LER-1979-016, /03L-0 on 790506:during Surveillance Test, Isolator Condenser Isolation Sensor Setpoint a Measured Two Inches of Excess Water.Caused by Instrument Drift in Excess of Design Accuracy.Switch Was Recalibr & Put Back in Svc |
| Event date: |
|
|---|
| Report date: |
|
|---|
| 2191979016R03 - NRC Website |
|
text
7 77)
LICENSEE EVENT REPORT CbNTROL BLOCK: l l
l l
l l
lh (PLEASE PRINT oR TYPE ALL REQutRED INFoRMATioN) e' 1
6 l N l J l 0 l C l P l 1 l@l 0l 0l - l 0 l 0 l 0 l 0 l 0 l-l 0 l 0 l@l 4 l 1 l 1 l 1 l 1 l@l l
l@
o t
8 9 LICENSEE CODE 14 15 LICENSE NUMBER 25 26 LICENSE s'YPE JO 57 CAT 56 CON'T
~
lTTT)
,g l L lgl 0 l 5 l 0 l 0 l 0 l 2 l 1 l 9 lgl 0 l 5 l 0 l 6 l 7 l 9 lgl 0 l 6 l 0l 5 l 719 l@
a 8
6q 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT OESCRIPTION AND PROBABLE CONSEQUENCES h l On May 6', 1979 during a surveillance test for isolation condenser pipe o
2 break isolation, "A" isolation condenser isolation sensor IBilAl set-g g,3 point was found to be 29.0 inches of water instead of 27 0 inches as re-g o,a ois I quired ky Tech. Specs. Table 3.1.1.H.2.
The safety significance of this l
o,e l event i,s considered minimal since redundant sensor IB11A2 would have op-g
- o,7 l erated at the required value to isolate "A" isolation condenser upon a l
high flow condition.
l o,e 80 g
S Y S T E '.'
CAUSE
CAUSE COYP.
VALVE COOE C;OE Sus: ODE COYPCad*:T CODE St.;eCCDE SUECOCE
@ lZ l@
c191 l S l F l@ lX l@ lZ l@ l II N S l T l R l U l@
E 12 18 19 20 7
9 10 11 SE QUENTI AL OCCURRENCE REFORT R E VISION r :. r n EVENT YE AR R EPORT NO.
CCDE TYPE N O.
O d:g[
17 19 l l-l l0 l1 l6 l l/l 0l3l lL l l-l 0l 21 22 23 24 20 27 28 29 30 31 32 ACTICN rCTUAE EFFECT S*UTDCL_
ATTACHMENT NPRD4 PRIL*E COMD.
COYPONENT TAKEN AL, TION ON PLANT YETHOO HOURS SUBMITT ED FORM bub.
SU PP LI E R MANUFACTURER l E lgl X l@
l Z l@
lZ l@
0l 0 0l l
lYlg lYjg lNl@
l1l2l0 4lg 3J a
23 36 J
40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS l The cause of this occurrence is attributed to instrument drift in excess j
o of design accuracy.
Differential pressure indicating switch IBilAl was calibrated to operate at the required setpoint and placed back in
, l 3
l service.
Differential pressure switch IBilAl will be retested during the
[
week of June 4,1979 i
A 80 7
8 9
"%POAER OTH E R ST ATUS DIS O RY DISCO % ERf DESCRIPTION STA S NA l
l B l@l Surveillance Test l
[ G_J @ l0 l 0 l0-l @ l i
s ACTIVITY
'CO TENT RELEASED OF RELE ASE AMOUNT OF ACTIVITY LOCATIO OF RELEASE NA l
l N
l [Z_] @ l Z lgl_
i c
7 P 9 10 11 44 45 83 PERSONNEL EXPOSURES NUYBE R TYPE
DESCRIPTION
l 0 l 0 l 0 l@l Zl@l NA l
1 7
Po m.d',N,u'JiES 2255 11Z x5CR,P,,0Ne
~U...
