Similar Documents at Cook |
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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217J4721999-10-15015 October 1999 Forwards NRC Physical Security Insp Repts 50-315/99-27 & 50-316/99-27 on 990920-24.Two Violations Noted & Being Treated as Ncvs,Consistent with App C of Enforcement Policy. Areas Examined Exempt from Disclosure,Per 10CFR73.21 IA-99-379, First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety1999-10-0808 October 1999 First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety ML20217D9241999-10-0808 October 1999 First Final Response to FOIA Request for Documents.Documents Listed in App a Being Released in Entirety ML17335A5511999-10-0707 October 1999 Forwards LER 99-023-00, Inadequate TS Surveillance Testing of ESW Pump ESF Response Time. Commitments Identified in LER Listed ML20217D9361999-09-30030 September 1999 FOIA Request for Document Re Section 9.7 of SE by Directorate of Licensing,Us Ae Commission in Matter of Indiana & Michigan Electric Co & Indiana & Michigan Power Co,Dc Cook Nuclear Plan,Units 1 & 2 ML17326A1541999-09-20020 September 1999 Provides Notification of Change in Senior Licensed Operator Status.Operating Licenses for CR Smith,License SOP-30159-4 & Tw Welch,License SOP-30654-2 Are No Longer Required & Should Be Withdrawn ML17326A1441999-09-17017 September 1999 Submits Trace on Second Shipment of Two Plant,Unit 2 Steam Generators.Info Re Shipment Submitted ML17326A1261999-09-17017 September 1999 Forwards LER 99-022-00 Re Electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads.Listed Commitment Identified in Submittal ML17326A1531999-09-16016 September 1999 Submits Info Pertaining to Plant Proposed Operator Licensing Exam Requirements Through Yr 2003.NRC Form 536, Operator Licensing Exam Data, Which Provides Required Info Encl ML17326A1101999-08-27027 August 1999 Forwards LER 99-021-00, GL 96-01 Test Requirements Not Met in Surveillance Tests. List of Commitments Identified in LER Provided ML17326A0991999-08-26026 August 1999 Forwards LER 99-020-00,re EDGs Being Declared Inoperable. Commitments Made by Util Are Listed ML17326A1221999-08-23023 August 1999 Forwards Revised Page 2 to 1998 Annual Environ Operating Rept, for DC Cook Nuclear Plant,Correcting Omission to App I ML17326A0981999-08-23023 August 1999 Forwards fitness-for-duty Program Performance Data for Period of 990101-0630 for DC Cook Nuclear Plants,Units 1 & 2,per 10CFR26.71(d) ML17326A0891999-08-16016 August 1999 Forwards LER 99-019-00,re Victoreen Containment High Range Monitors Not Beign Environmentally Qualified to Withstand post-LOCA Conditions.Commitments Made by Util Are Listed ML17326A0811999-08-10010 August 1999 Notifies NRC of Changes in Commitments Made in Response to GL 98-01,supplement 1, Yr 2000 Readiness of Computer Sys Ar Npps, Dtd 990623 ML17326A0821999-08-0606 August 1999 Informs That Util Is Submitting Encl Scope & Objectives for 991026 DC Cook Nuclear Plant Emergency Plan Exercise to G Shear of NRC Plant Support Branch.Exercise Will Include Full State & County Participation ML17326A1451999-08-0404 August 1999 Requests Withholding of WCAP-15246, Control Rod Insertion Following Cold Leg Lbloca. ML17326A0751999-08-0404 August 1999 Forwards LER 98-029-01, Fuel Handling Area Ventilation Sys Inoperable Due to Original Design Deficiency. Supplemental Rept Represents Extensive Rev to Original LER & Replaces Rept in Entirely.Commitment Listed ML17326A0721999-07-29029 July 1999 Forwards LER 99-018-00 Re Refueling Water Storage Tank Suction Motor Operated Valves Inoperable,Due to Inadequate Design.Listed Commitments Were Identified in LER ML17326A0711999-07-27027 July 1999 Responds to 980123 RAI Re NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issue (USI) A-46. ML17326A0601999-07-22022 July 1999 Forwards UFSAR, IAW 10CFR50.71(e) & Rept of Changes,Tests & Experiments as Required by 10CFR50.59(b)(2) for DC Cook Nuclear Plant,Units 1 & 2.Without UFSAR ML17326A0631999-07-22022 July 1999 Forwards LER 98-014-03, Response