Similar Documents at Cook |
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217J4721999-10-15015 October 1999 Forwards NRC Physical Security Insp Repts 50-315/99-27 & 50-316/99-27 on 990920-24.Two Violations Noted & Being Treated as Ncvs,Consistent with App C of Enforcement Policy. Areas Examined Exempt from Disclosure,Per 10CFR73.21 IA-99-379, First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety1999-10-0808 October 1999 First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety ML20217D9241999-10-0808 October 1999 First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety ML17335A5511999-10-0707 October 1999 Forwards LER 99-023-00, Inadequate TS Surveillance Testing of ESW Pump ESF Response Time. Commitments Identified in LER Listed ML20217D9361999-09-30030 September 1999 FOIA Request for Document Re Section 9.7 of SE by Directorate of Licensing,Us Ae Commission in Matter of Indiana & Michigan Electric Co & Indiana & Michigan Power Co,Dc Cook Nuclear Plan,Units 1 & 2 ML17326A1541999-09-20020 September 1999 Provides Notification of Change in Senior Licensed Operator Status.Operating Licenses for CR Smith,License SOP-30159-4 & Tw Welch,License SOP-30654-2 Are No Longer Required & Should Be Withdrawn ML17326A1441999-09-17017 September 1999 Submits Trace on Second Shipment of Two Plant,Unit 2 Steam Generators.Info Re Shipment Submitted ML17326A1261999-09-17017 September 1999 Forwards LER 99-022-00 Re Electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads.Listed Commitment Identified in Submittal ML17326A1531999-09-16016 September 1999 Submits Info Pertaining to Plant Proposed Operator Licensing Exam Requirements Through Yr 2003.NRC Form 536, Operator Licensing Exam Data, Which Provides Required Info Encl ML17326A1101999-08-27027 August 1999 Forwards LER 99-021-00, GL 96-01 Test Requirements Not Met in Surveillance Tests. List of Commitments Identified in LER Provided ML17326A0991999-08-26026 August 1999 Forwards LER 99-020-00,re EDGs Being Declared Inoperable. Commitments Made by Util Are Listed ML17326A1221999-08-23023 August 1999 Forwards Revised Page 2 to 1998 Annual Environ Operating Rept, for DC Cook Nuclear Plant,Correcting Omission to App I ML17326A0981999-08-23023 August 1999 Forwards fitness-for-duty Program Performance Data for Period of 990101-0630 for DC Cook Nuclear Plants,Units 1 & 2,per 10CFR26.71(d) ML17326A0891999-08-16016 August 1999 Forwards LER 99-019-00,re Victoreen Containment High Range Monitors Not Beign Environmentally Qualified to Withstand post-LOCA Conditions.Commitments Made by Util Are Listed ML17326A0811999-08-10010 August 1999 Notifies NRC of Changes in Commitments Made in Response to GL 98-01,supplement 1, Yr 2000 Readiness of Computer Sys Ar Npps, Dtd 990623 ML17326A0821999-08-0606 August 1999 Informs That Util Is Submitting Encl Scope & Objectives for 991026 DC Cook Nuclear Plant Emergency Plan Exercise to G Shear of NRC Plant Support Branch.Exercise Will Include Full State & County Participation ML17326A1451999-08-0404 August 1999 Requests Withholding of WCAP-15246, Control Rod Insertion Following Cold Leg Lbloca. ML17326A0751999-08-0404 August 1999 Forwards LER 98-029-01, Fuel Handling Area Ventilation Sys Inoperable Due to Original Design Deficiency. Supplemental Rept Represents Extensive Rev to Original LER & Replaces Rept in Entirely.Commitment Listed ML17326A0721999-07-29029 July 1999 Forwards LER 99-018-00 Re Refueling Water Storage Tank Suction Motor Operated Valves Inoperable,Due to Inadequate Design.Listed Commitments Were Identified in LER ML17326A0711999-07-27027 July 1999 Responds to 980123 RAI Re NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issue (USI) A-46. ML17326A0601999-07-22022 July 1999 Forwards UFSAR, IAW 10CFR50.71(e) & Rept of Changes,Tests & Experiments as Required by 10CFR50.59(b)(2) for DC Cook Nuclear Plant,Units 1 & 2.Without UFSAR ML17326A0631999-07-22022 July 1999 Forwards LER 