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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML20045B3551993-06-11011 June 1993 LER 93-001-00:on 930429,refueling Jib Crane Moved in Vicinity of Spent Fuel Pool Using vendor-supplied Lifting Eye in Violation of NUREG-0612.Caused by Failure to Identify Crane as Heavy Load.Meetings held.W/930611 Ltr ML20024G7171991-04-22022 April 1991 LER 91-001-00:on 910324,RB Normal Ventilation Sys (Rbnvs) Outboard Exhaust Valve Closed for No Apparent Reason.Cause Inconclusive.Sys Restored to Normal Lineup & Rbnvs Outboard Valve Will Be Stroked on Routine basis.W/910422 Ltr ML20028H0231990-09-28028 September 1990 LER 90-007-00:on 900907,unplanned Actuation of ESF Sys Occurred During I&C Surveillance Test.Caused by Inadequate procedure.SP44.650.16 Revised to Require That Leads Lifted & Individually separated.W/900928 Ltr ML20012C5131990-03-16016 March 1990 LER 86-029-02:on 860718,19,21 & 870508,loss of Reactor Protection Sys Power Occurred Due to Spurious Tripping of Alternate Feed EPA Breakers.Caused by Low Output Voltage of Alternate Feed Transformer.Output adjusted.W/900316 Ltr ML20006E1571990-02-0909 February 1990 LER 90-001-00:on 900117,unplanned Actuation of ESF Reactor Bldg Standby Ventilation Sys B Occurred,Causing Interlocking Relays in Control Circuits to Deenergize.Caused by Transient Voltage Dip.Procedures Re Bus Loads modified.W/900209 Ltr ML19354D8331990-01-12012 January 1990 LER 89-011-00:on 891222,unplanned Actuation of ESF Primary Containment Isolation Sys Occurred When Performing Sys Layup Implementation Package for Hpci.Caused by Inadequate Procedure.Breaker Positions changed.W/900112 Ltr ML20005F8641990-01-11011 January 1990 LER 89-010-00:on 891212,unplanned Actuation of ESF Control Room Air Conditioning Train a Occurred.Caused by Removal of Leads from Relay During Test to Prevent ESF Sys Actuations. Electrical Relay Replaced & Wiring Mod made.W/900111 Ltr ML20011D2371989-12-15015 December 1989 LER 89-009-00:on 891115,notification Received of Potential Failure Mechanism of Four 3-way Solenoid Operated Pilot Valves.Caused by Incorrect Mounting of Valves.Valves Remounted Vertically & Field Walkdown done.W/891215 Ltr ML19332C5591989-11-15015 November 1989 LER 89-008-00:on 891016,control Room Alarms Received Indicating Fire Pump Had Started & Deluge Valve Had Opened. Caused by Actuation of Manual Pull Station.Deluge Sys Restored to Normal & Personnel interviewed.W/891115 Ltr 1993-06-11
[Table view] Category:RO)
MONTHYEARML20045B3551993-06-11011 June 1993 LER 93-001-00:on 930429,refueling Jib Crane Moved in Vicinity of Spent Fuel Pool Using vendor-supplied Lifting Eye in Violation of NUREG-0612.Caused by Failure to Identify Crane as Heavy Load.Meetings held.W/930611 Ltr ML20024G7171991-04-22022 April 1991 LER 91-001-00:on 910324,RB Normal Ventilation Sys (Rbnvs) Outboard Exhaust Valve Closed for No Apparent Reason.Cause Inconclusive.Sys Restored to Normal Lineup & Rbnvs Outboard Valve Will Be Stroked on Routine basis.W/910422 Ltr ML20028H0231990-09-28028 September 1990 LER 90-007-00:on 900907,unplanned Actuation of ESF Sys Occurred During I&C Surveillance Test.Caused by Inadequate procedure.SP44.650.16 Revised to Require That Leads Lifted & Individually separated.W/900928 Ltr ML20012C5131990-03-16016 March 1990 LER 86-029-02:on 860718,19,21 & 870508,loss of Reactor Protection Sys Power Occurred Due to Spurious Tripping of Alternate Feed EPA Breakers.Caused by Low Output Voltage of Alternate Feed Transformer.Output adjusted.W/900316 