ML14042A238

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IR 05000285-13-019; on 11/16/2013 - 12/31/2013; Fort Calhoun Station, Integrated Resident and Regional Report; Annual Inspection of Operator Requalification Program; Emergency Plan Biennial; and IMC 0350 Confirmatory Action Letter Inspectio
ML14042A238
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 02/10/2014
From: Hay M
NRC/RGN-IV/DRP
To: Cortopassi L
Omaha Public Power District
Hay M
References
IR-13-019
Download: ML14042A238 (60)


See also: IR 05000285/2013019

Text

U N IT E D S TA TE S

N U C LE AR R E GU LA TOR Y C OM MI S S I ON

R E G IO N I V

1600 EAST LAMAR BLVD

AR L I NG TO N , TE X AS 7 60 1 1 - 4511

February 10, 2014

Louis P. Cortopassi, Site Vice President

Omaha Public Power District

Fort Calhoun Station FC-2-4

P.O. Box 550

Fort Calhoun, NE 68023-0550

Subject: FORT CALHOUN - NRC INTEGRATED INSPECTION REPORT

NUMBER 05000285/2013019

Dear Mr. Cortopassi:

On December 31, 2013, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at the Fort Calhoun Station. On January 24, 2014, the NRC inspectors discussed the

results of this inspection with you and other members of your staff. Inspectors documented the

results of this inspection in the enclosed inspection report.

NRC inspectors documented one finding of very low safety significance (Green) in this report.

This finding involved a violation of NRC requirements.

Further, inspectors documented a licensee-identified violation which was determined to be of

very low safety significance in this report. The NRC is treating this violation as non-cited

violation (NCV) consistent with Section 2.3.2.a of the Enforcement Policy.

If you contest the violation or significance of the NCV, you should provide a response within

30 days of the date of this inspection report, with the basis for your denial, to the U.S. Nuclear

Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001; with

copies to the Regional Administrator, Region IV; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC resident

inspector at the Fort Calhoun Station.

If you disagree with a cross-cutting aspect assignment in this report, you should provide a

response within 30 days of the date of this inspection report, with the basis for your

disagreement, to the Regional Administrator, Region IV, and the NRC resident inspector at the

Fort Calhoun Station.

L. Cortopassi -2-

In accordance with Title 10 of the Code of Federal Regulations (10 CFR) 2.390, Public

Inspections, Exemptions, Requests for Withholding, a copy of this letter, its enclosure, and your

response (if any) will be available electronically for public inspection in the NRCs Public

Document Room or from the Publicly Available Records (PARS) component of the NRC's

Agencywide Documents Access and Management System (ADAMS). ADAMS is accessible

from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic

Reading Room).

Sincerely,

/RA/

Michael C. Hay, Chief

Project Branch F

Division of Reactor Projects

Docket No: 50-285

License No: DPR-40

Enclosure: NRC Inspection Report 05000285/2013019

w/Attachment: Supplemental Information

cc w/ encl: Electronic Distribution

[Accession Number]

SUNSI Rev Compl. Yes No ADAMS Yes No Reviewer Initials MCH

Publicly Avail. Yes No Sensitive Yes No Sens. Type Initials MCH

SRI:DRP/F RI:DRP/F C:DRP/F

JKirkland JWingebach MHay

/RA/E-Hay /RA/E-Hay /RA/

2/10/14 2/10/14 2/10/14

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket: 05000285

License: DPR-40

Report: 05000285/2013019

Licensee: Omaha Public Power District

Facility: Fort Calhoun Station

Location: 9610 Power Lane

Blair, NE 68008

Dates: November 16 through December 31, 2013

Inspectors: J. Kirkland, Senior Resident Inspector

J. Wingebach, Resident Inspector

R. Deese, Senior Reactor Analyst

B. Larson, Senior Operations Engineer

P. Elkmann, Senior Emergency Preparedness Inspector

S. Sanchez, Senior Emergency Preparedness Inspector, Region II

B. Larson, Senior Operations Engineer

G. Skaggs Ryan, Reactor Inspector

C. Zoia, Operations Engineer (RIII/DRS/OB)

G. Apger, Operations Engineer

W. Sifre, Senior Reactor Inspector

D. Kern, Senior Reactor Inspector (RI/DRS/EB2)

J. Dean, Senior Reactor Engineer (NRR/DSS/SNPB)

J. Drake, Branch Chief

C. Norton, Project Manager (NRR/JLD/JPSB)

D. Stearns, Health Physicist

Approved By: Michael Hay, Chief

Project Branch F

Division of Reactor Projects

-1- Enclosure

SUMMARY

IR 05000285/2013019; 11/16/2013 - 12/31/2013; Fort Calhoun Station, Integrated Resident and

Regional Report; Annual Inspection of Operator Requalification Program; Emergency Plan

Biennial; and IMC 0350 Confirmatory Action Letter Inspections

The inspection activities described in this report were performed between November 16, 2013,

and December 31, 2013, by the resident inspectors at the Fort Calhoun Station and five

inspectors from the NRCs Region IV office and other NRC offices. One finding of very low

safety significance (Green) is documented in this report. This finding involved a violation of

NRC requirements. Additionally, NRC inspectors documented one licensee-identified violation

of very low safety significance. The significance of inspection findings is indicated by their color

(Green, White, Yellow, or Red), which is determined using Inspection Manual Chapter 0609,

Significance Determination Process. Their cross-cutting aspects are determined using

Inspection Manual Chapter 0310, Components Within the Cross-Cutting Areas. Violations of

NRC requirements are dispositioned in accordance with the NRCs Enforcement Policy. The

NRC's program for overseeing the safe operation of commercial nuclear power reactors is

described in NUREG 1649, Reactor Oversight Process.

Cornerstone: Emergency Preparedness

Green. A Green noncited violation was identified for the failure of the licensee to correct

deficiencies identified as a result of four exercises conducted between March 27, 2012, and

May 7, 2013, as required by 10 CFR 50.47(b)(14). Specifically, the licensee failed to correct

deficiencies associated with team briefing and tracking in the Operations Support Center

(OSC) identified as a result of exercises conducted March 27, 2012; July 17, 2012;

March 5, 2013; and May 7, 2013.

The inspectors determined that the licensees failure to correct deficiencies identified by

licensee evaluators is a performance deficiency within the licensees control. This finding is

more than minor because it affected the emergency preparedness cornerstone objective

and the Emergency Response Organization Performance cornerstone attribute. This finding

was evaluated using the Emergency Preparedness Significance Determination Process and

was determined to be of very low safety significance because it was a failure to comply with

NRC requirements, was not a risk significant planning standard function, and was not a loss

of planning standard function. The finding was not a loss of planning standard function

because the licensee adequately corrected some deficiencies identified in exercises

conducted in 2012 and 2013. The finding was entered into the licensees corrective action

system as Condition Report 2013-22495. The finding was assigned a cross-cutting aspect

of Problem Identification and Resolution because the finding was reflective of current

performance and the licensee did not take appropriate corrective action to address safety

issues and adverse trends P.1(d). (Section 1EP1)

-2-

Licensee-Identified Violations

A violation of very low safety significance that was identified by the licensee has been reviewed

by the inspectors. Corrective actions taken or planned by the licensee have been entered into

the licensees corrective action program. This violation and associated corrective action

tracking numbers are listed in Section 4OA7 of this report.

-3-

PLANT STATUS

The plant began the inspection period in mode 5, with all fuel in the reactor vessel. On

December 18, 2013, the plant reached criticality, and the generator output breakers were closed

on December 21, 2013. The plant reached 100% power on December 26, 2013, where it

remained for the rest of the reporting period.

REPORT DETAILS

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, and Barrier Integrity

1R11 Licensed Operator Requalification Program and Licensed Operator Performance

(71111.11)

.1 Review of Licensed Operator Performance

a. Inspection Scope

On December 17 through December 24, 2013, the inspectors observed the performance

of on-shift licensed operators in the plants main control room. At the time of the

observations the plant was in a period of heightened activity due to the plant

startup. The inspectors provided continuous observation of the operators performance

of the plant startup and power ascension up to approximately 98% power. Additionally,

the inspectors observed non-licensed operator performance in the turbine and auxiliary

buildings, as well as the intake structure, during component startup to support the plant

startup. Over 350 hours0.00405 days <br />0.0972 hours <br />5.787037e-4 weeks <br />1.33175e-4 months <br /> of continuous observations were conducted.

In addition, the inspectors assessed the operators adherence to plant procedures,

including conduct of operations procedure and other operations department policies.

These activities constitute completion of one quarterly licensed operator performance

sample(s), as defined in Inspection Procedure 71111.11.

b. Observations

During these observations, inspectors regularly communicated observed behaviors to

management at Fort Calhoun Station and to the NRC. Positive behaviors observed

included adequate pre-job briefings, shift turnovers, control room supervision by station

management, reactivity control, surveillance testing, identification and control of new

operators and conservative decision making.

Several areas for improvement were identified that in some instances involved

unnecessary challenge to plant operators. These observations were discussed with

OPPD management as they were identified and included:

-4-

Inadequate vendor and station engineering support for turbine control system testing.

Operations staff did not receive the level of support expected when the newly

installed turbine control system operated erratically during power ascension. The

licensee was eventually able to make system adjustments and stabilize turbine

operation, but the delay in getting adequate technical support was an unnecessary

challenge to the operators.

The quality of the procedure used for testing of the new turbine control system was

poor, which slowed down test sequence.

Poor communications between the licensees Outage Control Center and Control

Room operators resulted in unnecessary delays in getting problems fixed (such as

malfunctioning control room annunciators).

The inspectors observed one example of a newly qualified operator

misunderstanding the operation of large feedwater system valve.

The inspectors observed one example of maintenance personnel not using

procedurally-required placekeeping tools (i.e. circle/slash), which resulted in a

missed procedural step and the need to re-perform the maintenance activity on a

non-safety related system.

Some inconsistencies were noted in documentation of control room and fire

impairment logs.

c. Findings

No findings were identified.

.2 Annual Inspection

The licensed operator requalification program involves two training cycles that are

conducted over a 2-year period. In the first cycle, the annual cycle, the operators are

administered an operating test consisting of job performance measures and simulator

scenarios. In the second part of the training cycle, the biennial cycle, operators are

administered an operating test and a comprehensive written examination. For this annual

inspection requirement, Fort Calhoun Station was in the first part of the training cycle.

a. Inspection Scope

The inspector reviewed the results of the operating tests for the station to satisfy the

annual inspection requirements.

On December 20, 2013, the licensee informed the lead inspector of the results,

11 of 11 crews passed the simulator portion of the operating test

-5-

46 of 49 licensed operators passed the simulator portion of the operating test

48 of 49 licensed operators passed the job performance measure portion of the

examination

The individuals that failed the simulator scenario portion of their operating test and the

individual who failed the job performance measure portion of their operating test were

successfully remediated, retested, and passed their retake operating test prior to

returning to licensed operator duties.

The inspector completed one inspection sample of the annual licensed operator

requalification program.

b. Findings

No findings were identified.

1R18 Plant Modifications (71111.18)

a. Inspection Scope

On December 4, 2013, the inspectors reviewed a temporary plant modification to provide

a furmanite repair of HCV-1108A, Steam Generator RC-2B Auxiliary Feedwater Inlet

Valve.

The inspectors verified that the licensee had installed this temporary modification in

accordance with technically adequate design documents. The inspectors verified that

this modification did not adversely impact the operability or availability of affected SSCs.

The inspectors reviewed design documentation and plant procedures affected by the

modification to verify the licensee maintained configuration control.

These activities constitute completion of one sample of temporary modifications, as

defined in Inspection Procedure 71111.18

b. Findings

No findings were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors observed one risk-significant surveillance test and reviewed test results

to verify that these tests adequately demonstrated that the structures, systems, and

components (SSCs) were capable of performing their safety functions,

December 4 2013, OP-ST-ESF-0001, Diesel Auto Start Initiating Circuit Check

-6-

The inspectors verified that this test met technical specification requirements, that the

licensee performed the tests in accordance with their procedures, and that the results of

the test satisfied appropriate acceptance criteria. The inspectors verified that the

licensee restored the operability of the affected SSCs following testing.

These activities constitute completion of one surveillance testing inspection sample, as

defined in Inspection Procedure 71111.22.

b. Findings

No findings were identified.

Cornerstone: Emergency Preparedness

1EP1 Exercise Evaluation (71114.01)

a. Inspection Scope

The inspectors observed the biennial emergency preparedness exercise conducted

December 3, 2013, to determine if the exercise acceptably tested major elements of the

emergency plan and provided opportunities to demonstrate key emergency response

organization skills. The scenario simulated:

A vehicle crash affecting vital equipment in the intake structure;

A loss of offsite power to the site;

Failure of a diesel generator to start with a second diesel generator unavailable

due to maintenance, resulting in a station blackout condition;

A large-break loss of coolant accident inside containment;

Uncovering of the fuel leading to fuel damage and a zirconium-water reaction

producing an explosive atmosphere inside containment; and,

A hydrogen gas burn damaging the containment purge system to create a

release path to the environment,to demonstrate the licensee personnels

capability to implement their emergency plan.

The inspectors evaluated exercise performance by focusing on the risk-significant

activities of event classification, offsite notification, recognition of offsite dose

consequences, and development of protective action recommendations, in the Control

Room Simulator and the following dedicated emergency response facilities:

Technical Support Center

Operations Support Center

Emergency Operations Facility

-7-

The inspectors also assessed recognition of, and response to, abnormal and emergency

plant conditions, the transfer of decision making authority and emergency function

responsibilities between facilities, onsite and offsite communications, protection of

emergency workers, emergency repair evaluation and capability, and the overall

implementation of the emergency plan to protect public health and safety and the

environment. The inspectors reviewed the current revision of the facility emergency

plan, emergency plan implementing procedures associated with operation of the

licensees emergency response facilities, procedures for the performance of associated

emergency functions, and other documents as listed in the attachment to this report.