98-014-03, Response to High-High Containment Pressure Procedure Not Consistent with Analysis of Record. Revised Info Marked by Sidebars in Right Hand Margin. Commitments Made by Util,Listed ML17326A0311999-07-0101 July 1999 Forwards LER 99-004-01 Re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitments Made by Util Are Listed ML20196K5961999-06-30030 June 1999 Ltr Contract:Task Order 40, DC Cook Extended Sys Regulatory Review Oversight Insp, Under Contract NRC-03-98-021 ML17326A0281999-06-28028 June 1999 Provides Response to 981116 & 960228 RAIs Re GL 92-01. Revised Pressurized Thermal Shock Evaluation Based on New Weld Chemistry Info & Copy of W Rept WCAP-15074, Evaluation of 1P3571 Weld Metal from Surveillance Programs... Encl ML17326A0241999-06-23023 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant & List of Commitments Encl ML17326A0121999-06-18018 June 1999 Forwards LER 99-014-00 Re Requirement of TS 4.0.5 Not Met for Boron Injection Tank Bolting.Commitments Identified in Submittal Listed ML17326A0111999-06-11011 June 1999 Provides Response to NRC RAI Re GL 97-01, Degradation of Crdm/Cedm Nozzle & Other Vessel Closure Head Penetrations. ML17325B6281999-06-0101 June 1999 Forwards LER 99-S03-00,re Nonconforming Vital Area Barriers.Commitments Made by Util Are Listed ML17325B6401999-06-0101 June 1999 Forwards LER 99-013-00 Re Safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Lead to ECCS Pump Failure.Listed Commitments Identified in Submittal ML17325B6331999-05-28028 May 1999 Forwards LER 99-S02-00,re Vulnerability in Safeguard Sys That Could Allow Unauthorized or Undetected Access to Protected Area.Commitments Made by Util Are Listed ML17265A8201999-05-24024 May 1999 Forwards LER 98-037-01,representing Extensive Rev to Original LER & Replacing Rept in Entirety.Listed Commitments Identified in Submittal ML20207A9201999-05-21021 May 1999 Ack Receipt of 990319 Response to Notice of Violation & Proposed Imposition of Civil Penalty .On 981124, Licensee Remitted Check for Payment of Civil Penalties. Licensee Requests for Extension for Response,Granted ML17325B6111999-05-21021 May 1999 Forwards Annual Radioactive Effluent Release Rept for 980101-1231 for DC Cook Nuclear Plant,Units 1 & 2. Transmittal of Submittal Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17325B6031999-05-21021 May 1999 Provides Response to NRC GL 98-04, Potential for Degradation of ECCS & Containment Spray Sys After LOCA Because of Const & Protective Coating Deficiencies & Foreign Matl in Containment. ML17325B5971999-05-20020 May 1999 Forwards LER 99-012-00,re Auxiliary Building ESF Ventilation Sys Not Being Capable of Maintaining ESF Room Temps post-accident.Commitment,listed ML17335A5281999-05-12012 May 1999 Forwards DC Cook Nuclear Plant Fitness for Duty Program Performance Dtd for six-month Period of 980701-1231,IAW 10CFR26.71(d).Info Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17335A5271999-05-11011 May 1999 Forwards Details Re Sources & Levels of Insurance Maintained for DC Cook,Units 1 & 2,as of 990401,per 10CFR50.54(w)(3). Info Was Delayed Beyond Required Date Due to Internal Oversight ML17325B5841999-05-10010 May 1999 Forwards LER 99-002-00 Re TS 4.0.5 Requirements Not Being Met Due to Improperly Performed Test.Commitments Identified in Ler,Listed ML17325B5871999-05-0707 May 1999 Forwards Current Revs of Expanded Sys Readiness Review (Essr) Implementing Procedures,For Info Purposes to Support Current NRC Insps.Current Esrr Schedule Provided for Info Purposes,Reflecting Revised Target Dates ML17325B5791999-05-0404 May 1999 Forwards LER 99-011-00,concerning Air Sys for EDG Not Supporting Long Term Operability.Commitments Made by Util Listed ML17325B5821999-05-0404 May 1999 Provides Addl Background,Description & Clarification of Previous & Revised Commitments Re UFSAR Revalidation Effort. Commitment Change Involved Alignment of UFSAR Revalidation Program Methodology