Ltr ML20006E1571990-02-0909 February 1990 LER 90-001-00:on 900117,unplanned Actuation of ESF Reactor Bldg Standby Ventilation Sys B Occurred,Causing Interlocking Relays in Control Circuits to Deenergize.Caused by Transient Voltage Dip.Procedures Re Bus Loads modified.W/900209 Ltr ML19354D8331990-01-12012 January 1990 LER 89-011-00:on 891222,unplanned Actuation of ESF Primary Containment Isolation Sys Occurred When Performing Sys Layup Implementation Package for Hpci.Caused by Inadequate Procedure.Breaker Positions changed.W/900112 Ltr ML20005F8641990-01-11011 January 1990 LER 89-010-00:on 891212,unplanned Actuation of ESF Control Room Air Conditioning Train a Occurred.Caused by Removal of Leads from Relay During Test to Prevent ESF Sys Actuations. Electrical Relay Replaced & Wiring Mod made.W/900111 Ltr ML20011D2371989-12-15015 December 1989 LER 89-009-00:on 891115,notification Received of Potential Failure Mechanism of Four 3-way Solenoid Operated Pilot Valves.Caused by Incorrect Mounting of Valves.Valves Remounted Vertically & Field Walkdown done.W/891215 Ltr ML19332C5591989-11-15015 November 1989 LER 89-008-00:on 891016,control Room Alarms Received Indicating Fire Pump Had Started & Deluge Valve Had Opened. Caused by Actuation of Manual Pull Station.Deluge Sys Restored to Normal & Personnel interviewed.W/891115 Ltr 1993-06-11
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20140G4481997-05-0101 May 1997 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby Diesel Generator Sys.Recommends That Springs Be Inspected on Periodic Basis,Such as During Refueling Outages ML20135D8011996-11-26026 November 1996 Part 21 Rept Re Two Safety Related Valves Supplied by Velan Valve Corp Were Not in Compliance W/Originally Supplied QA Documentation.Returned Valves to Velan in May 1996 & on 961120 Velan Advised That Valves Had Been Misplaced ML20080G4691995-01-26026 January 1995 Record of Telcon W/Nrc & Licensees 950126 to Clarify Position Re Dispositioning of Exempt Sources Listed in Section 6.3.3 of Shoreham Termination Survey Final Rept Dtd Oct 1994 ML20069F0001994-01-24024 January 1994 Vols 1-4 to Shoreham Decommissioning Project Termination Survey Final Rept ML20058K3841993-12-0909 December 1993 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby DG Sys,Regarding Potential Problem W/ Subcover Assembled Atop Power Head ML20057F2261993-09-30030 September 1993 Safety Evaluation Supporting Exemption Request from Requirements of 10CFR50.54(q) for License NPF-82 ML20056C7181993-07-14014 July 1993 SE Supporting Amend 10 to License NPF-82 ML20045B3551993-06-11011 June 1993 LER 93-001-00:on 930429,refueling Jib Crane Moved in Vicinity of Spent Fuel Pool Using vendor-supplied Lifting Eye in Violation of NUREG-0612.Caused by Failure to Identify Crane as Heavy Load.Meetings held.W/930611 Ltr ML20045C8881993-06-0808 June 1993 Vols 1 & 2 to Refueling Jib Crane 1T31-CRN-008A Incident Root Cause Analysis. W/One Oversize Encl ML20044C1181993-02-28028 February 1993 Shoreham Nuclear Power Station Updated Decommissioning Plan. ML20128P6451993-02-28028 February 1993 Snps Decommissioning Project Termination Survey Final Rept for Steam Turbine Sys (N31) ML20128P7431993-02-19019 February 1993 Rev 3 to 93X027, Nuclear QA Surveillance Rept ML20127H2301993-01-15015 January 1993 Part 21 Rept Re Potential Defeat in Component of Dsrv & Dsr Enterprise Standby DG Sys.Starting Air Distributor Housing Assemblies Installed as Replacement Parts at Listed Sites ML20126B0421992-12-17017 December 1992 Final