Actions were detailed for licensee implementation for identified transmitters l installed in a safety-related system. These same actions apply to identified '
transmitters presently held in inventory for later installation in a safety-related system.
With the gr< dual leakage of fill-oil, the transmitter would not have the l long term accuracy, time response, and reliability needed for its intended safety function. Further, this condition could go undetected over a long 3 period. Redundant instrument channels are subject to the same degradation mechanism. This increases the potential for a common mode failure. Thus, this potential failure mechanism raised concern for the reliability of reactor protection systems (RPS), engineered safety features (ESF) actuation systems, and anticipated transient without scram (ATWS) mitigating systems. To achieve )
- high functional reliability, there must be a low probability of component I failure while operating, with any failures readily detectable.
Supplement I to NRC Bulletin 90-01 (Reference 2) was issued on
! December 22, 1992. The Supplement informed licensees of NRC staff activities regarding the subject transmitters, and noted continuing reports of transmitter failures. The NRC requested licensee action to resolve the issue.
The Supplement also updated the information contained in the original t
l- bulletin. The licensee was requested to review the information and determine if it was applicable at their facility. Further, the licensee was requested j to modify their actions and enhanced surveillance monitoring programs to conform with the direction given. Finally, the licensee was instructed to 1
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fill-oil loss-caused degradation of the transmitter. Finally, this report addresses the interval of surveillance proposed by the licensee for any transmitters included in the enhanced surveillance program.
l Many Rosemount transmitter failures have been attributed to the use of i stainless steel "0"-rings between the sensing module and the process flanges. 1 Rosemount improved the manufacturing process for transmitters manufactured ;
after July 11, 1989. Those improvements included a limit of the torque !
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!' applied to the flange bolts. This limits the stress caused in the sensing i l module by the . "0"-ring. Post-production screening, including pressure testing !
of the sensing module for this potential latent defect, was also implemented l l_ at that time. Therefore, as described in Supplement 1 of NRC Bulletin 90-01, j l those Rosemount transmitters manufactured after July 11, 1989, are not subject to this review.
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Evaluation of Utility Response to Supplement 1 to NRC Bulletin 90-01: WNP-2 i
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- 1. INTRODUCTION l l
l The NRC issued Bulletin 90-01 on March 9,1990 (Reference 1). That l
Rulletin discussed certain Rosemount pressure and differential pressure transmitter models identified by the manufacturer as prone to fill-oil i leakage. The bulletin requested licensees to identify whether these transmitters were or may later be installed in safety-related systems.
Actions were det. ailed for licensee implementation for identified transmitters installed in a safety-related system. These same actions apply to identified '
transmitters presently held in inventory for later installation in a safety- ,
related system. ,
t With the gradual leakage of fill-oil, the transmitter would not have the long term accuracy, time response, and reliability needed for its intended safety function. Further, this condition could go undetected over a long period. Redundant instrument channels are subject to the same degradation mechanism. This increases the potential for a common mode failure. Thus, this potential failure mechanism raised concern for the reliability of reactor l protection systems (RPS), engineered safety features (ESF) actuation systems, and anticipated transient without scram (ATWS) mitigating systems. To achieve high functional reliability, there must be a low probability of component failure while operating, with any failures readily detectable.
l Supplement I to NRC Bulletin 90-01 (Reference 2) was issued on
! December 22, 1992. The Supplement informed licensees of NRC staff activities regarding the subject transmitters, and noted continuing reports of transmitter failures. The NRC requested licensee action to resolve the issue.
The Supplement also updated the information contained in the original L
bulletin. The licensee was requested to review the information and determine if it was applicable at their facility. Further, the licensee was requested to modify their actions and enhanced surveillance monitoring programs to conform with the direction given. Finally, the licensee was instructed to 1
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respond to the NRC. The Reouested Actions in Supplement I to NRC Bulletin 90- >
01 supersede the original NRC Bulletin 90-01 Reouested Actions.
In responding to Supplement I to NRC Bulletin 90-01, the licensee is l directed to address three items.
- 1. A statement either committing the licensee to take the NRC Bulletin 90-01, Supplement 1, Reouested Actions or taking exception to those actions.
- 2. Addressing the actions committed to in the above statement, '
provide:
- a. a list of the specific actions, including any justifications to be taken to complete the commitment, l
- b. a schedule for completion, and j
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- c. after completion, a statement confirming the actions l committed to are complete. l
- 3. A statement identifying the NRC Bulletin 90 u., Supplement 1,
! Reouested- Actions not taken, along with an evaluation providing. !
l the basis for exemption. .