NA l010101@l l
i EOzmoro'u.cE O F A:,t T e/
7906110I9 5' f
YWf f.,E v_ ut* T 8 ON
(
W @l NA i
9 go h
9 10 izjC$n.PtioNQ NRc usE onty NA l
llllllllllll [f l N l(44)I 6'
, Stations,-Nuclear (201) 455-8784 2
n r ave or PREPAHEr<
PHONE.
w ;-
Jersey Central Power & Light Cornpany w
(Y;
?
~ (
{-
Madison Avenue at Punch Bowt Road r s
.s T' _*
Morristown New Jersey 07960 (201)455 4200 0YSTER CREEK NUCLEAR GENERATING STATION Forked River, New Jersey 08731 Licensee Event Report Reportable Occurrence No. 50-219/79-16-3L Report D' ate June 5,'I979 Occurrence Date May 6, 1979 IJentification of Occurrence Tne setpoint of differential pressure indicating switch IBil Al was found to be less conservative than that specified in Table 3.1.1.H.2 of the Technical Specifications.
This event is, considered to be a reportable occurreace as defined in the Technical Specifications, paragraph 6.9.2.B.I.
Conditions Prior to Occurrence The plant was in a cold shutdown condition.
Plant parameters at the time of the occurrence were:
Reactor coolant temperature - 177'F Reactor level 81" Yarway All control rods fully inserted Description of Occurrence On Sundgy, May 6,1979, at approximately 1233 hours0.0143 days <br />0.343 hours <br />0.00204 weeks <br />4.691565e-4 months <br />, "A" isolation condenser isolation sensor IB11 A1 setpoint was found to be less conservative than that established by ~the Technical Specifications. The condition was discovered during performance of a routine surveillance test for isolation condenser pipe break isolation.
Pressure Switch Desired Setpoint As As Designation (Head Correction Included)
Found Left IBilAl 27" + 0" - 1" of H O 29 26 2
IBilA2 27" + 0" - 1" of H O 27 27 2
2255 113 J ', ~ Ui L J/.9'.N L T' COTO'iny G a f.*emD9f O' the Genera! Puchc Utd.:>es System
.Preportable. Occurrence No. 50-219/79-16-3L Page 2 June 5, 1979 Apparent Cause of Occurrence it is noted that the instrument was not operating within its design accuracy and the apparent cause of this occurrence is attributed to instrument drif t.
Analysis of Occurrence Differential pressure indicating switch IBilAl senses a high flow condition, which would indicate a pipe break, in the "A" isolation condenser condensate return ti.ne.
Upon sensing a high flow condition, sensor IBilAl would complete the logic circuit required to isolate the "A" isolation condenser.
Sensor IBilAl wculd have operated as required, but at a less conservative value than that required by the Technical Specifications.
The safety significance of this event is considered to be minimal since the redundant sensor IB11A2 would have operated at the required value, to isolate "A" isolation condenser upon a high flow condition.
Correc tive Action Differential pressure indicating switch IB11A1 was calibrated to operate at the required value and placed back into service.
Differential pressure switch IB11 A2 will be retested during, the week of June 4,1979 to determine if thei setpoint is operating within the design accuracy. Additionally, an invest ga-tion of the history of the surveillance test results pertaining to the pipe break sensors indicates that there are no generic drift problems associated with them.
