/03X-1 on 780908:during Normal Operation,Trip of Essential MCC B33A Supply Breaker 52-304 Resulted in Operation in Degraded Mode.Caused by Low Setpoint on Trip Device & by Loss of Dash Pot Oil in Trip Device| ML112760118 |
| Person / Time |
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| Site: |
Monticello  |
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| Issue date: |
01/29/1979 |
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| From: |
Galen Smith Northern States Power Co |
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| To: |
NRC/OI/RGN-III/FO |
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| Shared Package |
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| ML112760119 |
List: |
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| References |
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| LER-78-016-03X, LER-78-16-3X, NUDOCS 7902050206 |
| Download: ML112760118 (5) |
|
LER-1978-016, /03X-1 on 780908:during Normal Operation,Trip of Essential MCC B33A Supply Breaker 52-304 Resulted in Operation in Degraded Mode.Caused by Low Setpoint on Trip Device & by Loss of Dash Pot Oil in Trip Device |
| Event date: |
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| Report date: |
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| 2631978016R03 - NRC Website |
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text
,*
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:7902050200 DOC.DATE: 79/01/29 NOTOIZED: NO FACIL:50-263 Monticello Nuclear Generating Plant, Northern States AUTH.NAME AUTHOR AFFILIATION SMITHG.R.
Northern States Power Co.
RECIP.NAME RECIPIENT AFFILIATION Region 3, Chicago, Office of the Director SUBJECT: LER 78-016/03X-1 on 780908:during normal operationtrip of essential MCC B33A supply hreaker 52-304 resulted in ooeration in degraded mode.Caused hy low getpoint on trip device & by loss of dash pot oil in trip device.
0 DOCKET #
05000260 DISTRIBUTION CODE: A002S COPIES RECEIVED:L.TR ENCL SIZE:
I#a TITLE: INCIDENT REPORTS NOTES:
RECIPIENT COPIES RECIPIENT ID COL)E/NAME LTTR ENCL ID CODE/NAME
05 BC~p
~
4 4
14 TA/EDO 1
1 15 NOVAK/KNIEL 16 EEB 1
1 17 AD FOR ENGR 18 PLANT SYS BR 1
1 19 I&C SYS BR 20 AD PLANT SYS 1
1 21 AD SYS/PROJ 22 REAC SAFT BR 1
1 23 ENGR BR 24 KREGER 1
1 25 PWR SYS BR 26 AD/SITE ANAL 1
1 27 OPERA LIC BR 28 ACDENT ANLYS 1
1 E JORDAN/IE EXTERNAL:
03 LPDR 29 ACRS 16 16 1
16 04 NSIC COPIES LTTR ENCL 1
3 1
3 1
I 0
0 FEB 6 1979 TOTAL. NUMBER OF COPIES REQUIRED:
LTTR 4
C 4
45 ENCL 45
NORTHERN STATES POWER COMPANY MINNEAPOLIS. MINNESOTA 55401 January 29, 1979 Mr J G Keppler, Director Office of Inspection & Enforcement U S Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137
Dear Mr Keppler:
MONTICELLO NUCLEAR GENERATING PLANT Docket No. 50-263 License No. DPR-22 UPDATE REPORT Trip of Essential Motor Control Center 133 A Supply Breaker 52-304 The Licensee Event Report for this occurrence is reproduced on the back of this letter and continued on an attached sheet. Attached are three copies.
This event was reported on.October 6, 1978 in Technical Specification 6.7.B.2.b. The cause action items on the form.have been updated to further investigation of the event.
accordance with related and corrective reflect results of Yours very truly, 4'
Manager of Nuclear Support Services LOM/JAG/deh cc:
Director, IE, USNRC (30)
Director, MIPC, USNRC (3)
MPCA Attn: J W Ferman 790205cAol
- - over-17
NIM: I Oil 7
CON'T 7
8 win4 EF-0 8-IN OPERATION IN A DEGRZADED N E PERMITTED BY VARIOUS LIMITING)CONDITIONS FORl OERATION. SYSTEMS DEGRADED b CORE SPRAY (..3.5.A.2)
T7WO ISOLATION VALVES (T.S. 3.7.D.3), SBLC (T.S. 3.4.B. ), SBGI'S (T.S. 3.7.B.1a) N N
MREC EVC WATER PUMP.
