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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors ML17335A5171999-02-11011 February 1999 LER 99-002-00:on 990112,determined That RCS Pressurizer PORVs Had Not Been Tested,Per Ts.Caused by Inadequate Scheduling Controls Allowing Personnel Error.Surveillance Procedure Was Completed & Updated LER Will Be Submitted ML17335A5141999-02-10010 February 1999 LER 99-001-00:on 990106,noted That GE Hfa Relays Installed in EDGs May Not Meet Seismic Qualification.Caused by Operating Experience Info Incorrectly Dispositioned in 1985. Updated LER Will Be Submitted by 990405 ML17335A5011999-02-0101 February 1999 LER 98-060-00:on 981231,identified That Rt Sys Response Time Testing Did Not Comply with TS Definition.Caused by Inadequate Procedures.Corrective Actions Will Be Developed & Update to LER Will Be Submitted by 990415.With 990201 Ltr ML17335A4951999-01-29029 January 1999 LER 98-059-00:on 981230,interim LER -single Failure in Containment Spray Sys Could Result in Containment Spray Ph Outside Design Occurred.Investigation Into Condition Continuing.Update Will Be Submitted by 990514 Ltr ML17335A4961999-01-27027 January 1999 LER 98-057-00:on 981228,discovered That AFW Valves Were Not Tested IAW Inservice Testing Program.Caused by Failure to Recognize Design Bases Features Re Afws by Personnel. Updated LER Will Be Submittted by 990415.With 990127 Ltr ML17335A4921999-01-19019 January 1999 LER 98-052-01:on 981128,no Analysis for NSR Sc Manual Loader for Tdafwp Could Be Found in Original Design.Cause Due to All Failure Modes Not Considered When Compressed Air Sys Originally Designed.Performed Review of Components ML17335A4721999-01-0606 January 1999 LER 98-055-00:on 981207,potential for Condition Outside of Design Bases for Rod Control Sys Was Noted.Caused by Calibration Error Coupled with Single Rod Failure.Condition Rept Investigation Is Ongoing ML17335A4691999-01-0606 January 1999 LER 98-056-00:on 981211,hot Leg Nozzle Gaps Resulted in Plant Being in Unanalyzed Condition.Analyses Are Being Performed by W to Resolve Problem.Updated LER Will Be Submitted by 990211.With 990106 Ltr ML17335A4661999-01-0505 January 1999 LER 98-049-00:on 981020,emergency Boron Injection Flow Path Was Inoperable.Caused by Original Design Deficiency. Engineering Evaluation of Event Is Continuing ML17335A4631999-01-0404 January 1999 LER 98-054-00:on 981202,discovered That at Least One MSSV Had Not Been Reset as Required by Ts.Engineering Is Continuing Review of Extent of Condition for Event.Updated LER Will Be Submitted by 990129.With 990104 Ltr ML17335A4481998-12-30030 December 1998 LER 98-053-00:on 981130,discovered Use of Inoperable Substitute Subcooling Margin Monitor.Caused by Condition Existing Since Installation of Plant Process Computer in 1992.Updated LER Will Be Submitted.With 981230 Ltr ML17335A4581998-12-28028 December 1998 LER 98-052-00:on 981128,turbine Driven AFW Pump Speed Controller Failure Mode Occurred.Caused Because Not All Failure Modes Were Considered When Compressed Air Sys Was Originally Designed.Verified Current Design Change Process ML17335A4281998-12-22022 December 1998 LER 98-051-00:on 981122,reactor Trip Signal from Manual Safety Injection Not Verified as Required by TS Surveillance,Was Discovered.Maintenance Currently Evaluating Significance & Cause of Event ML17335A4111998-12-17017 December 1998 LER 98-047-00:on 981117,potential for Increase Leakage from Reactor Coolant Pump Seals Was Identified.Util Is Working with W to Resolve Issue.Current Expectations Are to Submit Update to LER by 990215.With 981217 Ltr ML17335A4141998-12-16016 December 1998 LER 98-058-00:on 981216,postulated High Line Break Could Result in Condition Outside Design Bases for AF Occurred. Caused by Deficiencies Associated with Administration of HELB Program.Analysis of AF Will Be Completed