to Strategy Contained in Current Plan ML17325B5741999-05-0303 May 1999 Forwards LER 99-010-00 Re RCS Leak Detection Sys Sensitivity Not in Accoradnce with Design Requirements.Listed Commitments Identified in Submittal ML17325B5631999-04-22022 April 1999 Forwards Results of Independent Chemical Evaluations Performed from Sept 1997 Through Feb 1999,re Resolution of Issues Related to License Amend 227 ML17325B5561999-04-16016 April 1999 Forwards LER 99-006-00, Fuel Crane Loads Lifted Over SFP Could Impact Energies Greater than TS Limits, IAW 10CFR50.73.Submittal Was Delayed to Allow for Resolution of Questions.Commitment Made by Licensee,Listed ML20205P0591999-04-14014 April 1999 Ninth Partial Response to FOIA Request for Documents.App Records Already Available in Pdr.Records in App T Encl & Being Made Available in Pdr.App U Records Being Released in Part (Ref FOIA Exemption 7).App V Records Withheld Entirely ML17325B5451999-04-12012 April 1999 Forwards LER 99-009-00 Re as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit.Commitments Identified in Submittal Listed ML17325B5301999-04-0707 April 1999 Forwards LER 99-S01-01, Vulnerability in Locking Mechanism of Four Vital Area Gates, Per 10CFR50.73.Commitments Made by Util,Listed ML17325B5241999-04-0505 April 1999 Forwards Revs 0 & 1 to Cook Nuclear Plant Restart Plan, Dtd 980307 & 0407.Rev 5 Is Current Cook Nuclear Plant Restart & Supercedes Previous Revs in All Respects ML17325B5121999-04-0101 April 1999 Forwards LER 99-007-00, Calculations Show That Divider Barrier Between Upper & Lower Containment Vols May Be Overstressed. Commitments Made by Util Are Listed 1999-09-30
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML17335A5511999-10-0707 October 1999 Forwards LER 99-023-00, Inadequate TS Surveillance Testing of ESW Pump ESF Response Time. Commitments Identified in LER Listed ML20217D9361999-09-30030 September 1999 FOIA Request for Document Re Section 9.7 of SE by Directorate of Licensing,Us Ae Commission in Matter of Indiana & Michigan Electric Co & Indiana & Michigan Power Co,Dc Cook Nuclear Plan,Units 1 & 2 ML17326A1541999-09-20020 September 1999 Provides Notification of Change in Senior Licensed Operator Status.Operating Licenses for CR Smith,License SOP-30159-4 & Tw Welch,License SOP-30654-2 Are No Longer Required & Should Be Withdrawn ML17326A1261999-09-17017 September 1999 Forwards LER 99-022-00 Re Electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads.Listed Commitment Identified in Submittal ML17326A1441999-09-17017 September 1999 Submits Trace on Second Shipment of Two Plant,Unit 2 Steam Generators.Info Re Shipment Submitted ML17326A1531999-09-16016 September 1999 Submits Info Pertaining to Plant Proposed Operator Licensing Exam Requirements Through Yr 2003.NRC Form 536, Operator Licensing Exam Data, Which Provides Required Info Encl ML17326A1101999-08-27027 August 1999 Forwards LER 99-021-00, GL 96-01 Test Requirements Not Met in Surveillance Tests. List of Commitments Identified in LER Provided ML17326A0991999-08-26026 August 1999 Forwards LER 99-020-00,re EDGs Being Declared Inoperable. Commitments Made by Util Are Listed ML17326A1221999-08-23023 August 1999 Forwards Revised Page 2 to 1998 Annual Environ Operating Rept, for DC Cook Nuclear Plant,Correcting Omission to App I ML17326A0981999-08-23023 August 1999 Forwards fitness-for-duty Program Performance Data for Period of 990101-0630 for DC Cook Nuclear Plants,Units 1 & 2,per 10CFR26.71(d) ML17326A0891999-08-16016 August 1999 Forwards LER 99-019-00,re Victoreen Containment High Range Monitors Not Beign Environmentally Qualified to Withstand post-LOCA Conditions.Commitments Made by Util Are Listed ML17326A0811999-08-10010 August 1999 Notifies NRC of Changes in Commitments Made in Response to GL 98-01,supplement 1, Yr 2000 Readiness of Computer Sys Ar Npps, Dtd 990623 ML17326A0821999-08-0606 August 1999 Informs That Util Is Submitting Encl Scope & Objectives for 991026 DC Cook Nuclear Plant Emergency Plan Exercise to G Shear of NRC Plant Support Branch.Exercise Will Include Full State & County Participation ML17326A1451999-08-0404 August 1999 Requests Withholding of WCAP-15246, Control Rod Insertion Following Cold Leg Lbloca. ML17326A0751999-08-0404 August 1999 Forwards LER 98-029-01, Fuel Handling Area Ventilation Sys Inoperable Due to Original Design Deficiency. Supplemental Rept Represents Extensive Rev to Original LER & Replaces Rept in Entirely.Commitment Listed ML17326A0721999-07-29029 July 1999 Forwards LER 99-018-00 Re Refueling Water Storage Tank Suction Motor Operated Valves Inoperable,Due to Inadequate Design.Listed Commitments Were Identified in LER ML17326A0711999-07-27027 July 1999 Responds to 980123 RAI Re NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issue (USI) A-46. ML17326A0601999-07-22022 July 1999 Forwards UFSAR, IAW 10CFR50.71(e) & Rept of Changes,Tests & Experiments as Required by 10CFR50.59(b)(2) for DC Cook Nuclear Plant,Units 1 & 2.Without UFSAR ML17326A0631999-07-22022 July 1999 Forwards LER 98-014-03, Response to High-High Containment Pressure Procedure Not Consistent with Analysis of Record. Revised Info Marked by Sidebars in Right Hand Margin. Commitments Made by Util,Listed ML17326A0311999-07-0101 July 1999 Forwards LER 99-004-01 Re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitments Made by Util Are Listed ML17326A0281999-06-28028 June 1999 Provides Response to 981116 & 960228 RAIs Re GL 92-01. Revised Pressurized Thermal Shock Evaluation Based on New Weld Chemistry Info & Copy of W Rept WCAP-15074, Evaluation of 1P3571 Weld Metal from Surveillance Programs... Encl ML17326A0241999-06-23023 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant & List of Commitments Encl ML17326A0121999-06-18018 June 1999 Forwards LER 99-014-00 Re Requirement of TS 4.0.5 Not Met for Boron Injection Tank Bolting.Commitments Identified in Submittal Listed ML17326A0111999-06-11011 June 1999 Provides Response to NRC RAI Re GL 97-01, Degradation of Crdm/Cedm Nozzle & Other Vessel Closure Head Penetrations. ML17325B6401999-06-0101 June 1999 Forwards LER 99-013-00 Re Safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Lead to ECCS Pump Failure.Listed Commitments Identified in Submittal ML17325B6281999-06-0101 June 1999 Forwards LER 99-S03-00,re Nonconforming Vital Area Barriers.Commitments Made by Util Are Listed ML17325B6331999-05-28028 May 1999 Forwards LER 99-S02-00,re Vulnerability in Safeguard Sys That Could Allow Unauthorized or Undetected Access to Protected Area.Commitments Made by Util Are Listed ML17265A8201999-05-24024 May 1999 Forwards LER 98-037-01,representing Extensive Rev to Original LER & Replacing Rept in Entirety.Listed Commitments Identified in Submittal ML17325B6111999-05-21021 May 1999 Forwards Annual Radioactive Effluent Release Rept for 980101-1231 for DC Cook Nuclear Plant,Units 1 & 2. Transmittal of Submittal Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17325B6031999-05-21021 May 1999 Provides Response to NRC GL 98-04, Potential for Degradation of ECCS & Containment Spray Sys After LOCA Because of Const & Protective Coating Deficiencies & Foreign Matl in Containment. ML17325B5971999-05-20020 May 1999 Forwards LER 99-012-00,re Auxiliary Building ESF Ventilation Sys Not Being Capable of Maintaining ESF Room Temps post-accident.Commitment,listed ML17335A5281999-05-12012 May 1999 Forwards DC Cook Nuclear Plant Fitness for Duty Program Performance Dtd for six-month Period of 980701-1231,IAW 10CFR26.71(d).Info Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17335A5271999-05-11011 May 1999 Forwards Details Re Sources & Levels of Insurance Maintained for DC Cook,Units 1 & 2,as of 990401,per 10CFR50.54(w)(3). Info Was Delayed Beyond Required Date Due to Internal Oversight ML17325B5841999-05-10010 May 1999 Forwards LER 99-002-00 Re TS 4.0.5 Requirements Not