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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:RO)
MONTHYEARML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 ML17313A3131998-03-21021 March 1998 LER 98-001-00:on 980301,surveillance Test Deficiency Found During Qaa Leads to TS 3.0.3/4.0.3 Entry.Caused by Personnel Error.Personnel Responsible for Inadequately Performed SR Were Coached ML17313A2251998-03-0505 March 1998 LER 93-005-00:on 930309,CR Personnel Discovered Missed TS LCO Action & Subsequently Performed Surveillance Satisfactorily.Caused by Personnel Error.Appropriate Disciplinary Action issued.W/980305 Ltr ML17313A2241998-02-26026 February 1998 LER 98-001-00:on 980130,reactor Protection & ESFAS Instrumentation Not Bypassed within one-hour Allowed by TS Occurred.Caused by Inadequate Procedures.Expectation to Detect Alarm Conditions Was Emphasized to CR Personnel ML17313A2081998-02-10010 February 1998 LER 97-007-00:on 971006,TS Violation Occurred Due to Inadequate Shutdown Cooling Flow During Modes 5 & 6 Operation.Independent Investigation of Event Was Conducted IAW APS CA program.W/980210 Ltr ML17313A2041998-02-0505 February 1998 LER 97-006-00:on 971028,missed TS 4.0.5 SR Was Noted.Caused by Personnel Error.Independent Investigation of Event Is Being Conducted IAW W/Aps Corrective Action Program ML17313A1201997-11-12012 November 1997 LER 97-006-00:on 971020,manual Reactor Trip Occurred Due to Vibration & Bearing Temp Increases in Reactor Coolant Pump. Caused by Failed Lower Journal Bearing.Bearing Assembly Was Disassembled,Inspected & Rebuilt ML17312B7181997-10-0707 October 1997 LER 97-003-00:on 970907,inadvertent Loss of Power & EDG Start Occurred Due to Procedural Error.Changed Train a & Train B Edg/Ist ST Procedures to Consistently Reflect Proper Pretest Staging Hand switches.W/971007 Ltr ML17312B7051997-09-26026 September 1997 LER 97-003-01:on 970215,seven Main Steam Safety Valves Were Found Out of Tolerance Prior to Refueling Outage.Safety Analysis Performed Based Upon as-found MSSV Data Which Demonstrated That MSSVs Would Perform Safety Functions ML17312B5531997-07-0707 July 1997 LER 97-002-00:on 970528,SR for Core Protection Was Not Performed Due to Inadequate Procedures.Revised Procedures ML17312B5501997-07-0707 July 1997 LER 97-003-00:on 970211,notified of Trevitest Activities Indicating That Total of Seven MSSVs Had as-found Lift Set Pressures Greater than 3 Percent Allowed by TS 3.7.1.1. Investigation Conducted.Seven MSSVs replaced.W/970707 Ltr ML17312B4971997-06-13013 June 1997 LER 97-002-00:on 970531,RT Occurred.Caused by Spurious Opening of All Four Rt Switchgear Breakers.Independent Investigation of Event Being Conducted in Accordance W/Util Corrective Action Program ML17312B1461996-12-17017 December 1996 LER 96-007-00:on 961119,surveillance Test Deficiencies Were Found During GL 96-01 Review Leading to TS 3.0.3 Entries. Caused by Increase in Scope of Required Testing.Supplement Will Be submitted.W/961217 Ltr ML17312A9511996-09-0404 September 1996 LER 96-003-00:on 960809,open Auxiliary Bldg Door Caused Full Bldg Essential Filtration Inoperability.Caused by Personnel Error.C/As Under consideration.W/960904 Ltr ML17312A8641996-07-17017 July 1996 LER 96-001-00:on 960621,inaccurate Gas Calculations for Post Accident Sampling Sys Occurred.Caused by Surveillance Test Worksheet Errors.Independent Investigation of Event Being conducted.W/960717 Ltr ML17300B2541996-06-11011 June 1996 LER 96-001-01:on 960404,inappropriate Grounding of Equipment Resulted in Condition Outside Design Basis of Plant. Established Fire Watches Required for Affected Areas ML17312A8081996-06-0909 June 1996 LER 96-002-00:on 960514,Tech Spec Violation Occurred Due to Erroneous Surveillance Requirement.Caused by Incorporation of C-E Generic Ts.Investigation Being conducted.W/960609 Ltr ML17312A7751996-05-17017 May 1996 LER 96-003-00:on 960122,missed Surveillance for Logic Check of Logs 1 & 2 Safety Excore Bypasses.Caused by Procedural Error.Log Power Functional Test Revised to Check Logs 1 & 2 Bypasses Regardless of Power level.W/960517 Ltr ML17312A7511996-05-0606 May 1996 LER 96-001-00:on 960404,smoke