LER-1981-018, /03L-0:on 810620,reactor Water Cleanup Sys Was Returned to Svc Following Maint W/Discharge Isolation Valve MO2399 Open & Inoperable.Caused by Torque Switch Failure. Motor & Torque Switch Replaced & Sys Returned to Svc |
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| 2631981018R03 - NRC Website |
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, NRC FORM 366 U.1. NUCLEAR REGULATORY COMMISSION (7 77)
LICENSEE EVENT REPORT
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8 9 LICENSEE CODE 14 tg LaCENSE NUMUEH 26 26 LICENSE TYPE JO b7 LAIb8 CON'T IOlil a",0 l h l@l o ! 5 l o f o f 012161 3l@l 01612101811'l@l 0171210 l 81 1l@
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8 6u 61 DOCKETNOVSER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROB ABLE CONSEQJENCES h I O I 2 I I Durine nonnal nower oneration. the RNGT system was returned to service followine l
I O 131 I maintenance with the RKOI di-charce isolation valve (Mn23991 open and inon rable. I 10111 l At lenst one en1ro in the return line uns not clnsod. ns vnnnired hv Tech.S ac.
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iOIsiI 3.7.D.2. (The RKOI discharecs to the feedwater line which has two check valves in I FO M ! I serios tn nrovian isnintinna m line isnintion chock valves fully onerable.
I I O I 7 I I No effect on health or safety.
No previous events.
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33 34 35 36 31 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS h l~TO l I Rwa! system niaced in service wit a isolation valve open and inoperable (due to I
! i l i I i toroue switch fa ilurel.
System operated 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> 6 53 minutes when Tech.Snec.
I iii2II problem realized and system was isolated.
Motor and torque switch replaced and j
ii#3l l system returned to service.
Tech. Spec. chance under Consideration tO remove valvp ii14l 1 from list of isolation valves (already tw isolation valves downstream of this value).
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% POWER OTHER S TA TUS DISCO RY DISCOVERY DESCRIPTION I i i s l l El@ l1 l 0 l 0 l@l NA l
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8 9 11 12 80 LOSS OF OR DAMAGE TO FACILITV TYPE
DESCRIPTION
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| 05000263/LER-1981-001, Forwards Updated LER 81-001/03X-1 | Forwards Updated LER 81-001/03X-1 | | | 05000263/LER-1981-001-03, While Performing Surveillance Test Mo 2035,HPCI Outboard Steam Supply Isolation Valve Failed to Close.Caused by Opened Limitorque SMB-O,240-volt Dc & Torque Switches.Switches Replaced | While Performing Surveillance Test Mo 2035,HPCI Outboard Steam Supply Isolation Valve Failed to Close.Caused by Opened Limitorque SMB-O,240-volt Dc & Torque Switches.Switches Replaced | | | 05000263/LER-1981-016, Forwards LER 81-016/01T-0 | Forwards LER 81-016/01T-0 | | | 05000263/LER-1981-017, Forwards Updated LER 81-017/03L-1 | Forwards Updated LER 81-017/03L-1 | | | 05000263/LER-1981-017-03, While Removing Insulation,Cracks Discovered on 4-inch & 1-inch Reactor Water Cleanup HX Piping,Where Connected to Hx.Caused by Poor fit-up & Welding.Slag Line Removed & Weld Repaired | While Removing Insulation,Cracks Discovered on 4-inch & 1-inch Reactor Water Cleanup HX Piping,Where Connected to Hx.Caused by Poor fit-up & Welding.Slag Line Removed & Weld Repaired | | | 05000263/LER-1981-018-03, /03L-0:on 810620,reactor Water Cleanup Sys Was Returned to Svc Following Maint W/Discharge Isolation Valve MO2399 Open & Inoperable.Caused by