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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO
MONTHYEARML20028H3861990-12-26026 December 1990 Ro:On 901126,fuel Oil Leak Discovered in Standby Diesel Generator 23 During Standby Diesel Generator Actuation Test. Caused by Crack Across Threaded Portion of Delivery Valve Holder.Valve Holder & Valve Spring Replaced ML20042E6561990-04-18018 April 1990 Final Special Rept:On 891128,diesel Generator Valid Failure Occurred.Caused by Presence of Improperly Drilled & Repaired Oil Passage Hole Serving Articulated Rod Pin Bushing in Master Connecting Rod Assembly.Crankshift Webs Repaired ML20012F1271990-03-29029 March 1990 Supplemental Special Rept:Correcting Design Description of Jacket Water Temp Switch,Per Two Nonvalid Failures of Standby Diesel Generator on 880813 & 26.Design Affects Extent of Corrective Action Taken to Prevent Recurrence ML20012E1881990-03-19019 March 1990 Special Rept:On 891227 & 900116,pressurizer Level Channel L-0466 Read Approx 10% Higher than Three Other Channels. Caused by Failure of Kerotest Valve to Fully Open,Preventing Steam from Entering Ref Leg.Ref Leg Filled ML20012C2631990-03-0909 March 1990 Special Rept:On 900209,standby Diesel Generator 11 Failed. Caused by Carbonization of 3UP Relay Socket & Base Due to Short Circuit During Tightening of Lug.Relay Socket & Base Cleaned & Diesel Successfully Tested ML20012B7361990-03-0505 March 1990 Special Rept:On 900202,discovered That Overspeed Fuel Shutoff & Governor Lever Valve Tripped.Caused by Operator Leaving Valve in Tripped Position While Performing Maint Activity on 900201.Valve Reset & Tested ML20005E1881989-12-27027 December 1989 Special Rept:On 891128,valid Failure of Diesel Generator Occurred.Caused by Improperly Drilled Oil Passage on Master Rod.Remedial Actions to Restore Standby Diesel Generator 22 Includes Crankshaft Straightening & Remachining ML19354D7401989-12-21021 December 1989 Special Rept:On 891121,generator Voltage Regulator Transformer in Standby Diesel Generator 22 Local Control Panel Overheated.Caused by Missing Insulation Between Transformer Core & Mounting Bolt.Transformer to Be Replaced ML20011D2301989-12-0606 December 1989 Special Rept:On 891029 & 1104,Train C of Reactor Vessel Water Level Sys Observed Alternating Indicating Wet & Dry Conditions in Display Processing Sys in Control Room.Caused by Failure of Fiber Optic Link.Fiber Optic Modum Replaced ML19332E8391989-12-0404 December 1989 Special Rept:On 891103,test Declared Valid Failure When Standby Diesel Generator 22 Attained Output Frequency of 58 Hertz.Caused by Oxidation of Relay 4EX3 in Governor Control Circuit.Contacts Cleaned & Burnished ML19325D7011989-10-19019 October 1989 Special Rept:On 890919,nonvalid Failure of Standby Diesel Generator Occurred.Caused by Failure of Reactor Operator to Read Correct Instrument Prior to Synchronization of Diesel Generator.Synchronization Procedure Revised ML19320A7911980-06-26026 June 1980 Ro:On 800529,during Design Review,Seismic Qualification of Essential Cooling Water Intake Structure Gantry Crane & Diesel Generator Fuel Storage Tank Found W/Deficient Response Spectra Values.New Seismic Evaluation in Progress 1990-04-18
[Table view] Category:LER)
