LER-1979-024, /03L-0:on 791220,during Normal Operation,Routine Operator Insp Revealed Steam Leak in 1-inch 90 Degree Elbow in Reactor Core Isolation Cooling Steam Line Drain to Condenser.Caused by Pinhole Failure of 3,000-lb Socket Weld |
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text
REGULATORY IN!
~AT1L)N DISTNif3UTION sYSFr 0 R105 A6CESSION NbR:6001250535 DUC.DAl't: 60/01/18 NOTARIZED): NO FACIL':.50-263 Monticello Nuclear Generating Plant, or ern States A0'I,NAME AUl'HUR AFFILIATiUN UVE.RLIV,1.W, Northern Sta tes Power Co.
RECXP,*NAme RECIHIENJ AFFILIATION Region 3p Chicagop Office of the Director L)OCKEl" #
0$000263-SUt3JECr: LEK 79-024/U3L"0:o, 791220,.during normal operationfroutine operator insp.revealed 'steam leak in 1-inch'90 degree elbow in reactor core insulation cooling steam line drain to Conaenser.Cawsed by pin~hole faih.,re of 3000 lb socket weld, DISTRIBUT ION CU&: A0028 COPIES RECEIVEL):LFR
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9'z TIrL~i Incideni keports
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NOT S -- - - - - - - - - - - -
RECIPITIJ I1) CODE/NAmE ACTION; 05 bC*
INTERNAL: 01.-jjIGiF1 14 TA/EDO lb EEB3 18 PLANT SYS 6H 20 At) PLANT1Si8 23 ENGR-8H 25 PWR SYS 8HR 27 OPERA-LIQC bR 29 AUX 5Y$6R H ANA) ERPSg ",
STS GROUP LLAOR COPIES 4 4 RECIPIENT ID) CODE/NAME 02 NHC PL)R 11 MPA 1$ NOVAK/KNiEL 17 AD FOR ENGR 19 1M2 S'YS t$
22 kEAC-sAFt8R 24* KREGtER 26 AU/SITE ANAL 28 ACOENT ANLYs E JORDAN/IE N IRELAND EXTERNAL:
03 LPDN 29 ACRS 1
16 04 NS1C JAN 2 8 1980 IOIALI, NUMUER OF COPIES REOUID: L1lR 5
NL C OPI.1ES LTN ENC, 1
1 50 ENC L 50 17
NORTHERN STATES POWER COMPANY MINNEAPOLIS, MINNESOTA 55401 January 18, 1980 Mr J G Keppler Office of Inspection & Enforcement U S Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137
Dear Mr Keppler:
MONTICELLO NUCLEAR GENERATING PLANT Docket No. 50-263 License No. DPR-22 RCIC Steam Drain Line Steam Leak The Licensee Event Report for this occurrence is reproduced on the back of this letter. Enclosed are three copies.
This event is reported in compliance with Technical Specification 6.7.B.2.d since it represents abnormal degradation of a line designed to contain radioactive material resulting from the fission process.
Yours very truly, L 0 Mayer, PE Manager 'of Nuclear Support Services LOM/DMMNjh cc:
Director, IE, USNRC (30)
Director, MIPC, USNRC (3)
MPCA Attn:
J W Ferman
- - over-8001250 ';
NRC FORM 366 (7-77)
[E]E 7
8 CON'T DE]
7 8
P 1
7 8
U.S. NUCLEAR REGULATORY COMMISSION no errect on system operability and no effect on public health or safety.
I 80 9
SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE UK e1LE@
e)IEl LxJ (9 I I llGlXIXI LAJ@O L 7
8 9
10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION 11 ERIO EVENT YEAR IREPORT NO.
CODE TYPE NO.
RERTm L_7L
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10 1 2 141 I In6
(
1] -4(--j
~NUMBER I 19
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024
&LJ LLJ LJ LQJi 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRD-4 PRIME COMP.
COMPONENT TAKEN ACTION ON PLANT METHOD HOURS 22 SUBMITTED FORM SUB.
SUPPLIER MANUFACTURER l^J@LW J@
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33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Pinhole failure of 3000 lb socket weld 900 elbow occurred due to suspected erosion l
from high velocity steam passing through a leaking valve. Leaking elbow, upstream I
elbow and connecting pipe replaced. Leaking valve will be repaired during appropriate outage when parts arrive. Remaining original fittings in line down-I stream of leaking valve will be replaced during next appropriate outage.