The inspectors compared the observed exercise performance with the requirements in

the facility emergency plan, 10 CFR 50.47(b), 10 CFR Part 50, Appendix E, and with the

guidance in the emergency plan implementing procedures and other federal guidance.

The inspectors attended the post-exercise critiques in each emergency response facility

to evaluate the initial licensee self-assessment of exercise performance. The inspectors

also attended a subsequent formal presentation of critique items to plant management to

understand the performance issues observed by licensee evaluators.

The inspectors also reviewed nine licensee event after-action reports and exercise

evaluation reports to identify weaknesses and deficiencies previously evaluated by the

licensee.

The specific documents reviewed during this inspection are listed in the attachment.

These activities constitute completion of one sample as defined in Inspection

Procedure 71114.01-05.

b. Findings

Introduction. A Green noncited violation was identified for the failure of the licensee to

correct deficiencies identified as a result of four exercises conducted between

March 27, 2012, and May 7, 2013, as required by 10 CFR 50.47(b)(14).

Description. The NRC identified that Fort Calhoun Station had not corrected deficiencies

associated with the Operations Support Center (OSC) identified as a result of exercises

conducted March 27, 2012; July 17, 2012; March 5, 2013; and May 7, 2013.

The inspectors reviewed the licensees post-exercise evaluation reports and associated

corrective action program entries for exercises conducted March 27, 2012;

July 17, 2012; March 5, 2013; and May 7, 2013. The inspectors noted that Fort Calhoun

Station had identified that the following performance deficiencies had occurred during

previous exercises:

Weak implementation of priorities to mitigate the accident (March 27, July 17,

March 5, and May 7);

-8-

Delays in dispatching Operations Support Center teams to mitigate the accident

(March 27 and March 5); and

Pre-job and post-job briefings for Operations Support Center teams to mitigate

the accident that were incomplete or not performed (July 17, March 5, and

May 7)

The inspectors reviewed six condition reports (corrective action program entries)

generated by the licensee following the March 27, 2012; July 17, 2012; March 5, 2013;

and May 7, 2013, exercises and noted the following:

CR 2012-02381, Lack of Repair Team Control, opened March 28, 2012, closed

November 6, 2012. The licensee delivered refresher training for Non-Licensed

Operators (Action 2, closed June 21, 2012), delivered refresher training for

Maintenance Department work planners (Action 3, closed August 27, 2012), and

sent a post-exercise lessons-learned email to OSC staff reminding them to

review Procedure OSC-9, Emergency Team Briefings (Action 5, closed

October 19, 2012);

CR 2012-07779, Examples of teams dispatched from the OSC without

emergency work instructions being completed, opened July 17, 2012, closed

September 19, 2012. The licensee sent OSC staff an email, dated

September 6, 2012, reminding them to review Procedure OSC-9, Emergency

Team Briefings (Action 3, closed September 6, 2012);

CR 2013-05146, TSC Bypasses OSC Director to Brief Electricians, opened

March 7, 2013, closed April 1, 2013. Performance was discussed at the

licensees post-exercise critique and no additional action was taken (Action 2,

closed April 1 2013);

CR 2013-05263, Lack of OSC Team Debriefs, opened March 8, 2013, closed

May 3, 2013. The licensee sent post-exercise lessons-learned email, dated

March 29, 2013, to OSC staff reminding them to review Procedure OSC-9,

Emergency Team Briefings. The issue of a lack of post-job briefings was not

addressed in the March 29, 2013, email;

CR 2013-05363, Control Room directed OSC teams without going through the

OSC process, opened March 11, 2013, closed March 26, 2013. The licensee

conducted a coaching session on March 15, 2013, for the Shift Manager and

Control Room Supervisor participating in the March 5, 2013, exercise. No

additional corrective actions were taken, and

CR-2013-10486, Concens over OSC Priority Setting, opened May 10, 2013,

closed May 30, 2013. This condition report was administratively closed without

taking corrective action.

-9-

The inspectors subsequently observed emergency response organization performance

in the Operations Support Center during the December 3, 2013, exercise and identified

the following performance deficiencies:

Non-Licensed Operators present in the Operations Support Center were

assigned work by the Control Room and not by the Operations Support Center

Director;

Delays in forming and briefing repair and mitigation teams to be dispatched into

the plant;

Ineffective tracking of repair and mitigation teams in the plant, including,

o No documentation by Control Room staff of tasks assigned Non-Licensed

Operators;

o No tracking method for Non-Licensed Operators leaving the Operations

Support Center;

o A single team dispatched three times, each time with different individuals,

without appropriate records; and,

o Incomplete documentation as evidenced by log and/or tracking board

records documenting 12 repair and mitigation teams dispatched into the

plant, records of 15 repair and mitigation teams returning from the plant,

and 8 pre-job briefing forms completed in the Operations Support Center.

Ineffective pre-job briefings, including:

o One team leaving the Operations Support Center with direction to receive

its pre-job briefing from the Control Room;

o A lack of discussion of safety hazards in the plant during station blackout

conditions; for example, a lack of discussion of available lighting, and not

ensuring that flashlights and other portable lighting were taken into the

plant;

o A lack of discussion of other plant safety requirements; for example,

repair teams were not briefed to transport flammable liquids in approved

metal containers, and subsequently {simulated} the transport of

flammable liquids in open buckets; and,

o A lack of any pre-job briefings for Non-Licensed Operators.

The Operations Support Center did not conduct post-job briefings for repair and

mitigation teams returning to the facility after performing simulated work on plant

equipment.

- 10 -

The inspectors observed the licensees preliminary critique of emergency response

organization performance in the December 3, exercise, conducted December 5, 2013.

The licensee identified and entered into the corrective action program, instances of

Technical Support Center staff directing repair and mitigation teams without going

through the Operations Support Center Director, failures to brief repair and mitigation

teams about changing plant and radiological conditions, and shortcuts in the work

planning process for repair and mitigation teams.

The inspectors determined that the performance deficiencies observed by the licensee in

the exercises conducted March 27, 2012; July 17, 2012; March 5, 2013; and

May 7, 2013, would preclude the effective implementation of the emergency plan if they

were to occur during an actual radiological emergency. Specifically, a lack of adequate

pre-job and post-job work briefings, lack of adequate controls over Non-Licensed

Operators, and delays in dispatching repair and mitigation teams could prevent the

licensee from bringing the plant into a safe and stable condition and terminating

radiological releases affecting the public. Inspectors also determined the licensee relied

on individual coaching and post-exercise emails as corrective actions for deficiencies

observed during exercises, with an emphasis on individual (e.g. non-directed) review of

Procedure OSC-9, Emergency Team Briefings. The inspectors concluded that

corrective actions for the exercises conducted March 27, 2012; July 17, 2012;

March 5, 2013; and May 7, 2013; were ineffective, in that the issues continued to re-

occur, and also recurred during the December 3, 2013, exercise. In addition, the

licensee repeated the same corrective actions multiple times without achieving results,

and did not evaluate their effectiveness. The inspectors concluded from the above

information that deficiencies identified as a result of exercises had not been

appropriately corrected as required by 10 CFR 50.47(b)(14).

The inspectors determined that some deficiencies identified by the licensee following the

exercises conducted March 27, 2012; July 17, 2012; March 5, 2013; and May 7, 2013,

had been corrected and did not recur during the December 3, 2013, exercise. These

deficiencies included a lack of sufficient Radiation Protection Technician support in the

Operations Support Center, emergency worker briefings for issuance of potassium

iodide that were ineffective or not performed, poor strategies for directing offsite

environmental monitoring, and degraded radiation protection for emergency workers in

the Technical and Operations Support Centers.

Analysis. A deficiency (weakness) is defined in Manual Chapter 0609, Appendix B,

Section 2.(o), as a level of performance by the emergency response organization

demonstrated during an exercise that would preclude effective implementation of the

emergency plan if it were to occur during an actual radiological emergency. The

inspectors determined that the licensees failure to correct deficiencies identified by

licensee evalutors as a result of four exercises conducted in 2012 and 2013 is a

performance deficiency within the licensees control. Specifically, the licensee did not

correct deficiencies in its ability to assign work to Operations Support Center teams, and

to dispatch and track work teams. This finding is more than minor because it affected

the emergency preparedness cornerstone objective and the Emergency Response

- 11 -

Organization Performance cornerstone attribute. The finding affected the emergency

preparedness cornerstone objective because an inability to dispatch and track

emergency work teams may prevent the licensee from implementing adequate

measures to protect the health and safety of the public during a radiological emergency.

The finding was associated with a violation of NRC requirements. This finding was

evaluated using the Emergency Preparedness Significance Determination Process and

was determined to be of very low safety significance because it was a failure to comply

with NRC requirements, was not a risk significant planning standard function, and was

not a loss of planning standard function. The finding was not a loss of planning standard

function because the licensee adequately corrected some deficiencies identified as a

result of exercises conducted in 2012 and 2013. The finding was assigned a cross-

cutting aspect in the area of Problem Identification and Resolution because the finding

was reflective of current performance and the licensee did not take appropriate

corrective action to address safety issues and adverse trends P.1(d).

Enforcement. Title 10 of the Code of Federal Regulations, Part 50.47(b)(14) states, in

part, that Periodic exercises are conducted to evaluate major portions of emergency

response capabilitiesdeficiencies identified as a result of exerciseswill be corrected.

Contrary to the above, Fort Calhoun Station failed to correct deficiencies identified as a

result of exercises. Specifically, Fort Calhoun did not correct deficiencies in the

assignment of work to Operations Support Center teams, and the dispatch and tracking

of in-plant work teams, identified in four exercises between March 27, 2012, and

May 7, 2013. Because this failure is of very low safety significance and has been

entered into the licensees corrective action system as Condition Report 2013-22495,

this violation is being treated as an NCV, consistent with Section 2.3.2(a) of the NRC

Enforcement Policy: 05000285/2013019-01, [Failure to Correct Deficiencies in

Operations Support Center Functions].

4. OTHER ACTIVITIES

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, Emergency

Preparedness, Public Radiation Safety, Occupational Radiation Safety, and

Security

4OA2 Problem Identification and Resolution (71152)

.1 Routine Review

a. Inspection Scope

Throughout the inspection period, the inspectors performed daily reviews of items

entered into the licensees corrective action program and periodically attended the

licensees condition report screening meetings. The inspectors verified that licensee

personnel were identifying problems at an appropriate threshold and entering these

problems into the corrective action program for resolution. The inspectors verified that

the licensee developed and implemented corrective actions commensurate with the

significance of the problems identified. The inspectors also reviewed the licensees

- 12 -

problem identification and resolution activities during the performance of the other

inspection activities documented in this report.

b. Findings

No findings were identified.

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)

.1 (Closed) Licensee Event Report 05000285/2012-017-01: Containment Valve Actuators

Design Temperature Ratings Below those Required for Design Basis Accidents

While performing an extent of condition review associated with the adequacy of air

operated equipment inside containment to withstand containment main steam line break

(MSLB) and loss of coolant accident (LOCA) temperatures, it was discovered that the

Reactor Coolant System (RCS) Loop 1A Charging Line Stop Valve, the RCS Loop 2A

Charging Line Stop Valve, and the Pressurizer RC-4 Auxiliary Spray Inlet Valve have nitrile

based elastomers used in the air filter regulator and actuator. The design temperature limit

for the nitrile elastomers used in the valves is 180°F which is acceptable for the normal

operating conditions inside containment of 120°F. However, during the main steam line

break and loss of coolant accident the temperature inside containment is analyzed to

reach 370°F. Since these valves have both open and close functions supported by an air

accumulator, failure of the nitrile based elastomers could prevent the valves from fulfilling

their intended safety function.

The causal analysis did not determine why the nitrile elastomers were installed during

original plant construction. However, it was determined that a procedural deficiency and

human error resulted in the wrong type of elastomer material being used in the instrument

air filter regulators when the air accumulators were added to the valves to support their

safety function.

The licensee event report is closed. Revision 2 of this licensee event report was submitted

on December 6, 2013.

.2 (Opened) Licensee Event Report 05000285/2012-017-02: Containment Valve Actuators

Design Temperature Ratings Below those Required for Design Basis Accidents

On July 26, 2012, while performing an extent of condition review associated with air

operated valves (AOV), it was discovered that several valves had nitrile based elastomers

used in the air filter regulator and actuator that may not be acceptable for harsh environment

conditions. On September 6, 2012, it was also identified that due to a lack of

documentation, the States terminal blocks associated with the AOV's control circuit may not

be acceptable for harsh environment conditions. These were entered into the station's

corrective action program as Condition Report 2012-08621 and 2012-12739.

During design basis accidents, the limiting analysis temperature inside containment

is 374.2 degrees Fahrenheit (F). The design service temperature for the nitrile elastomers

is 180 degrees Fahrenheit and the testing performed on the States terminal blocks did not

- 13 -

bound the required accident conditions. Since these valves have both open and/or close

functions, failure of the nitrile based elastomers or the States terminal blocks could prevent

the valves from fulfilling their intended safety function.

A causal analysis was conducted and found that the station did not fully implement and or

maintain the electrical equipment qualification program. This resulted in a lack of

qualification documentation and equipment not qualified for expected design basis accident

conditions.

.3 (Closed) Licensee Event Report 05000285/2013-001-00: Mounting of GE HFA Relays does

not Meet Seismic Requirements

On January 15, 2013, while reviewing a previous condition report, it was identified that a

previous operability determination (OD) completed for General Electric (GE) model HFA

relays was incorrect in that it did not appear to fully address the condition of the mounting

screws that required torqueing. The seismic test results stated that the GE HFA relays

passed the seismic testing, but the relays required two screws to be torqued to 5 foot-

pounds. This condition of the additional required torqueing was initially entered into the

corrective action program on December 21, 2012.

Currently, approximately 136 relays, that provide various indication and control functions in

systems such as high pressure safety injection, charging, containment ventilation, and the

emergency diesel generator, have been identified as potentially affected. Relay

replacement/torqueing is in progress. A cause analysis is in progress, the results of which

will be published in a supplement to this LER.