Failure Data IB11A1 -- ITT Barton Monterey, California Sertal Number:
278-964}}
jj4 S.W.P.:
1500 Differential Pressure:
0-60 WC
}}
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000219/LER-1979-001-03, /03L-0 on 790118:valve V-14-35 Failed to Open Completely During Routine Isolation Condenser Valve Operability Test.Caused by Dirty Torque Limit Switch Contacts,Which Were Subsequently Cleaned & Burnished | /03L-0 on 790118:valve V-14-35 Failed to Open Completely During Routine Isolation Condenser Valve Operability Test.Caused by Dirty Torque Limit Switch Contacts,Which Were Subsequently Cleaned & Burnished | | | 05000219/LER-1979-001, Forwards LER 79-001/03L-0 | Forwards LER 79-001/03L-0 | | | 05000219/LER-1979-002, Forwards LER 79-002/03L-0 | Forwards LER 79-002/03L-0 | | | 05000219/LER-1979-002-03, /03L-0 on 790206:while Performing Isolation Condenser Automatic Actuation Test & calibr,RE-15B Trip Point Was Less Conservative than Tech Spec Std.Caused by RE-15B Switch Not Set at 1068 Psig valve.RE-15B Reset | /03L-0 on 790206:while Performing Isolation Condenser Automatic Actuation Test & calibr,RE-15B Trip Point Was Less Conservative than Tech Spec Std.Caused by RE-15B Switch Not Set at 1068 Psig valve.RE-15B Reset | | | 05000219/LER-1979-010-03, /03L-0 on 790417:leak of Isotopic Concentration Noticed Near Inside Penetration within Pipe Tunnel.Caused by Component Failure.Drywell Equipment Drain Tank Line Rerouted to Prevent Further Leakage | /03L-0 on 790417:leak of Isotopic Concentration Noticed Near Inside Penetration within Pipe Tunnel.Caused by Component Failure.Drywell Equipment Drain Tank Line Rerouted to Prevent Further Leakage | | | 05000219/LER-1979-010, Forwards LER 79-010/03L-0 | Forwards LER 79-010/03L-0 | | | 05000219/LER-1979-011-03, /03L-0 on 790419:core Spray Pump NZO1A in Sys 1 Failed to Start Upon Initiation Signal.Caused by Fuse Failure.Fuse Replaced & Pump Test Successfully Completed | /03L-0 on 790419:core Spray Pump NZO1A in Sys 1 Failed to Start Upon Initiation Signal.Caused by Fuse Failure.Fuse Replaced & Pump Test Successfully Completed | | | 05000219/LER-1979-011, Forwards LER 79-011/03L-0 | Forwards LER 79-011/03L-0 | | | 05000219/LER-1979-012-03, /03L-0 on 790419:oxygen Level in Suppression Chamber Atmosphere Was Greater than 5%.Caused by Sensitivity of Sampling Sys & Position of Sample Flow Control Valve. Oxygen Analyzer Recalibr;Level Now Below 5% | /03L-0 on 790419:oxygen Level in Suppression Chamber Atmosphere Was Greater than 5%.Caused by Sensitivity of Sampling Sys & Position of Sample Flow Control Valve. Oxygen Analyzer Recalibr;Level Now Below 5% | | | 05000219/LER-1979-012, Forwards LER 79-012/03L-0 | Forwards LER 79-012/03L-0 | | | 05000219/LER-1979-016, Forwards LER 79-016/03L-0 | Forwards LER 79-016/03L-0 | | | 05000219/LER-1979-016-03, /03L-0 on 790506:during Surveillance Test, Isolator Condenser Isolation Sensor Setpoint a Measured Two Inches of Excess Water.Caused by Instrument Drift in Excess of Design Accuracy.Switch Was Recalibr & Put Back in Svc | /03L-0 on 790506:during Surveillance Test, Isolator Condenser Isolation Sensor Setpoint a Measured Two Inches of Excess Water.Caused by Instrument Drift in Excess of Design Accuracy.Switch Was Recalibr & Put Back in Svc | | | 05000219/LER-1979-017, Forwards LER 79-017/03L-0 | Forwards LER 