ML17271A034

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Issuance of Amendments Adopting Technical Specifications Task Force Traveler TSTF-349-A, Revision 1, TSTF-361-A, Revision 2, and TSTF-438-A, Revision 0 (CAC Nos. MF9101 - MF9107)
ML17271A034
Person / Time
Site: Mcguire, McGuire  Duke Energy icon.png
Issue date: 10/31/2017
From: Michael Mahoney
Plant Licensing Branch II
To: Capps S
Duke Energy Carolinas
Mahoney M, DORL/LPL2-1. 415-3867
References
CAC MF9102, CAC MF9103, CAC MF9104, CAC MF9105, CAC MF9106, CAC MF9107, EPID L-2017-LLA-0163, EPID L-2017-LLA-0164, EPID L-2017-LLA-0165
Download: ML17271A034 (18)


Text

UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 October 31, 2017 Mr. Steven D. Capps Vice President McGuire Nuclear Station Duke Energy Carolinas, LLC 12700 Hagers Ferry Road Huntersville, NC 28078-8985

SUBJECT:

MCGUIRE NUCLEAR STATION, UNITS 1 AND 2 - ISSUANCE OF AMENDMENTS ADOPTING TECHNICAL SPECIFICATIONS TASK FORCE TRAVELERS TSTF-349-A, REVISION 1, TSTF-361-A, REVISION 2, AND TSTF-438-A, REVISION 0 (CAC NOS. MF9102, MF9103, MF9104, MF9105, MF9106, AND MF9107; EPIDS L-2017-LLA-0163, L-2017-LLA-0164, AND L-2017-LLA-0165)

Dear Mr. Capps:

The U.S. Nuclear Regulatory Commission (the Commission) has issued the enclosed Amendment No. 303 to Renewed Facility Operating License No. NPF-9 and Amendment No. 282 to Renewed Facility Operating License No. NPF-17 for the McGuire Nuclear Station, Units 1 and 2, respectively. The amendments are in response to your application dated January 11, 2017.

The amendments modify Technical Specification (TS) Limiting Condition for Operation (LCO) 3.9.6, "Residual Heat Removal (AHR) and Coolant Circulation - Low Water Level," to add a note which allows all AHR pumps to be secured for less than or equal to 15 minutes to support the switching of the shutdown cooling loops from one train to another. Three conditions must also exist in order to secure the pumps: the core outlet temperature is maintained greater than 10 degrees Fahrenheit below saturation temperature; no operations are permitted that would cause introduction of coolant into the Reactor Coolant System (RCS) with boron concentration less than that required to meet the minimum required boron concentration of LCO 3.9.1, "Boron Concentration"; and no draining operations to further reduce RCS water volume are permitted.

A second note is added to allow one required AHR loop to be inoperable for up to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for surveillance testing, provided that the other RHR loop is operable and in operation.

The changes are consistent with Technical Specifications Task Force (TSTF) Travelers TSTF-349-A, Revision 1, "Add Note to LCO 3.9.5 Allowing Shutdown Cooling Loops Removal from Operation," TSTF-361-A, Revision 2, "Allow standby [Shutdown Cooling] SDC/RHR/[Decay Heat Removal] OHR loop to [be] inoperable to support testing," and TSTF-438-A, Revision 0, "Clarify Exception Notes to be Consistent with the Requirement Being Excepted."

A copy of the related Safety Evaluation is also enclosed. Notice of Issuance will be included in the Commission's biweekly Federal Register notice.

~ ~oney,

  • nc ly, (},.,

11

  • f tt 1chael Pr ct Manager Plant Licensing Branch 11-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation Docket Nos. 50-369 and 50-370

Enclosures:

1. Amendment No. 303 to NPF-9
2. Amendment No. 282 to NPF-17
3. Safety Evaluation cc w/enclosures: Distribution via Listserv

UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, O.C. 20555-0001 DUKE ENERGY CAROLINAS, LLC DOCKET NO. 50-369 MCGUIRE NUCLEAR STATION, UNIT 1 AMENDMENT TO RENEWED FACILITY OPERATING LICENSE Amendment No. 303 Renewed License No. NPF-9

