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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000322/LER-1989-0051990-05-16016 May 1990 LER 89-005-01:on 890321,results of Local Leak Rate Test of Core Spray Suction Valve a Determined That Leakage,When Combined W/All Type B & C Penetration Leakages,Exceeded Tech Spec Limit.Caused by Normal Valve Degradation 05000322/LER-1989-0031990-05-16016 May 1990 LER 89-003-01:on 890310,emergency Diesel Generator (EDG) 102 Manually Shutdown During 18-month Surveillance Test Due to Failure of EDG Output Breaker.Cause Not Determined. Replacement Breaker Installed in Cubicle 102-8 05000322/LER-1988-0171990-05-16016 May 1990 LER 88-017-01:on 881025,discovered That Seismic Monitoring Instrumentation Returned to Svc Prior to Verifying Sys Operability & Special Rept Not Written.Caused by Personnel Error.Surveillance Engineer Reassigned 05000322/LER-1988-0151990-05-16016 May 1990 LER 88-015-02:on 880916,seismic Monitoring Instrumentation, Including Peak Acceleration Recorders,Removed from Svc for More than 30 Days Due to Corrosion on Scratch Plates.Cover Gasket Replaced & Thermal Barrier Mount to Be Installed 05000322/LER-1988-0031990-05-16016 May 1990 LER 88-003-01:on 880322,unplanned Automatic Initiation of Reactor Bldg Standby Ventilation Sys Side a Occurred During Deenergization of Relay.Caused by Close Placement of Relay Terminals.Wiring Inside Electrical Panels Reworked 05000322/LER-1987-0351990-05-16016 May 1990 LER 87-035-02:on 871221,880106 & 0330,high Energy Line Break Logic Isolations of RWCU & Main Steam Line Drain Valves Occurred.Caused by Problems W/Temp Monitoring Units. Grounding Scheme Changed & Transformers Rewired 05000322/LER-1987-0221990-05-16016 May 1990 LER 87-022-01:on 870604,HPCI Test Valve to Condensate Storage Tank,Globe Valve & Hpci/Rcic Test Valve to Condensate Storage Tank Failed to Close Against Sys Operating Pressure.Disc of motor-operated Valve 37 Modified 05000322/LER-1987-0121990-05-16016 May 1990 LER 87-012-01:on 870504,uplanned Actuation of ESF Occurred. Caused by Technician Loosing Footing & Accidently Hitting Outside Cover of Level Switch.Permanent Ladders & Platforms Installed at Head Tank Level Switches 05000322/LER-1986-0391990-05-16016 May 1990 LER 86-039-01:on 861006,unplanned Initiation of Reactor Bldg Standby Ventilation Sys Occurred W/All Rods Inserted in Core.Caused by Faulty Design of Retaining Device.Warning Signs Attached to Valve Actuator & Valve Mod Initiated 05000322/LER-1986-0321990-05-16016 May 1990 LER 86-032-01:on 860728,RWCU Isolated on High Differential Flow Sensed by Steam Leak Detection Sys While Placing Filter Demineralizers in Operation.Cause Not Determined. Operating Procedures Revised to Monitor RWCU Sys 05000322/LER-1986-0141990-05-16016 May 1990 LER 86-014-01:on 860305,full Reactor Trip Occurred Due to Momentary False Low Vessel Level Signal,Causing Hydraulic Pressure Spike in Ref Leg A.Bourton Tube Type Pressure Transmitter Replaced W/Rosemount Model 1153 05000322/LER-1985-0591990-05-16016 May 1990 LER 85-059-01:on 851219,half Reactor Trip,Full NSSS Shutoff Sys Isolation & Reactor Bldg Standby Ventilation Sys Initiation Occurred Due to Loss of Power to Reactor Protection Sys Bus B.Assembly Breaker Reset 05000322/LER-1987-0091990-05-16016 May 1990 LER 87-009-01:on 870203,full Reactor Trip Occurred Due to Perturbation in Ref Leg.Caused by Spurious Low Level Reactor Pressure Vessel Water Level Signal.Existing Level & Pressure Transmitters Replaced W/Newer Models 1990-05-16
