ML17325A170

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LER 87-007-00:on 870520,8-hour Turbine Room Sump Samples Not Analyzed Due to Removal of Compositor for Routine Calibr. Caused by Personnel Error.Compositor Restored to Operation & Instrumentation Personnel counseled.W/870619 Ltr
ML17325A170
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 06/19/1987
From: Beilman T, Will Smith
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
LER-87-007, LER-87-7, NUDOCS 8706230281
Download: ML17325A170 (6)


Text

REGULAT .'NFORMATION DESTREBVTEOfi STEM <REDS>

ACCESSION NBR. 6706230281 DOC. DATE: 87/06/19 NOTAP.IZED: NQ DOCKET FACIL: 50-315 Donald C. Cook Nuclear Power Plant Unit li Indiana 05000315 AUTH. NAME AUTHOR AFFILIATION BEILMANiT. P. Indiana 8c Michigan El ec tr i c Cc.

SMITHS'. G. Indiana 4< Michigan Electric Co.

RECIP. NAME RECIP IENT AFFILIATION

SUBJECT:

LER 87-007-00: on 870520'urbine room sump effluent discharge floe sensor 8. recorders DFR-700' emoved from svc for routine calibrI compositer remained inoperable overnight. Caused bg personnel error. Sign posted to alert personnel. W/87061'7 ltr.

DISTRIBUTION CODE: IE22D COPIES RECEIVED: LTR ENCL I SIZE:

TITLE: 50. 73 Licensee Event Report (LER)i Incident Rpti etc.

NOTES:

RECIPIENT CQP IES. RECEPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTP. ENCL PD3-3 LA PD3-3 PD W I GG I'NG1 ON> D 1 1 lNTERNAL: ACRS MICHELSQN 1 ACRS MQELLER 2 2 AEOD/DOA 1 AEQD/DSP/ROAB 2 2

  • EOD/DSP/TPAB DEDRO NRR/DEBT/ADE 0 NRR/DEST/ADS 0 NRR/DFST/CEB 1 NRR/DEST/ELB NRR/DFST/ECSB NRR/DEST/MFB NRR/DEST/MTB 1 NRR/DEBT/PSB NRR/DEST/RSB 1 NRR/DEST/SGB 1 NRR/DLPQ/HFB NRR/DLPG/GAB NRR/DOEA/EAB 1 NRR/DREP/RAB NRR/DREP/RPB NRR/ AS/If RB 1 NRR/PMAS/PTSB 02 1 RES DEPY GE 1 RGN3 F ILE 01 1 EXTERNAL: EGC<G GRDHi M 5 5 H ST LOBBY NARD 1 1 LPDR NRC 1 2 NSIC HARRIS' PDR'SIC 1 MAYST G TOTAL NUMBER OF COPIES REGV'IRED: LTTR 42 ENCL 40

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NRC Form 344 U.S. NVCLEAR REGULATORY COMMISSION (943 I APPROVED OMB NO. 31504(OC EXPIRES! 4/31/44 LICENSEE EVENT REPORT (LER)

DOCKET NUMBER (1) PA FACILITY NAME (ll D. C. COOK NUCLEAR PLANT UNIT 1 0 5 0 0 0 3 1 5 1 OF 0 3 MISSED EVENT INITIATED SURVEILLANCE DUE TO FAILURE TO RECOGNIZE FLOW RECORDER EFFECT ON SLQIPLER EVENT DATE (5) LER NUMBER (Sl REPORT DATE (7) OTHER FACILITIES INVOLVED IS)

SSGVSNT/AL :rOO( RSV/CtQN MONTH DAY YEAR FACILITYNAMES DOCKET NUMBER(3)

MONTH OAY YEAR YEAR NVMSE/l C. Cook Plant-Unit 2 0 5 0 0 0 3 1 6 0 5 20 878 7 0 0 7 0 0 0 6 1 9 8 7 0 5 0 0 0 OPERATING THIS REPORT IS SUBMITTED PURSUANT T 0 THE REGUIREMENTB DF 10 cFR ()t /cnecft onc or moro of tnc for/or/fop/ (ill MODE (4)

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TELEPHONE NUMBER T. P. Beilman AREA CODE I&C/Planning Department Superintendent COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS. REPORT 113)

MANUFAC EPORTABLE Q y MANUFAC. EPORTABL CAUSE SYSTEM COMPONENT CAUSE SYSTEM COMPONENT TVRER TURER TO NPRDS TO NPRDS i

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'MM MWXW SVPPLEMENTAL REPORT EXPECTED (Ie) MONTH OAY YEAR EXPECTED SUBM/SSION DATE (151 YES /ff yct, compfcN EXPECTED $ (fpltlSSIOf/ DATE/ NO ABSTRACT /Lfmft to 140/) ipecet, /e., eppronfmetcfy If/teen ifnpfc ipece typcwr/Iten /Ined l14)

On May 20, 1987 at 1520 hours0.0176 days <br />0.422 hours <br />0.00251 weeks <br />5.7836e-4 months <br />, the Turbine Room Sump effluent discharge flow sensor and recorder, DFR-700, was removed from service for routine calibration. It was not recognized at that time that the Turbine Room Sump sample compositor received input from the flow instrument. Due to problems encountered, the compositor remained inoperable overnight and the eight hour samples were not analyzed as required by the action statement of Technical Specification 3.3.3.9.

The error was discovered on May 21 1987 at 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br /> and manual sampling was begun. The instrument was returned to an operable condition by 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br />.

