ML13333B224

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SALP Repts 50-206/84-32,50-361/84-31 & 50-362/84-32 for June 1983 - Sept 1984
ML13333B224
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 02/07/1985
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML13333B222 List:
References
50-206-84-32, 50-361-84-31, 50-362-84-32, NUDOCS 8502270030
Download: ML13333B224 (59)


See also: IR 05000206/1984032

Text

SALP BOARD REPORT

U.S. NUCLEAR REGULATORY COMMISSION

REGION V

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

CYCLE 5

Report Nos:

50-206/84-32

50-361/84-31

50-362/84-32

SOUTHERN CALIFORNIA EDISON COMPANY

SAN ONOFRE UNITS 1-3

ASSESSMENT PERIOD:

June 1, 1983 -

September 30, 1984

s5D0 2 2 700 3 OeO5002 6

ID A

O

5000

Table of Contents

Page

I.

Introduction

1

II.

Criteria

1

III. Summary of Results

2

IV. Performance Analyses

3

A.

Plant Operations

3

B.

Radiological Controls

7

C.

Maintenance

9

D.

Surveillance

12

E.

Fire Protection

15

F.

Emergency Preparedness

16

G.

Security

17

H.

Refueling

18

I.

Quality Programs and Administrative Controls

18

J.

Licensing Activities

22

K.

Startup Testing

28

V.

Supporting Data and Summaries

28

A.

Licensee Activities

28

B.

Inspection Activities

30

C.

Investigations and Allegations Review

31

D.

Escalated Enforcement Actions

31

E.

Management Conferences Held During Appraisal Period

32

F.

Review of 10 CFR 21 Reports and Licensee Event Reports 32

Tables

Table 1 -

Inspection Activity and Enforcement Summary

37

Table 2 -

Licensee Event Reports, Unit 1

38

Licensee Event Reports, Unit 2

39

Licensee Event Reports, Unit 3

50

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated NRC staff effort to collect available observations and data on

a periodic basis and to evaluate licensee performance based upon this

information. SALP is supplemental to normal regulatory processes used to

ensure compliance to NRC rules and regulations.

SALP is intended to be

sufficiently diagnostic to provide a rational basis for allocating NRC

resources and to provide meaningful guidance to the licensee's management

to promote quality and safety of plant construction and operation.

A NRC SALP Board, composed of the staff members listed below, met on

November 15, 1984, to review the collection of performance observations

and data to assess the licensee's performance in accordance with the

guidance in NRC Manual Chapter 0516, "Systematic Assessment of Licensee

Performance." A summary of the guidance and evaluation criteria is

provided in Section II of this report.

This report is the SALP Board's assessment of the licensee's safety

performance at the San Onofre Nuclear Generating Station (SONGS) for SALP

Cycle 5, covering the period June 1, 1983 through September 30, 1984.

SALP Board for San Onofre, Units 1-3:

D. F. Kirsch, Acting Director, Div. of Reactor Safety and Projects, RV

A. E. Chaffee, Chief, Reactor Projects Branch, RV

P. H. Johnson, Chief, Reactor Projects Section 3, RV

D. P. Haist, Project Inspector, RV

F. R. Huey, Senior Resident Inspector

J. P. Stewart, Resident Inspector, RV (by telephone)

A. J. D'Angelo, Resident Inspector, RV (by telephone)

A. D. McQueen, Physical Security Inspector, RV

G. P. Yuhas, Chief, Facilities Radiological Protection Section

H. S. North, Senior Radiation Specialist, RV

C. I. Sherman, Radiation Specialist

R. F. Fish, Senior Emergency Preparedness Analyst, RV

G. Temple, Emergency Preparedness Inspector

H. Rood, Project Manager SONGS-2/3, NRR

E. M. McKenna, Project Manager SONGS-1, NRR

II. CRITERIA

Licensee performance is assessed in selected functional areas, depending

on whether the facility is in a construction, preoperational, or

operating phase. Each functional area normally represents programmatic

areas significant to nuclear safety and the environment. Some functional

areas may not be assessed because of little or no licensee activities or

lack of meaningful observations.