Being Met Due to Improperly Performed Test.Commitments Identified in Ler,Listed ML17325B5871999-05-0707 May 1999 Forwards Current Revs of Expanded Sys Readiness Review (Essr) Implementing Procedures,For Info Purposes to Support Current NRC Insps.Current Esrr Schedule Provided for Info Purposes,Reflecting Revised Target Dates ML17325B5821999-05-0404 May 1999 Provides Addl Background,Description & Clarification of Previous & Revised Commitments Re UFSAR Revalidation Effort. Commitment Change Involved Alignment of UFSAR Revalidation Program Methodology to Strategy Contained in Current Plan ML17325B5791999-05-0404 May 1999 Forwards LER 99-011-00,concerning Air Sys for EDG Not Supporting Long Term Operability.Commitments Made by Util Listed ML17325B5741999-05-0303 May 1999 Forwards LER 99-010-00 Re RCS Leak Detection Sys Sensitivity Not in Accoradnce with Design Requirements.Listed Commitments Identified in Submittal ML17325B5631999-04-22022 April 1999 Forwards Results of Independent Chemical Evaluations Performed from Sept 1997 Through Feb 1999,re Resolution of Issues Related to License Amend 227 ML17325B5561999-04-16016 April 1999 Forwards LER 99-006-00, Fuel Crane Loads Lifted Over SFP Could Impact Energies Greater than TS Limits, IAW 10CFR50.73.Submittal Was Delayed to Allow for Resolution of Questions.Commitment Made by Licensee,Listed ML17325B5451999-04-12012 April 1999 Forwards LER 99-009-00 Re as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit.Commitments Identified in Submittal Listed ML17325B5301999-04-0707 April 1999 Forwards LER 99-S01-01, Vulnerability in Locking Mechanism of Four Vital Area Gates, Per 10CFR50.73.Commitments Made by Util,Listed ML17325B5241999-04-0505 April 1999 Forwards Revs 0 & 1 to Cook Nuclear Plant Restart Plan, Dtd 980307 & 0407.Rev 5 Is Current Cook Nuclear Plant Restart & Supercedes Previous Revs in All Respects ML17325B5121999-04-0101 April 1999 Forwards LER 99-007-00, Calculations Show That Divider Barrier Between Upper & Lower Containment Vols May Be Overstressed. Commitments Made by Util Are Listed ML17325B5141999-03-30030 March 1999 Forwards Rept on Status of Decommissioning Funding.Attached Rept Includes Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML17325B5191999-03-29029 March 1999 Forwards LER 99-001-00,re Degraded Component Cw Flow to Containment Main Steam Line Penetrations.Commitment, Listed ML20204F6401999-03-19019 March 1999 Responds to NRC 981013 NOV & Proposed Imposition of Civil Penalty.Violations Cited in Subject NOV Were Initially Identified in Referenced Five Insp Repts.Corrective Actions: Ice Condensers Have Been Completely Thawed of Any Blockage ML17325B4751999-03-18018 March 1999 Forwards LER 99-004-00,re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitment Made by Util,Listed ML17325B4721999-03-18018 March 1999 Forwards LER 99-005-00,re Reactor Trip Breaker Manual Actuations During Rod Drop Testing Not Previously Reported. Listed Commitments Identified in Submittal ML17325B4641999-03-17017 March 1999 Withdraws Response to Issue 1 of NRC Cal,Dtd 970919. Comprehensive Design Review Effort in Progress to Validate Resolution of Issue for Future Operation 1999-09-30
[Table view] |
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CATEGORY 1 REGUI ATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
CESSION NBR:9603150080 DOC.DATE: 96/03/09 NOTARIZED: YES DOCKET CIL:50-33.b Donald C. Cook Nuclear Power Plant, Unit 1, Indiana M 05000315
,-50-316 Donald C. Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH. NAME AUTHOR AFFILIATION FITZPATRICK,E. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele RECIP.NAME RECIPIENT AFFILIATION Document .Control Branch (Document Control Desk)
SUBJECT:
Forwards response to violations noted in Insp Repts 50-315/95-13 a 50-316/95-13.Corrective actions:appropriate scheduling logic changes have been incorporated for both turbine driven AFP,preclude TS surveillance.