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20140G4481997-05-0101 May 1997 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby Diesel Generator Sys.Recommends That Springs Be Inspected on Periodic Basis,Such as During Refueling Outages ML20135D8011996-11-26026 November 1996 Part 21 Rept Re Two Safety Related Valves Supplied by Velan Valve Corp Were Not in Compliance W/Originally Supplied QA Documentation.Returned Valves to Velan in May 1996 & on 961120 Velan Advised That Valves Had Been Misplaced ML20080G4691995-01-26026 January 1995 Record of Telcon W/Nrc & Licensees 950126 to Clarify Position Re Dispositioning of Exempt Sources Listed in Section 6.3.3 of Shoreham Termination Survey Final Rept Dtd Oct 1994 ML20069F0001994-01-24024 January 1994 Vols 1-4 to Shoreham Decommissioning Project Termination Survey Final Rept ML20058K3841993-12-0909 December 1993 Part 21 Rept Re Potential Defect in Component of Dsrv & Dsr Enterprise Standby DG Sys,Regarding Potential Problem W/ Subcover Assembled Atop Power Head ML20057F2261993-09-30030 September 1993 Safety Evaluation Supporting Exemption Request from Requirements of 10CFR50.54(q) for License NPF-82 ML20056C7181993-07-14014 July 1993 SE Supporting Amend 10 to License NPF-82 ML20045B3551993-06-11011 June 1993 LER 93-001-00:on 930429,refueling Jib Crane Moved in Vicinity of Spent Fuel Pool Using vendor-supplied Lifting Eye in Violation of NUREG-0612.Caused by Failure to Identify Crane as Heavy Load.Meetings held.W/930611 Ltr ML20045C8881993-06-0808 June 1993 Vols 1 & 2 to Refueling Jib Crane 1T31-CRN-008A Incident Root Cause Analysis. W/One Oversize Encl ML20044C1181993-02-28028 February 1993 Shoreham Nuclear Power Station Updated Decommissioning Plan. ML20128P6451993-02-28028 February 1993 Snps Decommissioning Project Termination Survey Final Rept for Steam Turbine Sys (N31) ML20128P7431993-02-19019 February 1993 Rev 3 to 93X027, Nuclear QA Surveillance Rept ML20127H2301993-01-15015 January 1993 Part 21 Rept Re Potential Defeat in Component of Dsrv & Dsr Enterprise Standby DG Sys.Starting Air Distributor Housing Assemblies Installed as Replacement Parts at Listed Sites ML20126B0421992-12-17017 December 1992 Final Part 21 Rept Re Potential Problem W/Steel Cylinder Heads.Initially Reported on 921125.Caused by Inadequate Cast Wall Thickness at 3/4-inch-10 Bolt Hole.Stud at Location Indicated on Encl Sketch Should Be Removed ML20125C7161992-12-0707 December 1992 Part 21 Rept Re Possibility for Malfunction of Declutching Mechanisms in SMB/SB-000 & SMB/SB/SBD-00 Actuators. Malfunction Only Occurs During Seismic Event.Balanced Levers May Be Purchased from Vendor.List of Affected Utils Encl ML20127P5861992-11-23023 November 1992 Followup to 921005 Part 21 Rept Re Potential Defect in SB/SBD-1 Housing Cover Screws.Procedure Re Replacement of SBD-1 Spring Cover Bolts Encl.All Fasteners Should Be Loosened & Removed.List of Affected Utils Encl ML20128B9641992-10-31031 October 1992 Rev 0 to Shoreham Decommissioning Project Termination Survey Plan ML20118B4391992-09-11011 September 1992 Part 21 Rept Re Degradation in Abb Type 27N Undervoltage Relays Used in Electrical Switchgear.Recommends That Users Review Applications Requiring Exposures Greater than 1E03 Rads TID W/Time Delay Function Option ML20099H5781992-07-31031 July 1992 Rev 4 to Shoreham Defueled Sar ML20114A6311992-07-28028 July 1992 Shoreham Decommissioning Plan ML20101K5791992-06-25025 June 1992 Long Island Power Authority Shoreham Decommissioning Project,Shoreham Nuclear Power Station,Technical Rept