ML20028E813

From kanterella
Jump to navigation Jump to search
LER 82-107/03L-0:on 821227,steam Generator 3 Stop Dump Valve MRV-231 Removed from Svc.Caused by Need to Repair Seat Leakage.Valve Stem,Stem Pin Plug,Seat & Cage Replaced
ML20028E813
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 01/21/1983
From: Wizner D
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20028E803 List:
References
LER-82-107-03L-01, LER-82-107-3L-1, NUDOCS 8301280215
Download: ML20028E813 (1)


Text

NRC#CRM 364 iM7)

  • U. S. NUCLEAR REGULATORY COMMIS$lCN

- o LICENSEE EVENT REPORT ccNTRet stocx: l 1 l I I I i 6 l@ acLsAsE PRINT OR TYPE ALL REQUIRED INFORMATiON) j o l t l l M l UCEN3tECOCE 7 + 3 I l D l C l C l141 J@l 0101 - l 010 l 0 l 010 l - l 0 l 0;5 l@l 4111 11 11 1(@l

'5 l

[@

UCEN3E N6MGER 26 LICENSE Tvet 40 57 CA T S4 OCN'T 13!51

' Z?,"c'60I L @l 01510101013 ) 1151@l 11212171812 @l o f 112 l1 la 13 l@ l 8

el OQcd ET NLMgga 64 69 EVENT QATE I4 75 REPORTArt 50 EVENT OESCRIPT1CN AND PRCBA8LE CONSEQUENCES O'o lo#2l f DURING NORMAL OPERATION, N0. 3 S/G STOP VALVE DUMP VALVE, MRV-231, WAS REMOVED FR

, e ,3 ; i SERVICE TO REPAIR SEAT LEAKAGE. THIS CONDITION PLACED N0. 3 STEAM GENERATOR STOP l

t0i4i l VALVE IN A LESS CONSERVATIVE CONFIGURATION THAN REQUIRED BY T.S. 3.7.1.5. THE I l3 is; i REDUNDANT VALVE REMAINED OPERABLE. ACTION REQUIREMENTS WERE MET. PUBLIC HEALTH I ia is i l AND SAFETY WERE NOT AFFECTED. SIMILAR OCCURRENCES: R0's82-085, 82-017 AND FOR I i c ! 71 l DOCKET 050-316;81-068, 81-069,81-070 AND 82-038. I i24i l i

  • c$c'e* #!!$l su"N$$s councusNTcoce s sSE"ce c l3: 2j 7 6

[ H j B [@ l E l@ l B l@ [ V l A l L l V l E l X l@ tYe"'c'slP l@ [D 9 10 11 12 13 18 13 20

~

EVENT YE AR RE Ar O CCE

@ g(ge oc

,,.)

l8 l2 l l_l l 1 l o j 7J jfl l 0l 3[ l Ll l__-j l8 l 22 23 24 ;6 27 til 29 ;J 31 32 K ?I IchfcN C # Nr V H lAfgl34 33 Zjg gg OS lEZl@ l 0l kA*0l 0l40 36 il 5

el t

[N lg PCR 8. 5 Petit l Njg lAl@ lFl1l2l7lg 42 VA UFAC RER 43 44 47 CAuSE cEsCRipTicN ANo ecRREcrivE ACricNS g iall THE VALVE WAS RtM0VED FROM SERVICE TO REPAIR SEAT LEAKAGE. THE VALVE STEM, STEM l I1 ,i1i PIN, PLUG, SEAT AND CAGE WERE REPLACED IN THE FISHER STYLE 657 EAS VALVE AND THE I

i i , i fi 1 VALVE WAS RETURNED TO SERVICE IN 3 HOURS AND 34 MINUTES. SEAT LEAKAGE IN VALVES IN I li iil l THIS TYPE OF SERVICE IS NOT TOTALLY PREVENTABLE. NO FURTHER ACTION IS PLANNED. I tue!I I C

's E ucwsR erssasrArus @ N oM N eiscoveny assenierics @

lii*l

' lE l @ l0 l8 l0 [@ l" NA l lAl@l OPERATOR OBSERVATION [

4!:,vir, ce'RTest " 8

.auun tec2ric~ c, Ritus @

l l i i s i I Z [ d. , musl Z!@lNA iuounr e, Acmirv @ J[ NA  !

. esc ~,2 u.:s Ls 3 stueEn W'E li171l01010l@l 4@lOEsCRIPr1CN

@ NA l

>sRsoNNeU:~,u' des **

Nuvu = ces:RiaTics@

l' t a 'l LQ 1010 i@!

NA I ce : '

o s4ctury g t

t Ir;9l1ZI@Vl

~

NA l

' ', 8301280215 830121

' actu$. y m<; PDR ADOCK 05000315

sy.e:  : Esc w icu S PDR NRC usE CNLY .

12 i e t ( N !@l NA I Iii!ifIII! IIil 7 3 s to 53 59 80 3 NAMF CF P9EFARER DAVID G. WIZNER pycy,; 616-465-5901 2 2