To prevent possible recurrence, Instrumentation personnel who may become involved with this instrument have been informed of this finding. Also, a sign has been added to the recorder informing personnel of its input to the Technical Specification required compositor.

s7o~"-so-8'ooosi5 87obi~

PDR ADOCK PD 8

U.S. NUCLEAR REGULATORY COMMISSION NRC Form 366A (583)

LICENSEE EVENT REPORT (LER) TEXT CONTINUAT N APPROVEO OMS NO. 3150&104 EXPIRESI 8/31/58 PACIUTY NAME (1( OOCKET NUMSER (21 LER NUMBER (61 PAGE (31 YEAA g~ SEGVENTIAL NVMSEA

@~II AEV IS ION NUM EA COOK NUCLEAR PLANT UNIT D~ C ~

1 o s o o o 31 58 7 0 0 7 0 0 020F0 3 TE3(T /S'axle Reoe 4 nquhsd, use aSSOlna////IC fcnn 36543/ (171 Conditions Prior to Occurrence Unit One Mode 1 (power operation) 79 percent reactor thermal power.

Unit Two Mode 1 (power operation) 80 percent reactor thermal power.

Descri tion of Event On May 20, 1987 at 1520 hours0.0176 days <br />0.422 hours <br />0.00251 weeks <br />5.7836e-4 months <br />, the Instrumentation and Control (I6C)

Section was calibrating the Turbine Room Sump effluent discharge flow recorder (EIIS/FR) for routine preventive maintenance. For this work, the flow sensor is disconnected from the recorder and test equipment is connected to supply a standardized simulated input. The calibration was not completed by t'e end of the shift and the test equipment was left connected and turned off. This action resulted in making the automatic sample compositor (EIIS/ASV) inoperable due to the simulated no-flow signal being applied.

The Chemical Section performs four-hour checks on the compositor receiver to verify automatic operation of the compositor. Due to abnormal work on the Turbine Room Sump causing very intermittent discharge flow, little increase in sample collection was expected. The compositor actuation was verified manually each time, but the automatic signal was not known to be inoperable.

However, by 0730 hours0.00845 days <br />0.203 hours <br />0.00121 weeks <br />2.77765e-4 months <br /> on May 21, 1987 when no increase in sample was noted, manual sampling was begun due to suspected failure of the automatic sampling. By 1045 hours0.0121 days <br />0.29 hours <br />0.00173 weeks <br />3.976225e-4 months <br />, the failure was confirmed by direct observation of flow from the sump with no automatic sample being taken by the compositor.

There were no inoperative structures, components or systems at the start of the event that contributed to the missed surveillance.

Cause of Event The cause of the event was the failure to recognize that the recorder supplies a signal input to the compositor, and to make contingency plans for removing the compositor from service. As the recorder's effect was learned during the calibration, the fact that the compositor being required by Technical Specification was not identified through job order evaluation (prior to job performance).

NAC POAM 36/IA

  • U.S GPO:1988.0 826 538/455

U.S. NUCLEAR REGULATORY COMMISSION NRC FONN 384A (843)

LICENSEE EVENT REPORT (LER) TEXT CONTINUATION APPROVEO OMB NO. 3150&10E EXPIRES: 8/31/88 DOCKET NUMBER (2) LER NUMBER (8) PAGE I3)

FACILITY NAME (ll

~rr /IEV/8/ON y~ > SEOUENZIAL Prr Err8 NUMBER NUMSER D. C. COOK NUCLEAR PLANT UNIT 1 0 5 0 0 0 3 1 5 87 0 0 7 00 03 OF 0 3

//mme f//fCf4 nqcdn4 I/fe ~ NR/Ene/A//IC %%d//II 35543/ (17)

Anal sis of Event The compositor was inoperable approximately 23.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. Sampling and analysis of the effluent flow was not performed for approximately 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br />. This incident is considered as a missed surveillance and reportable under 10CFR50.73 due to the fact that eight-hour alternate analysis was not performed as required by the action statement of Technical Specification 3.3.3.9.

As., the Turbine Room Sump sample compositor is the last point monitored for radioactive discharge, the related front line radiation monitors were reviewed for that time period and found to be operable. The daily sample requirement of the NPDES permit was determined to be met. A special report was required to estimate flow for the time the recorder was being calibrated, which was submitted.

Corrective Actions When the Chemical Section notified I&C of the problem with the compositor, steps were taken to restore the recorder. The compositor was declared operable at 1500 hours0.0174 days <br />0.417 hours <br />0.00248 weeks <br />5.7075e-4 months <br /> on May 21, 1987.

To prevent recurrence, the I&C supervisors and job order evaluation group have been informed of the findings in this system. Also, a sign has been added to the recorder informing personnel of its input to the Technical Specification required compositor.

Failed Com onent Identification None.

Previous Similar Events None.

NRC fORM SEOA fU.S GPO:)088 0 52A 538/EBS

~4riaen lactrle IMIANA8 MICHIGAIJIHE'CTRIC COMPAIIIY DONALD C. COOK NUCLEAR PLANT P.O. Box 458, Brldpcman, Ml 49106 Telephone {616) 465 5901 June 19, 1987 United States Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Operating License DPR-58 Docket No. 50-315 Document Control Manager:

In accordance with the criteria established by 10 CFR 50.73 entitled Licensee Event Re ortin S stem, the following report is being submitted:

87-007-0 Sincerely, W. G. Smith, Jr.

Plant Manager

/afh Attachment, CC: A. B. Davis, Region D. L. Wigginton, NRC III J. E. Dolan M. P. Alexich R. F. Kroeger H. B. Brugger R. W. Jurgensen G. Charnoff, Esq.

R. C. Callen, MPSC D. Hahn, MDPH INPO NRC Resident Inspector Dottie Sherman, ANI Library A. A. Blind PNSRC File