to High-High Containment Pressure Procedure Not Consistent with Analysis of Record. Revised Info Marked by Sidebars in Right Hand Margin. Commitments Made by Util,Listed ML17326A0311999-07-0101 July 1999 Forwards LER 99-004-01 Re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitments Made by Util Are Listed ML20196K5961999-06-30030 June 1999 Ltr Contract:Task Order 40, DC Cook Extended Sys Regulatory Review Oversight Insp, Under Contract NRC-03-98-021 ML17326A0281999-06-28028 June 1999 Provides Response to 981116 & 960228 RAIs Re GL 92-01. Revised Pressurized Thermal Shock Evaluation Based on New Weld Chemistry Info & Copy of W Rept WCAP-15074, Evaluation of 1P3571 Weld Metal from Surveillance Programs... Encl ML17326A0241999-06-23023 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant & List of Commitments Encl ML17326A0121999-06-18018 June 1999 Forwards LER 99-014-00 Re Requirement of TS 4.0.5 Not Met for Boron Injection Tank Bolting.Commitments Identified in Submittal Listed ML17326A0111999-06-11011 June 1999 Provides Response to NRC RAI Re GL 97-01, Degradation of Crdm/Cedm Nozzle & Other Vessel Closure Head Penetrations. ML17325B6281999-06-0101 June 1999 Forwards LER 99-S03-00,re Nonconforming Vital Area Barriers.Commitments Made by Util Are Listed ML17325B6401999-06-0101 June 1999 Forwards LER 99-013-00 Re Safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Lead to ECCS Pump Failure.Listed Commitments Identified in Submittal ML17325B6331999-05-28028 May 1999 Forwards LER 99-S02-00,re Vulnerability in Safeguard Sys That Could Allow Unauthorized or Undetected Access to Protected Area.Commitments Made by Util Are Listed ML17265A8201999-05-24024 May 1999 Forwards LER 98-037-01,representing Extensive Rev to Original LER & Replacing Rept in Entirety.Listed Commitments Identified in Submittal ML17325B6111999-05-21021 May 1999 Forwards Annual Radioactive Effluent Release Rept for 980101-1231 for DC Cook Nuclear Plant,Units 1 & 2. Transmittal of Submittal Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17325B6031999-05-21021 May 1999 Provides Response to NRC GL 98-04, Potential for Degradation of ECCS & Containment Spray Sys After LOCA Because of Const & Protective Coating Deficiencies & Foreign Matl in Containment. ML20207A9201999-05-21021 May 1999 Ack Receipt of 990319 Response to Notice of Violation & Proposed Imposition of Civil Penalty .On 981124, Licensee Remitted Check for Payment of Civil Penalties. Licensee Requests for Extension for Response,Granted ML17325B5971999-05-20020 May 1999 Forwards LER 99-012-00,re Auxiliary Building ESF Ventilation Sys Not Being Capable of Maintaining ESF Room Temps post-accident.Commitment,listed ML17335A5281999-05-12012 May 1999 Forwards DC Cook Nuclear Plant Fitness for Duty Program Performance Dtd for six-month Period of 980701-1231,IAW 10CFR26.71(d).Info Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17335A5271999-05-11011 May 1999 Forwards Details Re Sources & Levels of Insurance Maintained for DC Cook,Units 1 & 2,as of 990401,per 10CFR50.54(w)(3). Info Was Delayed Beyond Required Date Due to Internal Oversight ML17325B5841999-05-10010 May 1999 Forwards LER 99-002-00 Re TS 4.0.5 Requirements Not Being Met Due to Improperly Performed Test.Commitments Identified in Ler,Listed ML17325B5871999-05-0707 May 1999 Forwards Current Revs of Expanded Sys Readiness Review (Essr) Implementing Procedures,For Info Purposes to Support Current NRC Insps.Current Esrr Schedule Provided for Info Purposes,Reflecting Revised Target Dates ML17325B5791999-05-0404 May 1999 Forwards LER 99-011-00,concerning Air Sys for EDG Not Supporting Long Term Operability.Commitments Made by Util Listed ML17325B5821999-05-0404 May 1999 Provides Addl Background,Description & Clarification of Previous & Revised Commitments Re UFSAR Revalidation Effort. Commitment Change Involved Alignment of UFSAR Revalidation Program Methodology to Strategy Contained in Current Plan ML17325B5741999-05-0303 May 1999 Forwards LER 99-010-00 Re RCS Leak Detection Sys