on Water Processing & Water Mgt Activities for Reactor Pressure Vessel & Wet Cutting Station ML20094L1271992-03-13013 March 1992 Amend 1 to Part 21 Rept 159 Re Potential Defect in Power Cylinder Liner.Initially Reported on 920115.Caused by Liner/ Block Fit & Localized Matl Microstructure.All Drawings & Specs Revised to Address Matl Design Requirements ML20082M5081991-08-26026 August 1991 Rev 3 to Shoreham Defueled Sar PM-91-125, Monthly Operating Rept for Jul 1991 for Shoreham Nuclear Power Station1991-07-31031 July 1991 Monthly Operating Rept for Jul 1991 for Shoreham Nuclear Power Station PM-91-112, Monthly Operating Rept for Jun 1991 for Shoreham Nuclear Power Station1991-06-30030 June 1991 Monthly Operating Rept for Jun 1991 for Shoreham Nuclear Power Station PM-91-075, Monthly Operating Rept for Apr 1991 for Shoreham Nuclear Power Station1991-04-30030 April 1991 Monthly Operating Rept for Apr 1991 for Shoreham Nuclear Power Station ML20024G7171991-04-22022 April 1991 LER 91-001-00:on 910324,RB Normal Ventilation Sys (Rbnvs) Outboard Exhaust Valve Closed for No Apparent Reason.Cause Inconclusive.Sys Restored to Normal Lineup & Rbnvs Outboard Valve Will Be Stroked on Routine basis.W/910422 Ltr SNRC-1806, Revised Pages 2 & 6 to Encl a of 10CFR50.59 Annual Rept for 19901991-04-15015 April 1991 Revised Pages 2 & 6 to Encl a of 10CFR50.59 Annual Rept for 1990 PM-91-058, Monthly Operating Rept for Mar 1991 for Shoreham Nuclear Power Station1991-03-31031 March 1991 Monthly Operating Rept for Mar 1991 for Shoreham Nuclear Power Station PM-91-037, Monthly Operating Rept for Feb 1991 for Shoreham Nuclear Power Station1991-02-28028 February 1991 Monthly Operating Rept for Feb 1991 for Shoreham Nuclear Power Station PM-91-016, Monthly Operating Rept for Jan 1991 for Shoreham Nuclear Power Station1991-01-31031 January 1991 Monthly Operating Rept for Jan 1991 for Shoreham Nuclear Power Station SNRC-1797, 10CFR 50.59 Annual Rept of Facility Changes,Procedure Changes,Tests & Experiments for Jan-Dec 19901990-12-31031 December 1990 10CFR 50.59 Annual Rept of Facility Changes,Procedure Changes,Tests & Experiments for Jan-Dec 1990 SNRC-1794, Shoreham Nuclear Power Station Annual Operating Rept,19901990-12-31031 December 1990 Shoreham Nuclear Power Station Annual Operating Rept,1990 SNRC-1799, Lilco 1990 Annual Rept1990-12-31031 December 1990 Lilco 1990 Annual Rept ML20069Q3901990-12-31031 December 1990 Shoreham Nuclear Power Station Decommissioning Plan. (Filed in Category P) ML20028H0231990-09-28028 September 1990 LER 90-007-00:on 900907,unplanned Actuation of ESF Sys Occurred During I&C Surveillance Test.Caused by Inadequate procedure.SP44.650.16 Revised to Require That Leads Lifted & Individually separated.W/900928 Ltr ML20056A2001990-07-31031 July 1990 Safety Evaluation Supporting Amend 6 to License NPF-82 PM-90-097, Monthly Operating Rept for June 1990 for Shoreham Nuclear Power Station1990-06-30030 June 1990 Monthly Operating Rept for June 1990 for Shoreham Nuclear Power Station ML20055E3911990-06-25025 June 1990 Safety Evaluation Supporting Amend 5 to License NPF-82 PM-90-083, Monthly Operating Rept for May 1990 for Shoreham Nuclear Power Station1990-05-31031 May 1990 Monthly Operating Rept for May 1990 for Shoreham Nuclear Power Station 05000322/LER-1988-0151990-05-16016 May 1990 LER 88-015-02:on 880916,seismic Monitoring Instrumentation, Including Peak Acceleration Recorders,Removed from Svc for More than 30 Days Due to Corrosion on Scratch Plates.Cover Gasket Replaced & Thermal Barrier Mount to Be