Discovered in Back Boards Area of CR by Security Officer,Performing Hourly Fire Watch Tour. Caused by Improperly Grounded Circuit.Investigation for Inappropriate Grounding of Low Voltage Power Sys Initiated ML17312A7241996-04-25025 April 1996 LER 96-002-00:on 960401,inappropriate Work Practice Resulted in Esfa of Train B Edg.Night Order Was Issued to All Three Units Describing event.W/960425 Ltr ML17312A6861996-04-0606 April 1996 LER 95-007-01:on 950512,determined That Bench Settings of air-operated Letdown & Containment Isolation Valves Adversely Affected Ability of Valves to Perform 10CFR50 App R Safety Function.Affected Valves Modified ML17312A5631996-02-22022 February 1996 LER 95-016-00:on 951212,containment Spray TS Violation Occurred Due to Unrecognized Valve Failure.Shim/Band Was Placed Around Stator of 1JSIBUV665 Motor Operator to Maintain Stator in Correct position.W/960222 Ltr ML17311B3381996-01-0909 January 1996 LER 95-014-00:on 951209,reactor Tripped Following Degradation of Main FW Flow.Caused by Malfunction of Fwcs Power supply,NNN-D11,transfer switch.NNN-D11 Aligned to Normal Power supply.W/960109 Ltr ML17311B3331995-12-31031 December 1995 LER 95-013-00:on 951201,AFW Sys Was Outside Design Basis of Plant.Caused by Design Error.Performed Assessment to Demonstrate That Existing Condition Does Not Pose Addl Safety concerns.W/951231 Ltr ML17311B2801995-11-23023 November 1995 LER 95-011-00:on 951018,identified Procedural Deficiency W/Msiv & FWIV ISTs Due to Personnel Error.Verified Operability of MSIVs & FWIVs.W/951123 Ltr ML17311B2531995-10-20020 October 1995 LER 95-002-00:on 950924,identified That Abnormal Blowdown Valves to Blowdown Flash Tank (Bft) Isolated,Resulting in Reactor Core Power Exceeding 3,800 Mwt Due to Personnel Error.Procedure for Aligning Blowdown to Bft Revised ML17311B1991995-09-21021 September 1995 LER 95-010-00:on 950727,equipment Qualification of Air Handling Unit Caused Essential Cw Pump to Be Inoperable. Used Work Orders to Drill Weep Holes in Motor Lead Connection boxes.W/950921 Ltr ML17311B1741995-09-0404 September 1995 LER 95-004-01:on 950329,containment Electrical Penetration Overcurrent Protective Devices Found Outside Design Basis. Caused by Error on Part of Original Architect Engineer. Modified Affected Circuits Critical to Normal Operational ML17311B1561995-08-27027 August 1995 LER 95-003-00:on 950729,switchyard Voltage Dropped Below Administratively Imposed Limit of 524 Kv for Approx 10 Seconds Due to Transient Grid Voltage.No C/A Taken Since Transmission Sys Transient Short duration.W/950827 Ltr ML17311B1551995-08-25025 August 1995 LER 95-002-01:on 950303,identified That Slb Analyses Failed to Consider as Initial Condition One Percent SDM for All Rods in (ARI) Due to Lack of Coordination & Unclear Div of Responsibilities.Ari Core Data Book SDM Curves Modified ML17311B1211995-08-16016 August 1995 LER 95-005-00:on 950717,RT on Low SG Water Level Was Result Following Degradation of MFW Flow.Completed Evaluation of Event ML17311B0841995-07-28028 July 1995 LER 94-005-01:on 941019,completed TS Required Shutdown Due to Expiration of LCO Time Limit.Design Change Options Identified & Will Be Reviewed to Determine If Valve &/Or Motor Operator Replacement or Mod Necessary ML17311B0721995-07-20020 July 1995 LER 95-004-00:on 950706,identified Four Occassions Between 950407 & 0630 When Conditional Surveillance in TS LCO 3.8.4.1 Action a Not Performed Due to Inattention to Detail. CR Copy of Temporary Procedure 40TP-9ZZ04 Corrected ML17311B0081995-07-0606 July 1995 LER 95-003-00:on 950613,TS LCO 3.0.3 Entered Following Loss of Both Trains of Essential Cw Sys & Both Hydrogen Recombiners.Caused by Spurious Actuations Due to Broken EDG Speed Probe Connector.Connector replaced.W/950706 Ltr 1999-08-27