79-017/03L-0 | | | 05000219/LER-1979-017-03, /03L-0 on 790517:during Routine Surveillance of Core Spray Sys Ii,Parallel Isolation Valve V-20-21 Failed to Operate.Caused by Circuit Breaker Contacts Making Poor Contact in B Phase,Creating Overcurrent.Part Replaced | /03L-0 on 790517:during Routine Surveillance of Core Spray Sys Ii,Parallel Isolation Valve V-20-21 Failed to Operate.Caused by Circuit Breaker Contacts Making Poor Contact in B Phase,Creating Overcurrent.Part Replaced | | | 05000219/LER-1979-018, Forwards LER 79-018/03L-0 | Forwards LER 79-018/03L-0 | | | 05000219/LER-1979-018-03, /03L-0 on 790517:snubber 51/21,core Spray Sys II, Had Signs of Grease on Alemite Fitting on Accumulator.Cause Unknown But Appears Related to Rigorous Svc Conditions. Snubber Replaced | /03L-0 on 790517:snubber 51/21,core Spray Sys II, Had Signs of Grease on Alemite Fitting on Accumulator.Cause Unknown But Appears Related to Rigorous Svc Conditions. Snubber Replaced | | | 05000219/LER-1979-019-03, /03L-0 on 790526:reactor High Pressure Isolation Condenser Initiation Switch RE-15A Tripped at 3 Psig Greater than Specified.Caused by Instrument repeatability.RE-158 Reset to Trip at 1,068 Psig | /03L-0 on 790526:reactor High Pressure Isolation Condenser Initiation Switch RE-15A Tripped at 3 Psig Greater than Specified.Caused by Instrument repeatability.RE-158 Reset to Trip at 1,068 Psig | | | 05000219/LER-1979-019, Forwards LER 79-019/03L-0 | Forwards LER 79-019/03L-0 | | | 05000219/LER-1979-020, Forwards LER 79-020/01T-0 | Forwards LER 79-020/01T-0 | | | 05000219/LER-1979-020-01, /01T-0 on 790613:secondary Containment Integrity Breached When Reactor Bldg Airlock Doors Were Opened Simultaneously.Caused by Failure of Procedure to State Correct Method for Securing Airlock Doors.Procedure Revised | /01T-0 on 790613:secondary Containment Integrity Breached When Reactor Bldg Airlock Doors Were Opened Simultaneously.Caused by Failure of Procedure to State Correct Method for Securing Airlock Doors.Procedure Revised | | | 05000219/LER-1979-021-03, /03L-0 on 790620:during Surveillance Testing Activities,Instrument 1P15A Was Found to Trip at Valve Higher than Allowed by Tech Specs.Instrument Found to Be within Expected Accuracy Attainable | /03L-0 on 790620:during Surveillance Testing Activities,Instrument 1P15A Was Found to Trip at Valve Higher than Allowed by Tech Specs.Instrument Found to Be within Expected Accuracy Attainable | | | 05000219/LER-1979-021, Forwards LER 79-021/03L-0 | Forwards LER 79-021/03L-0 | | | 05000219/LER-1979-022, Forwards LER 79-022/03L-0 | Forwards LER 79-022/03L-0 | | | 05000219/LER-1979-022-03, /03L-0 on 790627:leak Detected on Emergency Svc Water Side of Containment Spray Heat Exchanger 1-2.Caused by Leaking Nipple Connection Between Water Box & Piping to Valve V-3-83,due to Corrosion.Nipple Replaced | /03L-0 on 790627:leak Detected on Emergency Svc Water Side of Containment Spray Heat Exchanger 1-2.Caused by Leaking Nipple Connection Between Water Box & Piping to Valve V-3-83,due to Corrosion.Nipple Replaced | | | 05000219/LER-1979-023-01, /01T-0 on 790719:reactor Power Was Reduced Above Value for Removal of a Feedwater String.Caused by Removal of Recirculating Pump Reactor for Maint.Inboard & Outboard Collector Rings Resurfaced & Pump Returned to Svc | /01T-0 on 790719:reactor Power Was