MONTHYEARML20028H3861990-12-26026 December 1990 Ro:On 901126,fuel Oil Leak Discovered in Standby Diesel Generator 23 During Standby Diesel Generator Actuation Test. Caused by Crack Across Threaded Portion of Delivery Valve Holder.Valve Holder & Valve Spring Replaced ML20042E6561990-04-18018 April 1990 Final Special Rept:On 891128,diesel Generator Valid Failure Occurred.Caused by Presence of Improperly Drilled & Repaired Oil Passage Hole Serving Articulated Rod Pin Bushing in Master Connecting Rod Assembly.Crankshift Webs Repaired ML20012F1271990-03-29029 March 1990 Supplemental Special Rept:Correcting Design Description of Jacket Water Temp Switch,Per Two Nonvalid Failures of Standby Diesel Generator on 880813 & 26.Design Affects Extent of Corrective Action Taken to Prevent Recurrence ML20012E1881990-03-19019 March 1990 Special Rept:On 891227 & 900116,pressurizer Level Channel L-0466 Read Approx 10% Higher than Three Other Channels. Caused by Failure of Kerotest Valve to Fully Open,Preventing Steam from Entering Ref Leg.Ref Leg Filled ML20012C2631990-03-0909 March 1990 Special Rept:On 900209,standby Diesel Generator 11 Failed. Caused by Carbonization of 3UP Relay Socket & Base Due to Short Circuit During Tightening of Lug.Relay Socket & Base Cleaned & Diesel Successfully Tested ML20012B7361990-03-0505 March 1990 Special Rept:On 900202,discovered That Overspeed Fuel Shutoff & Governor Lever Valve Tripped.Caused by Operator Leaving Valve in Tripped Position While Performing Maint Activity on 900201.Valve Reset & Tested ML20005E1881989-12-27027 December 1989 Special Rept:On 891128,valid Failure of Diesel Generator Occurred.Caused by Improperly Drilled Oil Passage on Master Rod.Remedial Actions to Restore Standby Diesel Generator 22 Includes Crankshaft Straightening & Remachining ML19354D7401989-12-21021 December 1989 Special Rept:On 891121,generator Voltage Regulator Transformer in Standby Diesel Generator 22 Local Control Panel Overheated.Caused by Missing Insulation Between Transformer Core & Mounting Bolt.Transformer to Be Replaced ML20011D2301989-12-0606 December 1989 Special Rept:On 891029 & 1104,Train C of Reactor Vessel Water Level Sys Observed Alternating Indicating Wet & Dry Conditions in Display Processing Sys in Control Room.Caused by Failure of Fiber Optic Link.Fiber Optic Modum Replaced ML19332E8391989-12-0404 December 1989 Special Rept:On 891103,test Declared Valid Failure When Standby Diesel Generator 22 Attained Output Frequency of 58 Hertz.Caused by Oxidation of Relay 4EX3 in Governor Control Circuit.Contacts Cleaned & Burnished ML19325D7011989-10-19019 October 1989 Special Rept:On 890919,nonvalid Failure of Standby Diesel Generator Occurred.Caused by Failure of Reactor Operator to Read Correct Instrument Prior to Synchronization of Diesel Generator.Synchronization Procedure Revised ML19320A7911980-06-26026 June 1980 Ro:On 800529,during Design Review,Seismic Qualification of Essential Cooling Water Intake Structure Gantry Crane & Diesel Generator Fuel Storage Tank Found W/Deficient Response Spectra Values.New Seismic Evaluation in Progress 1990-04-18
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217K9441999-10-15015 October 1999 SER Accepting Util Alternative Proposed Relief Request RR-ENG-2-4 for Second 10-year ISI Interval at Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) ML20217K9151999-10-15015 October 1999 SER Authorizing Util Relief Request RR-ENG-2-3 for Second 10-year ISI Interval of Stp,Units 1 & 2 Pursuant to 10CFR50.55a(a)(3)(i) NOC-AE-000676, Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for South Texas Project,Units 1 & 2.With ML20217D0531999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 2 Cycle 7 Colr ML20217D0481999-09-30030 September 1999 Rev 1 to STP Electric Generating Station Unit 1 Cycle 9 Colr ML20211P8411999-09-0909 September 1999 Safety Evaluation Supporting Alternative Proposed by Licensee to Surface Exam to Perform Boroscopic VT-1 Visual Exam of Pump Casing Welds within Pump Pits for Welds Covered by Relief Request RR-ENG-24 ML20211P7811999-09-0909 September 1999 SER Approving Second 10-year Interval Inservice Insp Program Plan Relief Request