1. The Nuclear Regulatory Commission (the Commission) has found that:

A. The application for amendment to the McGuire Nuclear Station, Unit 1 (the facility), Renewed Facility Operating License No. NPF-9, filed by Duke Energy Carolinas, LLC (the licensee), dated January 11, 2017, complies with the standards and requirements of the Atomic Energy Act of 1954, as amended (the Act), and the Commission's rules and regulations as set forth in 10 CFR Chapter I;

8. The facility will operate in conformity with the application, the provisions of the Act, and the rules and regulations of the Commission; C. There is reasonable assurance (i) that the activities authorized by this amendment can be conducted without endangering the health and safety of the public, and (ii) that such activities will be conducted in compliance with the Commission's regulations set forth in 10 CFR Chapter I;
0. The issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public; and E. The issuance of this amendment is in accordance with 10 CFR Part 51 of the Commission's regulations and all applicable requirements have been satisfied.

Enclosure 1

2. Accordingly, the license is hereby amended by page changes to the Technical Specifications as indicated in the attachment to this license amendment, and paragraph 2.C.(2) of Renewed Facility Operating License No. NPF-9 is hereby amended to read as follows:

(2) Technical Specifications The Technical Specifications contained in Appendix A, as revised through Amendment No. 303, are hereby incorporated into this renewed operating license. The licensee shall operate the facility in accordance with the Technical Specifications.