7 8
9 FACILITY METHOD OF STATUS
%POWER OTHERSTATUS DISCOVERY DISCOVERY DESCRIPTION [i]
W3 0191 1(31 NB I Operator observation 7
8 9
10 12 13 44 45 46 ACTIVITY CONTENT 3
RELEASED OF RELEASE AMOUNT OF ACTIVITY L
[E] L @
JI NA I
NA 7
8 9
10 11 44 45 PERSONNEL EXPOSURES 80 NUMBER TYPE DESCRIPTION (B 1 01 0 0 () Z ()I NA 1
7 8
9 11 12 13 80 PERSONNEL INJURIES NUMBER
DESCRIPTION
0 10 1 0 I
NA 7
8 9
11 12 LOSS OF OR DAMAGE TO FACILITY TYPE
DESCRIPTION
7 8
9 10 80 PUBLICITY NRC USE ONLY ISSUED
DESCRIPTION
NA 01 1 LZ 1L NA 1
8 9
10 68 69 80 T W 612/295-5151 0
NAME OF PREPARMER OFPHONE 80012508 LICENSEE EVENT REPORT CONTROL BLOCK:
(PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6
INIMI NIP 1 1ll 0 o0 - lo loll olo 1-10 lo l0l 41 11 11 1l11 10L L D
9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 REPORT L
0 5 010 10 21 61 3l l 11 21 21 01 71 91 1 01 111 18 18 I0 SOURCE
@__________1____
60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES During normal operation routine operator inspection revealed a steam knlk in n one inch 90o elbow in the RCIC steam line drain to the condenser. Reportable under TS 6.7.B.2.d. One previous similar occurrence (M-RO-79-09), Event had
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| 05000263/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000263/LER-1979-001-03, /03L-0 on 790110:during Normal Operation,Steam Leak Found in Elbow on Turbine Main Steam Bypass Header 1 Inch Drain Line to Condenser,Due to Erosion Caused by Steam & Water Flow of Restricting orifice,RO-2569 | /03L-0 on 790110:during Normal Operation,Steam Leak Found in Elbow on Turbine Main Steam Bypass Header 1 Inch Drain Line to Condenser,Due to Erosion Caused by Steam & Water Flow of Restricting orifice,RO-2569 | | | 05000263/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000263/LER-1979-002-03, /03L-0 on 790118:during Normal Operation,Weekly Average Power Range Monitor Functional Scram Test Was Not Completed within Time Allowed.Caused by Personnel Error | /03L-0 on 790118:during Normal Operation,Weekly Average Power Range Monitor Functional Scram Test Was Not Completed within Time Allowed.Caused by Personnel Error | | | 05000263/LER-1979-003, Forwards LER 79-003/01T-0 | Forwards LER 79-003/01T-0 | | | 05000263/LER-1979-003-01, /01T-0 on 790301:containment Vent & Purge Isolation Valves Would Not Close During DBA-LOCA.Cause Unknown.Fisher Continential 18 & 20 Inch,Type 9220 Butterfly Valves Opening Is Administratively Controlled | /01T-0 on 790301:containment Vent & Purge Isolation Valves Would Not Close During DBA-LOCA.Cause Unknown.Fisher Continential 18 & 20 Inch,Type 9220 Butterfly Valves Opening Is Administratively Controlled | | | 05000263/LER-1979-004-01, /01T-0 on 790313:shipping Cask Model B-2 Found W/ Two Missing Lid Bolt Nuts,Missing Inner Lid Gasket & Damaged Outer Lid Gasket.Caused by Inadequate Insp & Maint by Supplier.Cask Returned Empty | /01T-0 on 790313:shipping Cask Model B-2 Found W/ Two Missing Lid Bolt Nuts,Missing Inner Lid Gasket & Damaged Outer Lid Gasket.Caused by Inadequate Insp & Maint by Supplier.Cask Returned Empty | | | 05000263/LER-1979-005-03, /03L-0 on 790315:results of Special Test of Safety Relief Valve Effects on Torus Indicated Possible Excessive Opening Delay Time.Caused by Improper Installation of Insulation on Valve 67F.Maint Procedure to Modified | /03L-0 on 790315:results of Special Test of Safety Relief Valve Effects on Torus Indicated Possible Excessive Opening Delay Time.Caused by Improper Installation of Insulation on Valve 67F.Maint Procedure to Modified | | | 05000263/LER-1979-006-01, /01T-0 on 790317:during Recirculator Motor Generator Shutdown,Associated Field Breaker Failed to Trip. Caused by Metal Bead Fused to Arc Chute.Bead Removed,Breaker Tested & Returned to Svc | /01T-0 on 790317:during Recirculator Motor Generator Shutdown,Associated Field Breaker Failed to Trip. Caused by Metal Bead Fused to Arc Chute.Bead Removed,Breaker Tested & Returned to Svc | | | 05000263/LER-1979-007-03, /03L-0 