RR-ENG-2-8 (to Use Code Case N-491-2) for South Texas Project,Units 1 & 2 ML20211Q6731999-09-0909 September 1999 Safety Evaluation Accepting First 10-yr Interval ISI Program Plan Request for Relief from ASME Code Case N-498 NOC-AE-000643, Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for South Texas Project,Units 1 & 2.With ML20212E5191999-08-31031 August 1999 Rev 3 to SG-99-04-005, STP 1RE08 Outage Condition Monitoring Rept & Final Operational Assessment ML20211F4531999-08-24024 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative to Defer Partial First Period Exams of flange-to-shell Weld to Third Period & Perform Required Ultrasonic Exams,Both Manual & Automated,During Third Period ML20211F5111999-08-23023 August 1999 Safety Evaluation Supporting Licensee Proposed Alternative Contained in Request for Relief RR-ENG-30 ML20210C9411999-07-31031 July 1999 Rev 1 to SG-99-07-002, South Tx,Unit 1 Cycle 9 Voltage- Based Repair Criteria 90-Day Rept, Jul 1999 ML20210R3631999-07-31031 July 1999 Monthly Operating Repts for July 1999 for South Tx Project, Units 1 & 2.With ML20210D9161999-07-23023 July 1999 Safety Evaluation Accepting Inservice Testing Relief Request RR-56 Re Component Cooling Water & Safety Injection Sys Containment Isolation Check Valve Closure Test Frequency ML20210D4821999-07-21021 July 1999 1RE08 ISI Summary Rept for Steam Generator Tubing of South Texas Project Electric Generating Station Unit 1 ML20210D4491999-07-21021 July 1999 Revised Chapters to Operations QA Plan, Including Rev 9 to Chapter 1.0, Organization & Rev 6 to Chapter 16.0, Independent Technical Review NOC-AE-000583, LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With1999-07-15015 July 1999 LER 99-S03-00:on 990619,failure to Revitalize Sdg Number 11 Was Noted.Caused by Failure to Communicate Status of Sdg. Subject Sdg Revitalized on 990619 & Licensee Will Develop Security Force Instruction Re Sdgs.With ML20207H6361999-07-0808 July 1999 Safety Evaluation Approving 2nd 10 Yr Interval ISI Program Plan Request to Use ASME Section XI Code Case N-546 for Licenses NPF-76 & NPF-80,respectively ML20216D7481999-07-0707 July 1999 1RE08 ISI Summary Rept for Welds & Component Supports of STP Electric Generating Station,Unit 1 NOC-AE-000593, Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Stp,Units 1 & 2. with NOC-AE-000570, LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With1999-06-28028 June 1999 LER 99-S01-00:on 990527,discovered That Unescorted Access Had Been Inappropriately Granted.Caused by Failure to Follow Procedure.Util Verified That Individual Did Not Have Current Unescorted Access at STP or Any Other Util.With ML20196G5821999-06-23023 June 1999 LER 99-S02-00:on 990601,failure to Maintain Positive Control of Vital Area Security Key Was Noted.Caused by Lack of Attention to Detail.Discussed Event with Operator Involved IAW Constructive Discipline Program ML20195J6871999-06-17017 June 1999 Safety Evaluation Supporting Proposed Alternative Contained in RR-ENG-2-5.Proposed Alternative Authorized Per 10CFR50.55a(a)(3)(i) for 2nd ISI Interval ML20196A2391999-06-15015 June 1999 Change QA-042 to Rev 13 of Operations QAP, Reflecting Current Organizational Alignment for South Texas Project & Culminating Organizational Realigment That Has Been Taking Place During Past Several Months NOC-AE-000563, Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Stp,Units 1 & 2. with ML20206U5411999-05-18018 May 1999 Non-proprietary Errata Pages for Rev 2,Addendum 1 to WCAP-13699, Laser Welded Sleeves for 3/4 Inch Diamete Tube Feedring Type & W Preheater SGs Generic Sleeving Rept ML20206A7721999-04-30030 April 1999 STP Electric Generating Station Unit 1 Cycle 9 Colr