3. This license amendment is effective as of its date of issuance and shall be implemented within 120 days of issuance.

FOR THE NUCLEAR REGULATORY COMMISSION

~~~

Michael T. Markley, Chief Plant Licensing Branch 11-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation

Attachment:

Changes to Renewed License No. NPF-9 and Technical Specifications Date of Issuance: October 31, 2017

UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 DUKE ENERGY CAROLINAS, LLC DOCKET NO. 50-370 MCGUIRE NUCLEAR STATION UNIT 2 AMENDMENT TO RENEWED FACILITY OPERATING LICENSE Amendment No. 282 Renewed License No. NPF-17

1. The Nuclear Regulatory Commission (the Commission) has found that:

A. The application for amendment to the McGuire Nuclear Station, Unit 2 (the facility), Renewed Facility Operating License No. NPF-17, filed by the Duke Energy Carolinas, LLC (the licensee), dated January 11, 2017, complies with the standards and requirements of the Atomic Energy Act of 1954, as amended (the Act), and the Commission's rules and regulations as set forth in 10 CFR Chapter I; B. The facility will operate in conformity with the application, the provisions of the Act, and the rules and regulations of the Commission; C. There is reasonable assurance (i) that the activities authorized by this amendment can be conducted without endangering the health and safety of the public, and (ii) that such activities will be conducted in compliance with the Commission's regulations set forth in 10 CFR Chapter I; D. The issuance of this amendment will not be inimical to the common defense and security or to the health and safety of the public; and E. The issuance of this amendment is in accordance with 10 CFR Part 51 of the Commission's regulations and all applicable requirements have been satisfied.

Enclosure 2

2. Accordingly, the license is hereby amended by page changes to the Technical Specifications as indicated in the attachment to this license amendment, and paragraph 2.C.(2) of Renewed Facility Operating License No. NPF-17 is hereby amended to read as follows:

(2) Technical Specifications The Technical Specifications contained in Appendix A, as revised through Amendment No. 282, are hereby incorporated into this renewed operating license. The licensee shall operate the facility in accordance with the Technical Specifications.

3. This license amendment is effective as of its date of issuance and shall be implemented within 120 days of issuance.

FOR THE NUCLEAR REGULATORY COMMISSION

~-;:~

Michael T. Markley, Chief Plant Licensing Branch 11-1 Division of Operating Reactor Licensing Office of Nuclear Reactor Regulation

Attachment:

Changes to Renewed License No. NPF-17 and Technical Specifications Date of Issuance: October 31 , 2o1 7

ATIACHMENT MCGUIRE NUCLEAR STATION, UNITS 1AND2 LICENSE AMENDMENT NO. 303 RENEWED FACILITY OPERATING LICENSE NO. NPF-9 DOCKET NO. 50-369 AND LICENSE AMENDMENT NO. 282 RENEWED FACILITY OPERATING LICENSE NO. NPF-17 DOCKET NO. 50-370 Replace the following pages of the Renewed Facility Operating Licenses with the attached revised pages. The revised pages are identified by amendment number and contain marginal lines indicating the areas of change.

Remove Insert NPF-9, page 3 NPF-9, page 3 NPF-17, page 3 NPF-17, page 3 Replace the following pages of the Appendix A Technical Specifications (TS) with the attached revised pages. The revised pages are identified by amendment number and contain marginal lines indicating the areas of change.

Remove Insert 3.9.6-1 3.9.6-1 3.9.6-2 3.9.6-2 3.9.6-3

(4) Pursuant to the Act and 10 CFR Parts 30, 40 and 70, to receive, possess and use in amounts as required any byproduct, source or special nuclear material without restriction to chemical or physical form, for sample analysis or instrument calibration or associated with radioactive apparatus or components; (5) Pursuant to the Act and 10 CFR Parts 30, 40 and 70, to possess, but not separate, such byproducts and special nuclear materials as may be produced by the operation of McGuire Nuclear Station, Units 1 and 2, and; (6) Pursuant to the Act and 10 CFR Parts 30 and 40, to receive, possess and process for release or transfer such byproduct material as may be produced by the Duke Training and Technology Center.

C. This renewed operating license shall be deemed to contain and is subject to the conditions specified in the Commission's regulations set forth in 10 CFR Chapter I and is subject to all applicable provisions of the Act and to the rules, regulations, and orders of the Commission now or hereafter in effect; and is subject to the additional conditions specified or incorporated below:

(1) Maximum Power Level The licensee is authorized to operate the facility at a reactor core full steady state power level of 3469 megawatts thermal (100o/o).

(2) Technical Specifications The Technical Specifications contained in Appendix A, as revised through Amendment No. 303, are hereby incorporated into this renewed operating license. The licensee shall operate the facility in accordance with the Technical Specifications.