NO SIGNIFICANT OCC CE TOOK PLACE AS A ULT OF THE EVENT.
NO EFFECT ON PUBLIC HEALTH OR SAFETY.
DUNDANT PORTIONS F ALL SYSTEMS MENTIONED ONE PRE\\QUS EVENT REPO/
(78-009).
7 89 SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUICODE C
lPONENT CODE SUBCODE SUUCODE 09 W
@ A WXO IC K TB R KG
_A WZ 7
8 9
10 11 12 13 18 19 20 SEQUENTIAL (0
UIlIONCE REPORT LER/RO EVENT YEAR REPORT NO.
CODE TYPE
@ g 0 _]
L-_J 1
11 61 1-0 LxJ1 1--J NUM 7 1 21 22 23 24
?G 27 2H 29 30 311 ACTION FUTURE EFFECT SHODOWN AT1 CHMENT NPHD-4 PRIME COMP.
TAKEN ACTION ON PLANT METHOD HOURS
- 2)
S ITTED FORM SUB.
SUPPLIER LA] 0H8 Lz@
LO I ol ol ol ol WL L[Ale 33 34 35 36 37 40 41 42 43 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 16 80 REVISION NO.
LOJ 32 COMPONENT MANUFACTURER I
1l ol 81 o1@
44 47 SEE ATTACHED SHEET.
7 89 FACILITY STATUS
%POWER OTHERSTATUS S ] E 1 I1 01 0 NA 7
8 9
10 12 11 44 ACTIVIiY CONTENT RELEASED OF HELEANF AMOUN O
AC1 V
EE LzJ Z
L ZJ l NA 7
8 9
10 1144 PERSONNEL FXPOSURES NUMBER TYPE
DESCRIPTION
9 WT1 ol1 01 z R NA 7
8 9
1 1 12 13 PEHSONNEL INJUR1ES NUMBER
DESCRIPTION
I I 01 01 011 NA 7
8 9
11 12 1O'S OF OR DAMAGE TO FACIL TYPE
)DESCRIPTION ZNA 7
8 9
10 PUBLICI TY 1SSUED DESCRIPT N (
.I 16]1ue 79020E
/M 89 1
S NAME OF PREPARER R.
SMITH I
80 METHOD OF DISCOVERY LAjOL 45 41 L
NA 45 DISC VERY DESCRIPTION OPERATOR OBS VATION
- - J 80 LOCAlI ON\\HELEASE S 80 80 80 80 NRC USE ONLY 68 69 80 '
612/295-5151 M 3h6 IJ. S NIllIC All Ill (Hll.AlOIlY COMMISSION UPDATE
.ICLNSI IV NI II P I
(I
- - PREVIOUS REPORT DATE 10-6-78 CON 11101 BLOCK :
(PLEASE PHlIN I OIl TYPE ALL 14LOUIHED INF OilMATION)
IM IN IM IN P 1 0 0
0 0 0 0 0 00 1 41 1 1 11 101 1
9 LICENSEE CODE 14 5
LICENSE NUMIIER 25 20 LICENSE TYPE 57 CAT 58 0 5 1 0 0 0 2 6 310 19 0 18 17 18(
0')0 2 9 7 l9 60 61 DocKE UMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CO EQUENCES DURING NORMAL OPERATION A T IP OF ESSENTIAL MCC B33A SUPPLY BRF R 52-304 RESULTED WERE AVAILABLE AND OPERABLE.
0 PHO I
J 80
NIHC I OitM 366 v/ in UPDATE tJ JCI I.All III (.1UI.AltOIY COMMISSION I ICI.NStI' I V N I ill Poit I - PREVIOUS REPORT DATE 10-6-78 CONiOL.