Special areas may be added to highlight

significant observations.

The following evaluation criteria were used to assess each functional

area, as appropriate.

1.

Management involvement and control in assuring quality

2

2.

Approach to resolution of technical issues from a safety standpoint

3.

Responsiveness to NRC initiatives

4.

Enforcement history

5.

Reporting and analysis of reportable events

6.

Staffing (including management)

7.

Training effectiveness and qualification

The SALP Board, however, is not limited to these criteria and others may

have been used where appropriate.

Based upon the SALP Board assessment each functional area evaluated is

classified into one of three performance categories. The definition of

these performance categories is:

Category 1. Reduced NRC attention may be appropriate. Licensee

management attention and involvement are aggressive and oriented toward

nuclear safety; licensee resources are ample and effectively used so that

a high level of performance with respect to operational safety or

construction is being achieved.

Category 2. NRC attention should be maintained at normal levels.

Licensee management attention and involvement are evident and are

concerned with nuclear safety; licensee resources are adequate and are

reasonably effective so that satisfactory performance with respect to

operational safety or construction is being achieved.

Category 3. Both NRC and licensee attention should be increased.

Licensee management attention or involvement is acceptable and considers

nuclear safety, but weaknesses are evident; licensee resources appear to

be strained or not effectively used so that minimally satisfactory

performance with respect to operational safety or construction is being

achieved.

III. SUMMARY OF RESULTS

Overall the board finds that licensee performance is acceptable and

directed toward safe facility operation.

In addition, the board finds

that the licensee's overall performance has improved since the last SALP

evaluation period.

Individual areas which contributed to this overall

improvement are plant operations, maintenance, radiological controls and

security. The board found aggressive management attention and a high

level of performance in the areas of quality programs and administrative

controls and SONGS-3 startup testing, which were not specifically

addressed in the previous SALP evaluation period. The licensee's

performance rating in the area of plant operations has improved, but

requires continued attention to minimize instances of personnel error

and inadvertent compromises of engineered safety feature availability.

3

Rating

Rating

Trend During

Functional Area

Last Period

This Period

This Period

A. Plant Operations

3

2

Improving

B. Radiological Controls

3

2

Improving

C. Maintenance

2

1

Improving

D. Surveillance

2

2

None Apparent

E. Fire Protection

2

2

None Apparent

F. Emergency Preparedness

1

1

None Apparent

G. Security

2

1

Improving

H. Refueling

1

N/A

N/A

I. Quality Programs and

N/A

1

N/A

Administrative Controls

(includes Unit-I modifications)

J. Licensing Activities

2

2

None Apparent

K. Startup Testing (Unit 3) N/A

1

N/A

IV. PERFORMANCE ANALYSIS

A.

Plant Operations

1.

Analysis

During the current SALP assessment period, 3924 hours0.0454 days <br />1.09 hours <br />0.00649 weeks <br />0.00149 months <br /> of direct

inspection effort were applied in the area of plant operations

at San Onofre Units 1, 2 and 3. These inspection activities

resulted in the issuance of 4 notices of violation and 3 civil

penalties totaling $165,000. The summary assessment of

individual unit operation, overall conclusion as to site

performance category and board recommendations are discussed

below. With regard to the assignment of an overall site

performance category, it should be noted that more emphasis was

placed on Unit 2/3 performance than on Unit 1, which was shut

down during the entire assessment period.

Unit 1 Operations

During this SALP period, Unit 1 has remained in Mode 5 for the

completion of seismic modification activities. No violations

were issued during this period in the area Unit 1 operations.

Management has emphasized the use of prior planning and

assignment of priorities for the control of activities.

Conservatism is routinely exhibited by management at the Onsite

Review Committee meeting in that references are made to the

standard technical specification and any differences which

exist with the San Onofre technical specification.