(3) Updated Final Safety Analysis Report The Updated Final Safety Analysis Report supplement submitted pursuant to 10 CFR 54.21(d), as revised on December 16, 2002, describes certain future activities to be completed before the period of extended operation. Duke shall complete these activities no later than June 12, 2021, and shall notify the NRC in writing when implementation of these activities is complete and can be verified by NRC inspection.

The Updated Final Safety Analysis Report supplement as revised on December 16, 2002, described above, shall be included in the next scheduled update to the Updated Final Safety Analysis Report required by 10 CFR 50.71(e)(4), following issuance of this renewed operating license.

Until that update is complete, Duke may make changes to the programs described in such supplement without prior Commission approval, provided that Duke evaluates each such change pursuant to the criteria set forth in 10 CFR 50.59 and otherwise complies with the requirements in that section.

Renewed License No. NPF-9 Amendment No. 303

(4) Pursuant to the Act and 10 CFR Parts 30, 40, and 70, to receive, possess and use in amounts as required any byproduct, source or special nuclear material without restriction to chemical or physical form, for sample analysis or instrument calibration or associated with radioactive apparatus or components:

(5) Pursuant to the Act and 10 CFR Parts, 30, 40 and 70, to possess, but not separate, such byproducts and special nuclear materials as my be produced by the operation of McGuire Nuclear Station, Units 1 and 2; and, (6) Pursuant to the Act and 10 CFR Parts 30 and 40, to receive, possess and process for release or transfer such by product material as may be produced by the Duke Training and Technology Center.

C. This renewed operating license shall be deemed to contain and is subject to the conditions specified in the Commission's regulations set forth in 10 CFR Chapter I and is subject to all applicable provisions of the Act and to the rules, regulations, and orders of the Commission now or thereafter in effect; and is subject to the additional conditions specified or incorporated below:

(1) Maximum Power Level The licensee is authorized to operate the facility at a reactor core full steady state power level of 3469 megawatts thermal (100°/o).

(2) Technical Specifications The Technical Specifications contained in Appendix A, as revised through Amendment No. 282, are hereby incorporated into this renewed operating license. The licensee shall operate the facility in accordance with the Technical Specifications.

(3) Updated Final Safety Analysis Report The Updated Final Safety Analysis Report supplement submitted pursuant to 10 CFR 54.21(d), as revised on December 16, 2002, describes certain future activities to be completed before the period of extended operation.

Duke shall complete these activities no later than March 3, 2023, and shall notify the NRG in writing when implementation of these activities is complete and can be verified by NRG inspection.

The Updated Final Safety Analysis Report supplement as revised on December 16, 2002, described above, shall be included in the next scheduled update to the Updated Final Safety Analysis Report required by 10 CFR 50.71(e)(4), following issuance of this renewed operating license.

Until that update is complete, Duke may make changes to the programs described in such supplement without prior Commission approval, provided that Duke evaluates each such change pursuant to the criteria set forth in 10 CFR 50.59, and otherwise complies with the requirements in that section.

Renewed License No. NPF-17 Amendment No. 282

RHR and Coolant Circulation - Low Water Level 3.9.6 3.9 REFUELING OPERATIONS 3.9.6 Residual Heat Removal (RHR) and Coolant Circulation - Low Water Level LCO 3.9.6 Two RHR loops shall be OPERABLE, and one RHR loop shall be in operation.


NOTES---------------------------------------------

1. All RHR pumps may be removed from operation for ::s; 15 minutes when switching from one train to another provided:
a. The core outlet temperature is maintained> 10 degrees F below saturation temperature,
b. No operations are permitted that would cause introduction of coolant into the Reactor Coolant System (RCS) with boron concentration less than that required to meet the minimum required boron concentration of LCO 3.9.1, and
c. No draining operations to further reduce RCS water volume are permitted.
2. One required RHR loop may be inoperable for up to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for surveillance testing, provided that the other RHR loop is OPERABLE and in operation.

APPLICABILITY: MODE 6 with the water level < 23 ft above the top of reactor vessel flange.

ACTIONS CONDITION REQUIRED ACTION COMPLETION TIME A Less than the required A.1 Initiate action to restore Immediately number of RHR loops required RHR loops to OPERABLE. OPERABLE status.

A.2 Initiate action to establish Immediately

~ 23 ft of water above the top of reactor vessel flange.

(continued)

McGuire Units 1 and 2 3.9.6-1 Amendment Nos. 303/282