The licensee event report is closed. Revision 1 of this licensee event report was submitted

on December 5, 2013.

.4 (Opened) Licensee Event Report 05000285/2013-001-01: Mounting of GE HFA Relays

does not Meet Seismic Requirements

On January 15, 2013, while reviewing a previous condition report, it was identified that the

initial I operability determination (OD) completed for General Electric (GE) model HFA relays

was incorrect in that it did not appear to fully address the condition of the mounting screws

that required torqueing. The seismic test results stated that the GE HFA relays passed the

seismic testing, but the relays required two back plate mounting screws to be torqued

to 5 foot-pounds. The condition of the additional required torqueing had been initially

entered into the corrective action program on December 21, 2012.

Approximately 136 relays that provide various indication and control functions in systems

such as high pressure safety injection, charging, containment ventilation, and the

emergency diesel generator, were identified as potentially affected. Relay replacement

torqueing has been completed for all identified relays. An investigation found that poor

communication (both in writing of technical documents and in interfacing between

individuals) was the cause of not identifying the need for the two back plate mounting

- 14 -

screws to be torqued to 5 foot-pounds when first reported by the vendor. Corrective actions

to provide training on the event and revise procedures have been initiated.

.5 (Closed) Licensee Event Report 05000285/2013-003-00: Calculations Indicate the HPSI

Pumps will Operate in Run-out During a DBA

At approximately 1721 Central Standard Time, on January 30, 2013, during hydraulic

evaluations for the alternate hot leg injection project, Design Engineering determined that

design basis calculations indicated that the high pressure safety injection (HPSI) pumps

would operate in a run-out condition under worst case design basis accident conditions.

Previous changes to the operation of the HPSI pumps and the containment spray pumps

have resulted in an increase in the injection phase time and an increase in HPSI pump flow

during the accident. This could have resulted in the HPSI pumps operating in run-out for

longer than the one hour manufacturer's recommended time limit.

A preliminary causal analysis identified that the station failed to obtain vendor technical

information on HPSI pump performance in a 10 CFR 50, Appendix B, Quality Assurance

validated format. An analysis of HPSI pump performance during the injection phase will be

performed and design or procedural actions to prevent HPSI pump operation in the

extended flow region and to ensure that sufficient net positive suction head is available will

be taken.

The licensee event report is closed. Revision 1 of this licensee event report was submitted

on November 27, 2013.

.6 (Opened) Licensee Event Report 05000285/2013-003-01: Calculations Indicate the HPSI

Pumps will Operate in Run-out During a DBA

At approximately 1721 Central Standard Time, on January 30, 2013, during hydraulic

evaluations for the alternate hot leg injection project, Design Engineering determined that

the high pressure safety injection (HPSI) pumps would operate in a run-out condition under

worst case design bases accident conditions. The calculated HPSI pump flow is beyond the

manufacturer's head-flow curves developed from original pump testing. The station was

shutdown in Mode 5 when discovered and the condition was entered into the station's

corrective action program as Condition Report 2013-02100. The HPSI pumps were

declared inoperable.

A causal analysis identified that the initial HPSI pump cross-tie valve (HCV-304 and HCV-

305) required position, impeller design, and runout characteristics identified during pre-

operational testing were not translated into design and licensing basis documents. This

allowed several HPSI system configuration and procedural changes that reduced the margin

to reliable pump operation. A new analysis shows that a new design flow rate of 450 gpm is

acceptable for up to 1000 hours0.0116 days <br />0.278 hours <br />0.00165 weeks <br />3.805e-4 months <br />. Orifices have been installed and tested that limits

maximum flow to prevent the HPSI pumps from operating beyond 450 gpm during a design

basis accident.

- 15 -

.7 (Closed) Licensee Event Report 05000285/2013-008-00: Previously Installed GE IVA

Relays Failed Seismic Testing

On April 11, 2013, the test results of seven General Electric (GE) IAV relays indicated that

three safety-related, seismically qualified, relays did not pass seismic testing. The condition

was entered in to the Station's corrective action program. A causal analysis determined that

the failure was caused by the control spring in the relay contacting either the disk or the drag

magnet during seismic testing resulting in a short. A wire used to support the spring was not

installed in the relays that failed the testing, allowing the control spring to sag and make

electrical contact.

There are a total of 45 GE IAV relays identified in the plant, of which 32 are safety-related.

Twelve of these had previously been replaced and two more were verified to have the

support wire installed. The remaining 18 relays will be inspected, and if the support wire is

missing, they will be replaced prior to plant startup.

The licensee event report is closed. Revision 1 of this licensee event report was submitted

on December 18, 2013.

.8 (Opened) Licensee Event Report 05000285/2013-008-01: Previously Installed GE IVA

Relays Failed Seismic Testing

On April 11, 2013, the test results of seven General Electric (GE) IVA relays, indicated that

three safety-related, seismically qualified, relays did not pass seismic testing. The condition

was entered into the Station's corrective action program. A causal analysis determined that

the failure was caused by the control spring in the relay contacting either the disk or the drag

magnet during seismic testing resulting in a short. A wire used to support the spring was not

installed in the relays that failed the testing allowing the control spring to sag and make

electrical contact.

There are a total of 4 GE IAV relays identified in the plant, of which 32 are safety-related.

Twenty-seven of the relays required replacement due to missing the support wire.

.9 (Opened) Licensee Event Report 05000285/2013-014-00: Unqualified Components used in

Safety System Control Circuit

On October 3, 2013 station personnel identified that a condition with the control loop for

HCV-1369, Turbine-Driven Auxiliary Feedwater Pump FW-10 Recirculation Valve, was

incorrectly evaluated as not reportable. The original condition was identified on

October 18, 2012, which identified unqualified components in the control loop whose failure

could cause a spurious closure of HCV-1369 and result in pump damage. The station was

shutdown in MODE 5 when discovered.

The condition was entered in to the station's corrective action program as Condition

Report 2013-18752. Engineering is reviewing this condition and the results of this review

will be used to update this report. This report was previously submitted on

December 9, 2013 with a duplicate LER number.

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.10 (Opened) Licensee Event Report 05000285/2013-017-00: Containment Spray Pump

Design Documents do not Support Operation in Runout

Fort Calhoun Station (FCS) has identified that design basis documents for the containment

spray (CS) pumps SI-3A, SI-3B and SI-3C did not fully support pump operation during

runout conditions which could occur under certain system configurations. On

October 31, 2013, additional design work was completed which showed that the

containment spray pumps would not meet their required mission time under specific

accident scenarios. However, the analysis also showed that the containment peak pressure

for the limiting design basis accident occurs at 202.3 seconds, which is prior to the

containment spray delay time of 228.2 seconds. Therefore, the peak containment pressure

would not be affected by this failure.

Fort Calhoun Station has completed a calculation necessary to support a temporary

modification which throttles the containment spary pump discharge valves to increase

system resistance. A new containment spray pump curve has been issued to include

operation in the extended pump operating range. A permanent modification to prevent

containment spray pump runout is being pursued.

.11 (Opened) Licensee Event Report 05000285/2013-018-00: Postulated Fire Event Could

Result in Shorts Impacting Safe Shutdown

On October 9, 2013, an event notification applicable to Callaway Nuclear Power Plant was

posted that documented a postulated fire event regarding the impact of unfused direct

current (DC) ammeter circuits in the control room (CR). In the postulated event, a fire in the

control room could cause one of the ammeter wires to short to the ground plane.

Simultaneously, if the fire causes another direct current wire from the opposite polarity on

the same battery to also short to the ground plane, a ground loop would be established

through the unprotected ammeter wiring. This event could result in excessive current flow

(heating) in the ammeter wiring to the point of causing a secondary fire in the raceway

system. The secondary fire could adversely affect safe shutdown equipment and potentially

result in the loss of the ability to conduct a safe shutdown as required by 10 CFR50

Appendix R. Plant engineering personnel reviewed the information against station electrical

schematics and at approximately 1230 central daylight time on October 28, 2013, an 8-hour

notification was made pursuant to 10 FR 50.72(b)(3)(ii)(8). The station was in Mode 5 when

the condition was identified.

An hourly fire watch was established in the affected locations of the station. Fort Calhoun

Station will install fuses in the direct current ammeter circuitry as determined by Engineering

Change 62826, Add Fuses to the direct current Ammeter Circuitry for Ammeters.

4OA4 IMC 0350 Inspection Activities (92702)

Inspectors continued implementing IMC 0350 inspection activities, which include follow-up on

the restart checklist items contained in the Confirmatory Action Letter (CAL) issued

February 26, 2013 (EA-13-020, ML 13057A287). The purpose of these inspection activities is to

- 17 -

assess the licensees performance and progress in addressing its implementation and

effectiveness of Fort Calhoun Stations Integrated Performance Improvement Plan (IPIP),

significant performance issues, weaknesses in programs and processes, and flood restoration

activities.

Inspectors used the criteria described in baseline and supplemental inspection procedures,

various programmatic NRC inspection procedures, and IMC 0350 to assess the licensees

performance and progress in implementing its performance improvement initiatives. Inspectors

performed on-site and in-office activities, which are described in more detail in the following

sections of this report. This report covers inspection activities from November 16 through

December 31, 2013. Specific documents reviewed during this inspection are listed in the

attachment.

The following inspection scope, assessments, observations, and findings are documented by

CAL restart checklist item number.

.1 Causes of Significant Performance Deficiencies and Assessment of Organizational

Effectiveness

Section 1 of the restart checklist contains those items necessary to develop a

comprehensive understanding of the root causes of safety-significant performance

deficiencies identified at Fort Calhoun Station. In addition, Section 1 includes the

independent safety culture assessment with the associated root causes and findings. The

integration of the assessments under Item 1.f identifies the fundamental aspects of

organizational performance in the areas of organizational structure and engagement,

values, standards, culture, and human behaviors that have resulted in the protracted

performance decline and are critical for sustained performance improvement. Section 1

reviews also include an assessment against appropriate NRC Inspection Procedure 95003

key attributes. These assessments are documented in section 4OA4.5.

.a Flooding Issue - Yellow Finding

Item 1.a is included in the restart checklist for the failure of Fort Calhoun Station to

maintain procedures and equipment that protects the plant from the effects of a design

basis flood. These deficiencies resulted in a yellow (substantial safety significance)

finding.

(1) Inspection Scope

i. The team assessed the licensees actions taken since NRC Inspection

Report 05000285/2013008. As documented in NRC Inspection

Report 05000285/2013008, the inspectors reviewed this area for closure and noted

discrepancies in the extent of condition area and a number of deficiencies noted in

the technical bases for the flooding procedure which led to restart checklist

items 1.a.1, 1.a.2, and 1.a.3 remaining open. The inspectors reviewed licensee

actions to address the inspectors concerns to ascertain whether they were sufficient

to ensure plant safety and support closure of the restart checklist items.

- 18 -

ii. Open items (Licensee Event Reports (LER) and violations (VIO) for this portion of

the restart checklist) specifically related to the Yellow finding were reviewed by the

team. The team reviewed the adequacy of the licensees causal analyses and extent

of condition evaluations related to the associated deficiencies that protect the plant

from the effects of a design basis flood. In addition, the NRC verified that adequate

corrective actions were identified associated with the licensees causal analyses and

extent of condition evaluations and that implementation of these corrective actions

were either implemented or appropriately scheduled for implementation.

Open items reviewed were:

LER 2012-001, Inadequate Flooding Protection Procedure

LER 2012-019, Traveling Screen Sluice Gates Found with Dual Indication

LER 2011-003, Inadequate Flooding Protection Due to Ineffective Oversight

VIO 2012002-01, Inadequate Procedures to Mitigate a Design Basis Flood Event

VIO 2012002-02, Failure to Classify Intake Structure Sluice Gates as Safety

Class III

VIO 2012002-03, Failure to Meet Design Basis Requirements for Design Basis

Flood Event

VIO 2010007-01, Failure to Maintain External Flood Procedures

(2) Observations and Findings

i. Resolution of Root Cause, Corrective Action, and Extent of Condition Issues

a) Licensees Evaluations and Associated Improvement Actions Related to the Yellow

Flooding Finding

From previous inspections, the major aspects which the licensee had not adequately

addressed for the root cause analyses and associated efforts for the Yellow flooding

finding were extent of condition review and addressing deficiencies in the technical

bases for the licensees flood mitigation procedures. The inspectors reviewed

licensee actions below.

Resolution of Extent of Condition Review Weaknesses. In NRC Inspection

Report 05000/285/2013008, the team noted several areas where the licensee had

not adequately addressed the extent of condition of the inadequate flooding

procedure. Inspectors identified the following observations which were previously

documented related to extent of condition.

URI 05000285/2013008-01, Inadequate Procedure for Combatting Frazil Ice

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FIN 05000285/2013008-02, Frazil Ice Monitor Not Operational

NCV 05000285/2013008-03, Lack of Safety-Related Equipment For Design

Basis Low River Level

NCV 05000285/2013008-04, Non-conservative Value for Declaring An Alert

on Low River Level

NCV 05000285/2013008-05, Inadequate Procedure for Combating Loss of

Raw Water

The inspectors observed that the licensee had entered each of these conditions into

their corrective action program for resolution.

To address the overall concern that the licensees review of the extent of condition

for the inadequate procedure which led to the Yellow flooding finding, the licensee

performed additional reviews of their abnormal operation procedures. Additionally,

the licensee has post-restart actions in place to perform additional reviews

associated with a procedural quality improvement effort that is part of the licensees

Performance Improvement Integrated Matrix (PIIM). Action Numbers 2013-0031

and 2013-0086 of the PIIM cover the procedural improvement program by the

licensee.

The inspectors determined that the licensees actions addressing the identified

deficiencies associated with the extent of condition coupled with the licensee

conducting a procedure improvement initiative were adequate to address the

weaknesses in the licensees extent of condition review for the Yellow flooding

finding.