NOC-AE-000543, Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Stp,Units 1 & 2. with ML20205H0321999-03-31031 March 1999 Change QA-040 to Rev 13 of Operations QA Plan NOC-AE-000507, Monthly Operating Repts for Mar 1999 for Stp,Units 1 & 2. with1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Stp,Units 1 & 2. with ML20205A3781999-03-22022 March 1999 STP Electric Generating Station Simulator Certification Four Yr Rept for Units 1 & 2 ML20204B2711999-03-15015 March 1999 Safety Evaluation Authorizing 990201 Request to Authorize Alternative to Regulations Per 10CFR50.55a(a)(3)(i) That Would Revise Start of Second 120-month IST Interval to No Later than 011201 ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results NOC-AE-000468, Monthly Operating Repts for Feb 1999 for South Texas Project Electric Generating Station.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for South Texas Project Electric Generating Station.With ML20207D1101999-02-24024 February 1999 Change QA-039 to Rev 13 of Operations QA Plan, for STP ML20203H8361999-02-17017 February 1999 Safety Evaluation Supporting Request for Relief from ASME Code Requirements for Class 3 Piping for Plant ML20202H9621999-02-0303 February 1999 SER Accepting Change to EALs Used in Classification of Emergency Conditions ML20202E8471999-01-31031 January 1999 2RE06 ISI Summary Rept for SG Tubing of STP Electric Generating Station,Unit 2 ML20216G2011999-01-31031 January 1999 City Public Svc of San Antonio Annual Rept 1998-1999 ML20199G5961999-01-31031 January 1999 Cycle 7 Voltage-Based Repair Criteria Rept for Jan 1999 ML20199K7711999-01-21021 January 1999 Safety Evaluation Accepting ISI Program Request for Relief for ASME Cose Repair Requirements for Code Class 3 Piping ML20199G8161999-01-19019 January 1999 SER Accepting Util 970707 Response to NRC 970509 RAI Re GL 92-08, Thermo-Lag 330-1 Fire Barriers. NRC Finds No Significant Safety Hazards Based on Application of Util Ampacity Derating Methodology ML20199H4981999-01-11011 January 1999 2RE06 ISI Summary Rept for Welds & Component Supports of Stp,Unit 2 ML20206Q3751999-01-0404 January 1999 2RE06 ISI Summary Rept for Sys Pressure Tests (Class 1 & 2) ML20206Q3721999-01-0404 January 1999 2RE06 ISI Summary Rept for Repairs & Replacements ML20216G2171998-12-31031 December 1998 Houston Industries 1998 Annual Rept. App a 1998 Financial Statements & Us Securities & Exchange Commission Form 10-K Encl NOC-AE-000403, Monthly Operating Repts for Dec 1998 for South Texas Project Unit 1 & 2.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for South Texas Project Unit 1 & 2.With ML20216G1521998-12-31031 December 1998 Central & South West Corp 1998 Summary Annual Rept & Securities & Exchange Commission Form 10-K ML20198M3431998-12-28028 December 1998 SER Accepting Util Request for Relief from ASME Code Repair Requirements for ASME Code Class 3 Piping for South Texas Project,Unit 2 1999-09-09
[Table view] |
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The Light i company .--,,---.- --(
P.O. Box 1700 Houston Texas 77001 713 228 9211 Houston Lighting & Power _ _ --- ~~ -- -- .m. -~)~- -
December. 27,-1989 'I ST-HL-AE-3326 File No.: G02 'l 10CFR50 .J U. S. Nuclear Regulatory Commission .
Attention: Document Control Desk Washington, DC 20555
.v-South Texas Project Electric Generating Station Unit 2 Docket No. STN 50-499 Interim Special Report Regarding A Diesel Generator Valid Failure on November 28. 1989 Pursuant to the South Texas Project Electric Generating Station Technical Specifications 4.8,1,1.3 and 6.9.2, Houston Lighting & Power submits the attached Interim Special Report regarding a diesel generator valid failure which occurred on November 28, 1989.