ULUC:[
(PLEASE PHINI Oil TYPE ALL HLOUIHED INI OR1MATION)
IM IN IM IN 1P 1 ) 0 0 -
0 0 Ou 1 -
0
!41 CNE TYP E0 57 7
s 9
LICENSEE CODE 14 15 LICENSE NUMIEII 28 26 LICEN 2so 7
8 I
METHOD OF FTATS
% POWER OTHER STATUS DISCOVERY DISCOVERY DESCRIPTION STTU
%~i POE Ii 0 o LAJ I OPERATOR OBSERVATION 8
-]LE_ J@ 11 01 0 1
NA 80 7
8 9
10 1 2 1 1 4 4 4M 4UL ACTIVI TY CONTENT IIIyLC O
F1EES RELE*A5EI)(IF IiELE Ali AMOLINI 0I ACtI:Y~J OAIN rFEES E
L (D L.0 I NA I
NA 7
8 9
10 11 PERSONNEL FXPOSURES NUMBER TYPE
DESCRIPTION
[1 7 I o 01 01 ol@LzJ l NA 7
8 9 11 12 13 PEHSONNEL INJURIES NUMBER DESCRIPTION 6 01 o 01 A
1-NA S
8 9 11 12 10;S OF OR DAMAGE TO FACILITY TYPE
DESCRIPTION
I z 18 NA 7
8 9
10 80 PUBLICITY INSUER DESCRIPU ION 2 Li NA 790205OG"6ILLLLLLJ
)
9 1
68 69 80 R
9 10 PIIONE 612/295-5151 NAME OF PREPARER GARY R. SMITH o"
H I
I 0 15 10 10 E1 0 12 6 13 0 19 10 18 17 18
@ 0 I 11 121917 19 8 7
8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 78 REPURT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES DURING NORMAL OPERATION A TRIP OF ESSENTIAL MCC B33A SUPPLY BREAKER 52-304 RESULTED I
IN OPERATION IN A DEGRADED MODE PERMITTED BY VARIOUS LIMITING CONDITIONS FOR OPERATION.
SYSTEMS DEGRADED WERE CORE SPRAY (T.S. 3.5.A.2),
TWO ISOLATION VALVES I
(T.S. 3.7.D.3),
SBLC (T.S. 3.4.B.1),
SBGTS (T.S. 3.7.B.1a) AND ONE EMERGENCY SERVICE j FOr6 IWATER PUMP.
NO SIGNIFICANT OCCURRENCE TOOK PLACE AS A RESULT OF THE EVENT.
NO I
EFFECT ON PUBLIC HEALTH OR SAFETY.
REDUNDANT PORTIONS OF ALL SYSTENS MENTIONED I
WERE AVAILABLE AND OPERABLE.
ONE PREVIOUS EVENT REPORT (78-009).
SYSTEM
CAUSE
CAUSE COMP VALVE CODE CODE SU RCOIE COMPONENT CODE SUHCODE SUBCODE OB 93 1 L 0 1X1AJ9 C I K ITIBIRIKI LAJ (
L C
7 8
9 10 1 1 12 13 1 8 19 w0 SEQUENTIAL OCCUIHIIENCE REPORT REVISION LER;RO IEVENT YEAR REPORT NO.
CODE TYPENO REPORT
[
NUMBE 122 21116 10 a3J LLJ 1=1j W
. 1 2
23
'14 2G 27
'11 29 30 11 72 ACTION FUTURE EFFECT SHLT DOWN AT1ACHMENT NPD4 PRIME COMP.
COMPONENT 22 SUBMITTED FORM,UB.
SUPPLIER MANUFACTURER TAKEN ACTION ON PLANT METHOD HOURS (
LALU I Z
1olololol 23 LY. 2 44 I 0 1 81 0@
33 3
536 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS 0 SEE ATTACHED SHEET.
0
- 27.
CAUSE DESCRIPTION AND CORRECTIVE ACTIONS.
Low setpoint on trip device. Type of offsite personnel uncertain.
Contributing cause was a loss of dash pot oil in the trip device (GE Type EC-2A).
Parts were replaced in kind and setpoints adjusted.