Reduced Above Value for Removal of a Feedwater String.Caused by Removal of Recirculating Pump Reactor for Maint.Inboard & Outboard Collector Rings Resurfaced & Pump Returned to Svc | | | 05000219/LER-1979-023, Forwards LER 79-023/01T-0 | Forwards LER 79-023/01T-0 | | | 05000219/LER-1979-024, Forwards LER 79-024/03L-0 | Forwards LER 79-024/03L-0 | | | 05000219/LER-1979-024-03, /03L-0:on 790730,control Rod Drive Pump a Discovered Spraying Water Through Seal.Caused by Failure of Mechanical Seal.Inboard Mechanical Seal & Inboard Bearing Replaced | /03L-0:on 790730,control Rod Drive Pump a Discovered Spraying Water Through Seal.Caused by Failure of Mechanical Seal.Inboard Mechanical Seal & Inboard Bearing Replaced | | | 05000219/LER-1979-025, Forwards LER 79-025/03L-0 | Forwards LER 79-025/03L-0 | | | 05000219/LER-1979-025-03, /03L-0:on 790806,10,000 Gallons of Torus Water Drained & Ability of Primary Containment Degraded.Caused by Isolation Valve Left Open After Water Samplings.Change to Sampling Procedure Submitted on Use of Valve | /03L-0:on 790806,10,000 Gallons of Torus Water Drained & Ability of Primary Containment Degraded.Caused by Isolation Valve Left Open After Water Samplings.Change to Sampling Procedure Submitted on Use of Valve | | | 05000219/LER-1979-026-03, /03L-0:on 790807,while Excavating to Repair Equipment Drain Tank Line,Leak in Laundry Tank Discharge Pipe Discovered.Caused by Levels of Mn-54 & Co-60.Line Temporarily Rerouted Until Repairs Made | /03L-0:on 790807,while Excavating to Repair Equipment Drain Tank Line,Leak in Laundry Tank Discharge Pipe Discovered.Caused by Levels of Mn-54 & Co-60.Line Temporarily Rerouted Until Repairs Made | | | 05000219/LER-1979-026, Forwards LER 79-026/03L-0 | Forwards LER 79-026/03L-0 | | | 05000219/LER-1979-027, Forwards LER 79-027/01T-0 | Forwards LER 79-027/01T-0 | | | 05000219/LER-1979-027-01, /01T-0 on 790807:four Seismic restraints,NZ-2-R5 NZ-2R7,NZ-2-R8 & NZ-2-R9,in Positions Other than Required by Original Design.Caused by Improper Installation & Damage Due to Unrestrained Pipe Movement | /01T-0 on 790807:four Seismic restraints,NZ-2-R5 NZ-2R7,NZ-2-R8 & NZ-2-R9,in Positions Other than Required by Original Design.Caused by Improper Installation & Damage Due to Unrestrained Pipe Movement | | | 05000219/LER-1979-028, Forwards LER 79-028/03L-0 | Forwards LER 79-028/03L-0 | | | 05000219/LER-1979-028-03, /03L-0:on 790807,during Routine Surveillance of Core Spray Sys 1,parallel Isolation Valve V-20-15 Became Inoperable in Open Position.Caused by High Motor Current Drawn When Close Signal Inadvertently Initiated | /03L-0:on 790807,during Routine Surveillance of Core Spray Sys 1,parallel Isolation Valve V-20-15 Became Inoperable in Open Position.Caused by High Motor Current Drawn When Close Signal Inadvertently Initiated | | | 05000219/LER-1979-029, Forwards LER 79-029/03L-0 | Forwards LER 79-029/03L-0 | | | 05000219/LER-1979-029-03, /03L-0:on 790822,rod Block Trip Setting Was Below 100 Counts Per Second 26 Times During QA Audit.Caused by Calibr Procedure Setting Rod Trip at Tech Spec Limit.Rod Withdrawal Block Setpoint Increased | /03L-0:on 790822,rod Block Trip Setting Was Below 100 Counts Per Second 26 Times During QA Audit.Caused by Calibr Procedure Setting Rod Trip at Tech Spec Limit.Rod Withdrawal Block Setpoint Increased | | | 