Installed 05000322/LER-1986-0391990-05-16016 May 1990 LER 86-039-01:on 861006,unplanned Initiation of Reactor Bldg Standby Ventilation Sys Occurred W/All Rods Inserted in Core.Caused by Faulty Design of Retaining Device.Warning Signs Attached to Valve Actuator & Valve Mod Initiated 05000322/LER-1986-0321990-05-16016 May 1990 LER 86-032-01:on 860728,RWCU Isolated on High Differential Flow Sensed by Steam Leak Detection Sys While Placing Filter Demineralizers in Operation.Cause Not Determined. Operating Procedures Revised to Monitor RWCU Sys 05000322/LER-1987-0091990-05-16016 May 1990 LER 87-009-01:on 870203,full Reactor Trip Occurred Due to Perturbation in Ref Leg.Caused by Spurious Low Level Reactor Pressure Vessel Water Level Signal.Existing Level & Pressure Transmitters Replaced W/Newer Models 05000322/LER-1987-0221990-05-16016 May 1990 LER 87-022-01:on 870604,HPCI Test Valve to Condensate Storage Tank,Globe Valve & Hpci/Rcic Test Valve to Condensate Storage Tank Failed to Close Against Sys Operating Pressure.Disc of motor-operated Valve 37 Modified 05000322/LER-1989-0051990-05-16016 May 1990 LER 89-005-01:on 890321,results of Local Leak Rate Test of Core Spray Suction Valve a Determined That Leakage,When Combined W/All Type B & C Penetration Leakages,Exceeded Tech Spec Limit.Caused by Normal Valve Degradation 05000322/LER-1989-0031990-05-16016 May 1990 LER 89-003-01:on 890310,emergency Diesel Generator (EDG) 102 Manually Shutdown During 18-month Surveillance Test Due to Failure of EDG Output Breaker.Cause Not Determined. Replacement Breaker Installed in Cubicle 102-8 05000322/LER-1985-0591990-05-16016 May 1990 LER 85-059-01:on 851219,half Reactor Trip,Full NSSS Shutoff Sys Isolation & Reactor Bldg Standby Ventilation Sys Initiation Occurred Due to Loss of Power to Reactor Protection Sys Bus B.Assembly Breaker Reset 05000322/LER-1987-0351990-05-16016 May 1990 LER 87-035-02:on 871221,880106 & 0330,high Energy Line Break Logic Isolations of RWCU & Main Steam Line Drain Valves Occurred.Caused by Problems W/Temp Monitoring Units. Grounding Scheme Changed & Transformers Rewired 05000322/LER-1988-0031990-05-16016 May 1990 LER 88-003-01:on 880322,unplanned Automatic Initiation of Reactor Bldg Standby Ventilation Sys Side a Occurred During Deenergization of Relay.Caused by Close Placement of Relay Terminals.Wiring Inside Electrical Panels Reworked 1997-05-01
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text
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PACILITY NAME Hi DOCKET NVMSER (75 PAGE
- Shoreham Nuclear Power Station Unit 1 o is lo lo lo p ! 2 l2 i jorl0 l 4 Full RpS actuation while an I&C Tech was valving in a level transmitter to the reference lec after maintenanm hM wn rMnmv9 nn it EVENT DAf t (81 LtR NUnsetR lei REPORT DATE (T) OTHER S ACILillES INVOLVED ISI 88 '*' vtAR DOCntT NUM6tRisi MONTM DAY YEAR YEAR , , MONTH DAY ' ACILit v hauts o]6l0lojol l l 0k o l rj 0 l4 d7 8 7 8l7 O l 0l 9 0 l1 1lA _
0 1 5l0 toioi l l OPE R ATING TMis REPORT as $UDMITTf D PUR$UANT TO THE RtOUIREMENTS OF 10 CPR { (Caeca one or more et rae resto me) 01)
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NAME TELEeHONE NUMBim George D. Schnaars, Operational Ccnpliance Engineer el3lA 9 2l9 t- i 8l3 p l0 1
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CAust sysTIM COMPONENT $C n CAV$t 8 Y STE M COMPONE NT *j%$C R O hPA I I I i i l I I I I I I I I l l l l l 1 l l l 1 I I I I SUPPLEMENTAL REPORT E XPECTED 114> MONTH DAY vtAR