Resolution of Procedural Technical Bases Observations. In NRC Inspection

Report 05000/285/2013008, the team noted several areas where the licensee had

not adequately addressed weaknesses in the technical bases of the flooding

mitigation procedures. The team reviewed the technical bases for procedural steps

in the revised flooding procedure. The technical bases prove that the procedures

and the equipment they call upon would work when demanded under a design basis

flood. In Inspection Report 05000285/201008, the team identified the following

issues related to FCS personnels ability to adequately address technical

inadequacies in the procedures to mitigate flooding:

NCV 05000285/2013008-06, Failure to Account for Worst Case Conditions

in Fuel Oil Inventory Calculation

URI 05000285/2013008-07, Administrative Controls for a Technical

Specification for Low River Level

NCV 05000285/2013008-08, Sluice Gate Leakage Not Periodically Verified

- 20 -

NCV 05000285/2013008-09, Failure to Prevent Failures of the Sluice Gates

to Close

NCV 05000285/2013008-10, Failure to Accurately Model Raw Water Flow

into the Intake Structure

NCV 05000285/2013008-11, Failure to Account for Usable Fuel Oil Tank

Level in Inventory

The inspectors observed that the licensee had entered each of these conditions into

their corrective action program for resolution.

To address the overall concern with inadequacies in the technical bases of their

flooding mitigation procedures, the licensee performed additional reviews of their

abnormal operation procedure for acts of nature, their emergency plan implementing

procedures, and their second level support procedures called on in their flooding

procedure AOP-01, Acts of Nature. This review and future reviews were and will

be part of the larger review performed for the procedural quality improvement effort

post restart as part of the PIIM. Action Numbers 2013-0031 and 2013-0086 of the

PIIM cover the procedural improvement program by the licensee.

The team concluded that Fort Calhoun Station had adequately resolved the identified

technical issues associated with technical bases for their flooding mitigation

procedures by their actions to address the identified deficiencies coupled with the

effort to conduct a procedure improvement initiative as described in the their PIIM.

Conclusion

The inspectors determined that the licensee had adequately addressed the extent of

condition and procedural technical bases areas which had previously been of

concern associated with Restart Checklist Bases Document Items 1.a.1, Flooding

Yellow Finding root and contributing cause evaluation, 1.a.2, Flooding Yellow

Finding extent of condition and cause evaluation, and 1.a.3, Flooding Yellow

Finding corrective actions addressing root and contributing causes.

Items 1.a.1, 1.a.2, and 1.a.3 are closed.

ii. Resolution of Open Items Related to the Yellow Flooding Finding on the Restart

Checklist Basis Document

a) LER 2012-001, Inadequate Flooding Protection Procedure

Licensee Event Report LER 2012-001 documented the deficiencies in Procedure

AOP-01, Acts of Nature, that were associated with the NRC Yellow finding.

The inspectors reviewed and closed the causal analyses, corrective actions, and

extent of condition for this issue in Section a above.

This LER is closed.

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b) LER 2012-019, Traveling Screen Sluice Gates Found with Dual Indication

Licensee Event Report LER 2012-019 documented a condition where intake

sluice gates were found with dual indication. With this indication, the position of

the sluice gates could not be positively confirmed to be closed as required by the

licensees flood procedure. The licensee entered this condition into their CAP

and reviewed the licensees corrective actions. The licensee took action to close

the sluice gates and ensure the flooding mitigation feature was restored. The

inspectors began inspection of this item in NRC Inspection

Report 05000285/2012012 and included its review under Finding

FIN 5000285/2012012-03, Failure to Properly Manage the Functionality of the

River Sluice Gates. To address any future concerns with conflicting information

for the position of the sluice gates, the licensee revised their maintenance

procedure to provide an affirmative method of ensuring the sluice gates were

closed. The inspectors reviewed this method and considered the method

adequate.

This LER is closed.

c) LER 2011-003, Inadequate Flooding Protection Due to Ineffective Oversight

Licensee Event Report LER 2011-003 documented that the predominant cause

of the Yellow flooding finding for an inadequate flooding mitigation procedure was

historical ineffective oversight by station management. The licensee came to this

conclusion as a result of their root cause analyses. The inspectors noted that

station management had been changed and new managers in the principal

positions were supplied in an operating agreement with Exelon Nuclear. The

remaining aspects for the inadequate flooding protection were addressed under

CR 2010-2387. The inspectors reviewed this and the licensees actions during

the review of the causal analyses, corrective actions, and extent of condition for

this issue in Section a above.

This LER is closed.

d) VIO 2012002-01, Inadequate Procedures to Mitigate a Design Basis Flood

Event

Violation VIO 2012004-01 documented multiple examples of a violation of

Technical Specification 5.8.1.a, Procedures, for failure to establish and maintain

procedures to mitigate an external flooding event. The procedural guidance for

flooding was inadequate to mitigate the consequences of external flooding. The

inadequacies were a failure to provide operators with sufficient information to

ensure a transfer of power from offsite to an onsite emergency diesel generator

prior to a loss of offsite power; a failure to identify that the class-1E powered

motor operators of the six intake structure sluice gates were located at an

elevation of 1,010 feet mean sea level (below the design basis flood level); a

failure to identify that three of the six sluice gate motor operators would be de-

energized when offsite power was transferred from offsite to one onsite

- 22 -

emergency diesel generator; and a failure to adequately ensure the fuel transfer

hose to emergency diesel generator day tanks was staged prior to river level

exceeding 1,004 feet mean sea level. The licensee entered these conditions into

their CAP as Condition Report CR 2010-2387. The inspectors reviewed the

licensees corrective actions.

The failures were adequately corrected by the licensee with procedure revisions.

The inspectors conducted walkthroughs with licensee operators and

maintenance personnel in the simulator to ensure the revisions adequately

addressed the issues.

This violation is closed.

e) VIO 2012002-02, Failure to Classify Intake Structure Sluice Gates as Safety

Class III

Violation VIO 2011002-02 documented a violation of 10 CFR Part 50, Appendix

B, Criterion III, Design Control, for failure of the licensee to classify the six

intake structure exterior sluice gates and their motor operators as Safety Class

III. Inspectors identified that the licensees previous mitigation scheme to raise

and lower the intake cell sluice gates as a method to control level in those cells

would require the sluice gates to be classified as safety class equipment. The

licensee originally denied this violation, but the NRCs further independent review

re-affirmed the validity of the original violation. The licensee entered this

condition into their CAP as Condition Report CR 2010-2387. The inspectors

reviewed the licensees corrective actions. These actions included a modification

to the plant and the licensees submittal of license amendment request that is

currently under review.

The new method uses four new lines which tap off of the circulating water system

trash rack blowdown piping. This method requires all sluice gates to be fully

closed and not used for controlling cell level. Four new valves in the blowdown

piping would be used to control the intake cell level during a flood. Inspectors

reviewed the modification and the licensees operability determination to use this

new method while the licensing amendment is under review and found them

adequate to support plant safety.

This violation is closed.

f) VIO 2012002-03, Failure to Meet Design Basis Requirements for Design Basis

Flood Event

Violation VIO 2012002-03 documented a violation of 10 CFR 50, Appendix B,

Criterion III, Design Control, for the failure to meet design basis requirements

for protection of the safety related raw water system during a design basis flood

for flood levels between 1,010-1,014 feet mean sea level (msl) as identified in

Updated Safety Analysis Report, Section 9.8, Raw Water System. Specifically,

the design basis states, in part, that water level inside the intake cells can be

- 23 -

controlled during a design basis flood by positioning the exterior sluice gates to

restrict the inflow into the cells. Inspectors identified that the sluice gate motor

operators would be submerged below 1,014 feet msl adversely affecting the

abilty to position the sluice gates. The licensee entered this condition into their

CAP as Condition Report CR 2010-2387. The inspectors reviewed the licensees

corrective actions. These actions, as previously discussed, included a

modification to the plant and the licensees submittal of license amendment

request, both related to a change in the licensees method of controlling intake

cell level during flooding conditions up to the design basis flood.

This violation is closed.

g) VIO 2010007-01, Failure to Maintain External Flood Procedures

Violation VIO 2010007-01 documented the original concern the NRC identified

with the licensees ability to mitigate a design basis flood. The NRC conducted

numerous follow-up inspections of the licensees actions to address their

readiness for a design basis flood event. The root cause analyses for the

condition were reviewed during the inspections of Sections 1.a.1, 1.a.2, and 1.a.3

of the Restart Checklist Basis Document. Inspection Report 05000285/2013008

identified areas of concern which were re-inspected and deemed to be

satisfactorily addressed by the licensee as previously documented in this report.

This violation is closed.

(3) Assessment Results

i. Licensees Evaluations and Associated Improvement Actions Related to the Yellow

Flooding Finding

Based on the licensees efforts to address the discrepancies previously identified by

the inspectors in the extent of condition area and the in the technical bases for the

flooding procedure, restart checklist items 1.a.1, 1.a.2, and 1.a.3 were closed.

ii. Resolution of open Items associated with the Yellow Flooding Finding

Based on the reviews the team conducted, the following items were closed:

a) LER 2012-001, Inadequate Flooding Protection Procedure

b) LER 2012-019, Traveling Screen Sluice Gates Found with Dual Indication

c) LER 2011-003, Inadequate Flooding Protection Due to Ineffective Oversight

d) VIO 2012002-01, Inadequate Procedures to Mitigate a Design Basis Flood

Event

e) VIO 2012002-02, Failure to Classify Intake Structure Sluice Gates as Safety

Class III

- 24 -

f) VIO 2012002-03, Failure to Meet Design Basis Requirements for Design

Basis Flood Event

g) VIO 2010007-01, Failure to Maintain External Flood Procedures

iii. Overall Assessment of Item 1.a: Flooding Issue - Yellow Finding (CLOSED)

Closure of all individual items in Section 1.a, Yellow Flooding Finding, of the

Restart Checklist are closed.

.b Reactor Protection System Contactor Failure - White Finding

Item 1.b is included in the restart checklist for the failure of Fort Calhoun Station to

correct a degraded contactor, which subsequently failed, in the reactor protection

system. These deficiencies resulted in a white (low to moderate safety significance)

finding.

(1) Inspection Scope

The team reviewed the licensees assessment of the failure of the M-2 contactor in the

reactor protection system that occurred June 14, 2010. The team verified that the

licensee adequately identified the root and contributing causes of the risk significant

issue; verified that the extent of condition and extent of causes of the risk significant

issue were identified, and verified that the corrective actions adequately addressed the

causes to preclude repetition. (Restart Checklist Basis Document Items 1.b.1; 1.b.2;

1.b.3)

An open item specifically related to the White finding was reviewed by the team. The

team verified that the licensee had performed adequate root cause and extent of

condition evaluations related to the associated deficiencies. In addition, the NRC

verified that adequate corrective actions were identified associated with the licensees

root and contributing causes and extent of condition evaluations and that implementation

of these corrective actions are either implemented or appropriately scheduled for

implementation. (VIO 2011007-01)

Specifically, the team assessed Revision 4 of the Root Cause Analysis (RCA) for CR

2011-00451, for which the problem statement was:

Reactor Protection System M-2 contractor was identified as chattering on

November 3, 2008 and non-conforming maintenance was performed. The M-2

contractor remained in a degraded and non-conforming condition without an

appropriate analysis to evaluate until it failed surveillance testing on June 14, 2010.

This revision to the root cause changed the wording significantly.

- 25 -

The teams assessment was based on the evaluation criteria from Section 02.02 of NRC

Inspection Procedure 95001, which aligned with this item. The inspection objectives

were to:

Provide assurance that the root and contributing causes of risk-significant issues

were understood;

Provide assurance that the extent-of-condition and extent-of-cause of risk-

significant issues were identified;

Provide assurance that the licensee's corrective actions for risk-significant

performance issues were, or will be, sufficient to address the root and

contributing causes and to preclude repetition.

(2) Observations and Findings

Determine that the problem was evaluated using a systematic methodology to identify

the root and contributing causes.

The team determined that the licensee evaluated this problem using a systematic

methodology to identify the root and contributing causes. Specifically, RCA 2011-00451

employed the use of event and causal factor charting, barrier analysis, comparative

analysis, and causal factor test, root and contributing cause statements, and the root

and contributing cause testing. The barrier analysis and event and causal factor chart

associated with RCA 2011-00451 identified a number of failed barriers that appeared to

play a significant role in the events leading to the failure of the reactor protection system

M-2 contactor. Included in the analysis were failures of the Preventive maintenance

program, operations procedures, system engineering, operations degraded non-

conforming process, work control process, and the Plant Review Committee Process.

Based on the analysis, the licensee concluded the following were the root and

contributing causes of the failure to address the degraded M-2 contactor in the reactor

protection system:

RC-1: Electrical Maintenance workers did not follow the procedure / work order

instructions for the M-2 contactor issue. When presented with conditions outside

of the expected, they did not use the Human Performance Tool DUCS

(Distracted, Uncertain, Confused, Stop) to obtain the necessary guidance to

correct the issue.

RC-2: The Operations Department did not have an effective nuclear safety

culture and ownership of plant equipment necessary to challenge unexpected

events and take prompt action to drive the action to restore degraded equipment

to reliable operation.

- 26 -

CC-1: System Engineering did not recognize and implement their responsibility to

perform appropriate evaluations to address plant technical issues and act as the

site technical conscience.

CC-2: Preventive Maintenance strategies were not implemented to replace the

M-contactors before they exhibited degradation and did not consider the

increased failure rate associated with their reaching end of service life.

CC-3: Engineering judgment used to support Operability Evaluations was not

rigorous or formally documented.

CC-4: The Plant Review Committee Degraded / Nonconforming condition

subcommittee process was allowed to change operations department decisions

on whether equipment was degraded without operations concurrence or formal

documentation of the basis.

CC-5: Operations surveillance test guidance allowed pausing surveillance tests

to perform repairs, which is a practice that is contrary to industry practices and

regulatory guidance.