Sensitivity Not in Accoradnce with Design Requirements.Listed Commitments Identified in Submittal ML17325B5631999-04-22022 April 1999 Forwards Results of Independent Chemical Evaluations Performed from Sept 1997 Through Feb 1999,re Resolution of Issues Related to License Amend 227 ML17325B5561999-04-16016 April 1999 Forwards LER 99-006-00, Fuel Crane Loads Lifted Over SFP Could Impact Energies Greater than TS Limits, IAW 10CFR50.73.Submittal Was Delayed to Allow for Resolution of Questions.Commitment Made by Licensee,Listed ML20205P0591999-04-14014 April 1999 Ninth Partial Response to FOIA Request for Documents.App Records Already Available in Pdr.Records in App T Encl & Being Made Available in Pdr.App U Records Being Released in Part (Ref FOIA Exemption 7).App V Records Withheld Entirely ML17325B5451999-04-12012 April 1999 Forwards LER 99-009-00 Re as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit.Commitments Identified in Submittal Listed ML17325B5301999-04-0707 April 1999 Forwards LER 99-S01-01, Vulnerability in Locking Mechanism of Four Vital Area Gates, Per 10CFR50.73.Commitments Made by Util,Listed ML17325B5241999-04-0505 April 1999 Forwards Revs 0 & 1 to Cook Nuclear Plant Restart Plan, Dtd 980307 & 0407.Rev 5 Is Current Cook Nuclear Plant Restart & Supercedes Previous Revs in All Respects ML17325B5121999-04-0101 April 1999 Forwards LER 99-007-00, Calculations Show That Divider Barrier Between Upper & Lower Containment Vols May Be Overstressed. Commitments Made by Util Are Listed 1999-09-30
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML17335A5511999-10-0707 October 1999 Forwards LER 99-023-00, Inadequate TS Surveillance Testing of ESW Pump ESF Response Time. Commitments Identified in LER Listed ML20217D9361999-09-30030 September 1999 FOIA Request for Document Re Section 9.7 of SE by Directorate of Licensing,Us Ae Commission in Matter of Indiana & Michigan Electric Co & Indiana & Michigan Power Co,Dc Cook Nuclear Plan,Units 1 & 2 ML17326A1541999-09-20020 September 1999 Provides Notification of Change in Senior Licensed Operator Status.Operating Licenses for CR Smith,License SOP-30159-4 & Tw Welch,License SOP-30654-2 Are No Longer Required & Should Be Withdrawn ML17326A1261999-09-17017 September 1999 Forwards LER 99-022-00 Re Electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads.Listed Commitment Identified in Submittal ML17326A1441999-09-17017 September 1999 Submits Trace on Second Shipment of Two Plant,Unit 2 Steam Generators.Info Re Shipment Submitted ML17326A1531999-09-16016 September 1999 Submits Info Pertaining to Plant Proposed Operator Licensing Exam Requirements Through Yr 2003.NRC Form 536, Operator Licensing Exam Data, Which Provides Required Info Encl ML17326A1101999-08-27027 August 1999 Forwards LER 99-021-00, GL 96-01 Test Requirements Not Met in Surveillance Tests. List of Commitments Identified in LER Provided ML17326A0991999-08-26026 August 1999 Forwards LER 99-020-00,re EDGs Being Declared Inoperable. Commitments Made by Util Are Listed ML17326A1221999-08-23023 August 1999 Forwards Revised Page 2 to 1998 Annual Environ Operating Rept, for DC Cook Nuclear Plant,Correcting Omission to App I ML17326A0981999-08-23023 August 1999 Forwards fitness-for-duty Program Performance Data for Period of 990101-0630 for DC Cook Nuclear Plants,Units 1 & 2,per 10CFR26.71(d) ML17326A0891999-08-16016 August 1999 Forwards LER 99-019-00,re Victoreen Containment High Range Monitors Not Beign Environmentally Qualified to Withstand post-LOCA Conditions.Commitments Made by Util Are Listed ML17326A0811999-08-10010 August 1999 Notifies NRC of Changes in Commitments Made in Response to GL 98-01,supplement 1, Yr 2000 Readiness of Computer Sys Ar Npps, Dtd 990623 ML17326A0821999-08-0606 August 1999 Informs That Util Is Submitting Encl Scope & Objectives for 991026 DC Cook Nuclear Plant Emergency Plan Exercise to G Shear of NRC Plant Support Branch.Exercise Will Include Full State & County Participation ML17326A1451999-08-0404 August 1999 Requests Withholding of