by 990122 ML17335A4181998-12-16016 December 1998 LER 98-050-00:on 980814,ancillary Equipment Installed in Ice Condenser Was Not Designed to Withstand Design Basis Accident/Earthquake Loads.Caused by Lack of Established Design Criteria.Developed Design Criteria ML17335A3871998-12-11011 December 1998 LER 98-031-01:on 980610,potential Common Mode Failure of RHR Pumps Were Noted.Caused by Inaccurate Values.Accurate Miniflow Numbers Have Been Determined by Flow Testing ML17335A3821998-12-0808 December 1998 LER 98-039-01 Re EOP Step Conflicts with Small Break LOCA Analysis.Ler 98-039-00 Has Been Canceled.With 981208 Ltr ML17335A3781998-12-0707 December 1998 LER 98-007-00:on 981106,high Energy Line Break Effects in Auxiliary FW Sys Was Noted.Cause of Event Is Under Investigation & Will Be Completed by 990220.Updated LER Will Be Submitted by 990310.With 981207 Ltr ML17335A3771998-12-0303 December 1998 LER 98-046-00:on 981103,determined That Afs Was Unable to Meet Design Flow Requirements During Special Test.Caused by Failure to Consider All Aspects of Sys Operation in Design of Suction Basket Strainers.Sys Will Be Redesigned ML17335A3741998-12-0202 December 1998 LER 97-011-02:on 970822,operation Was Noted Outside Design Bases for ECCS & CSP for Switchover to Recirculation Sump Suction.Caused by Ineffective Change Mgt.Revised Procedure for Switchover 01(02) Ohp 4023.ES-1.3 1999-09-17
[Table view] Category:RO)
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors ML17335A5171999-02-11011 February 1999 LER 99-002-00:on 990112,determined That RCS Pressurizer PORVs Had Not Been Tested,Per Ts.Caused by Inadequate Scheduling Controls Allowing Personnel Error.Surveillance Procedure Was Completed & Updated LER Will Be Submitted ML17335A5141999-02-10010 February 1999 LER 99-001-00:on 990106,noted That GE Hfa Relays Installed in EDGs May Not Meet Seismic Qualification.Caused by Operating Experience Info Incorrectly Dispositioned in 1985. Updated LER Will Be Submitted by 990405 ML17335A5011999-02-0101 February 1999 LER 98-060-00:on 981231,identified That Rt Sys Response Time Testing Did Not Comply with TS Definition.Caused by Inadequate Procedures.Corrective Actions Will Be Developed & Update to LER Will Be Submitted by 990415.With 990201 Ltr ML17335A4951999-01-29029 January 1999 LER 98-059-00:on 981230,interim LER -single Failure in Containment Spray Sys Could Result in Containment Spray Ph Outside Design Occurred.Investigation Into Condition Continuing.Update Will Be Submitted by 990514 Ltr ML17335A4961999-01-27027 January 1999 LER 98-057-00:on 981228,discovered That AFW Valves Were Not Tested IAW Inservice Testing Program.Caused by Failure to Recognize Design Bases Features Re Afws by Personnel. Updated LER Will Be Submittted by 990415.With 990127 Ltr ML17335A4921999-01-19019 January 1999 LER 98-052-01:on 981128,no Analysis for NSR Sc Manual Loader for Tdafwp Could Be Found in Original Design.Cause Due to All Failure Modes Not Considered When Compressed Air Sys Originally Designed.Performed Review of Components ML17335A4721999-01-0606 January 1999 LER 98-055-00:on 981207,potential for Condition Outside of Design Bases for Rod Control Sys Was Noted.Caused by Calibration Error Coupled with Single Rod Failure.Condition Rept Investigation Is Ongoing ML17335A4691999-01-0606 January 1999 LER 98-056-00:on 981211,hot Leg Nozzle Gaps Resulted in Plant Being in Unanalyzed Condition.Analyses Are Being Performed by W to Resolve Problem.Updated LER Will Be Submitted by 990211.With 990106 Ltr ML17335A4661999-01-0505 January 1999 LER 98-049-00:on 981020,emergency Boron Injection Flow Path Was Inoperable.Caused by Original Design Deficiency. Engineering Evaluation of Event Is Continuing ML17335A4631999-01-0404 January 1999 LER 98-054-00:on 981202,discovered That at Least One MSSV Had Not Been Reset as Required by Ts.Engineering