CC-6: Operations knowledge of Technical Specification requirements related to

the M-contactors was inadequate resulting in entry into TS 2.15(1) instead of TS 2.0.1.

Determine that the root cause evaluation was conducted to a level of detail

commensurate with the significance of the problem.

The team determined that the RCA was conducted to a level of detail commensurate

with the significance of the problem. Specifically, the licensee performed a significant

revision to the RCA based on the inspection concerns documented in IR 2013-008. The

licensee systematically used Methods 1 and 2 for cause testing as defined by

FCSG 24 5, Condition Report and Cause Evaluation. The eight causal statements,

developed from merged causal factors, were evaluated using the flow chart. Two causal

statements were identified as Root Causes and the other six were determined to be

Contributing Causes.

Determine that the root cause evaluation included a consideration of prior occurrences

of the problem and knowledge of prior operating experience.

The team determined that the RCA included evaluation of both internal and industry

operating experience as documented in Attachment 4 to RCA 2011-00451.

Determine that the root cause evaluation addressed the extent of condition and the

extent of cause of the problem.

The team reviewed the licensees RCA as it relates to extent of condition and extent of

cause.

- 27 -

For extent of condition, the licensee used same-same, same-similar, similar-same, and

similar-similar evaluation method which is documented as Attachment 3 to

RCA 2011-00451. Based on this analysis, the licensee determined that an extent of

condition does exist. The licensee based this conclusion, in part, on the findings of

Condition Report CR 2012-09494, related to deficiencies in identifying

degraded/nonconforming conditions and in the performance of operability

determinations.

For extent of cause, the licensee determined an extent of cause does exist for the root

causes identified in this analysis. They believe the extent of causes have been

addressed by the collective sum of all corrective actions from the following RCAs:

2011-01719, Incorrect Technical Specification Entered when AI-3-M2 Contactor

failed

2011-03025, Area for Improvement (EN 1-1)

2012-03986, Organizational Ineffectiveness

2012-08125, Engineering Design / Configuration Control

2012-08132, Site Operational Focus and Conservative Decision Making

2012-08135, Human Performance

2012-08134, Equipment Reliability / Work Mangement

2012-08137, Regulatory Process and Infrastructure

2012-09491, End of Service Life

2012-09494, Deficiencies in Identifying Degraded and Non-Conforming Condition

and Performing Operability Determinations

2013-05570, Design and Licensing Bases Configuration Control

The team concluded that RCA 2011-00451 determined an appropriate extent of

condition and appropriate extent of cause for the root cause related to the reactor

protection system M-2 contactor issue.

Determine that the root cause, extent of condition, and extent of cause evaluations

appropriately considered the safety culture components as described in IMC 0310.

The root cause, extent of condition, and extent of cause evaluations appropriately

considered the safety culture components as described in IMC 0310. Specifically, the

licensee documented their consideration of the IMC 0310 cross-cutting aspects in

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Attachment 9 of RCA 2011-00451. The licensee identified several cross-cutting aspects

in the area of human performance, problem identification and resolution (PI&R), and

other components that were applicable to issues related to deficiencies in

degraded/nonconforming condition review and operability evaluations. The final

evaluation concluded that only a small number of the safety culture attributes were not to

be applicable to RCA 2011-00451.

Determine that appropriate corrective actions are specified for each root and contributing

cause.

The team reviewed Attachment K to 2011-00451 and determined that generally the

licensees proposed corrective actions were appropriate to address the root and

contributing causes identified.

Determine that a schedule has been established for implementing and completing the

corrective actions.

The team determined that due dates have been established for implementation and

completion of corrective actions.

Determine that quantitative or qualitative measures of success have been developed for

determining the effectiveness of the corrective actions to prevent recurrence.

The team determined that quantitative or qualitative measures of success have been

developed for determining the effectiveness of the corrective actions to prevent

recurrence.

(3) Assessment Results

The team concluded that for Item 1.b: Reactor Protection System Contact

Failure - White Finding, the root and contributing causes of risk-significant issues were

understood; the extent-of-condition and extent-of-cause of risk-significant issues were

identified; and, the licensees corrective actions for risk-significant performance issues

were, or will be, sufficient to address the root and contributing causes and to preclude

repetition.

All items in Section 1.b, Reactor Protection System Contactor Failure - White Finding,

are closed.

.2 Flood Restoration and Adequacy of Structures, Systems, and Components

Section 2 of the Restart Checklist contains those items necessary to ensure that important

structures, systems, and components affected by the flood and safety significant structures,

systems and components at Fort Calhoun Station are in appropriate condition to support

safe restart and continued safe plant operation.

.b System Readiness for Restart Following Extended Plant Shutdown

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Systems that have been shut down for prolonged periods may be subject to different

environments than those experienced during power operations. The NRC verified that

the licensee adequately evaluated the effects of the extended shutdown to ensure that

the structures, systems, and components are ready for plant restart and they conform to

the appropriate licensing and design bases requirements.

(1) Inspection Scope

.ii Detailed Review of Alternating and Direct Current Electrical Distribution, and High

Pressure Safety Injection Systems

The licensee performed a comprehensive review to evaluate and verify the capability

of selected systems to fulfill their intended safety functions as defined by the

licensing and design basis and identified broad-based safety, organizational, and

performance issues. The review was structured consistent with NRC Inspection

Procedure 95003 (Sections 02.03 and 03.03). The selected systems for detailed

review (vertical slice) as part of the Reactor Safety Strategic Performance Area were

based on their high risk significance, input from system health reports, performance

indicators, condition reports, and licensee event reports. Teams of Omaha Public

Power District and independent external experts performed the Reactor Safety

Strategic Performance Area reviews.

Systems selected are:

AC and DC Electrical Distribution Systems. These systems include the 4160V

breakers, 480V breakers, batteries, and battery chargers. Electrical distribution

systems at Fort Calhoun Station provide necessary power for Mitigating

Systems. The AC and DC systems provide power to key pumps, motors, valves,

and instruments required to monitor and respond to plant conditions. From the

plants probabilistic assessment, the AC and DC electrical systems account for a

substantial portion of plant risk. The electrical distribution system was selected

for self assessment by the licensee based on both identified issues and their

importance to safety.

Emergency Core Cooling System. This includes the high pressure injection

system. This system is important to provide mitigation for postulated accident

conditions in the reactor plant. This review assessed and validated key aspects

of the suction and discharge pathways, system alignments, power sources, and

emergency actuation.

Results and insights from these reviews were incorporated into the Integrated

Performance Improvement Plan that supported the restart of Fort Calhoun Station.

The NRC inspected each of the licensees detailed reviews and select samples for

independent verification that the licensee properly assessed each system.

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(2) Observations and Findings

No findings or observations.

(3) Assessment Results

Inspectors concluded that based on their reviews of the cause evaluations, and the

extent of cause/extent of condition reviews, that this area has been reviewed by the

licensee to a sufficient level of detail.

Items 2.b.2.1, 2.b.2.2, 2.b.2.3, and 2.b.2.4 are closed.

.3 Adequacy of Significant Programs and Processes

Section 3 of the Restart Checklist addresses major programs and processes in place at

FCS. Section 3 reviews will also include an assessment of how the licensee appropriately

addressed the NRC Inspection Procedure 95003 key attributes as described in Section 6.

.a Corrective Action Program

(1) Inspection Scope

i. The team assessed the licensees actions taken since NRC Inspection

Report 05000285/2013008. In Inspection Report 05000285/2013008, the inspectors

reviewed this area for closure and observed that because the licensee was

continuing implementation of corrective actions to improve the effectiveness of the

CAP, the licensee had unsatisfactory results on effectiveness reviews, and because

the licensee was still generating additional corrective actions to address CAP

effectiveness, items 3.a.1, 3.a.2, 3.a.3, and 3.a.4 remained open.

The inspectors reviewed licensee actions to address the inspectors concerns to

ascertain whether they were sufficient to ensure the CAP was adequate to support

plant restart. Also, the team reviewed the licensees assessment of the Fundamental

Performance Deficiency associated with the CAP.

In addition, the team reviewed the licensees assessment of the past issues involving

inadequate operating experience reviews identified in NRC Inspection

Report 05000285/2013008. In that report, the team determined that the effort by the

licensee to lump operating experience weaknesses in the RCA did not provide for

the proper analysis needed to address this deficiency which was prevalent in nearly

all of the Fundamental Performance Deficiency RCAs. Therefore, restart checklist

items 3.a.8, 3.a.9, 3.a.10, and 3.a.11 remained open pending the verification of the

effective resolution. The inspectors reviewed licensee actions to ascertain whether

they were sufficient to ensure that operating experience reviews by the licensee were

adequate.

Finally, in NRC Inspection Report 05000285/2013008, the team performed a

problem identification and resolution team inspection. That team concluded that

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overall, the CAP at FCS was functional in identifying, evaluating, and correcting

issues with various degrees of effectiveness. The team had a large number of

observations provided in each of the areas of CAP, and observed that there was

significant room for improvement. Based on all the observations identified by the

team, in all 3 areas of CAP, restart checklist item 3.a.12 remained open for additional

inspections to ensure an improved implementation of the CAP was in place. The

inspectors reviewed licensee actions to address the inspectors concerns to

ascertain whether they were sufficient to ensure the CAP was being adequately

implemented.

ii. Open items (Licensee Event Reports (LER), noncited violations (NCV), and

violations (VIO) specifically related to the corrective action program were reviewed

by the team. The team reviewed the adequacy of the licensees causal analyses and

extent of condition evaluations related to the associated deficiencies noted in the

licensees corrective action program. In addition, the NRC verified that adequate

corrective actions were identified associated with the licensees causal analyses and

extent of condition evaluations and that implementation of these corrective actions

were either implemented or appropriately scheduled for implementation.

Open items reviewed were:

VIO 2011006-02, Inadequate Corrective Actions to Ensure Reliability of Raw

Water Pump Power

NCV 2011006-06, Failure to Implement an Adequate Trending Program

NCV 2010003-01, Failure to Provide Adequate Limiting Condition for

Operation for High River Level

LER 2012-007, Failure of Pressurizer Heater Sheath

LER 2012-004, Inadequate Analysis of Drift Affects Safety Related

Equipment

LER 2012-010, Seismic Qualification of Instrument Racks

(2) Observations and Findings

i. Corrective Action and Operational Experience Programs Assessment

a) Resolution of Corrective Action Program Deficiencies

NRC Inspection Report 05000/285/2013008 documented that based on the

ongoing implementation of corrective actions, the licensees unsatisfactory

results on effectiveness reviews, and because the licensee was still generating

additional corrective actions to address CAP effectiveness, restart checklist

items 3.a.1, 3.a.2, 3.a.3, and 3.a.4 would remain open.

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The inspectors assessed licensee actions addressing the noted deficiencies.

The inspectors reviewed CR 2013-08675 which was initiated after the inspection

documented in Inspection Report 05000285/2013008. The licensee performed a

root cause analysis to evaluate the quality and timeliness of CAP actions and the

fact that prior actions taken to prevent recurrence of problems had not been fully

effective.

The root cause was determined by the licensee to be:

Station personnel have not consistently followed CAP procedures and station

leadership has not reinforced CAP procedure compliance, as a result

improvements in CAP performance have been limited.

Corrective actions taken to address this were the establishment of a CAP

oversight function and to develop and implement CAP Fundamentals reinforced

through an accountability model for specific CAP behaviors. Each of these

actions were put in place with periodic effectiveness measures being used to

monitor progress. The inspectors reviewed the first effectiveness measurement

results and noted continued improvement in the functioning of the CAP. The final

effectiveness measures and continued actions for improvement of the CAP are

contained in the PIIM in Action Plan Numbers 2013-0055, CAP Excellence

Plan - Problem Identification, 2013-0065, CAP Excellence Plan - Root Cause

and Apparent Cause Quality, and 2013-0062, CAP Excellence Plan - Corrective

Action Closure.

The licensee also identified six contributing causes that included:

CAP volume has significantly increased without significant process or

prioritization changes to ensure quality and timeliness requirements can be

maintained.

The CAP strategy for improving performance was not well implemented and

understood at all levels in the organization.

The ActionWay software is not being used as an effective barrier to ensure

that certain required actions within the CAP process are performed and that

certain prohibited actions are prevented.

Inadequate procedure guidance for action types in ActionWay has led to

inappropriate use and untimely resolution of conditions adverse to quality.

Station personnel have not received the requisite training to assure that

station leadership and staff have the knowledge and skills to effectively and

efficiently implement the CAP program.

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Station trending has been time consuming and ineffective due a large number

of flat level codes, the inability to trend on common subjects, and the lack of

connectivity between event and cause codes.

The inspectors reviewed the licensees actions to address these contributing

causes. The inspectors determined that the corrective actions to address the

contributing causes appeared to adequately address the deficiencies. Based on

the licensees improvements in CAP performance, continued effectiveness

measurement to monitor sustained improvement and make corrections when

needed, and the continued station focus on CAP improvements contained in the

PIIM, the inspectors considered that the CAP was adequately healthy and should

continue to improve.

Based on this assessment Restart Checklist Basis Document Items 3.a.1,

Licensee Assessment of Corrective Action Program, 3.a.2, Adequacy of

Extent of Condition and Extent of Causes, 3.a.3, Adequacy of Corrective

Actions, and 3.a.4, Adequacy of Effectiveness Measures to Monitor Program

Improvements, are closed.

b) Resolution of the Functional Performance Deficiency Associated with the CAP

In NRC Inspection Report 05000/285/2013008, the team noted that the licensee

had chartered a team to perform another root cause analysis in this area and

therefore assessing closure of this area would not be appropriate until that effort

was completed and inspected by the NRC. The licensee completed the root

cause analysis as part of CR 2013-08675. This root cause addressed both the

CAP deficiencies and the functional performance deficiency associated with the

CAP since both were closely related. Actions to correct the fundamental

performance deficiency were reviewed and found to be adequate. The

inspectors noted the actions were bounded by the actions to improve the

effectiveness of the CAP, including the emphasis of the continued CAP

improvements contained in the PIIM.