RHR and Coolant Circulation - Low Water Level 3.9.6 ACTIONS lcontinuedl CONDITION REQUIRED ACTION COMPLETION TIME B. No RHR loop in B.1 Suspend operations that Immediately operation. would cause introduction of coolant into the RCS with boron concentration less than required to meet the boron concentration of LCO 3.9.1.

AND B.2 Initiate action to restore Immediately one RHR loop to operation.

AND B.3 Close all containment 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> penetrations providing direct access from containment atmosphere to outside atmosphere.

McGuire Units 1 and 2 3.9.6-2 Amendment Nos. 303/282

RHR and Coolant Circulation - Low Water Level 3.9.6 SURVEILLANCE REQUIREMENTS SURVEILLANCE FREQUENCY SR 3.9.6.1 Verify one RHR loop is in operation and circulating l n accordance with reactor coolant at a flow rate of ::c: 1000 gpm and RCS the Surveillance temperature is:::; 140°F. Frequency Control Program SR 3.9.6.2 Verify correct breaker alignment and indicated power In accordance with available to the required RHR pump that is not in the Surveillance operation. Frequency Control Program SR 3.9.6.3 Verify RHR loop locations susceptible to gas In accordance with accumulation are sufficiently filled with water. the Surveillance Frequency Control Program McGuire Units 1 and 2 3.9.6-3 Amendment Nos. 303/282

UNITED STATES NUCLEAR REGULATORY COMMISSION WASHINGTON, D.C. 20555-0001 SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO AMENDMENT NO. 303 TO RENEWED FACILITY OPERATING LICENSE NO. NPF-9 AND AMENDMENT NO. 282 TO RENEWED FACILITY OPERATING LICENSE NO. NPF-17 DUKE ENERGY CAROLINAS, LLC MCGUIRE NUCLEAR STATION UNITS 1 AND 2 DOCKET NOS. 50-369 AND 50-370

1.0 INTRODUCTION

By letter to the U.S. Nuclear Regulatory Commission (NRC, the Commission) dated January 11, 2017 (Agencywide Documents Access and Management System (ADAMS)

Accession No. ML17025A069), Duke Energy Carolinas, LLC (Duke, the licensee) requested changes to the Technical Specifications (TSs) for McGuire Nuclear Station, Units 1 and 2 (McGuire).

The amendments would modify TS Limiting Condition for Operation (LCO) 3.9.6, "Residual Heat Removal (AHR) and Coolant Circulation - Low Water Level," to add a note which would allow all RHR pumps to be secured for less than or equal to 15 minutes to support the switching of the shutdown cooling loops from one train to another. Three conditions would be required to exist in order to secure the pumps: the core outlet temperature would have to be maintained greater than 10 degrees Fahrenheit (F) below saturation temperature; no operations would be permitted that would cause introduction of coolant into the Reactor Coolant System (RCS) with boron concentration less than that required to meet the minimum required boron concentration of TS LCO 3.9.1, "Boron Concentration"; and no draining operations to further reduce RCS water volume would be permitted. A second note would also be added to allow one required AHR loop to be inoperable for up to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for surveillance testing, provided that the other RHR loop is operable and in operation.

The proposed changes are consistent with Technical Specifications Task Force (TSTF)

Travelers TSTF-349-A, Revision 1, "Add Note to LCO 3.9.5 Allowing Shutdown Cooling Loops Removal from Opera1ion" (ADAMS Accession No. ML003723263), TSTF-361-A, Revision 2, "Allow standby [Shutdown Cooling] SDC/RHR/[Decay Heat Removal] OHR loop to [be]

Enclosure 3

inoperable to support testing" (ADAMS Accession No. ML003735328), and TSTF-438-A, Revision 0, "Clarify Exception Notes to be Consistent with the Requirement Being Excepted" (ADAMS Accession No. ML021580334).

The amendments would adopt previously NRG-approved TSTF-349-A, Revision 1, TSTF-361-A, Revision 2, and TSTF-438-A, Revision 0, in order to bring the McGuire TSs into closer alignment with NUREG-1431, "Standard Technical Specifications - Westinghouse Plants" (Westinghouse Owners Group 0JVOG) Standard Technical Specifications (STS)- hereafter "WOG STS" or "STS").

The NRC did not issue a letter approving TSTF-349, Revision 1; however, this change was incorporated by the NRG into Revision 2 of the STS (ADAMS Accession Nos. ML011840211 and ML011840219). The NRG approved TSTF-361, Revision 2, by letter dated October 31, 2000 (ADAMS Accession No. ML003765449). The NRG approved TSTF-438, Revision 0, by letter dated October 21, 2002 (ADAMS Accession No. ML022940574).

2.0 REGULATORY EVALUATION

In Title 10 of the Code of Federal Regulations (10 CFR) Section 50.36, "Technical Specifications," the NRC established its regulatory requirements related to the content of TSs.

Pursuant to 10 CFR 50.36(c), TSs are required to include items in the following categories related to plant operation: (1) safety limits, limiting safety system settings, and limiting control settings; (2) LCOs; (3) surveillance requirements; (4) design features; and (5) administrative controls. However, the regulation does not specify the particular requirements to be included in a plant's TSs. The LCOs are the lowest functional capability or performance levels of equipment required for safe operation of the facility. When an LCO of a nuclear reactor is not met, the licensee shall follow any remedial actions permitted by the TS until the condition can be met or shall shut down the reactor.