Is Continuing Review of Extent of Condition for Event.Updated LER Will Be Submitted by 990129.With 990104 Ltr ML17335A4481998-12-30030 December 1998 LER 98-053-00:on 981130,discovered Use of Inoperable Substitute Subcooling Margin Monitor.Caused by Condition Existing Since Installation of Plant Process Computer in 1992.Updated LER Will Be Submitted.With 981230 Ltr ML17335A4581998-12-28028 December 1998 LER 98-052-00:on 981128,turbine Driven AFW Pump Speed Controller Failure Mode Occurred.Caused Because Not All Failure Modes Were Considered When Compressed Air Sys Was Originally Designed.Verified Current Design Change Process ML17335A4281998-12-22022 December 1998 LER 98-051-00:on 981122,reactor Trip Signal from Manual Safety Injection Not Verified as Required by TS Surveillance,Was Discovered.Maintenance Currently Evaluating Significance & Cause of Event ML17335A4111998-12-17017 December 1998 LER 98-047-00:on 981117,potential for Increase Leakage from Reactor Coolant Pump Seals Was Identified.Util Is Working with W to Resolve Issue.Current Expectations Are to Submit Update to LER by 990215.With 981217 Ltr ML17335A4141998-12-16016 December 1998 LER 98-058-00:on 981216,postulated High Line Break Could Result in Condition Outside Design Bases for AF Occurred. Caused by Deficiencies Associated with Administration of HELB Program.Analysis of AF Will Be Completed by 990122 ML17335A4181998-12-16016 December 1998 LER 98-050-00:on 980814,ancillary Equipment Installed in Ice Condenser Was Not Designed to Withstand Design Basis Accident/Earthquake Loads.Caused by Lack of Established Design Criteria.Developed Design Criteria ML17335A3871998-12-11011 December 1998 LER 98-031-01:on 980610,potential Common Mode Failure of RHR Pumps Were Noted.Caused by Inaccurate Values.Accurate Miniflow Numbers Have Been Determined by Flow Testing ML17335A3821998-12-0808 December 1998 LER 98-039-01 Re EOP Step Conflicts with Small Break LOCA Analysis.Ler 98-039-00 Has Been Canceled.With 981208 Ltr ML17335A3781998-12-0707 December 1998 LER 98-007-00:on 981106,high Energy Line Break Effects in Auxiliary FW Sys Was Noted.Cause of Event Is Under Investigation & Will Be Completed by 990220.Updated LER Will Be Submitted by 990310.With 981207 Ltr ML17335A3771998-12-0303 December 1998 LER 98-046-00:on 981103,determined That Afs Was Unable to Meet Design Flow Requirements During Special Test.Caused by Failure to Consider All Aspects of Sys Operation in Design of Suction Basket Strainers.Sys Will Be Redesigned ML17335A3741998-12-0202 December 1998 LER 97-011-02:on 970822,operation Was Noted Outside Design Bases for ECCS & CSP for Switchover to Recirculation Sump Suction.Caused by Ineffective Change Mgt.Revised Procedure for Switchover 01(02) Ohp 4023.ES-1.3 1999-09-17
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17335A5641999-10-18018 October 1999 LER 99-024-00:on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With 991018 Ltr ML17335A5531999-10-0707 October 1999 LER 99-023-00:on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented ML17335A5631999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 1.With 991012 Ltr ML17335A5621999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for DC Cook Nuclear Plant,Unit 2.With 991012 Ltr ML17335A5481999-09-30030 September 1999 Non-proprietary DC Cook Nuclear Plant Units 1 & 2 Mods to Containment Sys W SE (Secl 99-076,Rev 3). ML17335A5451999-09-28028 September 1999 Rev 1 to Containment Sump Level Design Condition & Failure Effects Analysis for Potential Draindown Scenarios. ML17326A1291999-09-17017 September 1999 LER 99-022-00:on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary ML17326A1481999-09-17017 September 1999 Independent Review of Control Rod Insertion Following Cold Leg Lbloca,Dc Cook,Units 1 & 2. ML17326A1211999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 