Based on this assessment Restart Checklist Basis Document Items 3.a.5,

Licensee Assessment of the Fundamental Performance Deficiency Associated

with the Corrective Action Program, 3.a.6, Adequacy of Extent of Condition and

Extent of Causes, and 3.a.7, Adequacy of Corrective Actions, are closed.

c) Resolution of Operational Experience Program Deficiencies

In NRC Inspection Report 05000/285/2013008, the team concluded that the

licensees assessment of Performance Improvement initiatives, specific to

operating experience, was too general to effectively address the operating

experience portion of the CAP. The NRCs concern with the licensees practices

with operating experience was that the site Operating Experience Program was

not effectively being implemented to enhance the performance of FCS.

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During this inspection the inspectors noted actions by the licensee to enhance

the use of operating experience. An example of this was in CR 2013-02062

where the licensee noted the operating experience program should be reviewed

to determine if any changes can be made to enhance the security organization

use of operating experience. The inspectors noted similar instances in other

areas, including improved use of operating experience in root cause analyses.

The inspectors noted that improvement in the use of operating experience was

incoroporated into the PIIM in Action Plan Number 2013-0061, Human

Performance, to improve human performance at the station. Operating

Experience was also included in the PIIM as part of the Performance

Improvement Program ensuring the CAP Coordinators for each department drive

the use of operating experience. Based on these observations, the inspectors

concluded that the licensee had taken adequate actions to increase the use of

operating experience in various station work processes and had inititiatives in

their PIIM to continue improvements in this area.

Based on this assessment Restart Checklist Basis Document Items 3.a.8,

Licensee Assessment of Operating Experience Action Program, 3.a.9,

Adequacy of Extent of Condition and Extent of Causes, 3.a.10, Adequacy of

Corrective Actions, and 3.a.11, Adequacy of Effectiveness Measures to Monitor

Program Improvements, are closed.

d) NRC Problem Identification and Resolution Team Inspection

In NRC Inspection Report 05000/285/2013008, it was documented that the NRC

performed a problem identification and resolution team inspection but did not

close Item 3.a.12, noting the need for additional inspections to ensure an

improved implementation of the CAP was in place. Since that inspection, the

licensee performed the additional root cause in CR 2013-08675 and

implemented corrective actions. These corrective actions were reviewed by the

NRC and it was determined that they adequately addressed the main

deficiencies noted during the previous inspection.

Based on the extensive NRC inspection efforts to assess the licensees actions

addressing improvements to the CAP that determined adequate actions have

been taken by the licensee and future actions will continue to be implemented

and effectiveness monitored, Restart Checklist basis Document Item 3.a.12,

Perform NRC Team Problem Identification and Resolution inspection, is

complete.

e) Overall Assessment

The inspectors determined that the corrective actions to address the root and

contributing causes addressing the CAP deficiencies appeared comprehensive

and were resulting in performance improvements. Additionally, the licensee has

implemented measurement processes to monitor the effectiveness of

improvements so that corrections can be implemented when needed. The

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station has in place CAP improvements initiatives contained in the PIIM that will

drive continued improvements to the program.

ii. Resolution of Open Items Related to the Correction Action Program Area in the

Restart Checklist Basis Document

a) (Discussed) VIO 05000285/2011006-02, Inadequate Corrective Actions to Ensure

Reliability of Raw Water Pump Power

This violation inovled the failure to take effective corrective action following the initial

discovery of water intrusion in cable vault manholes MH-5 and MH-31 in 1998,

2005, 2009, and 2011. Specifically, the licensee failed to take effective corrective

action to establish an appropriate monitoring frequency which took into account

variable environmental conditions to mitigate potential common mode failure of raw

water 4160 V motor cables in underground ducts and manholes identified during the

Component Design Basis Inspection performed in 2009.

This item was inspected as part of the 2013 License Renewal inspection and was

documented in Inspection Report 05000285/2013009. That team determined that

the licensee initiated Condition Report 2013-11857 for the condition. The team

concluded that, although the licensee had installed an alarm system to identify a high

water level, the licensee had insufficient time to demonstrate reliability and

effectiveness of the system.

This violation remains open pending future inspection of completed corrective

actions. The inspectors determined the corrective actions appeared adequate and

closed this item on the Restart Checklist Basis Document.

b) NCV 05000285/2011006-06, Failure to Implement an Adequate Trending Program

This item was identified as a Green non-cited violation as part of the 2011 Problem

Identification and Resolution Team Inspection and documented in NRC Inspection

Report 05000285/2011006. That team identified a deficiency regarding the

licensees inability to implement adequate procedures for gathering, analyzing, and

communicating information related to low-level performance vulnerabilities and

repeat occurrences prior to the emergence of more significant events. Inspectors

originally reviewed licensee actions as part of the team inspection documented in

Inspection Report 05000285/2013008 from which they concluded the licensee still

had performance gaps in effective trending to resolve issues at lower levels,

especially equipment trending. The inspectors noted that the licensee took action to

address this condition as part of Condition Report CR 2013-08675 in April 2013. The

root cause found that trending was not effective due to the lack of configuration of

the CAP software to provide the functionality to efficiently and accurately code and

trend condition reports. The inspectors reviewed the licensees actions which

included software changes to the CAP software to establish a tiered coding structure

and utilize the existing Exelon fleet model for trending codes. The inspectors

reviewed recent examples of trends and noted improvement in trending within the

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CAP. From this, the inspectors considered that the licensee had adequately

addressed this noncited violation and this Restart Checklist Basis Document item is

closed.

c) NCV 05000285/2010003-01, Failure to Provide Adequate Limiting Condition for

Operation for High River Level

This NCV documented a failure to include an adequate limiting condition for

operation in the technical specification. Specifically, the reactor could not be placed

in a cold shutdown condition using normal operating procedures when the river level

exceeded 1009 feet mean sea level, as required by Technical Specification 2.16.

The inspectors confirmed that licensee entered this condition into their corrective

action program. The inspectors noted that the licensee had changed procedure

AOP-01, Acts of Nature, to administratively shutdown the reactor and place it in

cold shutdown at a time where plant and flood conditions permitted. The inspectors

also confirmed that the licensee submitted a license amendment request to change

Technical Specification 2.16, River Level to require plant shutdown at 1004 feet

mean sea level. The inspectors reviewed this level relative to the actions and time

needed to place the plant in cold shutdown and considered them adequate. On

January 28, 2014, the NRC issued Amendment No. 274 to OPPD approving the

changes to Techncial Specification 2.16, River Level, (ADAMS ML 14003A003).

This NCV is closed on the Restart Checklist Basis Document.

d) (Closed) Licensee Event Report 05000285/2012-007, Failure of Pressurizer Heater

Sheath

This LER documented a condition where a pressurizer heater sheath

(Number 26 heater) was found cracked after it had failed. This condition was

considered a degradation of the reactor coolant system boundary. The licensee

conducted a root cause for the condition and concluded that fabrication of the heater

sheath during the manufacturing process induced high tensile residual stresses on

the outer surface of the sheaths which led to the failure. The inspectors reviewed

this causal analysis and the corrective actions associated with it. The inspectors

observed that the heater sheath has been removed and replaced, and that other

heater sheaths have been inspected and none of them had indications of cracking.

The inspectors also concluded that the heater design, which included a secondary

seal (not the RCS pressure boundary) prevented any leakage from the reactor

coolant system, and functioned as anticipated for such a condition. The inspectors

also confirmed that future inspections of heaters were included as corrective actions

for this condition. This LER and Restart Checklist Basis Document item is closed.

e) (Closed) Licensee Event Report 05000285/2012-004, Inadequate Analysis of Drift

Affects Safety Related Equipment

This LER documented a condition where Static "0" Ring pressure switches with

certain housing styles exhibit a setpoint shift when exposed to a change in

temperature if the switch body is not vented. These pressure switches that provide

- 37 -

signals for high containment pressure to the reactor protection system and

engineered safeguards actuation circuitry had this configuration. The inspectors

determined that from a review of an evaluation of actual data that safety analysis

limits were not exceeded. The inspectors also examined the instruments and

confirmed that as corrective action the licensee had removed the vent plugs. Also,

the inspectors confirmed that the causal factor of inadequate vendor documentation

was addressed by the licensee. This LER and Restart Checklist Basis Document

item is closed.

f) (Closed) Licensee Event Report 05000285/2012-010, Seismic Qualification of

Instrument Racks

This LER documented an incident where safety-related reactor coolant system

pressure instruments were installed in non-seismically qualified instrument racks.

The licensee performed an analysis and demonstrated that the instrument racks

were designed to withstand the loads from a seismic event, and retracted the event

report. The enforcement aspects of this finding are discussed in Section 4OA7. This

LER and Restart Checklist Basis Document item is closed.

.5 Assessment of NRC Inspection Procedure 95003 Key Attributes

Section 5 of the Restart Checklist is provided to assess the key attributes of NRC Inspection

Procedure 95003. Performing Inspection Procedure 95003 will provide the NRC with

supplemental information regarding licensee performance, as necessary to determine the

breadth and depth of safety, organizational, and programmatic issues. While the procedure

does allow for focus to be applied to areas where performance issues have been previously

identified, the procedure does require that some sample reviews be performed for all key

attributes of the affected strategic performance areas. The key attributes are listed as separate

subsections below. It is intended that the activities in these subsections be conducted in

conjunction with reviews and inspections for Sections 1 - 4, rather than a stand-alone review.

.c Procedure Quality

Item 5.c is included in the restart checklist because the licensee performed an integrated

assessment and identified 15 Fundamental Performance Deficiencies (FPD) that

resulted in the overall performance decline at the station. One of the deficiencies

identified was Procedure Quality/Procedure Management. This FPD was entered into

the licensees corrective action program as CR 2012-08136.

The NRC assessed the thoroughness of the licensees Procedure Quality/Procedure

Management evaluation, adequacy of extent of condition and extent of causal analysis,

and adequacy of associated corrective actions.

a. Inspection Scope

During April 2013, a two-week NRC onsite inspection was conducted to review the

thoroughness of the licensees Procedure Quality/Procedure Management evaluation.

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The inspectors conducted a review of the status of operations department procedures,

including Emergency Operating Procedures (EOPs), Abnormal Operating Procedures

(AOPs), Operating Procedures (OPs), Alarm Response Procedures (ARPs) and

Operating Instructions (OIs).

In addition, the inspectors also reviewed several internal and external

assessments conducted for Operations Department procedures, condition

reports, root cause analyses and apparent cause analyses. These reviews were

conducted to provide the inspection team an insight into the current quality of

operations procedures as well as the anticipated quality of procedures required

to support restart of the unit.

The observations and findings of this inspection were documented in NRC

IMC 0350 Inspection Report 05000285/2013010, dated July 11, 2013. Overall,

the inspection team concluded that the status of procedures used by Operations

was not of sufficient quality to support closure of this area.

The scope of this inspection was to 1) evaluate known deficiencies in Operations

procedures and verify the licensee implemented adequate corrective actions

commensurate with their importance to safety, and 2) assess the adequacy of

licensee actions to be taken prior to restart to gain assurance that Operations

procedures are adequate.

This inspection reviewed the following Restart Checklist Basis Document items:

5.c.1 - Licensee Assessment of the Fundamental Performance Defiency

of Procedure Quality/Procedure Management,

5.c.2 - Adequacy of extent-of-condition and extent of cause, and

5.c.3 - Adequacy of corrective actions.

b. Observations and Findings

Following the inspection in April 2013, the licensee initiated and completed a

Procedure Recovery project (CR 2013-08856) to address procedure quality

concerns. This project included almost 300 procedures, identified by six Priority

definitions:

Priority 1: procedures included all safety related ARPs, EOPs and AOPs that

branch to OIs, OIs associated with the EOP/AOP set, and procedures with

prior NRC concerns.

Priority 2: procedures included EOPs and AOPs without present OI

branching, and AOPs associated with safety systems.

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Priority 3: procedures included OIs associated with safety related systems

Priority 4: procedures included AOPs and OIs associated with only non-safety

related systems.

Priority 5: procedures included OIs associated with systems that will neither

be used nor conditions encountered before completion of the review process.

Priority 6: procedures included OIs designated as non-safety related.

The process used to conduct the recovery project included the following

elements:

Verification - process of ensuring procedures are technically correct,

operational correctness, and procedures accurately adhere to guidance in the

procedure writers guide, including human factors.

Validation - process of confirming procedures are compatible with expected

operator responses and plant equipment. Validation methods included walk-

through, table-top, simulator, and reference.

To assess the adequacy of the Procedure Recovery project in meeting the

inspection requirements, a sample of each procedure type was selected and

reviewed. The review consisted of the procedure revision in use prior to the

upgrade project, the electronic change package (including requisite forms,

markups, reviews, comments, etc.) and the new procedure revision issued.

In addition, condition reports, root and apparent cause analyses, external and

internal procedure assessments, and procedure related training documentation

were reviewed.

c. Assessment Results

The inspector concluded that the licensee adequately scoped the set of

Operations procedures to be reviewed and upgraded prior to plant restart. The

licensee adequately evaluated and corrected known procedure deficiencies as

well as identified and corrected a substantial number of deficiencies identified

during implementation of the Procedure Recovery project. Based on the results

of the NRC reviews it was determined that the licensees Procedure Recovery

Project effectively improved Operations procedures to support a safe plant

restart. Restart Checklist Basis Document items 5.c.1, 5.c.2 and 5.c.3 are

closed.

(1) Restart Checklist Basis Document Items 5.c - NCV 2012301-01, 04 and 06

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a. Inspection Scope

The inspectors reviewed the adequacy of licensees actions in resolving the

following non-cited violations that were specific items in the Restart Checklist

Basis Document:

NCV 2012301-01, Seven Examples of Inadequate Procedures for the

Mitigating Systems Cornerstone,

NCV 2012301-04, Five Examples of Inadequate Procedures for the

Initiating Events Cornerstone, and

NCV 2012301-06, Inadequate Procedures with Four Examples for the

Barrier Integrity Cornerstone.