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17300B3811999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Pvngs,Units 1,2 & 3.With 991007 Ltr ML17300B3271999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for Pvngs,Units 1,2 & 3 ML17313B0751999-08-27027 August 1999 LER 99-002-00:on 990730,test Mode Trip Bypass for EDG Output Breakers Not Surveilled.Cause Under Investigation.Operations Personnel Conservatively Invoked SR 3.0.3 for SR 3.8.1.13. with 990827 Ltr ML17313B0611999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Pvngs,Units 1,2 & 3.With 990810 Ltr ML17313B0191999-07-16016 July 1999 LER 99-005-00:on 990618,RT on Low DNBR Was Noted.Caused by Hardware Induced Calculation Error.Cr Operator Was Taken to Place Reactor in Stable Condition IAW Appropriate Operating Procedure ML17300B3151999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Pvngs,Units 1,2 & 3.With 990714 Ltr ML17313A9921999-06-21021 June 1999 Special Rept:On 990525,RMS mini-computer Was Removed from Service to Implement Yr 2000 Mod & Was OOS Longer than 72 H Allowed.Caused by Planned Y2K Mods.Preplanned Alternate Sampling Program Was Initiated ML17313A9911999-06-18018 June 1999 Special Rept:On 990510,loose-part Detection Sys Channel 2 Was Declared Inoperable.Caused by Malfunction of Mineral Cable Connector to Accelerometer.Licensee Will Implement Modifications Which Will Enhance loose-part Detection Sys ML17313A9731999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Pvngs,Units 1,2 & 3.With 990608 Ltr ML17313A9281999-05-0707 May 1999 LER 99-004-00:on 990408,PSV Lift Pressures Were Outside of TS Limits.Caused by Lift Pressure Setpoint Drift.Psvs Have Been Tested,Disassembled,Inspected,Reassembled & Certified at Wyle Labs ML17313A9201999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Pvngs,Units 1,2 & 3.With 990512 Ltr ML17313A8951999-04-14014 April 1999 LER 99-003-00:on 990317,required Surveillance Requirement Not Completed Due to Deficient Procedure,Was Determined. Caused by Cognitive Personnel Error.St Procedures Revised to Require Chiller to Be Operating & Oil Temperature Checked ML17313A8921999-04-13013 April 1999 LER 98-003-01:on 980902,discovered That MSSV as-found Lift Pressures Were Outside TS Limits.Caused by Bonding of Valve Disc to Nozzle Seat.Affected Valves Were Adjusted,Retested & Returned to Svc ML17313A8891999-04-0909 April 1999 LER 99-001-00:on 990310,RT on High Pressurizer Pressure Was Noted.Caused by Loss of Heat Removal.Cr Supervisor Was Removed from Shift Duties for Diagnostics Skills Training. with 990409 Ltr ML17300B3071999-03-31031 March 1999 Seismic Portion of Submittal-Only Screening Review of Palo Verde Nuclear Generating Station Units Ipeee. ML17313A8801999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Pvngs,Units 1,2 & 3.With 990412 Ltr ML20207M9231999-03-12012 March 1999 Amended Part 21 Rept Re Cooper-Bessemer Ksv EDG Power Piston Failure.Total of 198 or More Pistons Have Been Measured at Seven Different Sites.All Potentially Defective Pistons Have Been Removed from Svc Based on Encl Results ML20207H7471999-03-10010 March 1999 1999 Emergency Preparedness Exercise 99-E-AEV-03003 ML17313A8361999-03-0101 March 1999 LER 99-001-00:on 990103,TS Violation for Power Dependent Insertion Limit Alarm Being Inoperable.Caused by Personnel Error.Revised Procedure to Clarify How Computer Point Is to Be Returned to Scan Mode.With 990302 Ltr ML17313A8501999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Palo Verde Nuclear Generating Station.With 990311 Ltr ML17313A7791999-02-0505 February 1999 Safety Evaluation Accepting Licensee Rev to Emergency Plan That Would Result in Two Less Radiation Protection Positions Immediatelu Available During Emergencies ML17313A8061999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Pvngs,Units 1,2 & 3.With 990218 Ltr ML17313A7701999-01-15015 January 1999 LER 96-008-00:on 960507,inadequate Procedure Results in Nuclear Power Channels Not Calibrated During Power Ascension Tests Occurred.Caused by Deficient Procedure.Procedure Revised ML17313A7381998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.With 990113 Ltr ML20206H2101998-12-31031 December 1998 SCE 1998 Annual Rept ML17313A7031998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Pvngs,Unit 1,2 & 3. with 981209 Ltr ML17313A6701998-11-0404 November 1998 Rev 2 to PVNGS Unit 2 Colr. ML17313A6741998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Pvngs,Units 1,2 & 3.With 981109 Ltr ML17313A6611998-10-24024 October 1998 LER 98-008-00:on 980729,EQ of Electrical