The following actions are planned:
(1) retrain appropriate per sonnel in setpoint adjustment, (2) check the setpoints on similar devices, (3) rebuild devices in safety related breakers and periodi cally replace devices in all breakers if oil leaks occur.
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| 05000263/LER-1978-001-01, /01T-0:on 780105,nonconconforming Bolts Found in Radwaste Shipping Cask.Caused by Cask Supplier Error.Cask Handling Procedure Will Be Revised to Include Verification of Proper Bolt Size | /01T-0:on 780105,nonconconforming Bolts Found in Radwaste Shipping Cask.Caused by Cask Supplier Error.Cask Handling Procedure Will Be Revised to Include Verification of Proper Bolt Size | | | 05000263/LER-1978-002-01, /01T-0:on 780202,torus to Drywell Vacuum Breaker AO-2382B Failed to Close as Required by Tech Spec 3.7.A.4. Caused by Excess Friction Between Shaft & Bushings.Bushings Will Be Replaced | /01T-0:on 780202,torus to Drywell Vacuum Breaker AO-2382B Failed to Close as Required by Tech Spec 3.7.A.4. Caused by Excess Friction Between Shaft & Bushings.Bushings Will Be Replaced | | | 05000263/LER-1978-003-03, /03L-0:on 780228,during Surveillance Test,Min Flow in a Train SBGTS Could Not Be Attained as Required by Tech Spec 3.7.B.1.Caused by Foreign Matl in BV-4 Positioner. Replaced Positioner | /03L-0:on 780228,during Surveillance Test,Min Flow in a Train SBGTS Could Not Be Attained as Required by Tech Spec 3.7.B.1.Caused by Foreign Matl in BV-4 Positioner. Replaced Positioner | | | 05000263/LER-1978-004-03, /03L-0:on 780421,during Surveillance Test RWCU Outboard Isolation Valve MO-2398 Failed to Close First Time Switch Placed in Close Position.Cause Unknown | /03L-0:on 780421,during Surveillance Test RWCU Outboard Isolation Valve MO-2398 Failed to Close First Time Switch Placed in Close Position.Cause Unknown | | | 05000263/LER-1978-007-03, /03L-0:on 780508,steam Leak Discovered in 45 Degree Elbow on HPCI Steam Supply Line Drain Line to Condenser.Caused by Erosion.Temporary Clamp Repair Made | /03L-0:on 780508,steam Leak Discovered in 45 Degree Elbow on HPCI Steam Supply Line Drain Line to Condenser.Caused by Erosion.Temporary Clamp Repair Made | | | 05000263/LER-1978-008-03, /03L-0:on 780525,inlet Air Heater Operating at Reduced Capacity Due to Fuse Failure.Fuse Block & Fuses Replaced in Kind | /03L-0:on 780525,inlet Air Heater Operating at Reduced Capacity Due to Fuse Failure.Fuse Block & Fuses Replaced in Kind | | | 05000263/LER-1978-009-03, /03L-0:on 780525,trip of Essential MCC B33A Supply Breaker 52-304 Resulted in Operation in Degraded Mode Permitted by Various Lco.Cause Unknown.Evaluation Continuing | /03L-0:on 780525,trip of Essential MCC B33A Supply Breaker 52-304 Resulted in Operation in Degraded Mode Permitted by Various Lco.Cause Unknown.Evaluation Continuing | | | 05000263/LER-1978-010-03, /03L-0:on 780605,CRD 06-19 Delayed for Indefinite Period of Time.Caused by Buna N Disc in Scram Pilot Solenoid Plunger Broken in Several Pieces.Plunger Including Disc Replaced | /03L-0:on 780605,CRD 06-19 Delayed for Indefinite Period of Time.Caused by Buna N Disc in Scram Pilot Solenoid Plunger Broken in Several Pieces.Plunger Including Disc Replaced | | | 05000263/LER-1978-011-01, /01T-0:on 780606,four of Six APRM Scram Trip Settings Three