I In implementing the replacement option of the NRC Reouested Actions, plant shutdown exclusively for replacing the transmitters.is not required. ;
l This allowance infers that replacements can be scheduled. With. replacement in
) a timely manner, enhanced surveillance monitoring for interim operation is not ;
j required. ;
The Washington Public Power Supply System, the licensee for the l Washington Nuclear Project-2 (WNP-2), responded to Supplement 1 of NRC Bulletin 90-01 with a letter dated March 8,1993 (Reference 3). The licensee provided additional information on May 23, 1994 (Reference 4). This technical L evaluation report evaluates the completeness of these submittals. It also determines whether proposed surveillance methods are adequate to determine 2
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fill-oil loss-caused degradation of the transmitter. Finally, this report l
addresses the interval of surveillance proposed by the licensee for any l transmitters included in the enhanced surveillance program.
Many Rosemount transmitter failures have been attributed to the use of j stainless steel "0"-rings between the sensing module and the process flanges.
Rosemount improved the manufacturing process for transmitters manufactured after July 11, 1989. Those improvements included a limit of the torque applied to the flange bolts. This limits the stress caused in the sensing module by the "0"-ring. Post-production screening, including pressure testing of the sensing module for this potential latent defect, was also implemented at that time. Therefore, as described in Supplement 1 of NRC Bulletin 90-01, j those Rosemount transmitters manufactured after July 11, 1989, are not subject to this review.
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- 2. NRC SPECIFIED REQUESTED ACTIONS The NRC staff specified the following Recuested Actions of licensees of operating reactors.
- 1. Review plant records and identify the following Rosemount transmitters l
(if manufactured before July 11,1989) that either are used in or may be used in either safety-related or ATWS mitigating systems.
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- Rosemount Model 1153, Series B
- Rosemount Model 1153, Series D -
- Rosemount Model 1154 Following identification, the licensee is to establish the following:
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- a. For those identified transmitters having a normal operating pressure greater than 1500 psi, and are installed as part of reactor protection trip systems, ESF actuation systems, or ATWS mitigating systems, either replace the transmitter in an expedited manner, or monitor monthly, for the life of the transmitter, using an enhanced surveillance program.
! If the identified transmitter exceeds the 60,000 psi-month or the 130,000 psi-month criterion (depending on the range code of the transmitter) established by Rosemount, enhanced surveillance on a refueling (not exceeding 24 months) basis is acceptable. Under this option, justification must be based on the service record and the specific safety function of the transmitter. That justification can be based on high functional reliability provided by redundancy or diversity,
- b. For those identified transmitters having a normal operating pressure greater than 1500 psi, and are installed as part of a safety-related system other than reactor protection trip systems, ESF actuation, or ATWS mitigating systems, either replace the transmitter or monitor quarterly, for the life of the transmitter, using an enhanced surveillance program.
If the identified transmitter exceeds the 60,000 psi-month or the 130,000 psi-month criterion (depending on the range code of the transmitter) established by Rosemount, enhanced surveillance on a refueling (not exceeding 24 months) basis is acceptable. Under this option, justification inust be based on the service record and the specific safety function of the transmitter. That i
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l by redundancy or diversit". l l i l l l c. For boiling water reactors (BWR)-- l l
l For those identified transmitters having a normal operating - 1 l pressure greater than 500 psi and less than or equal to
' 1500 psi, and are installed as part of reactor protection trip systems, ESF actuation systems, or ATWS mitigating ,
systems, either replace the transmitter, or monitor monthly- !
t with an enhanced surveillance monitoring program, until the P
transmitter reaches the designated (by Rosemount) psi-month ;
criterion (60,000 psi-month or 130,000 psi-month, depending on the transmitter range code).
- For transmitters that provide signals to the RPS or ATWS {
trips for high pressure or low water level, the enhanced j surveillance must be monthly. For other transmitters in '
this classification, enhanced. surveillance on a refueling (not exceeding 24 months) basis is acceptable. Under this i option, justification must be based on the service record l and the specific safety function of the transmitter. That justification can be based on high functional reliability ,
provided by redundancy or diversity.