DISTRIBUTION CODE: IE01D COPIES RECEIVED:LTR .ENCL SIZE:
TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-1 PD 1 1 HICKMANIJ 1 1 INTERNAL: AEOD/DEIB 1 1 AEOD/SPD/RAB 1 1 O~ 1 1 DEDRO 1 1 FILE CENTER 1 1 NRR/DI SP/PIPB 1 1 HHFB 1 1 NRR/DRPM/PECB 1 1 NRR/DRPM/PERB 1 1 NUDOCS-ABSTRACT 1 1 OE DIR 1 1 OGC/HDS2 1 1 RGN3 FILE 01 1 1 D
EXTERNAL: LITCO BRYCE,J H 1 1 NOAC 1 1 NRC PDR 1 1 0 U
N NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE) CONTACT THE DOCUMENT CONTROL DESK, ROOM OWFN 5D-5(EXT. 415-2083) TO ELIMINATE YOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEEDI TOTAL NUMBER OF COPIES REQUIRED: LTTR 18 ENCL . 18
indiana Michigan Power Company PO Box 16631 Columbus, OH 43216 INDMNA NICHEGAN POWER March 9, 1996 AEP: NRC: 1224G 10 CFR 2.201 Docket Nos.: 50-315 50-316 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C. 20555 1 Gentlemen:
Donald C. Cook Nuclear Plant Units 1 and 2 NRC INSPECTION REPORTS NO. 50-315/95013 (DRP)
AND 50-316/95013 (DRP)
REPLY TO NOTICE OF VIOIATIONS This letter is in response to a letter from W. J. Kropp dated February 8, 1996, that forwarded a notice of violation to Indiana Michigan Power Company. Two violations were identified during a routine safety inspection conducted by Messrs. Bartlett, Hartland, Orsini, Paul, Fuller, and Shah from December 5, 1995, through January 16, 1996. One violation is associated with Technical Specification surveillances which were not 'accomplished under suitably controlled conditions. The second violation is associated with not testing the Unit 2 CD diesel generator within the required surveillance interval including the maximum allowable extension.
Our reply to the violations is provided in the attachment to this letter. The reply does not contain any personal privacy, proprietary, or safeguards information.
pM E. E. Fitzpatrick Vice President SWORN TO AND SUBSCRIBED BEFORE ME THIS DAY OF 1996 Notary P blic
~-p/
9603150080 960309 PDR ADOCK 05000315 8 PDR
U. S. Nuclear Regulatory Commission AEP:NRC:1224G Page 2 pit Attachment CC: A. A. Blind G. Charnoff H. J. Miller NFEM Section Chief NRC Resident Inspector - Bridgman J. R. Padgett W. T. Russell - NRC NRR
ATTACHMENT TO AEP:NRC:1224G REPLY TO NOTICE OF VIOLATION'RC INSPECTION REPORT NOS. 50-315/95013 (DRP)
AND 50-316/95013 (DRP)
ATTACHMENT TO AEP NRC 1224G Page 1 During an NRC inspection conducted December 5, 1995, through January 16, 1996, two violations of NRC requirements were identified. In accordance with the "General Statement of Policy and Piocedures for NRC Enforcement Actions," (60 FR 34381, June 30, 1995) the violations and the Donald C. Cook Nuclear Plant response are provided below.