Licensee responsiveness is usually technically sound and

thorough as exhibited by recent actions such as the addition of

temporary diesel generators onsite during the Transamerica

DeLaval (TDI) diesel generator inspection effort. A total of 3

Licensee Event Reports (LER) were issued during the period

4

applicable to plant operations. All LER's were reported in a

timely manner and adequately described the event.

Staffing for the period was adequate and appeared to be well

controlled. Backlog work activities and overtime by the

operations staff have been infrequent and do not appear to be

degrading their performance. In this regard, no serious

operator errors have occurred.

The training and qualification program appears to be adequate.

It has been noted, however, that a weakness existed in recent

training activities in that some Unit 1 design changes had not

been distributed to the training organization for inclusion in

the training program. This oversight was promptly corrected by

the licensee.

Units 2/3 Operations

Site management has been actively involved in Unit 2/3

operations. They have been aggressive in their pursuit of the

underlying causes of plant problems and have been thorough and

innovative in addressing proper and effective corrective

actions, particularly during the second half of this period.

Plant managers are frequently involved in site activities and

key evolutions. Frequent NRC resident interface with various

levels of plant supervision and management have demonstrated

generally a clear understanding of technical issues involving

plant safety. The Onsite Safety Review Committee has been

active and effective in providing conservative and technically

sound resolution of plant problems affecting safety. The

licensee has been responsive and straightforward in

dealings with the NRC in all levels of interface.

Staffing for the period was adequate and appeared to be

effectively controlled. Backlog work activities and light

overtime by the operations staff have been periodic but do not

appear to be degrading their performance. The training and

qualification program appears to be adequate; however, training

program weaknesses are indicated in the area of operator system

knowledge as demonstrated by the improper alignment of safety

system valves discussed below. The licensee has refocused the

operators training program in the areas of systems knowledge

and working knowledge of administrative controls to control

plant configuration. This has contributed to improved

performance in the second half of this period.

In spite of an overall aggressive pursuit of excellence by site

management, as noted above, a review of enforcement history and

reportable events during the current assessment period reveals

significant difficulty, during the first nine months of this

period, in the ability of management to effectively implement

and achieve the operational goals which they have set. As

noted above, the NRC cited, in the earlier part of this period,

four violations involving three civil penalties. The following

1)15

is a summary of all enforcement items and reportable events

occurring during this period.

Enforcement Items

1.

Improper isolation of charging pump rendered Unit 3

Emergency Core Cooling System inoperable on 9/29/83.

Level III violation. Civil penalty, $20,000.

2.

Failure to follow operating instruction S023-0-36, Control

of System Alignments, associated with the above item.

Level III violation. Civil penalty, $20,000.

3.

Improper isolation of Unit 3 containment spray system on

March 4, 1983, which was not discovered until March 17,

1984. Level III violation. Civil penalty, $125,000.

4.

Improper Mode 1 operation of Unit 3 with a diesel

generator inoperable and the redundant ESF train degraded

due to the inoperable containment spray system. Level III

violation.

A severity level IV violation, specifically identified in

Section B, Radiological Controls, was issued for failure to

declare and report an Unusual Event in a timely fashion. This

violation resulted from various contributing factors including

operator training and systems knowledge, response to alarms and

procedural inadequacies. In this case the alarm response

procedure did not refer the operator to the emergency plan

implementing procedure. Consequently, the alarm was not

recognized as signaling an Unusual Event. The operators failed

to consider recent past plant evolutions in the attempt to

identify and correct the cause of the release. When such

evolutions were evaluated, the release was promptly terminated.

The operators' evaluation of the event was hampered by the fact

that certain monitors were out of service and the indications

of available monitors appeared to be ambiguous unless the

peculiarities of the HVAC system were understood. The licensee

took prompt corrective action to deal with the identified

problems.