2.1 Licensee's Proposed Changes Current TS LCO 3.9.6 states:

Two RHR loops shall be OPERABLE, and one RHR loop shall be in operation.

Revised TS LCO 3.9.6, would state:

Two RHR loops shall be OPERABLE, and one RHR loop shall be in operation.


NOTES--------------------------------------------

1. All RHR pumps may be removed from operation for :s; 15 minutes when switching from one train to another provided:
a. The core outlet temperature is maintained > 10 degrees F below saturation temperature,
b. No operations are permitted that would cause introduction of coolant into the Reactor Coolant System (RCS) with boron concentration less than that required to meet the minimum required boron concentration of LCO 3.9.1, and
c. No draining operations to further reduce RCS water volume are permitted.
2. One required RHR loop may be inoperable for up to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for surveillance testing, provided that the other RHR loop is OPERABLE and in operation.

3.0 TECHNICAL EVALUATION

3.1 NRC Staff's Technical Evaluation of Licensee's Proposed Changes 3.1.1 TSTF-349-A, Revision 1 TSTF-349-A, Revision 1, revised WOG STS 3.9.6, "Residual Heat Removal (RHR) and Coolant Circulation - Low Water Level," to add a Note to the LCO statement allowing securing the operating train of RHR for up to 15 minutes to support switching operating trains.

The RHR system is used to remove core decay heat and reactor coolant sensible heat during unit cooldown and cold shutdown and to provide adequate mixing of borated coolant. Currently, McGuire's TS LCO 3.9.6 requires two RHR loops to be operable and one in operation when a unit is in Mode 6 with less than 23 feet of water above the top of the reactor vessel flange.

With the adoption of TSTF-349-A, Revision 1, the licensee proposes to add to McGuire TS LCO 3.9.6 a Note to allow all RHR pumps to be removed from operation for up to 15 minutes when switching from one train to another. This is a short period of time without coolant flow through the reactor core. The new Note would include three restrictions, when entering this condition.

The three restrictions are: the core outlet temperature is maintained greater than 10 degrees F below saturation temperature; no operations are permitted that would cause introduction of coolant into the RCS with boron concentration less than that required to meet the minimum required boron concentration of TS LCO 3.9.1; and no draining operations to further reduce RCS water volume are permitted. These restrictions would minimize the risk while switching trains and would improve the likelihood that RHR will be safely restored.

The proposed change is consistent with the allowances that are currently in McGuire TS 3.4.8, "RCS Loops - Mode 5, Loops Not Filled," which is consistent with the plant condition allowed by TS 3.9.6. Additionally, the proposed changes are consistent with NRG-approved TSTF-349-A, Revision 1. Based on the above, the NRC staff finds that safe operation of the facility is maintained if both RHR loops are removed from service for less than or equal to 15 minutes, with the operational restrictions described above.

Based on the above, the NRC staff concludes that safe operation of the plant is maintained and that the proposed changes to TS LCO 3.9.6 meet the requirements of 10 CFR 50.36, and, therefore, are acceptable.

3.1.2 TSTF-361-A, Revision 2 The purpose of the RHR system in MODE 6 is to remove decay heat and sensible heat from the RCS, to provide mixing of borated coolant, and to prevent boron stratification. Heat is removed from the RCS by circulating reactor coolant through the RHR heat exchangers where the heat is transferred to the component cooling water system. The coolant is then returned to the RCS via the RCS cold leg(s). Operation of the RHR system for normal cool-down decay heat removal is

manually accomplished from the control room. The heat removal rate is adjusted by controlling the flow of reactor coolant through the RHR heat exchanger(s) and the bypass lines. Mixing of the reactor coolant is maintained by this continuous circulation of reactor coolant through the RHR system.

The proposed changes would add a note to allow one of the RHR loops to be inoperable for up to 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> for surveillance testing, provided that the other RHR loop is operable and operating.

The allowance is needed to provide the operational flexibility to perform surveillance testing.

Since the reactor decay heat generation during Mode 6 is sufficiently low, a potential 2-hour interruption of decay heat removal, assuming a failure of the operating RHR loop during this time interval, would not result in a reactor safety concern. The 2-hour testing duration ensures that there is reasonable time for operators to respond to and mitigate any expected failures.