on 790318:valve Operability & Motor Current Check Signed Despite Current Outside Formula Spec.Caused by Misaligned Torque Switch.New Components Ordered | /03L-0 on 790318:valve Operability & Motor Current Check Signed Despite Current Outside Formula Spec.Caused by Misaligned Torque Switch.New Components Ordered | | | 05000263/LER-1979-008-01, /01T-0 on 790323:one Trip Output Relay Failed to Initiate Trip in No 12 Recirculation Motor Generator Set Field Breaker Trip Logic.Caused by Contact Which Was Disengaged from Socket.Contact re-engaged in Socket | /01T-0 on 790323:one Trip Output Relay Failed to Initiate Trip in No 12 Recirculation Motor Generator Set Field Breaker Trip Logic.Caused by Contact Which Was Disengaged from Socket.Contact re-engaged in Socket | | | 05000263/LER-1979-009-03, /03L-0 on 790404:steam Leak Found in 90 Degree Elbow in 1-inch Core Isolation Cooling Steam Supply Drain Pot Condenser Line.Caused by Erosion Due to High Velocity Steam from Leaking Valve.Hole Patched.Repairs Planned | /03L-0 on 790404:steam Leak Found in 90 Degree Elbow in 1-inch Core Isolation Cooling Steam Supply Drain Pot Condenser Line.Caused by Erosion Due to High Velocity Steam from Leaking Valve.Hole Patched.Repairs Planned | | | 05000263/LER-1979-010-01, /01T-0 on 790426:informed by General Motors of Potential Diesel Generator Turbocharger Problem.Caused by Inadequate Design of Lube Oil Sys.Mod Being Developed | /01T-0 on 790426:informed by General Motors of Potential Diesel Generator Turbocharger Problem.Caused by Inadequate Design of Lube Oil Sys.Mod Being Developed | | | 05000263/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000263/LER-1979-011-03, /03L-0 on 790529:no Min Flow in B Train Standby Gas Treatment Sys.Caused by Dilution Flow from Compressed Storage Not Isolated by BV-5.Replaced Positioner & Installed Filter in Cylinder Supply/Return Line | /03L-0 on 790529:no Min Flow in B Train Standby Gas Treatment Sys.Caused by Dilution Flow from Compressed Storage Not Isolated by BV-5.Replaced Positioner & Installed Filter in Cylinder Supply/Return Line | | | 05000263/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000263/LER-1979-012-03, /03L-0 on 790702:during Reactor Core Isolation Cooling Sys Test,Governor end-bearing Temp Alarm Received & Bearing Exhibited High Vibration.Sys Inoperative.Caused by Turbine Oil Pump Drive Gear Failure.Gears Replaced | /03L-0 on 790702:during Reactor Core Isolation Cooling Sys Test,Governor end-bearing Temp Alarm Received & Bearing Exhibited High Vibration.Sys Inoperative.Caused by Turbine Oil Pump Drive Gear Failure.Gears Replaced | | | 05000263/LER-1979-013, Forwards LER 79-013/03L-0 | Forwards LER 79-013/03L-0 | | | 05000263/LER-1979-013-03, /03L-0 on 790708:motor Operator Failed,Rendering Torus Cooling Injection Valve Inoperable During Normal Operation.Caused by Failure of Motor Winding Due to Limit Switch Not de-energizing Motor.Switch Replaced | /03L-0 on 790708:motor Operator Failed,Rendering Torus Cooling Injection Valve Inoperable During Normal Operation.Caused by Failure of Motor Winding Due to Limit Switch Not de-energizing Motor.Switch Replaced | | | 05000263/LER-1979-014, Forwards LER 79-014/03L-0 | Forwards LER 79-014/03L-0 | | | 05000263/LER-1979-014-03, /03L-0 on 790709:water Leak Discovered in 1/2 Inch Instrument Line from Reactor Water Cleanup Sys Nonregenerative Heat Exchanger.Cause Not Determined.Leaking Line Isolated & Will Be Further Investigated & Repaired | /03L-0 on 790709:water Leak Discovered in 1/2 Inch Instrument Line from Reactor Water Cleanup Sys Nonregenerative Heat Exchanger.Cause Not Determined.Leaking Line Isolated & Will Be Further Investigated & Repaired | | | 05000263/LER-1979-015, Forwards LER 79-015/03L-0 | Forwards LER 79-015/03L-0 | | | 05000263/LER-1979-015-03, /03L-0 on 790712:discovered Steam Leak from Intermediate Pressure Feedwater Heater.Cause Undetermined. Temporary Patch Installed Pending Replacement of Heater Shell | /03L-0 on 790712:discovered Steam Leak from