ML18093A140

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Special Rept 87-3:on 870514,svc Water Leak from Hole in Containment Fan Coil Unit 12 Detected.Caused by Corrosion. Spoolpiece Replaced.Program for Investigating Corrosion Problems Underway
ML18093A140
Person / Time
Site: Salem PSEG icon.png
Issue date: 05/28/1987
From: Zupko J
Public Service Enterprise Group
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
87-3, IEB-80-24, NUDOCS 8706030328
Download: ML18093A140 (3)


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'*I Public Service Electric and Gas Company P.O. Box E Hancocks B1*idQe, New Jersey 08038 Salem Generating Station May 28, 1987 U. S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555

Dear Sir:

SALEM GENERATING STATION LICENSE NO. DPR-70 DOCKET NO. 50-272 UNIT NO. 1 REPORT 87-3 SPECIAL REPORT This Special Report describes the circumstances surrounding a Service Water leak inside the containment. This report is being submitted within fourteen days of the occurrence in accordance with the reporting requirements of I.E. Bulletin 80-24.

Sincerely yours, J. Uf. ~f ~"i ;r~

J. M. Zupko, Jr.

General Manager-Salem Operations RKH:pc Distribution 8706030328 870528 PDR ADOCK 05000272 PDR s

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SPECIAL REPORT NUMBER 8.3

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PLANT IDENTIFICATION:

Salem Generating Station - Unit 1 Public Service Electric & Gas Company Hancock's Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

SERVICE WATER LEAK INSIDE CONTAINMENT - NO. 12 CONTAINMENT FAN COIL UNIT MOTOR COOLER LEAK DUE TO CORROSION Event Date(s): 05/14/87 Report Date: 05/28/87 This report was initiated by Incident Report No.87-186 CONDITIONS PRIOR TO OCCURRENCE:

Mode 1 - Rx Power 100% - Unit Load 1152MWe DESCRIPTION OF OCCURRENCE:

On May 14, 1987, during routine power operation, the shift noticed an increase in the containment sump leak rate to 7.5 gpm. Due to the unidentified leakage being greater than 1 gpm, Action Statement 3.4.6.2 was entered at 0353 hours0.00409 days <br />0.0981 hours <br />5.83664e-4 weeks <br />1.343165e-4 months <br />. Subsequent performance of a Reactor Coolant System (RCS) Inventory did not indicate a leak from the Chemical Volume and Control System (CVCS) or the RCS. Therefore, a containment entry was performed and it was discovered that No. 12 Containment Fan Coil Unit (CFCU) had developed a leak in a carbon steel fitting in the two (2) inch motor cooler service water outlet line. The CFCU was isolated and Technical Specification Action 3.6.2.3.a was entered at 0434 hours0.00502 days <br />0.121 hours <br />7.175926e-4 weeks <br />1.65137e-4 months <br />. Action Statement 3.4.6.2 was subsequently terminated at 0457 hours0.00529 days <br />0.127 hours <br />7.556217e-4 weeks <br />1.738885e-4 months <br />, when leakage was demonstrated to be well within specified limits. The NRC was notified at 0500 hours0.00579 days <br />0.139 hours <br />8.267196e-4 weeks <br />1.9025e-4 months <br /> the same day. Subsequently, on May 17, 1987, at 2010 hours0.0233 days <br />0.558 hours <br />0.00332 weeks <br />7.64805e-4 months <br />, No. 12 CFCU was restored to operable status and Action Statement 3.6.2.3.a was terminated.

APPARENT CAUSE OF OCCURRENCE:

Upon investigation, a hole was found in the side wall of a two (2) inch service water "tee" fitting, which was the location of a thermo-well. The indications show the hole to have been formed by corrosion. No other similarly corroded fittings were discovered.

ANALYSIS OF OCCURRENCE:

An increase in containment sump inleakage is the primary indication of the development of RCS or other system leakage. Continuous monitoring of the sump inleakage allows early detection of a potential problem and provides a basis for initiation of appropriate actions to identify, isolate, and repair the leak.

UNIT 1 SPECIAL REPORT 8.3 ANALYSIS OF OCCURRENCE: (cont'd)

Performance of an RCS water inventory balance in conjunction with a containment entry to locate the source of the inleakage is the appropriate action.

The unavailability of one CFCU does not significantly affect the ability to provide containment cooling. During normal operation there are one or more idle CFCUs, depending on containment temperature. During an accident condition, the CFCUs provide one hundred percent (100%) redundancy to the. Containment Spray System for cooling and depressurizing the containment.

PSE&G performed a study in July 1985 (as documented by Engineering Safety Evaluation S-C-M600-NSE-228, Rev. 2, "Safety Considerations of a Containment Fan Coil Unit Tube Severance") which addresses concerns associated with service water leakage from a CFCU during LOCA conditions. The study concluded that the present detection systems (e.g., mismatch detection between service water inlet and outlet flow and the containment water level monitoring system) are adequate for detecting major service water leakage from the CFCUs. Also, minor leakage can be detected through sampling and administrative controls.

The study also addresses concerns associated with exceeding the design flood level, potential boron dilution, chloride contamination and pH effects. These concerns are adequately addressed by the current plant design and administrative controls in effect.

Based tipon the above analysis, this occurrence involved no undue risk to the health and safety of the public, and no equipment damage resulted from the service water leak. However, all service water leaks inside con~ainment are reportable in accordance with I.E.

Bulletin No. 80-24.

CORRECTIVE ACTION:

The entire spoolpiece containing the corroded "tee" fitting was replaced with one made from stainless steel. Our program for investigation of corrosion problems with the Service Water System and replacement of affected piping with piping made from more corrosion resistant materials is currently in progress. Additional research is continuing in this area.

J, ft!, l(yl, J/l)w General Manager -

Salem Operations RKH:pc SORC Mtg.87-035