2.With 990915 Ltr ML17326A1201999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Cook Nuclear Plant, Unit 1.With 990915 Ltr ML17326A1121999-08-27027 August 1999 LER 99-021-00:on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed ML17326A1011999-08-26026 August 1999 LER 99-020-00:on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs ML17326A0911999-08-16016 August 1999 LER 99-019-00:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 ML17326A0771999-08-0404 August 1999 LER 98-029-01:on 980422,noted That Fuel Handling Area Ventilation Sys Was Inoperable.Caused by Original Design Deficiency.Radiological Analysis for Spent Fuel Handling Accidents in Auxiliary Bldg Will Be Redone by 990830 ML17335A5461999-08-0202 August 1999 Rev 0 to Evaluation of Cook Recirculation Sump Level for Reduced Pump Flow Rates. ML17326A0871999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Unit 1.With 990812 Ltr ML17326A0861999-07-31031 July 1999 Monthly Operating Rept for July 1999 for DC Cook Nuclear Plant,Units 2.With 990812 Ltr ML17326A0741999-07-29029 July 1999 LER 99-018-00:on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves ML17326A0661999-07-26026 July 1999 LER 99-017-00:on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With 990722 Ltr ML17326A0651999-07-22022 July 1999 LER 98-014-03:on 980310,noted That Response to high-high Containment Pressure Procedure Was Not Consistent with Analysis of Record.Caused by Inadequate Interface with W. FRZ-1 Will Be Revised to Be Consistent with New Analysis ML17326A0491999-07-13013 July 1999 LER 99-016-00:on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With 990713 Ltr ML17326A0331999-07-0101 July 1999 LER 99-004-01:on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written ML17326A0511999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 2.With 990709 Ltr ML17326A0501999-06-30030 June 1999 Monthly Operating Rept for June 1999 for DC Cook Nuclear Plant,Unit 1.With 990709 Ltr ML17326A0151999-06-18018 June 1999 LER 99-014-00:on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified ML17325B6421999-06-0101 June 1999 LER 99-013-00:on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed ML17325B6311999-06-0101 June 1999 LER 99-S03-00:on 990430,vital Area Barrier Degradation Was Noted.Caused by Inadequate Insp & Maint of Vital Area Barrier.Repairs & Mods Were Made to Barriers to Eliminate Degraded & Nonconforming Conditions ML17326A0061999-05-31031 May 1999 Monthly Operating Rept for May 1999 for Dcp.With 990609 Ltr ML17326A0071999-05-31031 May 1999 Monthly Operating Rept for May 1999 for DC Cook Nuclear Plant,Unit 2.With 990609 Ltr ML17325B6351999-05-28028 May 1999 LER 99-S02-00:on 990428,vulnerability in Safeguard Sys That Could Allow Unauthorized Access to Protected Area Was Noted. Caused by Inadequate Original Plant Design.Mods Were Made to Wall Opening to Eliminate Nonconforming Conditions ML17265A8231999-05-24024 May 1999 LER 98-037-01:on 990422,determined That Ice Condenser Bypass Leakage Exceeds Design Basis Limit.Caused by Pressure Seal Required by Revised W Design Not Incorporated Into Aep Design.Numerous Matl Condition Walkdowns & Assessments Made ML17325B6001999-05-20020 May 1999 LER 99-012-00:on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed ML17325B5861999-05-10010 May 1999 LER 99-002-00:on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised ML17325B5811999-05-0404 May 1999 LER 99-011-00:on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared ML17325B5771999-05-0303 May 1999 LER 99-010-00:on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design ML17335A5301999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 1.With 990508 Ltr ML17335A5291999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for DC Cook Nuclear Plant,Unit 2.With 990508 Ltr ML17325B5581999-04-16016 April 1999 LER 