to Four Percent Low.Aprm Calibr at 50% Power. Gain Settings Corrected | /01T-0:on 780606,four of Six APRM Scram Trip Settings Three to Four Percent Low.Aprm Calibr at 50% Power. Gain Settings Corrected | | | 05000263/LER-1978-012-03, /03L-0:on 780616,lightning Storm Resulted in Plant Substation Lockouts Deenergizing Auxiliary Reserve Transformer.Relay Failed Due to Short Circuit Failure of Zener Diode in Trip Pulse Isolator Output | /03L-0:on 780616,lightning Storm Resulted in Plant Substation Lockouts Deenergizing Auxiliary Reserve Transformer.Relay Failed Due to Short Circuit Failure of Zener Diode in Trip Pulse Isolator Output | | | 05000263/LER-1978-013-03, /03L-0:on 780719,steam Leak in 90 Degree Elbow on Turbine Main Steam Bypass Header Drain Line to Condenser. Caused by Erosion.Restricting Orifice,Leaking Elbow & Addl Piping & Elbows to Be Inspected & Replaced | /03L-0:on 780719,steam Leak in 90 Degree Elbow on Turbine Main Steam Bypass Header Drain Line to Condenser. Caused by Erosion.Restricting Orifice,Leaking Elbow & Addl Piping & Elbows to Be Inspected & Replaced | | | 05000263/LER-1978-014-01, /01T-0:on 780728,CRD 30-47 Delayed Approx 1.4 Before Scramming.Disc in Scram Pilot Valve Solenoid Plunger Broken Into Several Pieces,Wedging & Preventing Valve from Venting Air on Scram Valves | /01T-0:on 780728,CRD 30-47 Delayed Approx 1.4 Before Scramming.Disc in Scram Pilot Valve Solenoid Plunger Broken Into Several Pieces,Wedging & Preventing Valve from Venting Air on Scram Valves | | | 05000263/LER-1978-015-03, /03L-0:on 780805,one APRM Scram Trip Setting at Four to Five Percent Low.Caused by Large Power Shape Changes Resulting in LPRM Output Changes.Gain Setting Corrected.W/ | /03L-0:on 780805,one APRM Scram Trip Setting at Four to Five Percent Low.Caused by Large Power Shape Changes Resulting in LPRM Output Changes.Gain Setting Corrected.W/ | | | 05000263/LER-1978-016-03, /03X-1 on 780908:during Normal Operation,Trip of Essential MCC B33A Supply Breaker 52-304 Resulted in Operation in Degraded Mode.Caused by Low Setpoint on Trip Device & by Loss of Dash Pot Oil in Trip Device | /03X-1 on 780908:during Normal Operation,Trip of Essential MCC B33A Supply Breaker 52-304 Resulted in Operation in Degraded Mode.Caused by Low Setpoint on Trip Device & by Loss of Dash Pot Oil in Trip Device | | | 05000263/LER-1978-016, Forwards LER 78-016/03X-1 | Forwards LER 78-016/03X-1 | | | 05000263/LER-1978-018, Forwards LER 78-018/03L-0 | Forwards LER 78-018/03L-0 | | | 05000263/LER-1978-018-03, /03L-0 on 781002:during Routine Surveillance Test, HPCI Isolation Temp Switch Model 17023-6 Failed to Trip,Due to Loose Wire Inside Switch.Redundant Switches Tested Satisfatorily | /03L-0 on 781002:during Routine Surveillance Test, HPCI Isolation Temp Switch Model 17023-6 Failed to Trip,Due to Loose Wire Inside Switch.Redundant Switches Tested Satisfatorily | | | 05000263/LER-1978-020-03, /03L-0 on 781121:during Normal Pwr Increase,Both Indicating Lights for MO-2014,LPCI a Loop Admission Valve Were Out Due to Blown Control Pwr Fuse.Fuse Had Opened on Slight Over Load for Extended Time Period & Was Replaced | /03L-0 on 781121:during Normal Pwr Increase,Both Indicating Lights for MO-2014,LPCI a Loop Admission Valve Were Out Due to Blown Control Pwr Fuse.Fuse Had Opened on Slight