If you should have any questions on this matter, please contact Mr. C. A..Ayala at (512) 972-8628 or myself at (512) 972-7921.
s'
. . Vaugh Vice President Nuclear Operatio s GEV/BEM/n1
Attachment:
Interim Special Report Regarding a Diesel Generator Valid Failure on November 28, 1989 9001040040 891227 // k
,PDR .ADOCK 05000499 S PDC
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$/*E' ST HLoAE 3326 Houston Lighting & Power Company File No.: C02 South Texas Project Electric Generating Station -Page 2
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Regional Administrator, Region IV -Rufus-S. Scott Nuclear Regulatory Commission Associate General Counsel ,
611 Ryan Plaza Drive, Suite 1000 Houston Lighting & Power Comparty Arlington, TX 76011 P. O. Box 61867 i Houston, TX 77208 George Dick, Project Manager U.S. Nuclear Regulatory Commission INPO Washington, DC 20555 Records Center l
.1100 Circle 75 Parkway '
J..I. Tapia Atlanta, CA 30339-3064 l Senior Resident Inspector I c/o U. S. Nuclear Regulatory Dr. Joseph M. Hendrie l Commission 50 Be11 port Lane P. O. Box 910 Be11 port, NY 11713 Bay City, TX 77414 D. K. Lacker J. R. Newman, Esquire Bureau of Radiation Control Newman & Holtzinger, P.C. Texas Department of Health 1615 L Street, N.W. 1100 West 49th Street Washington, DC 20036 Austin, TX 78704 D. E. Ward /R. P.-Verret Central Power & Light Company P. O. Box 2121-Corpus Christi, TX 78403 I J. C. Lanier Director of Generation l City of Austin Electric Utility L
721 Barton Springs Road I Austin, TX 78704 ,
R.,J. Costello/M T. Hardt City Public Service Board P. O. Box 1771 San Antonio, TX 78296 Revised 12/15/89 L4/NRC/
y, tj i? li .g Attachment ST-HL AE-3326 Page 1 of 3 -i South Texas Project Electric Generating Station Unit 2 Docket No. STN 50-499 Int'erim Special Report Regarding A Diesel Generator Valid Failure On November 28. 1989 Description of Event:
On November 28, 1989 Unit 2 was in Mode 5 for a maintsnance outage. The Technical Specification required twenty-four hour load test was being performed on Standby Diesel Generator (SDG) 22. At 0957 hours0.0111 days <br />0.266 hours <br />0.00158 weeks <br />3.641385e-4 months <br />, approximately ten hours into the test, a loud knocking noise was heard by two maintenance technicians. The technicians immediately evacuated the area. The #4 master connecting rod subsequently failed and the engine tripped. No indication of
-the trip was received by the control room. Immediate inspection of SDG 22 revealed that the #4 articulated rod, both #4 pistons and other debris had been ejected through the right centerframe door. The #4 crankcase overpressure relief valves.were pushed off the centerframe doors on both sides of the engine and the right sido centerframe door was driven into the adjacent starting air dryer. The master rod, cap and counterweights were in the engine base.
Investigation and recovery teams were formed to evaluate the failure and implement corrective actions. A. thorough inspection of the engine was performed. The following was observed:
The master connecting rod was broken into two pieces through the oil passage between the crankpin bore and the articulated rod pin bore and through the upper end of the balls.
The left side connecting rod cap bolts were broken and the right side bolts bent.
-~ ' -
All four cap nuts had been stripped from the studs.
- There was evidence of significant heating of the articulated rod pin, its bushing, and the rod on both the bail and load sides of the articulated pin.
The centerframe sustained minor damage including several cracks and l~ impact damage.
- The #4 crankpin was gouged at several locations The crankshaft runout was 0.003"
- There were numerous superficial gouges on the crankwebs and crankpin thrust faces.