99-006-00:on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold ML17325B5471999-04-12012 April 1999 LER 99-009-00:on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation ML17325B5321999-04-0707 April 1999 LER 99-S01-00:on 990308,discovered That Lock for Vital Gate Leading to Plant 4KV Switchgear Area Was Nonconforming & Vulnerable to Unauthorized Access.Caused by Inadequate Gate Design & Inadequate Procedures.Mods Are Being Made to Gate ML17325B5161999-04-0101 April 1999 LER 99-007-00:on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures ML17325B5491999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant Unit 2.With 990408 Ltr ML17325B5441999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for DC Cook Nuclear Plant,Unit 1.With 990408 Ltr ML17325B5221999-03-29029 March 1999 LER 99-001-00:on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing ML17325B4801999-03-18018 March 1999 LER 99-004-00:on 971030,failure to Perform TS Surveillance Analyses of Rc Chemistry with Fuel Removed Was Noted.Cause of Event Is Under Investigation.Corrected Written Job Order Activities Used to Control SD Chemistry Sampling ML17325B4741999-03-18018 March 1999 LER 99-005-00:on 940512,determined That Rt Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed ML17325B5671999-03-0202 March 1999 Summary of Unit 1 Steam Generator Layup Chemistry from 980101 to 990218. ML17325B4631999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Power Station,Unit 2.With 990308 Ltr ML17325B4621999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for DC Cook Nuclear Plant,Unit 1.With 990308 Ltr ML17325B4571999-02-24024 February 1999 LER 99-003-00:on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors 1999-09-30
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AC CELE RATED DlBUTI ON DE M ONSTRIQlON SYSTEM REGULATORY. INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:8910160148 DOC.DATE: .89/10/05 NOTARIZED: NO DOCKET I FACIL:50-315 Donald C. Cook Nuclear Power Plant, Unit 1, Indiana & 05000315 AUTH.,NAME ,AUTHOR AFFILIATION BAKER,K.R. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele BLIND,A.A. Indiana Michigan Power Co. (formerly Indiana & Michigan Ele RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 89-012-00:on 890913,SSPS surveillance testing performed on Train while Train safety injection pump inoperable.
B A W/8 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR J ENCL I 'IZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD3-1 LA 1' PD3-1 PD 1 1 GIITTER,J. 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 . AEOD/DOA 1 1 AEOD/DSP/TPAB DEDRO NRR/DEST/ESB 8D 1
1 1
1 1
1 AEOD/ROAB/DS P NRR/DEST/CEB 8H NRR/DEST/ICSB 7 1, '1 2
1 2
1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 .1 NRR/DEST/PSB 8D 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB NRR/DLPQ/PEB NRR DRE 8D 10 PB 10 1
1 2
1 1
2 NRR/DLPQ/HFB 10 NRR/DOEA/EAB NUDOCS-ABSTRACT ll 1 1
1 1
1 1
1 1 RES/DSIR/EIB 1 1 1 1 EXTERNAL EG&G WILLIAMSi S 4 4 L ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC MAYS,G 1 1 'NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 ~ 1 NCTE TO ALL '%IKS" RIKIPIHGS'LEASE HELP US TO REDUCE PRSTE! ~C1'HE DCX:XMEM7 COHIBOL DESK RXH Pl-37 (EXT. 20079) %0 EZiQGNATE KX3R NQQ FR% DISTRIBUTION LISTS FOR DXXIMENIS KÃJ DONiT NEEDI'ULL TEXT CONVERSION REQUIRED
'OTAL NUMBER OF COPIES REQUIRED: LTTR 39 ENCL 39
Indiana Michigan Power Company Cook Nuclear Plant PO. Box 458 Bridgn)an, I)II 49106
, 6164655901 INQMNA N ICHIGAIV POWER October 5, 1989 United States -Nuclear Regul'atory Commission Document Control Desk Rockville, Maryland 20852 Operating License DPR-58 Docket No. 50-315 Document Control Manager:
In accordance with the criteria established by 10 CFR 50.73 entitled Licensee Event Re ortin S stem, the following report is being submitted:
89-012-00 Sa:ncerely,
,k R.~
A.A. Blind Plant Manager AAB:clw Attachment.