Intermediate Pressure Feedwater Heater.Cause Undetermined. Temporary Patch Installed Pending Replacement of Heater Shell | | | 05000263/LER-1979-016-03, /03L-0 on 790731:turbine Tripped on Low Oil Pressure.Caused by Clogged Lube Oil Filter.Sys Drained, Inspected & Flushed | /03L-0 on 790731:turbine Tripped on Low Oil Pressure.Caused by Clogged Lube Oil Filter.Sys Drained, Inspected & Flushed | | | 05000263/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000263/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000263/LER-1979-017-03, /03L-0:on 790806,steam Leak Observed on Feedwater Extraction Steam Line Drain 15A.Caused by Steam Erosion Through Wall of Steam Trap on Line.Trap Isolated Pending Repair or Replacement at Next Appropriate Outage | /03L-0:on 790806,steam Leak Observed on Feedwater Extraction Steam Line Drain 15A.Caused by Steam Erosion Through Wall of Steam Trap on Line.Trap Isolated Pending Repair or Replacement at Next Appropriate Outage | | | 05000263/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000263/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000263/LER-1979-019-03, /03L-0:on 790923,ECCS Yarway Level Switches Indicated Falsely High Level & Would Not Have Tripped within Specified Settings.Caused by Effects of Leak Which Developed in Reactor Pressure Gauge During Normal Operation | /03L-0:on 790923,ECCS Yarway Level Switches Indicated Falsely High Level & Would Not Have Tripped within Specified Settings.Caused by Effects of Leak Which Developed in Reactor Pressure Gauge During Normal Operation | | | 05000263/LER-1979-020-03, /03L-0:on 791030,reactor Core Isolation Cooling Isolation Temp Switch Found to Trip Above Allowable Setpoint.Caused by Setpoint Drift.Switch Replaced | /03L-0:on 791030,reactor Core Isolation Cooling Isolation Temp Switch Found to Trip Above Allowable Setpoint.Caused by Setpoint Drift.Switch Replaced | | | 05000263/LER-1979-020, Forwards LER 79-020/03L-0 | Forwards LER 79-020/03L-0 | | | 05000263/LER-1979-021-03, /03L-0:on 791119,during IE Bulletin 79-02 Evaluation,Snubber SS-31 Base Plate Expansion Anchor Bolt Safety Factor Found to Be Less than One.Caused by Inadequate Base Plate & Expansion Anchor Bolts | /03L-0:on 791119,during IE Bulletin 79-02 Evaluation,Snubber SS-31 Base Plate Expansion Anchor Bolt Safety Factor Found to Be Less than One.Caused by Inadequate Base Plate & Expansion Anchor Bolts | | | 05000263/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000263/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000263/LER-1979-022-03, /03L-0:on 791213,during Normal Operation,Leak Discovered in 90-degree Elbow on 1-inch Condensate Line from Steam Supply to Recombiner Train Drain Trap.Caused by Erosion from Hot Steam Drains.Elbow Modified | /03L-0:on 791213,during Normal Operation,Leak Discovered in 90-degree Elbow on 1-inch Condensate Line from Steam Supply to Recombiner Train Drain Trap.Caused by Erosion from Hot Steam Drains.Elbow Modified | | | 05000263/LER-1979-023, Updated LER 79-023/01T-1:on 800103,one Fuel Type Noted to Exceed Max Allowable Max Average Planar Linear Heat Generation Rate Value & Another as Improperly Programmed in Plant Computer.Caused by Inadequate Review | Updated LER 79-023/01T-1:on 800103,one Fuel Type Noted to Exceed Max Allowable Max Average Planar Linear Heat Generation Rate Value & Another as Improperly Programmed in Plant Computer.Caused by Inadequate Review | | | 05000263/LER-1979-024-03, /03L-0:on 791220,during Normal Operation,Routine Operator Insp Revealed Steam Leak in 1-inch 90 Degree Elbow in Reactor Core Isolation Cooling Steam Line Drain to Condenser.Caused by Pinhole Failure of 3,000-lb Socket Weld | /03L-0:on 791220,during Normal Operation,Routine Operator Insp Revealed Steam Leak in 1-inch 90 Degree Elbow in Reactor Core Isolation Cooling Steam Line Drain to Condenser.Caused by Pinhole Failure of 3,000-lb Socket Weld | | | 05000263/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | |
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