During April 2013, a two-week onsite inspection was conducted to review the

three NCVs as part of the overall assessment of the procedural quality attribute.

The inspectors reviewed condition reports associated with these violations and

procedural changes incorporated as a result of these violations. The assessment

documented that Condition Report 2012-03140 was written to encompass all of

the examples of procedural deficiencies in the alarm response procedures that

were identified in non-cited violations NCV 2012301-01, NCV 012301-04, and

NCV 2012301-06. However, a revised apparent cause analysis was in progress

and therefore could not be inspected. Although the specific procedural

deficiencies documented in the three non-cited violations had been corrected, it

was decided these checklist items would remain open pending a future

inspection of the revised apparent cause analysis and any associated corrective

actions. Inspection results were documented in NRC IMC 0350 Inspection

Report 05000285/2013010, dated July 11, 2013.

The scope of this follow-up inspection is a review of the revised apparent cause

analysis for CR 2012-03140 and associated corrective actions.

b. Observations and Findings

Apparent Cause Analysis Report, Annunciator Response Procedure (ARP)

Quality Issues, Revision 1, was approved May 1, 2013. The revised Apparent

Cause Analyis concluded that there was a flaw in the original analysis. As a

result, the Apparent Cause Analysis identified apparent cause was changed; the

Extent of Condition was revised to bring this section into compliance with

FCSG 24-4, Condition Report and Cause Analysis, and FCSG-24-5, Cause

Evaluation Manual; and corrective actions were updated and revised based on

the completed actions and revised analysis.

Extent of Cause analysis and corrective actions resulted in improved verification

and validation processes through changes to procedures SO-G-30, Procedure

Change and Generation, and SO-G-74, EOP/AOP Procedure Generation

- 41 -

Program. Extent of Condition analysis identified some operating procedures

(EOPs, AOPs, Operating Instructions, Operating Procedures and Annunciaor

Response Procedure) were technically inaccurate, lacked clarity, and deviated

from the owner's group guidelines. Corrective actions included a Procedure

Recovery Project that included a review and validation of procedure technical

accuracy and clarity for all operating documents.

c. Assessment Results

The inspector concluded that the licensee adequately addressed the Apparent

Cause and Contributing Causes, Extent of Condition and Extent of Cause

through the revision of the Apparent Cause Analysis for CR 2012-03140.

Therefore, Restart Checklist Items 5.c - NCV 2012301-01, 04, and 06 are

closed.

(2) Restart Checklist Basis Document Item 5.c - NCV 2011002-01, Inadequate

Operating Instruction Results in a Loss of Auxiliary Feedwater

a. Inspection Scope

During April 2013, a two-week onsite inspection was conducted to review this

NCV as part of the overall assessment of the procedural quality attribute. The

inspectors reviewed Condition Report 2011-0839 and the associated Root Cause

Analysis. The inspectors documented one concern from this review associated

with Contributing Cause 8.2 (insufficient criteria to ensure periodic V&V

(verification and validation) of infrequently used procedures or procedure

sections) that did not have an associated corrective action. The licensee

documented this issue in Condition Report 2013-08677. It was decided this

checklist item would remain open until a corrective action for Contributing

Cause 8.2 was developed and implemented.

The scope of this follow-up inspection is a review of the corrective action for

Contributing Cause 8.2.

b. Observations and Findings

CR 2013-08677 was reviewed. Action Item 3, "Establish and implement criteria

to ensure periodic V&V of infrequently used procedures and procedure sections

is performed" was completed and approved by the station on July 18, 2013.

c. Assessment Results

The inspector reviewed the criteria and its implementation and concluded that the

licensee adequately addressed the corrective action for Contributing Cause 8.2

of CR 2011-0839. Therefore, Restart Checklist Item 5.c - NCV 2011002-01 is

closed.

- 42 -

(3) Restart Checklist Basis Document items 5.c - NCV 2010004-10, Inadequate

Maintenance Procedure Results in a Plant Shutdown

a. Inspection Scope

During April 2013, a two-week onsite inspection was conducted to review this

NCV as part of the overall assessment of the procedural quality attribute. The

inspectors reviewed LER 2010-002, Failed Feeder Cable Due to Inadequate

Procedure Causes Station Shutdown, and associated documents (condition

reports, causal analyses, procedures) to verify the licensee had performed

adequate casual analyses and extent of condition/extent of cause evaluations

related to this issue. In addition, the inspectors verified adequate corrective

actions were identified for the associated causes and extent of condition/extent of

cause evaluations and that implementation of these corrective actions were

either implemented or appropriately scheduled for implementation.

b. Observations and Findings

LER 2010-002 and CR 2010-1704 (including causal analysis and extent of

condition/extent of cause) were reviewed. Changes to procedure EM-PM-EX-

1100, 480 Volt Motor Control Center Maintenance, were reviewed and found to

adequately address the deficiencies.

c. Assessment Results

The inspector concluded that the licensee adequately identified Root and

Contributing Causes, and adequately addressed corrective actions to preclude

recurrence. Therefore, Restart Checklist Item 5.c - NCV 2010004-10 will be

closed.

.d Equipment Performance

a. Inspection Scope

The NRC issued NCV 2010004-09 for the failure of the licensee to perform vendor and

industry recommended testing on safety-related and risk significant 4160V and 480V

circuit breakers. The purpose of this review was to verify the licensee performed an

adequate cause analysis and established appropriate corrective actions to address the

issues.

b. Observations and findings

The inspectors reviewed the documentation of the licensees efforts. The licensees

cause analysis determined the causes of the issue were the lack of detail in the

Reliability Centered Maintenance (RCM) basis documentation for prescribing adequate

circuit breaker maintenance, failure to incorporate all sources of maintenance

recommendations, and insufficient coordination and ownership by separate engineering

- 43 -

groups to adequately trend breaker performance and identify all required maintenance

activities. The licensee corrective actions included completion of a gap analysis to

identify vendor and industry recommended breaker maintenance and deficiencies in the

FCS program. The licensee developed a detailed preventive maintenance basis

document for switchgear and breaker maintenance based on the results of the gap

analysis. The licensee revised applicable maintenance procedures to capture the new

maintenance requirements and also revised procedures for trending and monitoring

breaker performance, to include a system engineer review. The inspectors concluded

the cause analysis and corrective actions appear adequate to minimize recurrence of the

issue.

c. Assessment Results

This activity constitutes closure of NCV 2010004-09 as listed in the Restart Checklist

Basis Document.

.e Configuration Control

Review of LER 2012-008, Technical Specification Violation for Fuel Movement (VA-66)

a. Inspection Scope

The inspectors reviewed the licensee actions associated with LER 2012-008, Technical

Specification Violation for Fuel Movement (VA-66), that included associated documents

(condition reports, causal analyses, procedures) to verify the licensee had performed

adequate casual analyses and extent of condition/extent of cause evaluations related to

this issue. In addition, to verify adequate corrective actions were identified associated

with the causes and extent of condition/extent of cause evaluations and that

implementation of these corrective actions were either implemented or appropriately

scheduled for implementation.

b. Observations and Findings

A review of LER 2012-008, Condition Report 2011-07800 and Apparent Cause Analysis

Summary Report, Spent Fuel Storage Pool Area Charcoal Filter V A-66 Elemental

Iodine Removal Efficiency Test Failure, Revision 1 was conducted.

The Apparent Cause identified was lack of Management Oversight and failure of

Engineering to take a pro-active approach in the prevention of future test failures. Action

Items (AI) included:

1. Revision of procedure SE-ST-VA-0010, Spent Fuel Storage Pool Area

Charcoal Filter VA-66 Elemental Iodine Removal Efficiency Test to trend

charcoal sample results and predict replacement,

2. Replacement of the depleted charcoal currently installed, and

3. Change the frequency of the charcoal testing from eighteen months to 1 year.

- 44 -

Action Items 1 and 2 have been completed. Action Item 3 is scheduled to be completed

under EC 57850. The Apparent Cause Analysis Summary Report documented that the

Extent of Condition will be addressed under Condition Report 2011-7798.

c. Assessment Results

The inspector concluded that the licensee adequately assessed and developed

corrective actions to address the apparent cause of the performance deficiency

associated with this Licensee Event Report. Therefore, Restart Checklist Basis

Document Item 5.e (LER 2012-008) will be closed. However, LER 2012-008 will remain

OPEN until Action Item 3 is verified complete by inspection.

Review of LER 2012-012, Multiple Safety Injection Tanks Rendered Inoperable

a. Inspection Scope

The inspectors reviewed the licensees actions associated with LER 2012-012 that

included documents (condition reports, causal analyses, procedures) to verify the

licensee had performed adequate casual analyses and extent of condition/extent of

cause evaluations related to this issue. In addition, the inspectors verified that adequate

corrective actions were identified associated with the causes and extent of

condition/extent of cause evaluations and that implementation of these corrective actions

were either implemented or appropriately scheduled for implementation.

b. Observations and Findings

A review of LER 2012-012, Condition Reports 2012-01956, 2012-03140, 2012-04815

and 2013-09711, and Apparent Cause Analysis Report, Lack of Extent of Condition and

Extent of Cause Action for NRC Non-cited Violation, Revision 0 was conducted.

The Apparent Cause Analysis (ACA) from CR 2013-09711 identified the original

Apparent Cause Analysis for CR 2012-03140 (deficiencies in several ARPs found during

NRC Initial Licensed Operator exam - conducted in August 2012) was inaccurate in that

the ACA faulted the writers guide rather than an incorrect ARP validation process. The

ACA from CR 2013-09711 also documented the following causes and extent of

conditions:

Apparent Cause #1 (AC-1) - Operations Department corrective action program

prioritization valued correcting the specified condition to a much greater degree

than investigating the extent of condition and ensuring corrective action in a

timeframe commensurate with the risk of the problem recurring or extending to

other procedures.

Contributing Cause #1 (CC-1) - The original Apparent Cause Analysis for

CR 2012-03140 was inaccurate in that the Apparent Cause Analysis faulted the

writers guide rather than an incorrect ARP validation process.

- 45 -

An Extent of Condition exists with all ARPs.

An Extent of Cause exists with most EOPs, AOPs, and Operating Instructions.

The findings in the Apparent Cause Analysis contributed to the decision to conduct a

procedure upgrade project that included the Alarm Response Procedures identified

affected by LER 2012-012.

The Alarm Response Procedure (ARP-CB-4/A7, Annunciator Response Procedure A7

Control Room Annunciator A7) and Operating Instruction (OI-SI-1, Safety Injection -

Normal Operation) that were associated with sluicing of Safety Injection Tanks were

reviewed and compared with the revision prior to the changes identified by the upgrade

project.

c. Assessment Results

The inspector concluded that the licensee adequately assessed and developed

corrective actions to address the apparent cause of the performance deficiency

associated with this Licensee Event Report. Therefore, Restart Checklist Basis

Document Item 5.e (LER 2012-012) is closed.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On December 5, 2013, the inspectors presented the results of the onsite inspection of the

licensees biennial emergency preparedness exercise to Mr. L. Cortopassi, Site Vice President,

and other members of the licensees staff. The licensee acknowledged the issues presented.

The inspectors asked the licensee whether any materials examined during the inspection should

be considered proprietary. No proprietary information was identified.

The lead inspector obtained the final annual examination results and telephonically exited with

Mr. R. Cade, Manager, Operations Training, on December 30, 2013. The inspector did not

review any proprietary information during this inspection.

On January 24, 2014, the inspectors presented the inspection results to Mr. L. Cortopassi, Site

Vice President, and other members of the licensee staff. The licensee acknowledged the issues

presented. The licensee confirmed that any proprietary information reviewed by the inspectors

had been returned or destroyed.

4OA7 Licensee-Identified Violations

The following violation of very low safety significance (Green) was identified by the licensee and

is a violation of NRC requirements which meets the criteria of the NRC Enforcement Policy for

being dispositioned as a non-cited violation.

- 46 -

Title 10 CFR 50, Appendix B, Criterion III, Design Control, requires that measures shall be

established to assure that the design basis for those structures, systems, and components

to which this appendix applies are correctly translated into specifications, drawings,

procedures, and instructions. Contrary to this requirement, the licensee failed to assure that

the design basis for safety related instrument racks inside containment were correctly

translated into specifications, drawings, procedures, and instructions. The licensee initially

identified and documented this violation in CR 2012-03100 and CR 2013-10935. This

violation was of very low safety significance because it did not result in the loss of operability

or functionality of any system or train.