WCAP-15246, Control Rod Insertion Following Cold Leg Lbloca. ML17326A0751999-08-0404 August 1999 Forwards LER 98-029-01, Fuel Handling Area Ventilation Sys Inoperable Due to Original Design Deficiency. Supplemental Rept Represents Extensive Rev to Original LER & Replaces Rept in Entirely.Commitment Listed ML17326A0721999-07-29029 July 1999 Forwards LER 99-018-00 Re Refueling Water Storage Tank Suction Motor Operated Valves Inoperable,Due to Inadequate Design.Listed Commitments Were Identified in LER ML17326A0711999-07-27027 July 1999 Responds to 980123 RAI Re NRC GL 87-02, Verification of Seismic Adequacy of Mechanical & Electrical Equipment in Operating Reactors,Unresolved Safety Issue (USI) A-46. ML17326A0601999-07-22022 July 1999 Forwards UFSAR, IAW 10CFR50.71(e) & Rept of Changes,Tests & Experiments as Required by 10CFR50.59(b)(2) for DC Cook Nuclear Plant,Units 1 & 2.Without UFSAR ML17326A0631999-07-22022 July 1999 Forwards LER 98-014-03, Response to High-High Containment Pressure Procedure Not Consistent with Analysis of Record. Revised Info Marked by Sidebars in Right Hand Margin. Commitments Made by Util,Listed ML17326A0311999-07-0101 July 1999 Forwards LER 99-004-01 Re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitments Made by Util Are Listed ML17326A0281999-06-28028 June 1999 Provides Response to 981116 & 960228 RAIs Re GL 92-01. Revised Pressurized Thermal Shock Evaluation Based on New Weld Chemistry Info & Copy of W Rept WCAP-15074, Evaluation of 1P3571 Weld Metal from Surveillance Programs... Encl ML17326A0241999-06-23023 June 1999 Responds to GL 98-01,Suppl 1, Y2K Readiness of Computer Sys at Nuclear Power Plants. Y2K Readiness Disclosure for Plant & List of Commitments Encl ML17326A0121999-06-18018 June 1999 Forwards LER 99-014-00 Re Requirement of TS 4.0.5 Not Met for Boron Injection Tank Bolting.Commitments Identified in Submittal Listed ML17326A0111999-06-11011 June 1999 Provides Response to NRC RAI Re GL 97-01, Degradation of Crdm/Cedm Nozzle & Other Vessel Closure Head Penetrations. ML17325B6401999-06-0101 June 1999 Forwards LER 99-013-00 Re Safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Lead to ECCS Pump Failure.Listed Commitments Identified in Submittal ML17325B6281999-06-0101 June 1999 Forwards LER 99-S03-00,re Nonconforming Vital Area Barriers.Commitments Made by Util Are Listed ML17325B6331999-05-28028 May 1999 Forwards LER 99-S02-00,re Vulnerability in Safeguard Sys That Could Allow Unauthorized or Undetected Access to Protected Area.Commitments Made by Util Are Listed ML17265A8201999-05-24024 May 1999 Forwards LER 98-037-01,representing Extensive Rev to Original LER & Replacing Rept in Entirety.Listed Commitments Identified in Submittal ML17325B6111999-05-21021 May 1999 Forwards Annual Radioactive Effluent Release Rept for 980101-1231 for DC Cook Nuclear Plant,Units 1 & 2. Transmittal of Submittal Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17325B6031999-05-21021 May 1999 Provides Response to NRC GL 98-04, Potential for Degradation of ECCS & Containment Spray Sys After LOCA Because of Const & Protective Coating Deficiencies & Foreign Matl in Containment. ML17325B5971999-05-20020 May 1999 Forwards LER 99-012-00,re Auxiliary Building ESF Ventilation Sys Not Being Capable of Maintaining ESF Room Temps post-accident.Commitment,listed ML17335A5281999-05-12012 May 1999 Forwards DC Cook Nuclear Plant Fitness for Duty Program Performance Dtd for six-month Period of 980701-1231,IAW 10CFR26.71(d).Info Was Delayed Due to Administrative Error in Regulatory Affairs Dept ML17335A5271999-05-11011 May 1999 Forwards Details Re Sources & Levels of Insurance Maintained for DC Cook,Units 1 & 2,as of 990401,per 10CFR50.54(w)(3). Info Was Delayed Beyond Required Date Due to Internal Oversight ML17325B5841999-05-10010 May 1999 Forwards LER 99-002-00 Re TS 4.0.5 Requirements Not Being Met Due to Improperly Performed Test.Commitments Identified in Ler,Listed ML17325B5871999-05-0707 May 1999 Forwards Current Revs of Expanded Sys Readiness Review (Essr) Implementing