CC D.H. Nilliams, Jr.
A.B. Davis, Region M.P. Alexich III P.A. Barrett, J.E. Borggren R.F. Kroeger NRC Resident Inspector J.G. Giitter, NRC R.C. Callen G. Charnoff, Esq.
Dottie Sherman, ANI Library D. Hahn INPO PNSRC S,J ~ B1.ewer/B.P. Lau7au ~wg Pl
NRC Form 300 U.S. NUCLEAR REQULATOAY COMMISSION (0.03) APPROVED OMB NO. 31500104 I
EXPIRES'I 0/31/00 LICENSEE EVENT REPORT ILER)
DOCKS'7 NUMBER (2) A FACILITY NAME HI D., C. Cook Nuclear Plant Unit 1 0 5 0 0 0 OF 0 4
"'"'" Solid State Protection System Surveillance Testing Performed on The B3 Train5 While 1 1 The A Train Safety Injection Pump Was Inoperable Due to Personnel Error EVENT DATE (SI LER NUMBER (0) REPORT DATE (7) O'THER FACILITIES INVOLVED (SI FACILITY NAMES DOCKET NUMBER(SI MONTH DAY YEAR YEAR yQi" SEQUENTIAL NUMBER PP:
THB NUMNNR MONTH DAY YEAR 0 5 0 0 0 0 9 1 3 89 89 0 1 2 0010 THIS REPORT IS SUBMITTED PURSUANT T 0 THE REQUIREMENTS OF 10 CFR (I: (Check One or mori Of the follovvfnfl (ll 0 5 0 0 0 OPEAATINO MODE (0) 73.71(II)
] 20.402(0) 20.405( ~ I 00.73(el(2)(lv)
POWER 20.400 (~ HI I B) 50.30(e) (I ) 50.73(eH2Hv) 73.7 1(c)
LEYEL OTHER ISuecrfy In Auttrect 00.73(e)12HYN) 1 0 0 20.400( ~ l(1)(0) 50.30(cH2) uelow enrf ln Tent, NRC Eorm 20A05( ~ I (1)(NI I 50.73(e) (2)(ll 00.73(eHEHvillHA) 34EAI 20.405(e l(1 I Bv) 00.73(eH2) IN) 50,73(e) (2) (vNIH 0 )
20,405(eHIHvl 50.73(eH2)(Ni) 50,73(e)(2Hel LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE K. R. Baker, Operations Superintendent 6 1 6 4 6 5 5 9 0 1 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS AEPOAT I13I MANUFAC- EPOATABLE .:>jj:.tIr@Rgen)mmg~tm MANUFACi EPORTABL 9('fga()PALS(FABv)fEy CAUSE SYSTEM COMPONENT TO NPRDS CAUSE SYSTEM COMPONENT TURER TO NPRDS TURER
(~(evcm> .,&13(mli4I~e:::I(:
- 'Ii)IEIIIjII(IP'0:: j)I(7'jiN>~i@),jij%~,;
SUPPLEMENTAL REPORT EXPECTED (14l MONTH DAY YEAR EXPFCTEO SUBMISSION DATE (15)
YES Ilf yet, comulete EXPECTED SUBMISSION DATE/ NO ABSTRACT ILImlr to f400 tuecet, I e., euurovlmerely frltein tlnoli.tutti ryuevvntren llnnl 110)
At 0852 on September 13, 1989, the B Train of the Solid State Protection System (SSPS) was ma'de inoperable Eor SSPS and reactor trip breaker surveillance testing aEter receiving permission Erom the Shift Supervisor and Unit Supervisor. Due to the design of the circuitx'y, the B Train of safety injection is also made inoperable during the testing. The A Train safety injection pump was also inoperable during the testing due to being isolated for leak repairs. Therefore, both safety injection pumps were inoperable Erom 0852 until the B Train of SSPS was returned to operabilit'y at 1000 on September 13, 1989. This violation of T.S. 3.5.2 was recognized by a second Unit Supervisor when reviewing plant status in preparation for the A Train SSPS and reactor trip breaker testing.