Over Load for Extended Time Period & Was Replaced | | | 05000263/LER-1978-020, Forwards LER 78-020/03L-0 | Forwards LER 78-020/03L-0 | | | 05000263/LER-1978-021-03, /03L-0 on 781114:during Refueling Outage While Testing RHR SW Sys,A Pinhole Leak Was Discovered in CV-1729, RHR SW Differential Pressure Control Valve.Caused by Corrosion & Erosion of Upper Valve Body | /03L-0 on 781114:during Refueling Outage While Testing RHR SW Sys,A Pinhole Leak Was Discovered in CV-1729, RHR SW Differential Pressure Control Valve.Caused by Corrosion & Erosion of Upper Valve Body | | | 05000263/LER-1978-021, Forwards LER 78-021/03L-0 | Forwards LER 78-021/03L-0 | | | 05000263/LER-1978-022, Forwards LER 78-022/03L-0 | Forwards LER 78-022/03L-0 | | | 05000263/LER-1978-022-03, /03L-0 on 781117:steam Leak Was Discovered in a 1 Wye Strainer,YS-4002,on the Main Steam Equalizer Drain Line. Leak Caused by a Defective Casting & Dev After Two Days of Svc | /03L-0 on 781117:steam Leak Was Discovered in a 1 Wye Strainer,YS-4002,on the Main Steam Equalizer Drain Line. Leak Caused by a Defective Casting & Dev After Two Days of Svc | | | 05000263/LER-1978-027, Forwards LER 78-027/03L-0 | Forwards LER 78-027/03L-0 | | | 05000263/LER-1978-027-03, /03L-0 on 781121:during Normal Oper a Steam Leak Was Found in Tee Downstream of MO-1197 on the 2 HP Turbine U Bend Drain Line to Condenser,Probably Due to Flow of Steam & Water from Restricting Orifice Into Tee | /03L-0 on 781121:during Normal Oper a Steam Leak Was Found in Tee Downstream of MO-1197 on the 2 HP Turbine U Bend Drain Line to Condenser,Probably Due to Flow of Steam & Water from Restricting Orifice Into Tee | | | 05000263/LER-1978-028, Forwards LER 78-028/03L-0 | Forwards LER 78-028/03L-0 | | | 05000263/LER-1978-028-03, /03L-0 on 781124:during Normal Oper,Small Steam Leak Was Discovered in Weld of 45 Degree Elbow on HPCI Steam Supply Line 1 Inch Drain Line to Main Condenser Due to Corrrosion.Weld Repair Made at Leak.Awaiting Parts | /03L-0 on 781124:during Normal Oper,Small Steam Leak Was Discovered in Weld of 45 Degree Elbow on HPCI Steam Supply Line 1 Inch Drain Line to Main Condenser Due to Corrrosion.Weld Repair Made at Leak.Awaiting Parts | | | 05000263/LER-1978-029-01, /01T-0 on 781214:High Pressure Instrument Channel Relay Failed to Energize Due to Disengaged Agastat CR0095 Relay Socket Contact That Failed to Make Contact W/Agastat FPB750 Relay Contact.Contacts Were Reengaged | /01T-0 on 781214:High Pressure Instrument Channel Relay Failed to Energize Due to Disengaged Agastat CR0095 Relay Socket Contact That Failed to Make Contact W/Agastat FPB750 Relay Contact.Contacts Were Reengaged | | | 05000263/LER-1978-029, Forwards LER 78-029/01T-0 | Forwards LER 78-029/01T-0 | | | 05000263/LER-1978-030-01, X on 781218:found That MO-2-54A, Recirculation Loop 11 Discharge Bypass Valve Would Not Close.Cause of Failure Not Yet Determined | X on 781218:found That MO-2-54A, Recirculation Loop 11 Discharge Bypass Valve Would Not Close.Cause of Failure Not Yet Determined | | | 05000263/LER-1978-030, Forwards Revised LER 78-030/01X-1 to Correct Typographical Error in Valve Identification Number | Forwards Revised LER 78-030/01X-1 to Correct Typographical Error in Valve Identification Number | |
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