Procedures,For Info Purposes to Support Current NRC Insps.Current Esrr Schedule Provided for Info Purposes,Reflecting Revised Target Dates ML17325B5821999-05-0404 May 1999 Provides Addl Background,Description & Clarification of Previous & Revised Commitments Re UFSAR Revalidation Effort. Commitment Change Involved Alignment of UFSAR Revalidation Program Methodology to Strategy Contained in Current Plan ML17325B5791999-05-0404 May 1999 Forwards LER 99-011-00,concerning Air Sys for EDG Not Supporting Long Term Operability.Commitments Made by Util Listed ML17325B5741999-05-0303 May 1999 Forwards LER 99-010-00 Re RCS Leak Detection Sys Sensitivity Not in Accoradnce with Design Requirements.Listed Commitments Identified in Submittal ML17325B5631999-04-22022 April 1999 Forwards Results of Independent Chemical Evaluations Performed from Sept 1997 Through Feb 1999,re Resolution of Issues Related to License Amend 227 ML17325B5561999-04-16016 April 1999 Forwards LER 99-006-00, Fuel Crane Loads Lifted Over SFP Could Impact Energies Greater than TS Limits, IAW 10CFR50.73.Submittal Was Delayed to Allow for Resolution of Questions.Commitment Made by Licensee,Listed ML17325B5451999-04-12012 April 1999 Forwards LER 99-009-00 Re as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit.Commitments Identified in Submittal Listed ML17325B5301999-04-0707 April 1999 Forwards LER 99-S01-01, Vulnerability in Locking Mechanism of Four Vital Area Gates, Per 10CFR50.73.Commitments Made by Util,Listed ML17325B5241999-04-0505 April 1999 Forwards Revs 0 & 1 to Cook Nuclear Plant Restart Plan, Dtd 980307 & 0407.Rev 5 Is Current Cook Nuclear Plant Restart & Supercedes Previous Revs in All Respects ML17325B5121999-04-0101 April 1999 Forwards LER 99-007-00, Calculations Show That Divider Barrier Between Upper & Lower Containment Vols May Be Overstressed. Commitments Made by Util Are Listed ML17325B5141999-03-30030 March 1999 Forwards Rept on Status of Decommissioning Funding.Attached Rept Includes Amount of Decommissioning Funds Estimated to Be Required Pursuant to 10CFR50.75(b) & (C) ML17325B5191999-03-29029 March 1999 Forwards LER 99-001-00,re Degraded Component Cw Flow to Containment Main Steam Line Penetrations.Commitment, Listed ML20204F6401999-03-19019 March 1999 Responds to NRC 981013 NOV & Proposed Imposition of Civil Penalty.Violations Cited in Subject NOV Were Initially Identified in Referenced Five Insp Repts.Corrective Actions: Ice Condensers Have Been Completely Thawed of Any Blockage ML17325B4751999-03-18018 March 1999 Forwards LER 99-004-00,re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitment Made by Util,Listed ML17325B4721999-03-18018 March 1999 Forwards LER 99-005-00,re Reactor Trip Breaker Manual Actuations During Rod Drop Testing Not Previously Reported. Listed Commitments Identified in Submittal ML17325B4641999-03-17017 March 1999 Withdraws Response to Issue 1 of NRC Cal,Dtd 970919. Comprehensive Design Review Effort in Progress to Validate Resolution of Issue for Future Operation 1999-09-30
[Table view] |
Text
indiana Michigan Power Company P.O. Box i6631 Columbus, OH 432 s6 Z
INOlANA NK8l6rlPl laQlRfER AEP NRC 1184H1 10 CFR 2.201 Donald C. Cook Nuclear Plant Units 1 and 2 Docket Nos. 50-315 and 50-316
-License Nos. DPR-58 and DPR-74 NRC INSPECTION REPORTS NO. 50-315/93012 (DRS)
AND 50-316/93012 (DRS)
REPLY TO NOTICE OF VIOIATION (SYSTEM BASED INSTRUMENTATION AND 'CONTROL INSPECTION)
U. S. Nuclear Regulatory Commission Document Control Desk Vashington, D. C. 20555 Attn: J. B. Martin November 28, 1994
Dear Mr. Martin:
By letter dated January 4, 1994, (AEP:NRC:1184H), we responded to a Notice of Violation dated November 23, 1993, associated with the subject NRC inspection. The violations were associated with 1) errors in a setpoint calculation for refueling water storage tank level instrumentation and 2) the lack of an unreviewed safety question determination for Temporary Modification 2-93-015, which I I installed an to converter in the Unit 2 feedwater pump control circuitry.