Connectors Were Not Adequately Demonstrated.Caused Because Test Was Conducted with Only Single Lv Connector & Without Fully Ranged Inputs. Revised EQ Requirements ML17313A6561998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for PVNGS Units 1,2 & 3.With 981007 Ltr ML17313A5961998-09-14014 September 1998 LER 98-002-00:on 980814,B Train H Recombiner Was Noted Inoperable Due to cross-wired Power Receptacle.Cause of Event Is Under investigation.Cross-wired Power Supply Receptacle for B Train H Recombiner Was re-wired ML17313A5761998-09-0808 September 1998 LER 98-003-01:on 980113,discovered That One Channel of RWT Level Sys Had Failed High.Caused by Water Intrusion Into Electrical Termination Pull Box.Weep Holes Were Drilled Into Bottoms of Pull Boxes Nearest Level Transmitters ML17313A5591998-08-28028 August 1998 LER 98-001-00:on 980730,entered TS 3.0.3 Due to Safety Injection Flow Instruments Being Removed from Svc.Caused by Personnel Error.Transmitters Were Unisolated & Returned to svc.W/980828 Ltr ML20151S0941998-08-21021 August 1998 Rev 6 to COLR for PVNGS Unit 3 ML20151S0861998-08-21021 August 1998 Rev 4 to COLR for PVNGS Unit 1 ML20151S0901998-08-21021 August 1998 Rev 1 to COLR for PVNGS Unit 2 ML18066A2771998-08-13013 August 1998 Part 21 Rept Re Deficiency in CE Current Screening Methodology for Determining Limiting Fuel Assembly for Detailed PWR thermal-hydraulic Sa.Evaluations Were Performed for Affected Plants to Determine Effect of Deficiency ML17313A5401998-08-13013 August 1998 Special Rept:On 980715,declared PASS Inoperable.Caused by Failure of Offgas Flush/Purge Control Handswitch HS0101. Handswitch Replaced & Post Maintenance Retesting Was Initiated ML17313A5301998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Pvgns,Units 1,2 & 3.W/980812 Ltr ML17313A5201998-07-30030 July 1998 LER 98-004-00:on 980630,personnel Discovered That Pressure Safety Valve Had Not Received Periodic Set Pressure Test for ASME Class 1 Pressure Safety Valve.Caused by Personnel Error.Pressure Safety Valve reviewed.W/980730 Ltr ML17313A5791998-07-0707 July 1998 to PVNGS SG Tube ISI Results for Seventh Refueling Outage Mar & Apr 1998. ML17313A5001998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Palo Verde Nuclear Generating Station,Units 1,2 & 3.W/980710 Ltr ML17313A4671998-06-19019 June 1998 LER 98-007-00:on 980520,CR Personnel Observed Flow & Pressure Perturbations on Chemical & Vol Control Sys Letdown Sys.Caused by Cyclic Fatigue Due to Dynamic Pressure Transients.Unit Letdown Piping Replaced ML17313A4521998-06-19019 June 1998 Rev 5 to COLR for Pvngs,Unit 3. ML17313A4501998-06-19019 June 1998 Rev 4 to COLR for Pvngs,Unit 3. ML17313A4131998-06-0505 June 1998 LER 98-006-00:on 980507,determined That Plant Was Outside Design Basis Due to SI Discharge Check Valve Reverse Flow. Check Valve Was Disassembled,Examined & Reassembled, Whereupon Valve Met Acceptance Criteria ML17313A4211998-05-31031 May 1998 Monthly Operating Repts for May 1998 for Pvngs,Units 1,2 & 3.W/980609 Ltr ML17313A3951998-05-26026 May 1998 LER 98-005-00:on 980428,noted That Required Response Time Testing Had Not Been Performed.Caused by Personnel Error. Coached I&C Personnel Responsible for Reviewing Work Authorization Documentation ML17313A3691998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for PVNGS.W/980412 Ltr ML17313A3251998-04-0101 April 1998 LER 98-004-00:on 980304,safety Valves as-found Pressures Out of Tolerance.Cause of Event Is Under Investigation.Three Mssv'S & Psv Will Be Replaced W/Refurbished & Recertified Valves During Refueling Outage U1R7 1999-09-30
[Table view] |
Text
AC CELE RATED 1
Dl STRIBUTI ON t
DEMON STRATI 0. i SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RZDS)
ACCESSION NBR:8910120140 DOC.DATE: 89/10/03 NOTARIZED: NO DOCKET FACXL:STN-50-529 Palo Verde Nuclear Station, Unit 2, Arizona Publi 05000529 AUTH. NAME AUTHOR AFFILIATION SHRIVER,T.D. Arizona Public Service Co. (formerly Arizona Nuclear Power LEVINE,J.M. Arizona Public Service Co. (formerly Arizona Nuclear Power RECIP. NAME RECIPIENT AFFILIATION
SUBJECT:
LER 89-015-01:on 881203,action statement not met for inoperable radiation monitor.