$v8Vi$3 TON Yt$ 199 res, compiers txPEC110 Sv04*ISSION DA ttl NO l l l ASSTAACT (Wr to f e00 speces d e eooro=# mere'r t,Presa sme e spece tyPewrerrea haes> Del On_ February 3, 1987 at 1555, a full reactor trip occurred due to a
' perturbation in the reference leg while an Instrument and Controls (I&C) technician was valving in a level transmitter. The plant was -
J in Operational Condition 4 (Cold Shutdown) with the mode switch in ohutdown and all rods inserted in the core. After maintenance had been performed on it, a technician was preparing to valve l 1B21*LT155A back into service. Using extreme caution, due to :
recurring problems (refer to LERs85-006, 017, 020, 042,86-014, 1 021) with the reference and variable legs, the technician opened up the isolation valve causing a hydraulic oscillation in the line, i This action caused a momentary false low level signal, resulting in a full reactor trip. Operators verified the signal to be false and reset the trip. - Because of the recurring events, the event was anticipated and therefore deemed not reportable at the time, i However after a more careful review of the procedure used, on April 27, 1987, Plant Management determined that it was not part of a preplanned sequence and therefore reportable. The NRC was notified at this time per 10CFR50.72. This Supplemental Report is being i submitted to inform the Commission of the status of corrective I actions taken for this event. 1 2
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- 5 Of MANAGEMENT AND DVDGET.WAsMINGTON. DC 20603.
PACILITY leAME (11 DOCKET NUM$th (31 LtR sdWMBER {$l PA06136 vtan H QW8 hi - "' V 8'ON Shoreham Nuclear power Station Unit 1 rexT a- .w -=ac f assoim PLANT MQ_ SYSTEM IDENTIFICATION ;
' General Electric - Boiling Water Reactor
-Energy-Industry Identification System (EIIS) codes are identified in the text'as [xx). ,
1 IDENTIFICATIOH__OF_THE EVENT l t
i
-Full-Reactor Protection System (RPS) [JC) actuation due to l pertubation in reference leg caused by I&C technician valving in a
~ level transmitter, i
Event Date: 4/27/87 Report Date: S/16/90 :
l ;
CONDITIQHS_ PRIOR'TO THE EYEHI t
Operational Condition 4 (Cold Shutdown)
ModerSwitch - Shutdown RPV Pressure.= 0'psig RPV Temperature = 114 Degrees F i All rods inserted in the core.
L' DESCRIPTION OF THE EVENT lj On-February 3, 1987 at 1344, a full RPS actuation occurred while an I&C technician was valving in a level transmitter (1B21*LT-155A) to
- the reference leg. The instrument had just been repaired under a L -Maintenance Work Request (an MWR) and was in the process of returning:the. instrument to service per. approved Station Procedure.
?
1 41.012.02 (Reactor Vessel Reference Leg Instrument Removal and Return to Service).- The technician was fully aware of the potential for:a-reference les " bump" and a possible RPS actuation and was using extreme caution. Nevertheless, when he opened the isolation <
valve to. place the instrument back into service, a full RPS actuation occurred due to a spurious low RPV water level signal.
- Operators verified the signal as false, performed the Emergency Shutdown procedure (SP 29.010.01) and reset the trip.
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~When the actuation occurred, it was determined at the time that the svent was anticipated and therefore, not reportable per 10CFR50.72 and 73. . However, on April 23, 1987 the Plant review of Operations Committee (ROC) suggested that a more detailed investigation of the procedure was. warranted to determine if the " anticipated" actuation- .;
was part of a' pre planned sequence of events.