- The piston pins had slight impact damage.
The inlet valves were slightly bent on both heads, the rocker arms were cracked and the push rods were bent.
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A1/048.N10
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Attachment ST-HL-AE 3326 Page 2 of 3 Cause of Event:
The master rod was subjected to both macroscopic and scanning electron microscope examination. It was determined that a fatigue failure was initiated at an improperly drilled oil passage on the master rod (see Figures I and 2). In an attempt to repair the improperly drilled passage, the vendor ;
threaded and plugged it (see Figure 3. Case A) which left stress risers sufficient to form a fatigue crack initiation site. The cracking proceeded by high cycle fatigue to the transverse oil passage followed by failure of the rod balls and cap studs. Loss of lubrication to the articulated rod pin or l ingested debris caused overheating of the pin, bushing, connecting rod bore and connecting rod bails in the final stages of the fatigue failure. l Cooper Energy Services has identified that the repair of the master ;
connecting rod which failed was documented and dispositioned in accordance i with Cooper Energy Services procedures at the time of manufacture. This was the only master rod repaired in this manner. Laboratory analysis of the material composition and mechanical properties of the failed connecting rod j indicated that it met specification requirements.
l Other master connecting rods were inspected which exhibited similar, I though less severe, manufacturing defects (see Figure 3, Cases B and C) .
Therefore, it can be concluded that a less than adequate manufacturing process was in effect at Cooper Energy Services at the time of fabrication of the #4 l connecting rod. In this case, it is clear that an inappropriate repair !
disposition was approved by Cooper Energy Services engineering on the #4 master connecting rod. As licensee, HL&P was responsible for ensuring that i the vendor's quality program was properly implemented. An evaluation of the i HL&P vendor control program in effect at the time of SDG manufacture is being conducted to assure that any potential programmatic weaknesses have been !
identified and resolved to ensure that our present program is effective. This evaluation will be discussed in the final report of this valid failure, j Corrective Action:
)
Remedial actions are in progress to restore SDG 22 to operability.
These activities include:
1 Crankshaft straightening to within the specified runout of .002".
- Remachining of the crankshaf t rod journal Repair of the engine centerframe Repair of support equipment and instrumentation Reassembly and testing The current scheduled date for completion of these activities and return of SDG 22 to service is January 2,1990.
e A1/048.N10 J
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Attachment ST HL-AE 3326 ;
Page 3 of 3 Corrective Action Cont'd.
In order to determine if other incorrectly drilled or repaired connecting rods had been supplied, HL&P inspected two spare master rods. The-oil passage on one had been drilled all the way through and chamfered. The oil passage on the other rod had been drilled past the transverse oil passage.
These configurations are illustrated in Figure 3, Cases B and C, respectively.
Oil passages in the remaining master rods on SDG 22 were subsequently measured. Most were found to be partially drilled as shown in Figure 3, Case C. One was not overdrilled. None had been drilled through and repaired.
An evaluation of the as-found condition was performed to justify continued operation of Unit 1 and to justify restart of Unit 2 once repairs to SDG 22 are complete. Based on the unique nature of the rod failure, a qualitative analysis of operational data and industry experience, interim operation has been justified. Outside consultants are currently performing a finite element analysis of the effect of overdrilled oil passages on master rod integrity. This analysis will be used to confirm that safe operation of the SDC's may continue indefinitely.
Upon completion of the recovery effort and recurn of SDG 22 to operation, a final special report will be issued detailing the remaining corrective actions. This report is currently scheduled to be completed by March 15, 1990.
Additional Information:
Per the criteria of Regulation Guide 1.108, the failure described in this report has been classified as a valid failure. This is the third valid failure in the last twenty starts. The test interval is currently once per seven days due to the second valid failure which occurred on November 21, 1989. Due to the extensive rework associated with the failure described in this report, HL&P plans to secure certification that SDG 22 has been restored to like-new condition. If this certification is obtained, the test interval will be changed to once per thirty-one days.
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