W/8 ltr.
DISTRIBUTION CODE IE22T COPIES RECEIVED:LTR ENCL 'IZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:Standardized plant. 05000529 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 1 PD5 PD 1 1 CHAN,T 1 1 DAVIS,M 1 1 INTERNAL: ACRS MICHELSON 1 1 ACRS MOELLER 2 2 ACRS WYLIE 1 1 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 DEDRO 1 1 NRR/DEST/CEB 8H 1 1 NRR/DEST/ESB SD 1 1 NRR/DEST/ICSB 7 1 1 NRR/DEST/MEB 9H 1 1 NRR/DEST/MTB 9H 1 1 NRR/DEST/PSB SD 1 1 NRR/DEST/RSB 8E 1 1 NRR/DEST/SGB SD 1 1 NRR/DLPQ/HFB 10 1 1 NRR/DLPQ/PEB 10 1 1 NRR/DOEA/EAB 11 1 1 NRR/PREP/ PB 10 2 2 NUDOCS-ABSTRACT 1 1 G FILE 1 1 RES/DSIR/EIB 1 1 GNS FZQ> 01 1 1 EXTERNAL: EG&G WILLIAMSi S 4 L ST LOBBY NARD 1 1 LPDR 1 1 NRC PDR 1 1 NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 1 NOTES 1 1 NVZE K) ALL '%IKS" RECZPXIKIS~
PZEASE iUKiP US XQ RPXXRE %hfKEf CXKZACI.'IHE DOCUMENTS CXÃISOL DESKi RXM P1-37 (EXT. 20079) %0 RKiQCQMS RXSt NWS HCK DIBXRIBUZXCN LISTS XQR DQCQHRRXS VXJ DCSERT NREDf FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 41 ENCL 41
Arizona Public Service Company
'PALO VERDE NUCLEAR GENERATING STATION P,O, BOX 52034 ~ PHOENIX. ARIZONA 85072-2034 192-00533-JML/TDS/RJR October 3, 1989 U. S. Nuclear Regulatory Commission NRC Document Control Desk Washington, D.C. 20555
Dear Sirs:
Subject:
Palo Verde Nuclear Generating Station (PVNGS)
Unit 2 Docket No. STN 50-529 (License NPF-51)
Licensee Event Report 88-015-01 File: 89-020-404 Attached please find Supplement Number 1 to Licensee Event Report (LER) No.
88-015-00 prepared and submitted pursuant to the requirements of 10CFR 50.73.
In accordance with 10CFR 50.73(d), we are herewith forwarding a copy of this report to the Regional Administrator of the Region V Office.
If you have any questions, please contact T. D. Shriver, Compliance Manager at (602) 393-2521.
Very truly yours, J. H. Levine Vice President Nuclear Production JGH/TDS/RJR/kj Attachment CC: W. F. Conway (all w/a)
E. E. Van Brunt, Jr.
J. B. Hartin T. J. Polich H. J. Davis A. C. Gehr INPO Records Center 35'10120140 391003 PbR AEIOCK 0 000525 PDC
I' NRC Sotm 244 U.S. NUCLEAR RKOULATORY COMMISSION (903 l AppRDYED DMs Noi 21504(04 LICENSEE EVENT REPORT ILER1 f XPIRESI ~ ISIISS FACILITY NAME OI DOCKET NUMSER (2) PA TITLE Iel Palo Verde Unit 2 o 5 oo o 5291OF06 Action Statement not Het for Inoperable Radiation Monitor EVENT DATE (Sl LER NVMSER (SI REPORT DATE (7) OTHER FACILITIES INVOLVED LS)
SEOVENTIAL PC RevtetOte MONTH O*Y PACILI'TY NAM55 DOCKET NUMBER(5)
MONTH OAY YEAR YEAR NVM44 R V'i NVM45R YEAR III/A 0 5 0 0 0 1 2 0 3 8 8 8 8 ,01 5 01 10 03 89 N/A 0 5 0 0 0 THIS REPORT IS SUSMITTED PURSUANT T 0 THE REOUIRKMfNTS OF 10 csR (): Icneco one or more or tne Iollowingl IIII OPERATINO MODE ( ~ ) 20A02(4) 1 ~ 20.405(c) 50.72(e)(2)lhl Tl.71(4)
Ill(ill)
POWER 20A05(e) Ill)i) 50.24(e((II 50.72(e)(2)(rl 72 71(c)
LEvEL 1 0 0 20AOS(c) III(ill 50.24(el(2) 50.72(e) (ll(rS) DTHER ISpeciry In Aottrect ooiow errt In Tert, IYRC Form 20AOS(c) 50.72(e l(2) (ll 50.7l(e I (2)(r(4) (A) 444AI 20AOS(e IllI (le ) 50.Tile) (2)(5) 50.72(e) (2) (rill)(SI 20AOS(c) II I(rI 50.72(e)(2) (IS) 50.7l(e) (2)(e)
LICfNSEE CONTACT SOR THIS LKR (12)
NAME TELEPHONE NUMSER AREA CODE Timothy D. Shriver, Compliance Manager 60 23 93 2 52 1 COMtLKTE ONK LINK SOll EACH COMtONENT SAILURE OfSCRISED IN THIS REPORT (12)
MANUFAC. fPORTASLE '.'"Pa MANVFAC. EPORTASL CAUSE SYSTEM COMPONENT COMPONENT TVRER TO NPRDS 'P.P e CAUSE SYSTEM TVRER v
kWM cc X I L K I KO 20 S~r. P%