For pressurized water reactors (PWR)--
For those identified transmitters having a normal operating pressure greater than 500 psi and less than or equal to
, 1500 psi, and are installed as part of reactor protection >
l trip systems, ESF actuation systems, or ATWS mitigating !
systems, either replace the transmitter, or monitor with an j enhanced surveillance monitoring program, until the !
transmitter reaches the designated (by Rosemount) psi-month j criterion (60,000 psi-month or 130,000 psi-month, depending- j on the transmitter range code) on a refueling (not exceeding .
24 months) basis.
- d. For those identified transmitters having a normal operating pressure greater than 500 psi and less than or equal to 1500 psi, and are installed as part of a safety-related system other than ,
reactor protection trip systems, ESF actuation, or ATWS mitigating _.
systems, either replace the transmitter or monitor with an enhanced surveillance monitoring program, until the transmitter
! reaches the designated (by Rosemount) psi-month criterion (60,000 psi-month or 130,000 psi-month, depending on the transmitter range code) on a refueling (not exceeding 24 months) basis.
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- e. Those transmitters having a normal operating pressure greater than f 500 psi and less than or equal to 1500 psi, and have accumulated i sufficient psi-month operating history to exceed the criterion i established by Rosemount, may be excluded from the enhanced I surveillance monitoring program at the discretion of the licensee. !
However, the licensee should retain a high level of confidence -l that a high level of reliability is maintained and that- l transmitter failure due to-loss of fill-oil is detectable.
l f-. Those transmitters having a normal operatinq pressure less than or l equal to 500 psi may be excluded from the enhanced surveillance !
monitoring program at the discretion-of the licensee. However, the licensee should retain a high' level of confidence that a high j level of reliability is maintained and that transmitter failure ;
due .to loss of fill-oil is detectable. j i
- 2. Evaluate the enhanced surveillance monitoring program. -The evaluation i is to ensure the mearurement data has an accuracy commensurate with the i accuracy needed to compare the data to the manufacturers drift' data !
criteria. It is this comparison that determines the degradation- l threshold for loss of fill-oil failures of_ the subject transmitters. '
The Supplement also states ths NRC may conduct audits or inspections in
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l 3. EVALUATION l
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The licensee provided a response to Supplement 1 of NRC Bulletin 90-01 on March 8, 1993. The licensee provided additional information on May 23, 1994. Those responses were compared to the Bulletin Reportina Recuirements and Reauested Actions as described below. The licensee indicates they have 64 Rosemount transmitters that are subject to the Recuested Actions of the l
Supplement.
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3.1 Evaluation of Licensee Response to Reportino Recuirements In Reference 3, the licensee describes how they will take the Recuested Actions detailed in Supplement 1 of NRC Bulletin 90-01. Included with those I stitements are clarification, interpretation, and the limits placed on those commitments. The licensee described the specific actions taken to implement the Reauested Actions and the associated schedule for completion.
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In Reference 4, the licensee stated that the Reouested Actions are complete. H is included the replacement of two Rosemount transmitters during l
i the spring of 1993. Together, the licensee submittals conform with the i
Reportina Reauirements of Supplement 1 of NRC Bulletin 90-01. The submittals I
! identify where no licensee action is taken and provides evaluation and l I justification supporting the position that the action is not necessary.
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3.2 Evaluation of Licensee Response to Recuested Actions Supplement 1 of NRC Bulletin 90-01 requested licensee action to resolve the issue of fill-oil leakage in Rosemount transmitters. In this Technical Evaluation Report, the Reauested Actions and associated transmitter criteria are summarized in Section 2 of this report. The licensee identified a total of 64 Rosemount transmitters that are in the scope of this review. The licensee response is discussed in the following sections.
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3.2.1 Licensee Response to Recuested Action 1.a !
The licensee states there are no Rosemount transmitters from this j transmitter classification at WNP-2. -l 3.2.2 Licensee Response to Recuested Action 1.b The licensee states there are no Rosemount transmitters from this i transmitter classification at WNP-2. J l
1 3.2.3 Licensee Response to Recuested Action 1.c j i
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-In Reference 3, the licensee-states there are two Rosemount_ transmitters from this transmitter classification at WNP-2. The licensee notes that these transmitters, RRC-FT-14A and RRC-FT-140, are scheduled for-replacement during l refueling outage 8 (Spring 1993). In Reference 4, the licensee informed the l NRC that this replacement is complete.