- 47 -

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

D. Bakalar, Manager, Security

J. Bousum, Manager, Emergency Planning and Administration

C. Cameron, Supervisor Regulatory Compliance

L. Cortopassi, Site Vice President

K. Ihnen, Manager, Site Nuclear Oversight

T. Leeper, Manager, Human Resource Services

T. Lindsey, Director, Training

E. Matzke, Senior Licensing Engineer, Regulatory Assurance

B. Obermeyer, Manager, Corrective Action Program

T. Orth, Director, Site Work Management

E. Plautz, Supervisor, Emergency Planning

R. Short, Assistant Director, Engineering

T. Simpkin, Manager, Site Regulatory Assurance

S. Swanson, Manager, Operations

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

Containment Valve Actuators Design Temperature Ratings

05000285-2012-017-02 LER Below those Required for Design Basis Accidents (Section

4OA3)

Mounting of GE HFA Relays does not Meet Seismic

05000285-2013-001-01 LER

Requirements (Section 4OA3)

Calculations Indicate the HPSI Pumps will Operate in Run-

05000285-2013-003-01 LER

out During a DBA (Section 4OA3)

Previously Installed GE IVA Relays Failed Seismic Testing

05000285-2013-008-01 LER

(Section 4OA3)

Unqualified Components used in Safety System Control

05000285-2013-014-00 LER

Circuit (Section 4OA3)

Containment Spray Pump Design Documents do not Support

05000285-2013-017-00 LER

Operation in Runout (Section 4OA3)

Postulated Fire Event Could Result in Shorts Impacting Safe

05000285-2013-018-00 LER

Shutdown (Section 4OA3)

A-1 Attachment

Opened and Closed

Failure to Correct Deficiencies in Operations Support Center

05000285/2013019-01 NCV

Functions (Section 1EP1)

Discussed

05000285/2011006-02 VIO Inadequate Corrective Actions to Ensure Reliability of Raw

Water Pump Power

Closed

Inadequate Flooding Protection Due to Ineffective Oversight

05000285-2011-003-03 LER

(Section 4OA4)

05000285-2012-001-00 LER Inadequate Flooding Protection Procedure (Section 4OA4)

Inadequate Analysis of Drift Affects Safety Related

05000285-2012-004-02 LER

Equipment (Section 4OA4)

05000285-2012-007-01 LER Failure of Pressurizer Heater Sheath (Section 4OA4)

Technical Specification Violation for Fuel Movement (VA-66)

05000285-2012-008-01 LER

(Section 4OA4)

05000285-2012-010-00 LER Seismic Qualification of Instrument Racks (Section 4OA4)

Multiple Safety Injection Tanks Rendered Inoperable (Section

05000285-2012-012-01 LER

4OA4)

Containment Valve Actuators Design Temperature Ratings

05000285-2012-017-01 LER Below those Required for Design Basis Accidents (Section

4OA3)

Traveling Screen Sluice Gates Found with Dual Indication

05000285-2012-019-00 LER

(Section 4OA4)

Mounting of GE HFA Relays does not Meet Seismic

05000285-2013-001-00 LER

Requirements (Section 4OA3)

Calculations Indicate the HPSI Pumps will Operate in Run-

05000285-2013-003-00 LER

out During a DBA (Section 4OA3)

Previously Installed GE IVA Relays Failed Seismic Testing

05000285-2013-008-00 LER

(Section 4OA3)

Failure to Maintain External Flood Procedures (Section

05000285/2010007-01 VIO

4OA4)

Inadequate Procedures to Mitigate a Design Basis Flood

05000285/2012002-01 VIO

Event (Section 4OA4)

Failure to Classify Intake Structure Sluice Gates as Safety

05000285/2012002-02 VIO

Class III (Section 4OA4)

A-2

Closed

Failure to Meet Design Basis Requirements for Design Basis05000285/2012002-03 VIO

Flood Event (Section 4OA4)

Failure to Correct a Degraded Contactor in the Reactor

05000285/2011007-01 VIO

Protective System (Section 4OA4)

LIST OF DOCUMENTS REVIEWED

Section 1R11: Licensed Operator Requalification Program and Licensed Operator

Performance

Condition Reports (CRs)

2013-23048

Miscellaneous Documents

Number Title Revision

TQ-AA-150-F25 LORT Annual Exam Status Report 5

Section 1R18: Plant Modifications

Procedures

Number Title Revision

OP-ST-AFW-3010 Auxiliary Feedwater System Quarterly Category A and B 9

Valve Exercise Test

Work Orders (WO)

503315

Section 1R22: Surveillance Testing

Procedures

Number Title Revision

OP-ST-ESF-0001 Diesel Auto Start Initiating Circuit Check 42

Work Orders (WO)

360607

A-3

Section 1EP1: Exercise Evaluation

Procedures

Number Title Revision

TBD-EPIP-OSC- Technical Basis Document for the Emergency Action Levels, 2A

1A November 21, 2013

EPIP-EOF-1 Activation of the Emergency Operations Facility, June 6, 2013 19

EPIP-EOF-6 Dose Assessment, September 20, 2013 47

EPIP-EOF-7 Protective Action Guidelines, March 16, 2012 25

EPIP-EOF-11 Dosimetry Records, Exposure Extensions, and Habitability, April 29

2, 2013

EPIP-EOF-21 Potassium Iodide Issuance, June 25, 2009 9

EPIP-OSC-2 Command and Control Position, Actions/Notifications, June 26, 57

2012

EPIP-OSC-7 Emergency Response Organization Activation at the Emergency 4

Operations Facility, March 26, 2013

EPIP-OSC-9 Emergency Team Briefings, September 13, 2012 15

EPIP-OSC-15 Communicator Actions, July 19, 2013 30

EPIP-OSC-21 Activation of the Operations Support Center, May 5, 2011 20

EPIP-RR-11 Technical Support Center Director Actions, November 8, 2008 3

EPIP-TSC-1 Activation of the Technical Support Center, May 5, 2011 32

EPIP-TSC-8 Core Damage Assessment, September 29, 2011 20

EPT-20 Exercise Preparation and Control, November 20, 2012 36

EPT-48 Change Out of Protective Clothing in Emergency Facilities, 3

February 18, 2009

Evaluation Report for the June 6, 2011, Alert Classification

Evaluation Report for the Exercise conducted February 27, 2012

Evaluation Report for the Exercise conducted March 27, 2012

Evaluation Report for the Exercise conducted May 22, 2012

Evaluation Report for the Exercise conducted July 17, 2012

Evaluation Report for the Exercise conducted November 10,

2012

Evaluation Report for the Exercise conducted March 5, 2013

Evaluation Report for the Exercise conducted May 7, 2013

A-4

Section 1EP1: Exercise Evaluation

Procedures

Number Title Revision

Evaluation Report for the Exercise conducted June 18, 2013

Condition Reports (CR)

2012-02381 2012-07779 2013-05146 2013-05263 2013-05363

2013-10486 2013-22153 2013-22169 2013-22172 2013-22177

2013-22181 2013-22193 2013-22194 2013-22201 2013-22206

2013-22209 2013-22220 2013-22226 2013-22247 2013-22252

2013-22253 2013-22261 2013-22262 2013-22264 2013-22265

2013-22269 2013-22270 2013-22271 2013-22288 2013-22491

2013-22492 2013-22495 2013-22498

Miscellaneous Documents

Number Title

Fort Calhoun Station Radiological Emergency Response Plan

(revision by section)

Section 4OA2: Problem Identification and Resolution (71152)

Procedures

Number Title Revision

FCSG-24-1 Condition Report Initiation 5

FCSG-24-3 Condition Report Screening 7

FCSG-24-4 Condition Report and Cause Evaluation 7

FCSG-24-6 Corrective Action Implementation and Condition Report 10

Closure

SO-R-2 Condition Reporting and Corrective Action 53b

Section 4OA4: IMC 0350 Inspection Activities

Condition Reports (CR)

2010-05140 2013-03024 2013-00620 2013-11203 2013-11736

2013-02041 2009-02306 2012-17533 2009-02306 2013-03024

A-5

2012-05854 2012-05855 2013-08856 2013-09711 2012-08136

2010-1704 2010-2387 2011-0839 2012-03140 2013-08677

2011-07800 2011-07798 2012-01956 2012-03140 2012-04815

2013-08856 2013-09711 2013-10935 2012-04914 3023-03100

2012-00307 2012-00600 2012-00871 2012-00875 2012-00882

2012-00882 2012-00899 2012-00901 2012-00906 2012-00929

2012-00945 2012-00949 2012-00965 2012-00967 2012-00980

2012-00986 2012-00996 2012-00998 2012-01000 2012-01003

2012-01010 2012-01012 2012-01021 2012-01330 2012-02142

Work Orders (WO)

00484596

Procedures

Number Title Revision

FCSG-24-1 Condition Report Initiation 3

AOP-01 ACTS OF NATURE 37, 38

AOP-05 EMERGENCY SHUTDOWN 11, 12

AOP-17 LOSS OF INSTRUMENT AIR 14, 15

AOP-18 LOSS OF RAW WATER 7a, 8

ARP-AI-66A/A66A ANNUNCIATOR RESPONSE PROCEDURE A66A 15, 16

CONTROL ROOM ANNUNCIATOR A66A,

AFWAS/DSS

ARP-CB-1,2,3/A1 ANNUNCIATOR RESPONSE PROCEDURE A1 36, 37

CONTROL ROOM ANNUNCIATOR A1

ARP-CB-4/A20 ANNUNCIATOR RESPONSE PROCEDURE A20 45, 46

CONTROL ROOM ANNUNCIATOR A20

ARP-CB-4/A7 ANNUNCIATOR RESPONSE PROCEDURE A7 17, 18

CONTROL ROOM ANNUNCIATOR A7

EM-PM-EX-1100 480 Volt Motor Control Center Maintenance 23, 37

EOP/AOP EOP/AOP ATTACHMENTS 34

ATTACHMENTS

A-6

Procedures

Number Title Revision

EOP/AOP HEAT REMOVAL 0

ATTACHMENTS-HR

EOP/AOP MAINTENANCE OF VITAL AUXILIARIES 0

ATTACHMENTS-MVA

EOP/AOP FLOATING EOP/AOP FLOATING STEPS 3c, 4

STEPS

EOP-00 STANDARD POST TRIP ACTIONS 29, 30

EOP-03 LOSS OF COOLANT ACCIDENT 36, 37

EOP-20 FUNCTIONAL RECOVERY PROCEDURE 25a, 26

EPIP-TSC-2 Catastrophic Flooding Preparations 14

FCSG-20 Abnormal Operating Procedure and Emergency 9

Operating Procedure Writers Guide

FCSG-24-3 Condition Report Screening 6a

FCSG-24-4 Condition Report and Cause Evaluation 6a

FCSG-24-4 Condition Report and Cause Evaluation 5

FCSG-24-5 Cause Evaluation Manual 5, 6

FCSG-64 External Flooding of Site 1

M8145WD Flood Control Walk-down Exercise

NOD-QP-19 Cause Analysis Program 4

OI-AFW-4 AUXILIARY FEEDWATER STARTUP AND SYSTEM 87, 88

OPERATION

OI-CW-1 Circulating Water System Normal Operation 65 and 66

OI-RC-9 REACTOR COOLANT PUMP OPERATION 75, 76

OI-SI-1 SAFETY INJECTION - NORMAL OPERATION 136, 137

OP-1 MASTER CHECKLIST FOR PLANT STARTUP 111

OP-2A PLANT STARTUP 114

OPD-4-09 EOP/AOP Users Guidelines 12, 19

A-7

Procedures

Number Title Revision

OP-ST-SI-3001 SAFETY INJECTION SYSTEM CATEGORY A AND B 35a, 36

VALVE EXERCISE TEST

OP-ST-VX-3018 SAFETY INJECTION SYSTEM REMOTE POSITION 10, 11

INDICATOR VERIFICATION

SURVEILLANCE TEST

QC-ST-SI-3006 SAFETY INJECTION LEAKOFF PIPING FORTY 5, 6

MONTH FUNCTIONAL TEST

SE-ST-VA-0010 SPENT FUEL STORAGE POOL AREA CHARCOAL 6, 7

FILTER

VA-66 ELEMENTAL IODINE REMOVAL EFFICIENCY

TEST

SO-G-30 Procedure Changes and Generation 136

SO-G-74 Fort Calhoun Station EOP/AOP Generation Program 20

SO-O-1 CONDUCT OF OPERATIONS 84, 101

TBD-AOP-01 ACTS OF NATURE 37, 38

TBD-AOP-05 EMERGENCY SHUTDOWN 11, 12

TBD-AOP-17 LOSS OF INSTRUMENT AIR 14, 15

TBD-EOP/AOP TBD-EOP/AOP ATTACHMENTS 34

ATTACHMENTS

TBD-EOP/AOP TBD-EOP/AOP FLOATING STEPS 4

FLOATING STEPS

TBD-EOP-00 STANDARD POST TRIP ACTIONS 30

TBD-EOP-06 LOSS OF ALL FEEDWATER 17b, 18

TBD-EOP-20 FUNCTIONAL RECOVERY PROCEDURE 25a, 26

Calculations

Number Title Revision/Date

CN-OA-11-7 Intake Cell Level Control Using the Intake Sluice Gate April 21, 2011

During Flooding Conditions at the Ft. Calhoun Plant

CN-SEE-II-11-2 Intake Cell Level Control - Flood Alternate Flow Path April 5, 2011

Evaluation for Fort Calhoun Station

FC08030 Intake Structure Cell Level Control Using the Intake April 25, 2011

Structure Sluice Gates

A-8

FC08070 Validation of Backup Fuel Oil Transfer During Flooding

Conditions

FC08142 Seismic Evaluation of Instrument Racks 12

FC08174 Seismic Analysis of Rack AI-135C 13

FC05153 CQE Instrument Rack Analysis 02

EA93-084 Criteria For Anchors Installed In Concrete Toppings 0

Engineering Change (EC)

Number Title Revision

60326 Procedure Upgrade 0

57850 SE-ST-VA-0010 Procedure Change 0

58676 Containment 994' Elev. Instrument Rack Bolt 1

Replacement

FDCR 61877 Replace additional anchors securing instrument racks 8

on the 994' elevation

Miscellaneous Documents

Number Title Revision/Date

VERIFICATION PROCESS TO ADDRESS June 13, 2013

PROCEDURE QUALITY CONCERNS

Simulator Scenario Guide 82103e - Cable Spreading 1

Room Fire and Control Room Evacuation

Simulator Scenario Guide 82103f - 480VAC Bus 1B4A 0

Fire

EONT Qualification Manual

LER 2012-008 Technical Specification Violation for Fuel Movement 0, 1

(VA-66)

LER 2012-012 Multiple Safety Injection Tanks Rendered Inoperable 0, 1

FCS-95003-IACPD- IACPD - FCS Performance Goals Assessment

03 Performance Area

FCS-95003-IACPD- IACPD - FCS Audits and Assessments Assessment

08 Performance Area

A-9

Miscellaneous Documents

FCS-95003-IACPD- IACPD - FCS Significant Performance Deficiencies

02 Assessment Performance Area

Corrective Action Program CR 2012-08124

Fundamental Performance Deficiency Analysis

Security Self Assessment Report, August 2012

A-10