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On December 7, 1988 at approximately 0942 HST, a Unit 2 Chemistry Technician (contractor, non-licensed) discovered the new fuel area radiation monitor RU-19 was inoperable. RU-19 indicated a constant O.OOE-O millirem per hour radiation level instead of the actual level. RU-19 measures area radiation adjacent to the new fuel storage racks. A review of previous readings determined that the last accurate reading occurred on December 3, 1988 at approximately 0516 HST. On December 4, 1988 at approximately 0516 HST, area surveys were not performed within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> as required by Technical Specifications 3.3.3. 1 Action 22.
The cause of the inoperable monitor is believed to be a malfunction of a clock in the computer internal to the monitor. A root cause of failure was unable to confirm the cause. The cause of the missed action statement requirements is a cognitive personnel error contrary to an approved procedure. As immediate corrective action, on December 7, 1988 at approximately 1030 HST, the area monitor RU-19 was reset, tested, and declared operable.
NRC Seem 544
(Qi NAC FORM 368A U.S. NUCLEAR REGULATORY COMMISSION APPROVEO OMB NO. 31500104 (869),
EXPIRES: 4/30/92 ESTIMATED BUADEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT ILER) INFOAMATION COLLECTION AEQUESTI 500 HAS. FORWARD COMMENTS RFGAAOING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPOATS MANAGEMENT BRANCH (P4)30). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104). OFFICE OF MANAGEMENT AND BUDGET, WASHINGTON, OC 20503.
FACILITYNAME (1) DOCKET NUMBER (2) LER NUMBER (8) PAGE (3)
, SEOUENTIAL NVMSER s+iN(
REVISION NUMSER Palo Verde Unit 2 o so o o 52 98 8 0 1 5 01 0 2oF 0 6 TEXT /lfmoro Jpoco /I ooRI/&rod, ooo oddicorro/HRC Farm 368r('4)(12)
DESCRIPTION OF WHAT OCCURRED:
A. Initial Conditions:
Unit 2 was in Mode 1 (POWER OPERATION) at approximately 100 percent reactor power on December 3 through 7 during the entire period of this event. The Unit was in the second fuel cycle; thus, spent fuel existed in the fuel pool.
B. Reportable Event Description (Including Dates and Approximate Times of Hajor Occurrences):
Event Classification: Condition Prohibited by the Plant's Technical Specifications.
On December 7, 1988 at approximately 0942 NST, a Unit 2 Chemistry Technician (contractor, non-licensed) discovered that the new fuel area radiation monitor RU-19 did not indicate properly and was inoperable. The Chemistry Technician was performing checks of Technical Specification (TS) monitors when, he obtained a reading of 0.00E-00 millirem per hour on the Display Control Unit (DCU) for RU-19. In reviewing the daily averages for the previous three days on the DCU he found those also read O.OOE-OO millirem per hour.
The Chemistry Technician (contractor, non-licensed) then checked to determine if the monitor was operating locally. The monitor was found to be reading O.OOE-OO millirem per hour at the local indicator and thus, was not displaying the actual radiation in the area. The Shift Supervisor (operator, licensed) was notified on the inoperable monitor, and he initiated action to compensate for the condition.
At approximately 1015 HST December 7, 1988, a radiation survey'was taken in the area, and levels were found to be normal and within specification.
The Radiation Protection Technician (utility, non-licensed) reset the monitor by turning it off and then on again. The local indication then responded normally, and setpoints were verified satisfactory. Based on these results, the monitor was declared operable at approximately 1030 December 7, 1988.