Additionally, the proposed changes are consistent with the allowances that are currently in McGuire TS 3.4.8, which is consistent with the plant condition allowed by TS 3.9.6. The proposed changes are consistent with NRG-approved TSTF-361-A, Revision 2. Based on the above, the NRC staff finds that safe operation of the facility is maintained if one RHR loop is removed from service, as proposed by the licensee, for up to two hours with the other RHR loop in operation.

Based on the above, the NRC staff concludes that safe operation of the plant is maintained and that the proposed changes to TS LCO 3.9.6 meet the requirements of 10 CFR 50.36, and, therefore, are acceptable.

3.1.3 TSTF-438-A, Revision 0 The NRC staffs assessment of TSTF-438-A, Revision 0, is documented in a letter to the Nuclear Energy Institute, dated October 21, 2002 (ADAMS Accession No. ML022940574).

TSTF-438-A, Revision 0, revises the note which was added by adopting TSTF-349-A, Revision 1. TSTF-438-A, Revision 0, revises the wording of the note from "may not be in operation" to "may be removed from operation." The proposed change to McGuire TS 3.9.6 is consistent with NRG-approved TSTF-438-A, Revision 0. This proposed change does not alter the intent of the note, does not affect any safety analysis assumptions, and does not alter any methods of plant operation.

The proposed change is editorial in nature and does not change the intent of TS 3.9.6; therefore, the NRC staff finds that safe operation of the facility is maintained. Based on the above, the NRC staff concludes that safe operation of the plant is maintained and that the proposed changes to TS LCO 3.9.6 meet the requirements of 10 CFR 50.36, and, therefore, are acceptable.

3.2 NRC Staff's Conclusion The NRC staff evaluated the proposed changes to McGuire TS LCO 3.9.6 against the applicable regulations and guidance and found that the changes are consistent with those in the previously NRG-approved TSTF-349-A, Revision 1, TSTF-361-A, Revision 2, and TSTF-438-A, Revision 0, and continue to ensure safe operation of the facility. The NRC staff concludes that the proposed changes meet the requirements of 10 CFR 50.36 and, therefore, are acceptable.

4.0 STATE CONSULTATION

In accordance with the Commission's regulations, the NRC staff notified the North Carolina State official of the proposed issuance of the amendments on September 27, 2017. The State official confirmed on October 16, 2017 that the State of North Carolina had no comments.

5.0 PUBLIC COMMENTS On May 23, 2017, the NRC staff published a "Notice of Consideration of Issuance of Amendments to Facility Operating Licenses and Combined Licenses and Proposed No Significant Hazards Consideration Determination," in the Federal Register associated with the proposed amendment request (82 FR 23623). In accordance with the requirements in 10 CFR 50.91, the notice provided a 30-day period for public comment on the proposed no significant hazards consideration determination. One comment from a member of the public was received, however it was not related to the proposed no significant hazards consideration determination or to the proposed amendment request. The comment can be found at WvVw.requlatio11s_qov, reference NRC-2017-0120-0002.

6.0 ENVIRONMENTAL CONSIDERATION

The amendments change a requirement with respect to the installation or use of facility components located within the restricted area as defined in 10 CFR Part 20. The NRC staff has determined that the amendments involve no significant increase in the amounts and no significant change in the types of any effluents that may be released offsite and that there is no significant increase in individual or cumulative occupational radiation exposure. The Commission has previously issued a proposed finding that the amendments involve no significant hazards consideration, and there has been no public comment on this finding published in the Federal Register on May 23, 2017 (82 FR 23623). Accordingly, the amendments meet the eligibility criteria for categorical exclusion set forth in 10 CFR 51.22{c){9).

Pursuant to 10 CFR 51.22(b), no environmental impact statement or environmental assessment need be prepared in connection with the issuance of the amendments.

7.0 CONCLUSION

The Commission has concluded, based on the considerations discussed above, that: (1) there is reasonable assurance that the health and safety of the public will not be endangered by operation in the proposed manner, (2) there is reasonable assurance that such activities will be conducted in compliance with the Commission's regulations, and (3) the issuance of the amendments will not be inimical to the common defense and security or to the health and safety of the public.

Principal Contributors: D. Woodyatt, NRR R. Grover, NRR Date of issuance: October 31, 2017

ML17271A034 *b memorandum OFFICE DORL/LPL2-1/PM DORL/LPL2-1/LA DE/SRXB/BC DSS/STSB/BC NAME MM a honey KGoldstein EOesterle* JWhitman*

DATE 10/16/17 10/13/17 06/15/17 05/30/17 OGC - NLO subject to OFFICE email comments DORL/LPL2-1/BC DORL/LPL2-1/PM NAME JWachutka MMarkley MMahoney DATE 10/19/17 10/31/17 10/31/17