Reportable Events

Reportable events involving Unit 2 and 3 operations during this

SALP period resulted in the issue of 115 LER's. A review of

these LER's shows that 23 were the result of personnel error,

of which 20 were repetitive in nature. The repetitive events

appear to fall into four major areas:

1.

Lack of valve control -

9 LER's (Unit 2 83-118, 84-13;

Unit 3, 83-44, 83-46, 83-63, 83-73, 83-78, 84-09, 84-33).

2.

Lack of breaker control -

4 LER's (Unit 2 83-49, 83-85,83-100, 84-29).

6

3.

Lack of proper control of reactor coolant temperature

4 LER's (Unit 2 83-46,83-119, 83-151; Unit 3 83-80).

4.

Lack of proper manual control of steam generator water

level at low power -

2 LER's (Unit 2 84-20; Unit 3 84-32).

Of these LERs, approximately 80% occurred during the first

nine months of this period. This again shows a

comparative improvement during the SALP period.

The most significant weakness noted was in the area of

valve position control, of which 90% were identified in

the first nine months of this period. The control of

system valve lineups was identified as a significant

weakness during the last SALP period and carried over into

the first portion of this SALP period. The underlying

cause for this weak area appeared to be the inability of

site management to detect and correct remaining weaknesses

in the following areas:

a)

Inadequate administrative controls to ensure

independent verification of all critical valving

evolutions.

b)

Inadequate administrative controls to ensure

continuous operator understanding of the status of

critical plant valves.

c)

Inadequate monitoring of plant status changes by

operations supervision.

d)

Incomplete system knowledge by operators.

The licensee's aggressive attention to the problems

revealed during the first nine months of the SALP period

has resulted in measurable improvement, as demonstrated by

a reduction in the number of operator error caused LERs

and lack of any major enforcement actions. This has been

in large part due to a very aggressive management

involvement program which was initiated in May 1984. This

program has enabled the licensee to detect and correct

problems before violation of Technical Specifications

occurs. The most notable example was on August 7, 1984,

when licensee management successfully discovered a low

pressure safety injection pump suction valve in the

locked-closed position. The required position of this

valve for Mode 3 operation is locked-open. This valve

position error was identified by the licensee's Management

Monitoring Program prior to entry into Mode 3. Thus,

additional plant safety resulted. However, the licensee's

additional efforts have not been fully successful as

exemplified by an event on August 21, 1984.

In this event

both trains of Unit 3 HPSI were rendered inoperable for 18

minutes as a result of loss of control of valve status on

  • 0

7

one train in conjunction with an outage on the other

redundant train.

In this case, the licensee identified

the error on a subsequent shift.

Fortunately, the

operation causing the inoperability lasted for only 18

minutes and no violation occurred. However, this event

demonstrates clearly that continuing emphasis in this area

is necessary.

2.

Conclusion

The licensee's performance during the first portion of

this period, particularly in the area of enforcement and

its reflection on training, was a category 3. The

licensee's subsequent performance, as indicated by the

lack of enforcement action and a lower operator error

rate, was significantly improved. The licensee's success

in early detection and correction of problems has

measurably improved with the implementation of an

aggressive management involvement program.

Consideration of the enforcement criterion alone would

indicate Category 3 performance by the licensee in the

Plant Operations area. However after considering stronger

licensee performance in other attributes (refer to Section

II above), particularly management involvement, approach

to resolution of technical issues, responsiveness,

staffing, and improved regulatory performance in the later

portion of this period, the SALP Board considers the

licensee's overall performance in the Plant Operations

functional area to be Category 2.

3.

Board Recommendations

The licensee should continue to evaluate the

administrative controls for repositioning valves critical

to plant safety from the standpoint of the continuity and

visibility of valve status in the control room.

Particular attention to valves and components which affect

safety system operability must be maintained, and the

increased management involvement demonstrated in the

latter part of this period should be continually

emphasized.

B.

Radiological Controls

1.