The Chemistry Technician investigated the hourly printout of the monitor and found the last apparent accurate reading occurred at approximately 0516 HST December 3, 1988. Technical Specification 3.3.3. 1 ACTION 22 requires area surveys of the monitored area at least once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The only radiation survey of the monitored area during this event was on December 5, 1988 as part of NRC Form 366A (869)
0 l~ Jl J
NRC FORM SSSA U.S. NUCLEAR REGULATORY COIEMISSION APPROVED OMS NO. 31500104 (SS9)
EXPIRES: 4/30/92 ESTIMATED SURDFN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING SUROEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P4)30). U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104). OFFICE OF MANAGEMENTAND SUDGET, WASHINGTON, OC 20503.
FACILITYNAME (I) DOCKET NUMSER (2) LER NUMSER (5) PAGE (3) g'%EQUENTIAL ~+X REVrSION NUMEEII:..5 NUMEER Palo Verde Unit 2 o s o o o 52 98 8 0 1 5 01 0 3 oF0 6 TEXT ///moro 4/roco /4/or/rr/rorL rr>> or)/ 'orro/HRC Farm BASSA'4)(17) scheduled weekly surveys. This survey showed no abnormal radiation levels in the area.
C. Status of structures, systems, or components that were inoperable at the start of the event that contributed to the event:
Other than RU-19, no other structures, systems; or components were inoperable at the start of this event that contributed to this event.
D. Cause of each component or system failure, if known:
Since the monitor was turned off and then back on, the problem has not recurred. On December 3, 1988, the clock in the monitor's computer appears to have malfunctioned. This clock is necessary to tell the computer to update the raw data provided by the detector into a radiation reading each second. With the clock malfunctioned, the monitor will not perform the calculation and the readout will be zero, as observed. When the monitor was reset by turning it off and back on, the computer initialization program reset the clock which then allowed the monitor to operate normally. The data collected did not provide objective evidence of a component failure. Thus, the Engineering Evaluation was unable to positively identify a root cause of failure.
E. Failure mode, mechanism, and effect of each failed component, if known:
The failure in the monitor caused the Display Control Unit (DCU) to read zero.
For failures of components with multiple functions, list of systems or secondary functions that were also affected:
Not applicable - RU-19 provides an alarm action at a present level and has no automatic features. It also does not provide multiple functions.
G. For failures that rendered a train of a safety system inoperable, estimated time elapsed from the discovery of the failure until the train was returned to service:
Not applicable - RU-19 is not a safety-related monitor.
H. Method of discovery of each component or system failure or procedural error:
The failure of the monitor was discovered during a review of NRC Form 35SA (SSS)
(Qi 4
/
NRC FORM 366A U.S. NUCLEAR REGULATORY COIAMISSION APPROVED OMB NO. 31500104 (64)9)
EXPIRES'. 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT ILER) INFORMATION COLLECTION REOUEST: 500 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND RFPORTS MANAGEMENT BRANCH IP430). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, OC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31504))04). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON,OC 20503.
FACILITY NAME ll) DOCKET NUMBER l2) LER NUMBER (6) PAGE (3)
SEQUENTIAL REVrSION NUMSSII Ã5 rrUM66A Palo Verde Unit 2 o s o o o 52 988 0 1 5 01 04oF 0 6 TEXT /rf mare 4aeee /4//r/rer/ rree aeT/Or/en/ IYRC FrNm 366A'4/(17)
Technical Specification monitors.
I. Cause of Event:
The failure to recognize the inoperability of RU-19 was cognitive personnel error by the Control Room Operator (utility licensed) based on a misinterpretation of procedural instructions in the Surveillance Test. The Control Room Operator believed that the successful performance of step 8. 1. 1 of the Surveillance Test procedure was sufficient for the determination of OPERABILITY for RU-19. However, Appendix A of 42ST-2ZZ34 requires the performance of the second step (8. 1.2).
Step 8. 1. 1 of the Surveillance Test instructs the test performed to obtain a computer display of the operational status of all the monitors in the system. A non-flashing, green ormally indicates that a monitor channel is functioning properly and no alarms are present. If some other indication appears, the test performer is instructed to obtain the data base display for that channel for further evaluation. For the six performances of the Surveillance Test during the RU-19 inoperability, a non-flashing, green ppeared. This is the acceptance criterion given in step
- 8. 1. 1, which ends with the instruction "..record results in Appendix A.H Step 8. 1.2 instructs the performer to obtain an hourly trend display for each monitor listed in Appendix A and evaluate the data per step 8. 1.2.1, which states: "Further evaluate these one hour average readings by performing the following steps:
Verify that the current hourly average is consistent with current plant conditions.
Verify that any trends indicated by the 24 hourly averages were consistent with plant conditions during the same time frame.