By letter dated October 4, 1994, the NRC expressed concern with our response to violation No. 2. Our revised response to violation No. 2 is contained in the attachment to this letter.
J. B. Martin AEP:NRC:1184Hl This letter is submitted pursuant to 10 CFR 50.54(f) and, as such, an oath statement is attached.
Sincerely, E. E. Fitzpatrick Vice President eh Attachments CC: A. A. Blind G. Charnoff NFEM Section Chief NRC Resident Inspector - Bridgman J. R. Padgett W. T. Russell - NRC Region III
ATTAQBKNT TO AEP:HRC:118481 RESPONSE TO NRC CONCERNS REGARDING REPLY TO NOTICE OF VIOIATION: NRC INSPECTION REPORT NOS. 50-315/93012(DRS) AND 50-316/93012(DRS)
ATTACHMENT TO AEP:NRC: 1184H1 PAGE 1 C es o e t Re "With regard to your response to violation No. 2, we disagree with your position that this violation does not represent a departure with NRC regulations. Specifically, we do not agree with your interpretation of 10 CFR 50.59 that the specific speed control circuitry needs to be explicitly described in the UFSAR to prompt a safety evaluation. It is our position that if the structure, system or component (SSC) being modified can affect the performance of a larger'SC, in this case the speed control circuit affecting the feedwater pump, then a,safety evaluation must be performed.
The steam generator feedwater control system, the feedwater system, and the feedwater pump's variable speed mechanical drive are addressed in the UFSAR. In particular, UFSAR Section 10.5.1.1 states that "the variable speed turbine driven main feedwater pumps are designed to provide the required feedwater flow to the steam generators." The steam generator feedwater system is an important system in ensuring continued heat removal from the reactor core. A safety evaluation should have been performed to assess the potential consequences of modifying the turbine's speed control system with respect to, among others, the probability of occurrence of a loss of feedwater accident.
Because your screening process apparently focuses only on structures, systems, or components which are explicitly described in the UFSAR, the potential exists for modifications to be implemented without a thorough safety evaluation.
Please provide your response to this concern within 30 days of this letter."
s se In response to the concerns raised in the NRC's letter of October 4, 1994, we are amending our original response to violation 2 from the Notice of Violation. The revised response is contained below.
d V a Indiana Michigan Power admits to the violation as cited in the'RC Notice of Violation.
- 2. easo V ate The reason for the violation is a difference in
ATTACHMENT TO AEP:NRC: 118481 PAGE 2 interpretation of the requirements of 10 CFR 50.59.
Quoth respect to the design change of the I to I converter (Temporary Modification TM 2-93-015),
neither the function of the main feedwater pumps as described in the UFSAR (to provide feedwater flow to the steam generators) nor the method of performing the function as described in the UFSAR (with variable speed pumps) was impacted by the change.
Additionally, complete loss of feedwater (independent of the specific reason) was already an analyzed UFSAR Chapter 14 event. Thus, in the judgment of the individuals performing the screening;- the change represented neither an explicit nor an implicit change to the UFSAR, and therefore an unreviewed safety question determination was not performed.
- 3. ve The I to I converter was removed from the circuitry on September 12, 1994.
e ve t Prior to the SBICI inspection, we were performing Uareviewed Safety Question determinations for all Request for Changes and Minor Modifications (generally safety related/safety interface changes), regardless of the results of the 10 CFR 50.59 screening.
