Semantic search

Jump to navigation Jump to search
 Issue dateTitleTopic
ML20028H38626 December 1990Ro:On 901126,fuel Oil Leak Discovered in Standby Diesel Generator 23 During Standby Diesel Generator Actuation Test. Caused by Crack Across Threaded Portion of Delivery Valve Holder.Valve Holder & Valve Spring Replaced
ML20042E65618 April 1990Final Special Rept:On 891128,diesel Generator Valid Failure Occurred.Caused by Presence of Improperly Drilled & Repaired Oil Passage Hole Serving Articulated Rod Pin Bushing in Master Connecting Rod Assembly.Crankshift Webs RepairedFinite Element Analysis
ML20012F12729 March 1990Supplemental Special Rept:Correcting Design Description of Jacket Water Temp Switch,Per Two Nonvalid Failures of Standby Diesel Generator on 880813 & 26.Design Affects Extent of Corrective Action Taken to Prevent Recurrence
ML20012E18819 March 1990Special Rept:On 891227 & 900116,pressurizer Level Channel L-0466 Read Approx 10% Higher than Three Other Channels. Caused by Failure of Kerotest Valve to Fully Open,Preventing Steam from Entering Ref Leg.Ref Leg Filled
ML20012C2639 March 1990Special Rept:On 900209,standby Diesel Generator 11 Failed. Caused by Carbonization of 3UP Relay Socket & Base Due to Short Circuit During Tightening of Lug.Relay Socket & Base Cleaned & Diesel Successfully Tested
ML20012B7365 March 1990Special Rept:On 900202,discovered That Overspeed Fuel Shutoff & Governor Lever Valve Tripped.Caused by Operator Leaving Valve in Tripped Position While Performing Maint Activity on 900201.Valve Reset & Tested
ML20005E18827 December 1989Special Rept:On 891128,valid Failure of Diesel Generator Occurred.Caused by Improperly Drilled Oil Passage on Master Rod.Remedial Actions to Restore Standby Diesel Generator 22 Includes Crankshaft Straightening & RemachiningFinite Element Analysis
ML19354D74021 December 1989Special Rept:On 891121,generator Voltage Regulator Transformer in Standby Diesel Generator 22 Local Control Panel Overheated.Caused by Missing Insulation Between Transformer Core & Mounting Bolt.Transformer to Be Replaced
ML20011D2306 December 1989Special Rept:On 891029 & 1104,Train C of Reactor Vessel Water Level Sys Observed Alternating Indicating Wet & Dry Conditions in Display Processing Sys in Control Room.Caused by Failure of Fiber Optic Link.Fiber Optic Modum ReplacedReactor Vessel Water Level
ML19332E8394 December 1989Special Rept:On 891103,test Declared Valid Failure When Standby Diesel Generator 22 Attained Output Frequency of 58 Hertz.Caused by Oxidation of Relay 4EX3 in Governor Control Circuit.Contacts Cleaned & Burnished
ML19325D70119 October 1989Special Rept:On 890919,nonvalid Failure of Standby Diesel Generator Occurred.Caused by Failure of Reactor Operator to Read Correct Instrument Prior to Synchronization of Diesel Generator.Synchronization Procedure Revised
ML19320A79126 June 1980Ro:On 800529,during Design Review,Seismic Qualification of Essential Cooling Water Intake Structure Gantry Crane & Diesel Generator Fuel Storage Tank Found W/Deficient Response Spectra Values.New Seismic Evaluation in ProgressSafe Shutdown Earthquake
Operating Basis Earthquake