Analysis

A total of 29 inspections (Unit 1, 6; Unit 2, 12; and Unit 3,

11) were conducted by the Reactor Radiation Protection Section

during the appraisal period. A total of 385 inspection hours

were expended in the areas of:

a.

Radiation Protection

8

b.

Environmental Protection

c.

Waste Management

d.

Confirmatory Measurements

In addition, the resident inspectors provided continuing

observations in these areas.

During the appraisal period, two Severity Level III violations

were identified regarding the failure to conduct surveys

necessary to assure that contaminated materials were not

transferred or disposed in an unauthorized fashion. No

deviations or unresolved items were identified in these areas

during the appraisal period.

The preceding summary of enforcement history in this appraisal

area represents a significant reduction in the number of

violations identified when compared with the last SALP cycle (2

level III's, 4 level IV's and 3 level V's).

In addition, the

two level III violations resulted from activities which

predated this SALP cycle.

The enforcement history supports the previous SALP conclusion

that, "While the items of noncompliance are individually

important, they are not so closely related so as to conclude

that a serious breakdown of the licensee's 'radiological

control' responsibility has occurred."

The inspection

activities during this SALP cycle indicate that the area of

radiological controls has received strong and continuing

management support. This support has been evidenced in the

areas of radwaste shipping, audit program with resultant prompt

corrective actions and health physics reorganization to provide

for better outage support.

The licensee has demonstrated a positive approach to the

resolution of technical issues from a safety standpoint.

The

extensive and aggressive program to identify and recover

contaminated materials released from Unit 1, the improving

quality of environmental reports and the prompt action to

correct the degraded Unit 2/3 personnel decontamination

facilities are examples of the licensee's approach to such

issues.

Generally, the licensee has been responsive to NRC identified

issues, such as support of ALARA, and procedural compliance as

evidenced by the audit program. However, the licensee has

lagged in implementation of commitments with respect to

upgrading radiation monitoring systems and implementing

NUREG-0737 mandated PASS and monitoring system changes,

particularly with respect to Unit 1.

Reportable events have been reported in a timely fashion and

have provided adequate analysis of the events.

0

9

Licensee management support of staffing and training in the

radiological controls area has been both apparent and adequate.

The licensee has developed a well-qualified radiation

protection staff and a good radiation protection training

program.

The continued high Unit 3 primary system activity coupled with

present waste management practices, operational errors and

equipment problems has resulted in a significant number of

airborne radioactive material releases. The level of liquid

releases, while far above those proposed in the FSAR, have

remained within regulatory limits. Licensee efforts to

identify root causes and take effective corrective actions to

minimize releases should be aggressively pursued.

2.

Conclusion

The continued improvement in the areas of radiation protection,

radiological environmental monitoring and overall radiological

controls program supports an increase in the overall

performance classification. The delays in meeting Unit 1

commitments with respect to PASS and radiation monitoring

system modifications; in improving Unit 2/3 effluent monitoring

system performance; and in limiting Unit 2/3 radioactive

effluents are negative factors. An overall performance

classification of 2 is warranted in this functional area.

3.

Board Recommendation

The licensee is encouraged to continue the past strong support

of programs in this area which has been in evidence during this

appraisal period. Efforts to resolve the Unit 2/3 effluent

monitoring problems and to limit effluent releases should be

continued. With respect to Unit 1, timely resolution of PASS

and monitoring system problems is needed to support the return

to service effort.

C.

Maintenance

1.

Analysis

During the current SALP assessment period 143 hours0.00166 days <br />0.0397 hours <br />2.364418e-4 weeks <br />5.44115e-5 months <br /> of direct

inspection effort were applied in the area of plant maintenance

at San Onofre Units 1, 2 and 3. These inspection activities

resulted in one violation. The summary assessment of

individual unit maintenance activities, overall conclusion as

to site performance category and Board recommendations are as

follows.