Followiag the SBICI, we modified the Temporary Modification process such that Unreviewed Safety Question determiaations are now performed for all temporary modifications iavolving safety related and/or seismic class I or II equipment. Additionally, we will modify our design change process such that we perform Unreviewed Safety Question determinations for the balance of the design changes (Plant Modifications and non-safety related/non-seismic class I or II Temporary Modifications). This chaage will be implemented by December 31, 1994, for design changes for which physical work is not in progress as of that date.
e u v Pull compliance was achieved on September 12, 1994, when the I to I converter was removed from the circuitxy.
(ACCELEIUKTED Ril)S I'ROCI;SSIio)
REGULATORY XNFORMATION DISTRIBUTION SYSTEM (RIDS)
CESSION NBR:9412020086 DOC.DATE: 94/11/28 NOTARIZED: YES DOCKET
'ACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana M 05000315 50-316 Donald C. Cook Nuclear Power Plant, Unit 2, Indiana M 05000316 AUTH. NAME AUTHOR AFFILIATXON FITZPATRICK,E. Indiana Michigan Power Co. (formerly Indiana (t'ichigan Ele RECIP.NAME RECIPXENT AFFILIATION MARTIN,J.B. Document Control Branch (Document Control Desk)
SUBJECT:
Forwards revised response to violation 2 from NOV dtd 931123 associated w/Insp Repts 50-315/93-12 6 50-316/93-12.
Corrective actions:I to I converter removed from circuitry on 940912.
DISTRIBUTION CODE: IE01D COPIES RECEIVED:LTR ENCL SIZE:
'TITLE: General (50 Dkt)-Insp Rept/Notice of Vio ation Response NOTES RECXPIENT COPIES RECIPXENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-1 PD 1 1 HICKMAN,J 1 1 INTERNAL: AEOD/DEIB 1 1 AEOD/SPD/RAB 1 .1 AEOD/S PD/RRAB 1 1 AEOD/~C 1 1 DEDRO 1 1 ~FILE CENTET5 02 1 1 NRR/DORS/OEAB 1 1 NRR/'DRCH/HHFB 1 1 NRR/PMAS/IRCB-E 1 1 NUDOCS-ABSTRACT 1 1 OE DIR 1 1 OGC/HDS2 1 1 RGN3 FILE 01 1 1 ERNAL: LITCO BRYCE,J H 1 1 NOAC 1 1
'RC PDR 1 1 YOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE 4VASTE! COSTA('.T'I'I IE DQCL'ifEiT CONTROL DESK, ROOif Pl-37 (EXT. 5()4-00S3 ) TO I;LlhflNATE5'Ol'R XA) IL: I'ROTI DISTRIIIU'I'!ONLIS'I'S I:OR DO(.".Uif[ X'I'S YOU l)ON "IIII:.I)!
TOTAL NUMBER OF COPIES REQUIRED: LTTR 18 ENCL 18
fridicrc- fi'..* >>.q.
Power Compan~
P.O Box 16li);
Columba.< Oil -".:"r IMOMRA NlCHISAF4 PMFA AEP'NRC:1184H1 10 CFR 2.201 Donald C. Cook Nuclear Plant Units 1 and 2 Docket Nos. 50-315 and 50-316 License Nos. DPR-58 and DPR-74 NRC INSPECTION REPORTS NO. 50-315/93012 (DRS)
AND 50-316/93012 (DRS)
REPLY TO NOTICE OF VIOLATION (SYSTEM BASED INSTRUMENTATION AND CONTROL INSPECTION)
U. S. Nuclear Regulatory Commission Document Control Desk Vashington, D. C. 20555 Attn: J. B. Martin November 28, 1994
Dear Mr. Martin:
By letter dated January 4, 1994, (AEP:NRC:1184H), we responded to a Notice of Violation dated November 23, 1993, associated with the subject NRC inspection. The violations were associated with 1) errors in a setpoint calculation for refueling water storage tank level instrumentation and 2) the lack of an unreviewed safety question determination for Temporary Modification 2-93-015, which installed an I to I converter in the Unit 2 feedwater pump control circuitry.
By letter dated October 4, 1994, the NRC expressed concern with our response to violation No. 2. Our revised response to violation No. 2 is contained in the attachment to this letter.