The primary cause of this event was failure oE the Shift Supervisor and Unit Supervisor to recognize that the SSPS testing should not be done with the opposite train saEety injection pump inoperable. Also contributing to the event was the job planning process which did not consider the surveillance schedule and the lack of guidance in the surveillance procedure to ensure that opposite train equipment was operable. Preventive actions taken to prevent recurrence include revision of the surveillance procedure and inclusion of the surveillance schedule in the job planning process.'RC Form 300 (0 03 I
NRC Form 388A U.S~ NUCLEAR REGULATORY COMMISSION (943 I LICENSEE EVENT REPORT {LER) TEXT CONTINUATION APPROVED OMS NO. 3150&(04 EXPIRES: 8/31/88 FACILITY NAME (1> DOCKET NUMSER (3( LER NUMSER (8) ~ AGE (3I YEAR .C: SEGMENT/AL .'(". 4(ve/ON SdP. NUM 84 %iK HUMP(4 D. C. Cook Nuclear Plant Unit 1 0 5 0 0 0 .3 1 5 8 9 0 1 2 0 0 02oF 0 4 TEXT /limo/4 N/pcd ir /494ir4E 4/4 odd/dd44/PIRC Fd/m 388AS/ (1TI Conditions Prior to Occurrence Unit One in Mode 1 at 100 percent reactor thermal power'.
Descri tion of Event At 0852 on September 13, 1989, the B Train of the Solid State Protection System (SSPS) (EIIS/JC) was made inoperable for SSPS and reactor trip breaker (EIIS/AA-BKR) surveillance testing after receiving permission from the Shift Supervisor (Senior Licensed Operator) and the Unit Supervisor (Senior Licensed Operator).'ue to the design of the circuitry, the B Train of safety injection (EIIS/BQ) is also made inoperable during the testing.
Concurent with the B Train testing, the A Train safety injection pump was also inoperable due to it being isolated for leak repairs at 0450 on September 13, 1989. Therefore, both safety injection pumps were inoperable for one hour and eight minutes. One safety injection pump was isolated and the other would not have auto started in the event of an SI signal, from 0852 when the B Train was 'placed in test, until the B Train of SSPS was returned to operability at 1000 on September 13, 1989. This violation of Technical Specifi.cation 3.5.2 was. recognized by a second Unit Supervisor '(Senior Licensed Operator) when reviewing plant status prior to granting approval for the A Train SSPS and reactor trip breaker testing.
Cause of Event The primary cause of this event was that the Shift Supervisor and the Unit Supervisor failed to recognize that the B Train SSPS testing should not have been done while the A Train safety injection pump was inoperable. Both supervisors knew that the A Train safety injection pump was inoperable, but they did not make the connection when authorizing performance of the B Train SSPS testing.
Job planning inadequacy also contributed to this event. The Operations Department and Instrumentation & Control Department representatives, involved in planning of the work for the day, did not consider the surveillance test schedule when arranging for the A Train safety injection pump work.