Torque Switch Failure. Motor & Torque Switch Replaced & Sys Returned to Svc | /03L-0:on 810620,reactor Water Cleanup Sys Was Returned to Svc Following Maint W/Discharge Isolation Valve MO2399 Open & Inoperable.Caused by Torque Switch Failure. Motor & Torque Switch Replaced & Sys Returned to Svc | | | 05000263/LER-1981-018, Forwards LER 81-018/03L-0 | Forwards LER 81-018/03L-0 | | | 05000263/LER-1981-019-03, /03L-0:on 811022,flow Through B Train Standby Gas Treatment Noted Less than Tech Spec.Caused by Dirt in Tubing from Flow Sensor at Offgas Stack Resulting in Closed Inlet Dampers on Stack Dilution Fans.Tubing Blown Out | /03L-0:on 811022,flow Through B Train Standby Gas Treatment Noted Less than Tech Spec.Caused by Dirt in Tubing from Flow Sensor at Offgas Stack Resulting in Closed Inlet Dampers on Stack Dilution Fans.Tubing Blown Out | | | 05000263/LER-1981-019, Forwards LER 81-019/03L-0 | Forwards LER 81-019/03L-0 | | | 05000263/LER-1981-020-03, /03L-0:on 810724,main Steam Leak Revealed in Drain Line to Condenser.Caused by Piping Leaking Immediately Downstream of 45 Degree Elbow Due to Erosion & Impingement Resulting from Steam & Water Flow from Restricting Orifice | /03L-0:on 810724,main Steam Leak Revealed in Drain Line to Condenser.Caused by Piping Leaking Immediately Downstream of 45 Degree Elbow Due to Erosion & Impingement Resulting from Steam & Water Flow from Restricting Orifice | | | 05000263/LER-1981-020, Forwards LER 81-020/03L-0 | Forwards LER 81-020/03L-0 | | | 05000263/LER-1981-021-01, /01T-0:on 811024,during Cold Shutdown Primary Containment Isolation Sys Logic Relay Coil Failed & Relay Did Not Immediately Trip.Caused by Natural end-of-life. Replaced Relay | /01T-0:on 811024,during Cold Shutdown Primary Containment Isolation Sys Logic Relay Coil Failed & Relay Did Not Immediately Trip.Caused by Natural end-of-life. Replaced Relay | | | 05000263/LER-1981-021, /03L-0:on 811110,during Cold shutdown,4 Channel a Main Steam Line High Flow Switches Found Inoperable.Caused by Heating of Switching Element Due to Relay Coil Failure, Initially Reported in LER 81-021.Elements Replaced | /03L-0:on 811110,during Cold shutdown,4 Channel a Main Steam Line High Flow Switches Found Inoperable.Caused by Heating of Switching Element Due to Relay Coil Failure, Initially Reported in LER 81-021.Elements Replaced | | | 05000263/LER-1981-022-01, /01T-0:on 811030,during Inservice Insp on Core Spray Loop B Safe End to Reducer Weld,Detected Several non- through-wall Crack Indications in HAZ on Reducer.Probably Caused by Igscc.Replaced Reducer & Valve | /01T-0:on 811030,during Inservice Insp on Core Spray Loop B Safe End to Reducer Weld,Detected Several non- through-wall Crack Indications in HAZ on Reducer.Probably Caused by Igscc.Replaced Reducer & Valve | | | 05000263/LER-1981-022, Forwards LER 81-022/01T-0 | Forwards LER 81-022/01T-0 | | | 05000263/LER-1981-023, Forwards LER 81-023/03L-0 | Forwards LER 81-023/03L-0 | | | 05000263/LER-1981-024-01, /01T-0:on 811112,during Maint Shutdown & PM on Hpci,Discovered Abnormal Wear in Woodwear Governor Bracket. Caused by Failed Components Due to Thrust Washer Failure Causing Bushings to Seize to Shaft & Distort Casing | /01T-0:on 811112,during Maint Shutdown & PM on Hpci,Discovered Abnormal Wear in Woodwear Governor Bracket. Caused by Failed Components Due to Thrust Washer Failure Causing Bushings to Seize to Shaft & Distort Casing | | | 05000263/LER-1981-024, Forwards LER 81-024/01T-0 | Forwards LER 81-024/01T-0 | |
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