Part 21 Rept Re Potential Problem W/Steel Cylinder Heads.Initially Reported on 921125.Caused by Inadequate Cast Wall Thickness at 3/4-inch-10 Bolt Hole.Stud at Location Indicated on Encl Sketch Should Be Removed ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20128B9641992-10-31031 October 1992 Rev 0 to Shoreham Decommissioning Project Termination Survey Plan ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in Abb Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML20099H5781992-07-31031 July 1992 Rev 4 to Shoreham Defueled Sar ML20114A6311992-07-28028 July 1992 Shoreham Decommissioning Plan ML20101K5791992-06-25025 June 1992 Long Island Power Authority Shoreham Decommissioning Project,Shoreham Nuclear Power Station,Technical Rept on Water Processing & Water Mgt Activities for Reactor Pressure Vessel & Wet Cutting Station ML20094L1271992-03-13013 March 1992 Amend 1 to Part 21 Rept 159 Re Potential Defect in Power Cylinder Liner.Initially Reported on 920115.Caused by Liner/ Block Fit & Localized Matl Microstructure.All Drawings & Specs Revised to Address Matl Design Requirements ML20082M5081991-08-26026 August 1991 Rev 3 to Shoreham Defueled Sar PM-91-125, Monthly Operating Rept for Jul 1991 for Shoreham Nuclear Power Station1991-07-31031 July 1991 Monthly Operating Rept for Jul 1991 for Shoreham Nuclear Power Station PM-91-112, Monthly Operating Rept for Jun 1991 for Shoreham Nuclear Power Station1991-06-30030 June 1991 Monthly Operating Rept for Jun 1991 for Shoreham Nuclear Power Station PM-91-075, Monthly Operating Rept for Apr 1991 for Shoreham Nuclear Power Station1991-04-30030 April 1991 Monthly Operating Rept for Apr 1991 for Shoreham Nuclear Power Station ML20024G7171991-04-22022 April 1991 LER 91-001-00:on 910324,RB Normal Ventilation Sys (Rbnvs) Outboard Exhaust Valve Closed for No Apparent Reason.Cause Inconclusive.Sys Restored to Normal Lineup & Rbnvs Outboard Valve Will Be Stroked on Routine basis.W/910422 Ltr SNRC-1806, Revised Pages 2 & 6 to Encl a of 10CFR50.59 Annual Rept for 19901991-04-15015 April 1991 Revised Pages 2 & 6 to Encl a of 10CFR50.59 Annual Rept for 1990 PM-91-058, Monthly Operating Rept for Mar 1991 for Shoreham Nuclear Power Station1991-03-31031 March 1991 Monthly Operating Rept for Mar 1991 for Shoreham Nuclear Power Station PM-91-037, Monthly Operating Rept for Feb 1991 for Shoreham Nuclear Power Station1991-02-28028 February 1991 Monthly Operating Rept for Feb 1991 for Shoreham Nuclear Power Station PM-91-016, Monthly Operating Rept for Jan 1991 for Shoreham Nuclear Power Station1991-01-31031 January 1991 Monthly Operating Rept for Jan 1991 for Shoreham Nuclear Power Station SNRC-1797, 10CFR 50.59 Annual Rept of Facility Changes,Procedure Changes,Tests & Experiments for Jan-Dec 19901990-12-31031 December 1990 10CFR 50.59 Annual Rept of Facility Changes,Procedure Changes,Tests & Experiments for Jan-Dec 1990 SNRC-1794, Shoreham Nuclear Power Station Annual Operating Rept,19901990-12-31031 December 1990 Shoreham Nuclear Power Station Annual Operating Rept,1990 SNRC-1799, Lilco 1990 Annual Rept1990-12-31031 December 1990 Lilco 1990 Annual Rept ML20069Q3901990-12-31031 December 1990 Shoreham Nuclear Power Station Decommissioning Plan. (Filed in Category P) ML20028H0231990-09-28028 September 1990 LER 90-007-00:on 900907,unplanned Actuation of ESF Sys Occurred During I&C Surveillance Test.Caused by Inadequate procedure.SP44.650.16 Revised to Require That Leads Lifted & Individually separated.W/900928 Ltr ML20056A2001990-07-31031 July 1990 Safety