Also contributing to this event was a procedural weakness. The Unit One SSPS and reactor trip breaker surveillance test procedure did not contain direction to ensure the opposite train equipment was operable prior to commencing the test.
44C FOAM 3(dA (9831
NRC Form 388A U.S. NUCLEAR RECULATCRY COMMISSION (943(
LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVED OMS NO. 3150WIOI EXPIRES: 8/31/88 FACILITY NAME (II DOCKET NUMSER (1I LER NUMSER LSI PACE (31 YEAR SEOVENTIAL P<rr REVISION NVModrl NVMOTA D. C. Cook Nuclear Plant Unit 1 e ~ 0 o o 3 1 5 8 9 0 1 2 0 0 03<<0 4 TEXT llfmoro sosco ir oso/rwsrL o>> a /Tioiono///RC Form 36SA's/ (IT(
Anal sis of the Event This event is considered reportable pursuant to 10 CFR 50.73(a)(2)(vii).
During this event, all.of the A Train equipment was operable except for the North safety injection pump. If a safety injection signal had occurred during this event the B Train equipment would not have automatically started, but would have started upon manual action. The emergency operating procedure for a safety injection requires the operators to verify the safety injection .
pumps running and to manually start pumps as needed. It is conservatively estimated that the operators would have manually started the South safety injection pump within five minutes of the event initiation. The limiting accident when considering loss of high head safety injection is the small break loss of coolant accident. For the circumstances in question the A Train'centrifugal charging pump would have began injection upon event initiation, but when a conservative approach of no high hea'd safety injection is consi.dered, significant increases in core fluid temperature are not expected until well after the five minute point.
Since operator training and procedural guidance existed to ensure that'he B Train safety injection pump and charging pump would have been promptly started in the event of a safety injection, it is concluded that adequate safety injection flow would have been initiated far in advance of reaching an inadequate core cooli.ng situation.
Based on the above it is concluded that this event did not involve an unreviewed safety question as defined in 10 CFR 50.59.
Corrective Actions A memorandum was issued to Operations Department personnel to reinforce the necessity of maintaining opposite train equipment operable during SSPS'esting on the other train.
This event was discussed with the job planners to stress the need to consider the surveillance test schedules during the daily job planning meetings. The surveillance schedules are now being used during the job planning process.
I The Unit One SSPS and reactor trip breaker surveillance test procedures were revised with'change sheets on September 21, 1989, to add a requirement for the Shift Supervisor to ensure that the opposite train equipment is operable. The Unit Two procedures did not require revision as they had been previously revised to include the requirement.
NaC so/IM 3ddA (9 831
NRC Form 3ddA U.S. NUCLEAR REOULATCRY COMMISSION 1943)
LICENSEE EVENT REPORT ILER) TEXT CONTINUATION APPROVED OMB NO. 3'Is)WIOI EXPIRES: 8/31/88 FACILI'TY NAME III DOC)hET NUMSER 13) LER NIIMSER (8) PACE )3) yd*R ~u'SEQUENT/AL 5'rUM d4
@AN 4d V rdlQ rr r/v M 9 d 4 D. C. Cook Nuclear TEXT /// moro d/roco /I roduwo/L Plant -
uoo or)r/rohorho//VRC Form 3SSAS)
Unit
)IT) 1 0 5 0 0 0 3 I 5 8 9 0 l 20 0 0 4 oF 0 4 The procedure weakness was reviewed for generic implications. It was determined that the current practice for the writing of procedures is to provide the Shift Supervisor with sufficient information to allow determining the affect of performing the procedure on plant equipment, and systems. This practice is 'also specified in the Plant Manager Instruction (PMI-2010) for procedures. Since adequate guidance in this area is provided by PMI-2010, no new initiatives are warranted at this time.
Failed Com onent Identification None Previous Similar Events There were no previous similar events identified which involved SSPS surveillance testing on one train, while equipment was inoperable on the opposite train.
44C Foohr dddo 19 83)