3.2.4 Licensee Response to Recuested Action 1.d The-licensee states there is one Rosemount transmitter from this transmitter classification at WNP-2. This transmitter, RFW-DPT-48, provides a signal representing the reactor pressure vessel level to the reactor feedwater control system. The licensee states this transmitter will continue under the i enhanced surveillance program. The frequency for monitoring this transmitter is every refueling outage-(24 months).
This commitment fulfills Recuested Action 1.d of the Supplement and is acceptable.
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l l 3.2.5 Licensee Response to Reouested Action 1.e The licensee states there are 16 Rosemount transmitters from this classification at WNP-2. Ail have exceeded the 60,000 psi-month maturity criterion established by Rosemount and endorsed by the NRC. The licensee l
states these transmitters will remain part of the enhanced surveillance monitoring program. This gives continued assurance that these transmitters remain highly reliable, as required by the Supplement.
l 3.2.6 Licensee Response to Reauested Action 1.f The licensee states there are 45 Rosemount transmitters from this classification at WNP-2. The licensee states these transmitters will remain part of the enhanced surveillance monitoring program. This gives continued assurance that these transmitters remain highly reliable, as required by the Supplement.
l These 45 transmitters include some transmitters that observe pressure beyond 500 psi during system testing, yet are normally not subject to pressure. These transmitters include transmitters associated with the high pressure core spray system and the standby liquid control system. The accumulated psi-month operational history is small. The total number of transmitters included in this sub-classification was not identified by the licensee. With minimum time at pressure, these transmitters will not soon exceed the established Rosemount psi-mcnth criteria that establishes the transmitter is at risk of losing sufficient fill-oil to degrade the output signal. Rosemount Technical Bulletin No. 4 notes that transmitters in this type of ' standby' service are acceptable without enhanced surveillance. As the licensee includes these ' standby' service transmitters in their enhanced surveillance monitoring prograr., the licensee's actions regarding these transmitters is acceptable.
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3.2.7 Enhanced Surveillance Monitorina Proaram l t
f' The licensee determined, in consultation with Rosemount, that calibration data taken to two decimal places provides the required data accuracy for comparison to the Rosemount drift data criteria. The licensee-
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states their calibration instrumentation has an accuracy meeting this' )
requirement. I i :
l' In Reference 4, the licensee notes that their enhanced surveillance-monitoring program uses transmitter calibration data. This data comes from
' l the performance of normal calibration procedures. A computer is programmed to. !
chart the historical cumulative zero and span shifts. These shifts are l compared to the drift limits established by Rosemount for each transmitter,. -l
' t based on the transmitter range code. This program methodology-is based on the li technical information described in Rosemount Technical Bulletin No. ~4. (
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Based on the licensee description of their enhanced surveillance .;
monitoring program, we find the enhanced surveillance monitoring ' program for WNP-2 acceptable. l 10
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- 4. CONCLUSIONS 6
Based on our review, we find that the licensee has completed the j- reporting requirements of Supplement 1 of NRC Bulletin 90-01. Further, the l licensee conforms to the requested actions of Supplement I to NRC Bulletin 90-01. l l
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- 5. REFERENCES
- 1. NRC Bulletin No. 90-01: " Loss of Fill-oil in Transmitters Manufactured by Rosemount," March 9, 1990, OMB No. 3150-0011,
- 2. NRC Bulletin No. 90-01, Supplement 1: " Loss of Fill-oil in Transmitters Manufactured by Rosemount," December 22, 1992, OMF No. 3150-0011.
- 3. Letter, Washington Public Power Supply System (G. C. Sorensen) to NRC,
" Response to IEB 90-01, Supplement 1," March 8,1993, G02-93-055.
- 4. Letter, Washington Public Power Supply System (J. V. Parrish) to NRC,
" Response to Request for ~ Additional Information," May 23, 1994, G0-94-124.
12
I i
l ENCLOSURE _1 SALP INPUT I l
FACILITf NAME: yNP-2
SUMMARY
OF REVIEW The staff completed its review of the licensee's response to Nuclear Regulatory Commission Bulletin 90-01, . Supplement 1, submitted by Washington Public Power Su.cnly System for ;NP-2. We find the licensee's response for
+' :s item accept 11e.
NARRATIVE DISCUSSION OF_11_CENSEE PERFORMANCE "UNCTIONfL AREA The initial response provided to the staff was supplemented with addi'... .
information to meet the requested actions.
Author: D. Spaulding Date: July 18, 1994 i
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