Evaluation Supporting Amend 6 to License NPF-82 PM-90-097, Monthly Operating Rept for June 1990 for Shoreham Nuclear Power Station1990-06-30030 June 1990 Monthly Operating Rept for June 1990 for Shoreham Nuclear Power Station ML20055E3911990-06-25025 June 1990 Safety Evaluation Supporting Amend 5 to License NPF-82 PM-90-083, Monthly Operating Rept for May 1990 for Shoreham Nuclear Power Station1990-05-31031 May 1990 Monthly Operating Rept for May 1990 for Shoreham Nuclear Power Station 05000322/LER-1987-0351990-05-16016 May 1990 LER 87-035-02:on 871221,880106 & 0330,high Energy Line Break Logic Isolations of RWCU & Main Steam Line Drain Valves Occurred.Caused by Problems W/Temp Monitoring Units. Grounding Scheme Changed & Transformers Rewired 05000322/LER-1986-0321990-05-16016 May 1990 LER 86-032-01:on 860728,RWCU Isolated on High Differential Flow Sensed by Steam Leak Detection Sys While Placing Filter Demineralizers in Operation.Cause Not Determined. Operating Procedures Revised to Monitor RWCU Sys 05000322/LER-1987-0091990-05-16016 May 1990 LER 87-009-01:on 870203,full Reactor Trip Occurred Due to Perturbation in Ref Leg.Caused by Spurious Low Level Reactor Pressure Vessel Water Level Signal.Existing Level & Pressure Transmitters Replaced W/Newer Models 05000322/LER-1989-0031990-05-16016 May 1990 LER 89-003-01:on 890310,emergency Diesel Generator (EDG) 102 Manually Shutdown During 18-month Surveillance Test Due to Failure of EDG Output Breaker.Cause Not Determined. Replacement Breaker Installed in Cubicle 102-8 05000322/LER-1985-0591990-05-16016 May 1990 LER 85-059-01:on 851219,half Reactor Trip,Full NSSS Shutoff Sys Isolation & Reactor Bldg Standby Ventilation Sys Initiation Occurred Due to Loss of Power to Reactor Protection Sys Bus B.Assembly Breaker Reset 05000322/LER-1988-0151990-05-16016 May 1990 LER 88-015-02:on 880916,seismic Monitoring Instrumentation, Including Peak Acceleration Recorders,Removed from Svc for More than 30 Days Due to Corrosion on Scratch Plates.Cover Gasket Replaced & Thermal Barrier Mount to Be Installed 05000322/LER-1988-0031990-05-16016 May 1990 LER 88-003-01:on 880322,unplanned Automatic Initiation of Reactor Bldg Standby Ventilation Sys Side a Occurred During Deenergization of Relay.Caused by Close Placement of Relay Terminals.Wiring Inside Electrical Panels Reworked 05000322/LER-1986-0141990-05-16016 May 1990 LER 86-014-01:on 860305,full Reactor Trip Occurred Due to Momentary False Low Vessel Level Signal,Causing Hydraulic Pressure Spike in Ref Leg A.Bourton Tube Type Pressure Transmitter Replaced W/Rosemount Model 1153 05000322/LER-1987-0121990-05-16016 May 1990 LER 87-012-01:on 870504,uplanned Actuation of ESF Occurred. Caused by Technician Loosing Footing & Accidently Hitting Outside Cover of Level Switch.Permanent Ladders & Platforms Installed at Head Tank Level Switches 05000322/LER-1988-0171990-05-16016 May 1990 LER 88-017-01:on 881025,discovered That Seismic Monitoring Instrumentation Returned to Svc Prior to Verifying Sys Operability & Special Rept Not Written.Caused by Personnel Error.Surveillance Engineer Reassigned 1997-05-01
[Table view] |
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4,g LONG ISLAND LIGHTING COMPANY SHOREHAM NUCLEAR POWER STATION
- WADING RIVER. NEW YORK 11792 TEL.15.8) 929 8300 November 15, 1989 PM 89-202 U.S. Nuc} ear Regulatory Commission Docuinent Control Desk Washington, D.C. 20556 Dear Sir In accordance with 10CFR50.73, enc]osed is Shoreham Nuclear Power Station's Licensee Event Report (LER 89-008).
