ML18142B883

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LER 1975-007-00 for R. E. Ginna, Abnormal Degradation of Steam Generator Tubes
ML18142B883
Person / Time
Site: Ginna Constellation icon.png
Issue date: 04/07/1975
From: White L
Rochester Gas & Electric Corp
To: O'Reilly J
NRC/IE, NRC Region 1
References
LER 1975-007-00
Download: ML18142B883 (5)


Text

NRC DISTRIBUTION FOR PART 50 DOCKET MATERIAL (TEMPORARY FORiVI)

CO!!T!!OL NO: +

Fl E; INCID:"'.:T ."."-PC".,T FX F ROM: Rao= hes ter Gas 6 Elec. C DATE OF DOC DATE R EC'D LTR TWX RPT OTHER Rochester, N.Yo L D W TO: ORIG GC OTHER SENT AEC PDR James P, O'Reilly NOSE SENT LOCAL PDR CLASS UNC LASS PROP INFO INPUT NO CYS REC'D DOCKET NO:

XXX 50-244 DESCRIPTION: ENCLOSURES:

Ltr. trans the following..... Abnor. Occurr. 8 75-07 an 3-24-75, concern ing Steam, Generator tubes wall thining 0 ~ ~

( 40 cys..encl, rec'd)'.

filiQl PLANT MARIE: RE Ginna 81 FOR ACTION/INFOR!AVIATION VCR 4-11-75 BUTLER (L) SCH(VENCER (L) Zl EMANiV (L) REGAN (E)

W/ Copies W/ Copies W/ Copies IV/ Copies CLARK (L) STOLZ (L) DICKER (E) LEAR (L) w/ r'.ri pie s W/ Copies W/ Cooies W/ Conies PARR ll 1 VARSA I I O (L) KNI6HTON! (E) SPELS W/ Conies 1V/ Copies W/ Copies W/ Copies KNIEL (L) ~RPLE (L) YOUNGBLOOD (E)

W/ Copies .W/ Copies W/ Copies W/ Copies INTERiNAL DISTR I BUTION TECII REVIE';V DE i~lTO!U LIC ASST A/T IND RC PDR -

~SCHROEDER ~G R IMiES R. DIGGS (L) '.BRAITiViAN OGC, ROOi'~l P-506A MACCARY GAMMILL H. (L)

'EARIN SA LTZi'1AN GOSSICK/STAF F KNIGHT KASTNER ~ "E. O'OULBOURNE ME LTZ

~CASE PAWLICKI BALLARD P. (E) (L)'REUTZER 6 I AMBUSSO SHAO SPANGLER J. LFE (L) PLANS BOYD .'"~ STE LLO M. MAIGRET (L) MCDOiUALD MOOR E (L)::+<<HOUSTOiU E NVI RO S. REED (E) CHAPMAiU DEYOUNG (L) '""-~NOVAK MULLER M. SERVICE (I ) :DUBE (Ltr)

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-" . ~ TEDESCO IPPOLITO M.

P; COLLliUS YOUiNG BLOOD H. Si!1ITH (L) HARTFIELO (2)

DENISE LONG REGAN S. TEETS (L) <<KLECKER REG OPR LAINAS PROJECT LDR G. WILLIAMS(E) EISENHU Y. WILSON (L) ' WIGG I NTOU

- DEFILE & REGION (2) . BENAROYA

, ~T.R. WILSON(3) <<VOLLMER HAR LESS R. INGRA'i%1 (L) m F. V'ILLX."IS STEELE ~ ff EXTERN DISTRIBUTION a

~1 LOG~~ PDR r P DR-SAN/LA/II Y

~1 TIC (ASERNATH ) (1)(2)(10) i ATIONAL LABS 1 BROOKHA~'Ei~i 'AT LAB

~1 NSIC (BUCHAiUAfl) 1 W. PEiNiUliNGTO!U, Rm E.201 GT 1 1 ASLB 1 CONSULTANTS 1 G. ULR IKSOi I. Oi:

1 Newton Anderson NEWi>)ARK/BLUME/AGBABIAN 1 AGiVIED (RUTH GUSSY!AN

~w- ACRS S::.t TG LXC SST Rm 8-127 GT 1 J. D. RUiVKLES, Rm E-201 GT

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'L roar 4 1 A'Ie ROCHESTER GAS AND ELECTRlC CORPORATIOH o 89 EAST AVENUE, ROCHESTER, M.Y. 14649 LEON D. VA<ITE. JR. Q TeLepHONe vlcc pRenlneNT *me~ cone 7ic 546.2700 0 cQ Q~q p April 7, 1975

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coM"k~MI T L 0 5 0 0 2 4 4 3 2 4 7 5 0 4.0 7 7 5 7 8 57 58 59 60 61 68 69 74 75 80 I

EVENT DESCRIPTION Jog During eddy current inspection of Steam Generator (SG) tubes results showed 10 "A" SG 7 8 9 80 hot leg tubes and 12 "8" SG hot leg tubes with wall thinning of 50% or reater. Tube 7 8 9 80 t00j4 thinning in the "A" SG was previously reported, AOR 74-02, on 2/19/74 with a follow-7 8 80 Jog up report on 3/21/74. The above tubes are to be plugged. (Abnormal Occurrence 7 8 80 Jog 50-244/75-07) 7 8 9 PF4VIE 80 ~

SYSTEM CAUSE COMPONENT COMPONENT CODE CODE COMPONENT CODE SUPPUER MANUFACTURER VIOIATION

~07 ~CI 8 9 10 B H T B 7I C H ~N W 1 2 0 N 7 11 12 17 43 44 47 48 CAUSE DESCRIPTION IOOI Local corrosion of tube OD surface is believed to have been caused by phosphate

.7 8 9 80 Jog residue not removed on change to AVT chem. control. SG descri tive data and 7 8 9 Qio] measures to prevent recurrence are on attached page.

7 8 9 80 FACIUTY METHOO OF OTHER STATUS OISCOVERY OISCOVERY OESCRIPTION G ~00 0 N/A C eddy current test of tubes 7 8 9 10 12 13 44 45 46 80 FORM OF AMOUNT OF ACTIVITY LOCATION OF RELEASE N/A 7 8 9 10 11 44 45 80 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION

~00 0 B -

N A 7 8 9 11 12 13 80 PERSONNEL INJURIES 7 8 9 11 12 80 OFFSITE CONSEQUENCES N/A 7 89 80 LOSS OR DAMAGE TO FACILITY 7 89 10 PUBLICITY i N/A

.7 89 80 ADDITIONAL FACTORS

+18 Shell side sludge removal was done 3/74 and 11/74. An AVT S.G. chem. control 7 89 80 Q~g] program was started ll/74 and adherence to this has been good to date.

7 89 80 NAME: L. D. White, Jr. PHDNE 7 1 6/54 6-2 700, ext . 2420 GPO 88I 667

Licensee Event Rei ~rt 2.

50-244/75-07 Steam Generator Descri tive Data:

The steam generators are Westinghouse series 44, using Inconel series 600 tubes, size 0.875" OD, with .050" walls.

Measures to Prevent Recurrence:

a. The shell side of the tube sheets will be cleaned using a high pressure water lance. against attack which may be due to any remaining phosphates or caustics contained in sludge.
b. For further information on the tube degradation mechanism, at least two tube ends are to be extracted from the steam generators.
c. A series of mechanical modifications is being considered to decrease the area of the tube sheet which is susceptible to low flow conditions and sludge buildup.
d. A high blowdown rate during varying steam generator conditions will be continued to minimize dissolved and suspended solids, consistent with recommended all volatile treatment (AVT) steam generator chemistry control.
e. In the event that sludge accumulation continues to be observed in future

~

shutdowns, additional lancings may be considered to lower residual phosphate levels in the steam generators.