9412020086 9'41128 PDR ADOCK 05000315 g PDR
J. B. Martin AEP'NRC'1184Hl This letter is submitted pursuant to 10 CFR 50.54(f) and, as such, an oath statement is attached.
Sincerely, Vice President eh Attachments CC: A. A. Blind G. Charnoff NFEM Section Chief NRC Resident Inspector - Bridgman J. R. Padgett W. T. Russell - NRC Region III
STATE OF OHIO)
COUNTY OF FRANKLIN)
E. E. Fitzpatrick, being duly sworn, deposes and says that he is the Vice President of licensee Indiana Michigan Power Company, that he has read the foregoing Reply to Notice of Violation '(System Based Instrumentation and Control Inspection), and knows the contents thereof; and that said contents are true to the best of his knowledge and belief.
Subscribed and sworn to before day of me 19 ~.
this ~%~4 NOTAR PUBLIC
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0 ATTAQBKNT TO AEP'NRC'1184H1 RESPONSE TO NRC CONCERNS REGARDING REPLY TO NOTICE OF VIOIATION'RC INSPECTION REPORT NOS. 50-315/93012(DRS) AND 50-316/93012(DRS)
ATTACHMENT TO AEP:NRC'1184Hl PAGE 1 NRC Res on e to Re "With regard to your response to violation No. 2, we disagree with your position that this violation does not represent a departure with NRC regulations. Specifically, we do not agree with your interpretation of 10 CFR 50.59 that the specific speed control circuitry needs to be explicitly described in the UFSAR to prompt a safety evaluation. It is our position that if the structure, system or component (SSC) being modified can affect the performance of a larger SSC, in this case the speed control circuit affecting the feedwater pump, then a safety evaluation must be performed.
The steam generator feedwater control system, the feedwater system, and the feedwater pump's variable speed mechanical drive are addressed in the UFSAR. In particular, UFSAR Section 10.5.1.1 states that "the variable speed turbine driven main feedwater pumps are designed to provide the required feedwater flow to the steam generators." The steam generator feedwater system is an important system in ensuring continued heat removal from the reactor core. A safety evaluation should have been performed to assess the potential consequences of modifying the turbine's speed system with respect to, among others, the probability of .'ontrol occurrence of a loss of feedwater accident.
Because your screening process apparently focuses only on structures, systems, or components which are explicitly described in the UFSAR, the potential exists for modifications to be implemented without a thorough safety evaluation.
Please provide your response to this concern within 30 days of this letter."
es onse to C Co ce In response to the concerns raised in the NRC's letter of October 4, 1994, we are amending our original response to violation 2 from the Notice of Violation. The revised response is contained below.
dm so D e e ed V o at o Indiana Michigan Power admits to the violation as cited in the'RC Notice of Violation..
- 2. easo eVoato The reason for the violation is a difference in
ATTACHMENT TO AEP: NRC: 1184Hl PAGE 2 interpretation of the requirements of 10 CFR 50.59.
With respect to the design change of the I to I converter (Temporary Modification TM 2-93-015),
neither the function of the main feedwater pumps as described in the UFSAR (to provide feedwater flow to the steam generators) nor the method of performing the function as described in the UFSAR (with variable speed pumps) was impacted by the change.
Additionally, complete loss of feedwater (independent of the specific reason) was already an analyzed UFSAR Chapter 14 event. Thus, in the ]udgment of the individuals performing the screening, the change represented neither an explicit nor an implicit change to the UFSAR, and therefore an unreviewed safety question determination was not performed.
- 3. ect v t s a e d u c eved The I to I converter was removed from the circuitry on September 12, 1994.
- 4. o ective tio s ke o vo F e V at ns Prior to the SBICI inspection, we were performing Unreviewed Safety Question determinations for all Request for Changes and Minor Modifications (generally safety related/safety interface changes), regardless of the results of the 10 CFR 50.59 screening.
Following the SBICI, we modified the Temporary Modification process such that Unreviewed Safety Question, determinations are now performed for all temporary modifications involving safety related and/or seismic class I or II equipment. Additionally, we will modify our design change process such that we perform Unreviewed Safety Question determinations for the balance of the design changes (Plant Modifications and non-safety related/non-seismic class I or II
,Temporary Modifications). This change will be implemented by December 31, 1994, for design changes for which physical work is not in progress as of that dates
- 5. v d Full compliance was achieved on September 12, 1994,
-when the I to I converter was removed from the circuitry.