Sincerely yours,
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Jack A. Notaro Plant Manager JN/RP/jp Enclosure ec: Wil31am T. Russell, Regiona) Administrator Frank Crescenzo, Senior Resident Inspector Institute of Nuclear Power Operations, Records Center American Nuclear Insurers SR.A21.U200 8911280273 891115 PDR ADOCK 05000322 S PDC
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On 10/16/89, at 0845, during normal defueled conditions, Control ,
Room. alarms were received indicating a fire pump had started and a "
deluge valve had opened. This was followed shortly by an intraplant phone report of a pipe break on elevation 8' of the Reactor Building. The operator, after inspecting the area, found no evidence.of a fire and isolated the fire header in the Reactor Building. A subsequent walkdown of the affected area determined
.that a manual pull station had been actuated. This indicated that a person or persons may.have deliberately initiated the deluge system.
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An Unusual Event (attempted sabotage / tampering) was declared.
Actions required under the declaration of an Unusual Event were performed. The NRC was notified of the situation at 1016 per 10 CFR 73, Appendix G, I f.a) (3). Security obtained a computer printout of people in the Reactor Building at the time of the incident. At 1025, the deluge system was restored to nornal and the Unusual Event was terminated. A second walkdown of the area was then performed to check for equipment damage. The seven personnel in the area at the time of the event were interviewed. Water that was found inside electrical ju:ction boxes was wiped up.
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-ELAHI AND_SYSIEM_.lDENTIFICAIlON General Electric Boiling Water Reactor l- Energy.; Industry Identification System (EIIS) codes ~are identified L 11n the text as [xx).
, IDENIIEICAI1QH OF THE EVENT
- j. Unauthorized. Actuation of Deluge System :
Event Date: 10/16/89 i t
Report Date: 11/15/89
'GGHDITIONS_.ERIQR TO THE_EYENI Reactor Defueled - All fuel assemblies stored in the Spent Fuel Pool' Mode Switch - Shutdown a RPV Pressure O psig RPV Temperature =.98 Degrees F-POWER LEVEL - 0 All rods inserted in the core ,
DESCEIPTIQH_QE THE_EYEHI On 10/16/89 at 0845, with.the plant in its normal shutdown and
-defueled condition, alarms were received in the Control Room which indicated that the electric motor-driven fire pump (1M43-P-59) had started'and a fire suppression deluge valve (1M43-02-0430) [KP] had-opened. This particular deluge valve supplies water to nossles that spray-the vertical cable trays [FA) on elevation 8' of the' Reactor Building [NG]. (Elevation 8 is where the emergency core cooling system pumps [BJ, BM, BN, BO] ace located.) Shortly after the
- alarms, the Control Room received an intraplant phone report from a
. person in the Reactor Building stating that e pipe break had occurred. (This was later found to be the deluge spray water and not a pipe break). The actions required by Alarm Response Procedures for the vertical cable tray deluge valvo actuation were s
executed. An equipment operator was sent to check the area. After finding no evidence of a fire the Reactor Building fire header was isolated. A further investigation and system walkdown determined that the manual pull g,o.. u.. . .u s cro i.e.+.u us m
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S l0 0h 0F n lq Tur , . me war.nm station on elevation 8' for the vertical cable trays had been actuated. The station's handle had been pulled out, breaking a seal, and then pushed back in, which indicates that the action may not have been accidental. In accordance with Standing Order #37,
" Operational Response to Events Concerning Deliberate Acts Directed Against Plant Equipment", Security and management personnel were notified and the applicable portion of the Emergency Plan was executed. Thus, an Unusual Event-12 was declared based upon attempted sabotage / tampering. The NRC was notified per 10 CFR 73, Appendix G, I (a) (3). Seven people were in the Reactor Building at i the time of the incident as determined from the security computer.