Any SPIKE in the hourly averages of greater than 1 (one) decade from the current hourly average reading should be evaluated and documented in the test log.
If any inconsistencies occurred in any of the 3 (three) previous'steps, request that RP perform an evaluation of the monitor and document it in the test log.H NRC Form 366A (669)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED 0MB NO. 3)500104 (669)
E XP I R E S: 4/30/92 FSTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT ILER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN FSTIMATE TO THE RECORDS TEXT CONTINUATION ANO REPORTS MANAGEMENT BRANCH (F430). U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. DC 20555. ANO TO THE PAPERWORK REDUCTION PROJECT (31504104). OFFICE OF MANAGEMENTAND BUDGET. WASHINGTON, DC 20503.
FACILITY NAME (() DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR SEQUENTIAL pjw REVISION NUMSER Yrt NUMBER Palo Verde Unit 2 o s o o o 5 2 9 8 8 01 5 0 1 0 5oF 0 6 TEXT IIImom tottoit toOIt)od, oto tddidoINI IVRC Fomt 3664'4) (17)
No data is required in Appendix A, as the acceptance criteria only requires a "yes, no, or not applicable" be circled and the initials of the performer. Step 8. 1. 1 states, "Evaluate the data base display to determine if the monitor is OPERABLE. Record results in APPENDIX A". Thus, the test performer did not obtain and evaluate the hourly trend data, although the procedure does not provide for omitting step 8. 1.2, and Appendix A specifically refers to step
- 8. 1.2 for the acceptance criteria. Had step 8. 1.2 been performed,.
the change from variable readings to consistently zero readings would have been recognized and could have been investigated.
J. Safety System Response:
Not applicable - no safety system response was required or anticipated.
K. Failed Component Information:
RU-19 is a Kaman monitor model number 952109-001.
II. ASSESSMENT OF THE SAFETY CONSEQUENCES AND IMPLICATIONS OF THIS EVENT:
The OPERABILITY of the radiation monitoring channels ensures that: (1) the radiation levels are continually measured in the areas served by the individual channels and (2) the alarm is initiated when the radiation level trip setpoint is exceeded.
RU-19 is the area radiation monitor for the new fuel area of the fuel building. A second monitor is also located in the building and monitors the spent fuel area. Since the second monitor (RU-31) was operable throughout the event and since only spent fuel was in the fuel building at the time of the event, no safety hazards existed during the period of inoperability. Thus, this event represents no impact to the health and safety of the public.
III. CORRECTIVE ACTIONS:
A. Immediate:
As immediate corrective action, a survey of the area was conducted as required by the Technical Specifications. This was completed at approximately 1015 on December 7, 1988. Additionally, the monitor was reset and operated properly. Thus, at approximately 1030 HST on December 7, 1988 RU-19 was declared operable. A work request was submitted to troubleshoot the cause of the malfunction and replace or rework as necessary. However, the problem has not recurred and no further action on the work request has occurred.
NRC Form 366A (669)
,L 0 ((
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMB NO. 31500104 (64)9)
EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVENT REPORT (LER) INFORMATION COLLECTION REQUEST: 50.0 HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P4)30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500'l04). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
SSQUSNTIAI ~ii: IISVIS ION NUMSSII %Id NUM 6 II Palo Verde Unit 2 o s o o o 5 2 9 8 9 01 5 01 0 6oFO 6 TEXT ///more Spece /4 r/II/bred. o44 edd)/Oooo/HRC %%dmr 3564'4/ (17)
The Shift Supervisor (utility, licensed) informed Units 1 and 3 of the incident.
Unit 2 issued a night order to Operations directing that if a zero reading is received while performing the Surveillance Test, investigation is necessary to insure the zero reading is valid and the monitor is operating properly.
B. Action to Prevent Recurrence:
Changes in the configuration of the monitor were considered not possible due to internal constraints of the computer. The software cannot determine when a current radiation reading is valid or not.
Each monitor reports currently indicated conditions which must be .
analyzed with all other data available. Operational procedures will therefore continue to be used to validate parameters and operability of the monitor.
As action to prevent recurrence of the Human Performance problems identified in this event, the following actions are being taken:
The Radiation Honitoring System surveillance procedure is being revised to clarify instructions, acceptance criteria, and guidance on evaluation of a monitor's ability to perform its function. This revision is expected to be complete by October 31, 1989.
The training received by the performance group responsible for shiftly surveillance of the Radiation Honitoring System will be evaluated and upgraded as necessary. The completion of this task is expected by November 30, 1989.
IV ~ PREVIOUS S IHILAR'VENTS:
Although LERs have been submitted on the Radiation Honitoring System, this particular problem has not been previously reported.
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