_On April'27, 1987 at 1100, it was determined by Plant Management that although the RPS actuation was anticipated and numerous caution ,
O statements were located in the return to service procedure (SP 41.012.02), it was not part of the preplanned procedu're and ,
~
~therefore was reportable as an ESF actuation. At 1247, the NRC was notified.per 10CFR50.72. This Supplemental Report is being submitted to inform the Commission of the status of corrective '
actions taken for this event. .
CAUSE'OF THE EVENT The-perturbation in the reference leg occurred during the valve
. manipulations necessary to return.the instrument to service. The
- cause is believed to be a combination of: 1. The ability of-these instrument sensing lines to transmit hydraulic transients, 2. The censitivity of these reactor level transmitters, and 3. .The l-
' grouping of both RPS logics on common sensing lines. The technician f involved was adequately trained and qualified to perform this work.
He was aware of the sensitivity of the reference leg instruments from direct. experience, required reading and discussions-at section meetings covering similar incidents and level instrumentation training established as a result of earlier incidents.
. ANALYSIS OF THE EVENT This event resulted in an unplanned actuation of the Reactor Protection System and is reportable per 10CFR50.73(a)(2)(iv). There .I is no safety significance to the event. The section in the procedure being used to return the instrument to service can only be ;
performed while the plant is shutdown. The RPS operated as designed and operators carried out all required actions.
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- LICENSEE EVENT REP 3RT (LER)
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PA E WO ME U Te0N d 600 1 0F MANAGEMENT AND DVD0tt,W ASHINGTON. DC 20603.
I Y NAMS Hi DOCRET NUtett A (2) LtR NUMetR 161 PA04 (31 vi*a " C 0!.T. MYJJ:
Shoreham Nuclear power Station Unit 1 o ls l0 l0 lc l 3l 2l2 8l 7 -
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0 l1 0l 4 0F 0l4 Ts<tn .-.. = - we w am,wnn CORRECTIVE AQIlGHS Because of the frequent number of incidents involving valving in of instruments to the reference and variable legs, it was decided to expedite a modification (SM 88-023) that was originally scheduled for implementation during the first refueling outage. This modification involves the replacement of existing level and pressure transmitters with newer ones. The new transmitters have a greater dampening effect and thus will be less susceptible to hydraulic oscillations produced when returning these instruments to service.
Implementation of this modification has been deferred indefinitely due to the New York - LILCO Shoreham Settlement Agreement.
ADDITIONAL _lHEQRMATION
- a. Manuf.acturer_and_mndel_ number _cL.f. ailed _ component _Lal None
- b. LEE _ numbers of orevious_similar__ events 3 LER 85-006, 017, 020, 042 ,
~
86-014, 021 88-012 l l'
l l'
i l N EC Ferm 306A (649)
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05000322/LER-1987-009 | LER 87-009-01:on 870203,full Reactor Trip Occurred Due to Perturbation in Ref Leg.Caused by Spurious Low Level Reactor Pressure Vessel Water Level Signal.Existing Level & Pressure Transmitters Replaced W/Newer Models | | 05000322/LER-1987-012 | LER 87-012-01:on 870504,uplanned Actuation of ESF Occurred. Caused by Technician Loosing Footing & Accidently Hitting Outside Cover of Level Switch.Permanent Ladders & Platforms Installed at Head Tank Level Switches | | 05000322/LER-1987-014, Forwards LER 87-014 & Rev 1 to LER 86-029 | Forwards LER 87-014 & Rev 1 to LER 86-029 | | 05000322/LER-1987-022 | LER 87-022-01:on 870604,HPCI Test Valve to Condensate Storage Tank,Globe Valve & Hpci/Rcic Test Valve to Condensate Storage Tank Failed to Close Against Sys Operating Pressure.Disc of motor-operated Valve 37 Modified | | 05000322/LER-1987-035 | LER 87-035-02:on 871221,880106 & 0330,high Energy Line Break Logic Isolations of RWCU & Main Steam Line Drain Valves Occurred.Caused by Problems W/Temp Monitoring Units. Grounding Scheme Changed & Transformers Rewired | |
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