The operators reset the manual pull station and restored the deluge system and fire header to their normal lineups. When the fire header was repressurized a gasket blew out on a fire hose station on elevation 175' of the Reactor Building. This caused additional equipment to be sprayed with water and required that 2 fire hose stations on elevation 175' be isolated. Finally, in accordance with Standing Order #37, a general field check vf equipment in the Reactor Building was conducted using SP 22.000.02, "Non Technical Specification-Equipment Readings", to determine if any equipment irregularities existed. No equipment irregularities were found. ;
The Unusual Event was terminated at 1025.
The electrical panels and junction boxes sprayed by the deluge system were subsequently inspected for water damage by Quality Control and Maintenance personnel. Any water found was removed by hand toweling and the equipment covers were left open overnight to ,
assist in evaporating the moisture. Additionally, a review was !
performed to determine if environmental qualification standards were maintained during this event. The equipment affected by the deluge valve-actuation is operating normally. The leaking gasket on the
-fire hose ~ station on elevation 175' was repaired and the two fire j hose stations were returned to service.
l The people in the Reactor Building at the time of the event were interviewed by Site Security and a member of the Plant Staff.
Corporate Security personnel checked the pull station for fingerprints and along with Site Security conducted a second round of interviews. All of the above information was inconclusive.
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0p 0g or 0 15 texm . wanc a asuunn CAUSE_DE_IHE_EYEHI Based upon the available evidence, i.e., investigations by plant staff and security personnel, a check for fingerprints, interviews and past experience with the fire suppression deluge system, no definite conclusion as to the cause of the activation of the manual pull station has been made. This event is not considered to be a case of sabotage. It could be an isolated incident where a person tampered with a piece of equipment without realising the consequences of his actions.
AHALYSIS_0E_IHE_EYENI 1 The actuation of the manual pull station caused the opening of the l deluge valve and spraying of fire water onto the vertical cable trays on elevation 8' in the Reactor Building and also started the electric motor-driven fire pump.
The plant had been shutdown and defueled prior to this event. There was no fire and this event had no safety consequences. Even if the plant had been operating at power the safety consequences would have- t only been minor. The fire protection system performed as designed and the operators took the appropriate corrective actions.
COBEECIIYE_ACIl0HS During a meeting with site employees, the Plant Manager discussed the seriousness and consequences of this event. He emphasized the extent that the company went in investigating this event including the involvement of security personnel, the check for fingerprints and the company's intention to prosecute people who tamper with <
plant-equipment. This is being followed up'by a memorandum from the Plant Manager to site employees which emphasises that even though the plant is shutdown, the plant still contains operable and energized equipment and serious consequences can result from persons operating or tampering with this equipment.
The problem with water accumulating in certain electrical junction boxes has been referred to the Engineering Department for further I investigation.
The cause of the blown gasket is believed to be the pressure surge resulting from repressurising the fire header. This is still being investigated and if necessary, procedure changes will be made in order to prevent this from reoccurring.
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a.- Manufacturer _and_mndel_ number __of_ failed _com mnent_Ln1 None l
j b. LEB_ numbers _of_nr.exions_mimilar_eyents None i
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