05000219/LER-1979-030, Revised Attachment to LER 79-030/03L-0:on 790812,control Rod Drive Pump a Removed from Svc for Repair of Pump Vent Piping.Piping Cracked at Bushing at Entry to Pump Casing. Caused by Operator Carelessness.Bushing Replaced | Revised Attachment to LER 79-030/03L-0:on 790812,control Rod Drive Pump a Removed from Svc for Repair of Pump Vent Piping.Piping Cracked at Bushing at Entry to Pump Casing. Caused by Operator Carelessness.Bushing Replaced | | | 05000219/LER-1979-030-03, /03L-0:on 790812,control Rod Drive Pump Removed from Svc Due to Excessive Leakage from Pump Vent Piping. Piping Was Cracked at Bushing.Caused by Use of Vent Line as Operator Foot Support.Bushing & Pipe Nipple Replaced | /03L-0:on 790812,control Rod Drive Pump Removed from Svc Due to Excessive Leakage from Pump Vent Piping. Piping Was Cracked at Bushing.Caused by Use of Vent Line as Operator Foot Support.Bushing & Pipe Nipple Replaced | | | 05000219/LER-1979-031, Forwards LER 79-031/03L-0 | Forwards LER 79-031/03L-0 | | | 05000219/LER-1979-031-03, /03L-0:on 790829,seal Water Piping Found Cracked on Short Pipe Nipple Section Where Threaded Into Seal Cartridge.Caused by Operator Using half-inch Piping as Foot Support.Pipe Nipple Replaced | /03L-0:on 790829,seal Water Piping Found Cracked on Short Pipe Nipple Section Where Threaded Into Seal Cartridge.Caused by Operator Using half-inch Piping as Foot Support.Pipe Nipple Replaced | | | 05000219/LER-1979-032, Forwards LER 79-032/03L-0 | Forwards LER 79-032/03L-0 | | | 05000219/LER-1979-032-03, /03L-0:on 790914,leaks Discovered in Both Containment Spray Sys.Caused by Corrosion Accelerated by Galvanic Action.Matl Change in Nipple Recommended | /03L-0:on 790914,leaks Discovered in Both Containment Spray Sys.Caused by Corrosion Accelerated by Galvanic Action.Matl Change in Nipple Recommended | | | 05000219/LER-1979-033, Forwards LER 79-033/03L-0 | Forwards LER 79-033/03L-0 | | | 05000219/LER-1979-033-03, /03L-0:on 790917,electromatic Relief Valve Pressure Switch 1A83A Tripped at Pressure in Excess of Limit.Caused by Defective High Pressure Microswitch. Replacement Switch Installed | /03L-0:on 790917,electromatic Relief Valve Pressure Switch 1A83A Tripped at Pressure in Excess of Limit.Caused by Defective High Pressure Microswitch. Replacement Switch Installed | | | 05000219/LER-1979-034, Forwards LER 79-034/01T-0 | Forwards LER 79-034/01T-0 | | | 05000219/LER-1979-034-01, /01T-0:on 791008,both Personnel Access Air Lock 15ors of Reactor Bldg Were Simultaneoulsy Open.Caused by Contractor Personnel Disconnecting Automatic Closing Device on One Door.Device Reconnected | /01T-0:on 791008,both Personnel Access Air Lock 15ors of Reactor Bldg Were Simultaneoulsy Open.Caused by Contractor Personnel Disconnecting Automatic Closing Device on One Door.Device Reconnected | | | 05000219/LER-1979-035, Forwards LER 79-035/03L-0 | Forwards LER 79-035/03L-0 | | | 05000219/LER-1979-035-03, /03L-0:on 790926,during Normal Operation,Reading on Main Steam Line Radiation Monitor Lower than Other Three Monitors.Caused by Drift of Zero Setpoint of Amplifier in Monitor.Setpoint Reset to Zero | /03L-0:on 790926,during Normal Operation,Reading on Main Steam Line Radiation Monitor Lower than Other Three Monitors.Caused by Drift of Zero Setpoint of Amplifier in Monitor.Setpoint Reset to Zero | |
|