C Violat on I "10 CFR 50, Appendix B, Criterion II, '~ality Assurance',
requires, in part, that activities affecting quality shall be accomplished under suitably controlled conditions. Surveillance testing required by Technical Specifications (T/S) to verify operability of equipment is an activity affecting quality.
Contrary to the above, T/S surveillances were not accomplished under suitably controlled conditions, in that:
- l. In May and September 1994, the Unit 2 turbine driven auxiliary feedwater pump (TDAFP) trip and throttle valve was tested and the pump operated just prior to performing the T/S required surveillance 4.7.1.2.'.
On numerous occasions, including January 16, 1996, the Unit 2 AB emergency diesel generator (D/G) was rolled per surveillance procedure, OHP 4030 STP.027AB/CD. This roll used the starting air system and was performed prior to the part of. the surveillance that verified the D/G capability to meet T/S fast start criteria. This resulted in exercising several components in the starting air system prior to verifying the D/G fast start capabilities.
This is a Severity Level IV violation (Supplement I)."
es onse to NRC Violation dmission or Denial of t e lie ed Violatio Indiana Michigan Power admits to the violation as cited in the NRC Notice of Violation, except that, as a matter of record, the two instances cited with regard to the TDAFPs are incorrect: they occurred in April 1994 on the Unit 2 TDAFP and in September 1994 on the Unit 1 TDAFP.
In addition, the resident inspector brought to our attention a third instance of preconditioning that he discovered concerning a monthly preventive maintenance (PM) activity to lubricate and exercise the fuel racks on'the D/Gs. This is planned and scheduled independently of the monthly D/G T/S surveillance. On January 23, 1996, the resident inspector observed that the PM activity occurred prior to the T/S
ATTACHMENT TO AEP NRC 1224G Page 2 surveillance on the same day. This additional instance is also addressed in our response below.
- 2. easons o the Vio at o The reason for this violation is the absence of guidance that ensures that T/S surveillances are performed without preconditioning of the component or equipment prior to performing the surveillance.
- 3. Corrective Actions Taken and Results Achieved With regard to the TDAFPs, appropriate scheduling logic changes have been incorporated for both TDAFPs that preclude the T/S surveillance from being preceded by trip and throttle valve testing and pump operation. All quarterly T/S surveillances on TDAFPs since December 1995 have been performed using the revised scheduling logic. All of these T/S surveillances were completed with satisfactory results.
With regard to the Unit 2 AB D/G, appropriate procedure and work control process changes have been incorporated to modify how the D/G T/S surveillance is performed. These changes were made in accordance with the guidelines that were provided to the NRC in our letter AEP:NRC:1224D, dated January 6, 1996, which was made in response to unresolved item 95010-01. All D/Gs at Cook Nuclear Plant are presently considered operable.
With regard to the D/G fuel racks, notes have been added to the job orders for the PM tasks that will preclude the PM task from being scheduled immediately prior to the T/S surveillance.
- 4. Corrective Actions Taken to Avoid Further Violations In response to this notice of violation, a multi-disciplinary task force was created to address the issue of preconditioning on a generic basis. The task force is developing a program designed to ensure that preconditioning prior to T/S surveillances does not recur.
To preclude preconditioning, the following actions have been taken or are planned.
Written guidance will be issued by March 15, 1996, to address potential preconditioning concerns that may arise in the immediate future for associated T/S surveillance activities during the Unit 2 refueling outage and Units 1 and 2 normal plant operations. The guidance will provide direction in identification and
ATTACHMENT TO AEP 'NRC: 1224G Page 3 timely resolution of possible preconditioning items as they arise.
T/S surveillance procedures performed on an operating unit s equipment will be reviewed to identify and correct any procedures in which preconditioning is inadvertently caused by actions taken in procedure steps preceding the actual surveillance procedure steps. This will be accomplished prior to January 31, 1997.
T/S surveillance procedures performed during outages will be reviewed to identify and correct any procedures in which preconditioning is inadvertently caused by actions taken in procedure steps preceding the actual surveillance procedure steps. This will be accomplished on a schedule consistent with the procedure review requirements for future refueling outages: for Unit 1, September 1, 1996, for the spring 1997 refueling outage; for Unit 2, May 1, 1997, for the autumn 1997 refueling outage.
During work control process schedule periods in which a T/S surveillance is scheduled to be performed on equipment which is required to support an operating unit, should there be any type of potentially preconditioning activity scheduled for that same equipment during the same period, the situation will be evaluated to determine if the T/S surveillance should be performed prior to the other activities. Guidance will be provided to appropriate personnel to identify and address any preconditioning issues during the execution of the T/S surveillances. The scheduling philosophy and programmatic enhancements will be implemented prior to July 6, 1996.
- 5. ate w en ull Com 1 a ce W be c ivd Full compliance has been achieved with regard to the cited instances pertaining to the TDAFPs and D/Gs, and with regard to the additional item identified by the resident inspector.
With regard to ensuring that preconditioning does not recur at Cook Nuclear Plant, full compliance will be achieved on or prior to May 1, 1997, with the completion of the full review of all T/S surveillance procedures.
ATTACHMENT TO AEP:NRC: 1224G Page 4 C Violation II "Technical Specification 4.0.2 states that each surveillance requirement shall be performed within the specified time interval with a maximum allowable extension not to exceed 25% of the specified surveillance interval.
Technical Specification 4.8.1.1.2 states, in part, that each diesel generator shall be demonstrated operable .. in accordance with the
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frequency specified in Table 4.8-1.
Table 4.8-1 states, in part, that if the number of failures in the last 20 valid tests is greater than or equal to 2, then the diesel generator shall be tested at least once per 7 days.
Contrary to the above, from January 5 to January 15, 1996, with two failures in the last 20 valid tests, the licensee did not test the Unit 2 CD diesel generator (D/G) within the required surveillance interval including the maximum allowable extension.
This is a Severity Level IV violation (Supplement I)."
es onse to NRC Violation dm ssion or Den al o t e A e ed V o at o Indiana Michigan Power a'dmits to the violation as cited in the NRC Notice of Violation.
- 2. easons for the Violation The cause of the violation is personnel error. Unit 2 T/S Table 4.8-1 states that the number of D/G "failures" and the number of "valid tests" shall be determined in accordance with criteria specified in Regulatory Guide 1.108. On December 29, 1995, while the Unit 2 CD D/G was undergoing post-maintenance testing, the D/G experienced an incomplete start. Initially, in accordance with Unit 2 T/S Table 4.8-1 and Regulatory Guide 1.108, this incomplete start was considered a failure, and an increased-frequency surveillance schedule was established as required by T/S.
However, on January 2, 1996, based on an NRC letter stating that Regulatory Guide 1.108 had been incorporated into Regulatory Guide 1.9, engineering personnel incorrectly applied Regulatory Guide 1.9 to the incomplete start. This resulted in the improper categorization of the D/G incomplete start as "not a failure". T/Ss require performance of a weekly surveillance if there have been two failures within the last 20 diesel generator starts. Because the December 29, 1995, incomplete start was no longer considered a failure, the engineers believed that the weekly surveillance
ATTACHMENT TO AEP 'NRC: 1224G Page 5 requirement specified in T/Ss did not apply. The increased-frequency surveillance schedule was cancelled.
- 3. Corrective Actions a e a d esu ts eve Following additional review, it was determined that the criteria in Regulatory Guide 1.108 should have been applied to the December 29, 1995, D/G incomplete start. The incomplete start was reel,assified as a failure. The surveillance procedure was promptly performed on the Unit 2 CD D/G and the D/G was declared operable and placed on an increased-frequency surveillance schedule.
- 4. Corrective Actions Taken to Avoid Furt er V olations The engineering personnel involved with this event have been counseled on the need for strict compliance with the T/Ss and referenced documents. A T/S change request has been submitted for NRC consideration. The change, if approved, would modify T/S 3.8.1.1 to reference Regulatory Guide 1.9 instead of Regulatory Guide 1.108 for determination of diesel generator "failures" and "valid tests".
- 5. Date when Full Com liance Vill be Achieved Full compliance was achieved at 1648 hours0.0191 days <br />0.458 hours <br />0.00272 weeks <br />6.27064e-4 months <br /> on January 15, 1996, when operability of the Unit 2 CD diesel generator was demonstrated by successful completion of the surveillance procedure.
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