Unit 1 Maintenance

A large number of maintenance activities have taken place

during this period even though the plant has remained in Mode

5. Some of the significant activities included the following:

0

10

o

RHR system outage

0

CCW system outage

o

TDI diesel inspection and repair

0

DC battery #1 replacement

These activities are not routine or normal plant evolutions;

however, all activities appeared to be properly preplanned and

controlled in accordance with explicit procedures. Prior to

the residual heat removal and component cooling water system

outages, the licensee submitted proposed plans including

compensatory measures such as enhanced surveillance, for staff

approval. The licensee kept the staff well informed of its

plans regarding the No. 1 battery replacement and provided

temporary batteries as an alternate source of DC power. In

instances where technical problems were evaluated, the licensee

demonstrated a good understanding of associated safety issues

and the evaluation results appeared to be technically sound

with thorough approaches used in all cases.

A violation was cited in the housekeeping area involving

foreign material exclusion (FME). There were no apparent

indications of a programmatic breakdown of FME control;

however, the need for additional management involvement was

indicated. Corrective action by the licensee was prompt and

effective.

Four Licensee Event Reports were submitted by the licensee

during this period, of which only two involved personnel error.

The reports were made in a timely manner with appropriate

analyses performed when required. Corrective action appears to

have been effective to prevent recurrence.

Unit 2/3 Maintenance

During the assessment period no violations were identified in

the area of plant maintenance performed by the station

maintenance organizations. However, one violation was

identified in the area of housekeeping, and this violation is

identified in the plant modifications section of this report

since the housekeeping deficiencies were identified primarily

in the areas where equipment alterations were in progress.

During the assessment period the licensee's Maintenance

Department has stabilized and developed into a more efficient

work group. The licensee has dedicated resources to correct

previously identified weaknesses from the previous SALP period.

Progress has been noted in the following areas which were

previously identified as areas of concern:

proper

documentation of maintenance and work, incorporation of vendor

information into technical manuals and procedures, and the

post-maintenance retest program. Though the licensee's

S

11

0

performance in the area of verbatim compliance with procedures

has also improved during this SALP period compared to the

previous, period, and has reached a satisfactory level,

weaknesses in this area still indicate additional improvement

is needed. The following two events are examples of the

weaknesses which exist in the area of verbatim compliance:

(1)

failure of a contract instrumentation and control foreman to

turn in out-of-calibration test instrumentation for

recalibration and (2) the flooding of the Unit 3 Boric Acid

Makeup Tank Pump room, when the mechanic failed to perform the

required safety precautions stated in the procedure. The

licensee's management responded promptly on both of the above

events utilizing the maintenance error investigation system,

which the licensee has used as an effective management tool to

identify weaknesses in the occurrence of non-reportable

concerns as well as reportable events.

Although the above noted weaknesses in the maintenance program

indicate a need for management attention, significant

improvements have been made in several safety-related

maintenance activities. These activities in which improvements

have occurred include the following: maintenance of reactor

trip breakers, reactor coolant pump seals, limitorque valve

operators and steam generator repairs. Also a review of the

Licensee Event Reports for Units 2 and 3 indicate that

significant improvements have been made. Only fourteen

Licensee Event Reports were issued in the maintenance area

during the sixteen month period. This is an improvement from

the last SALP period.

The licensee's staffing of the Maintenance Department is

adequate and scheduling of maintenance tasks appears to be well

controlled with the use of the computer based San Onofre

Maintenance Management System (SOMMS). The licensee has given

proper attention and prioritization to the backlog of

maintenance orders which existed during the SALP period. The

reduction of the large backlog of deficiencies in control room

indicators and alarms during the SALP period has reduced the

distractions to which the reactor operators were subjected

during the previous SALP period.

The Maintenance staff's approach to resolving technical issues

from a safety standpoint has been conservative and timely in

almost all cases. Response to Bulletin 84-03 was technically

well thought out and sound, but the response indicated a minor

weakness within the licensee's organization in the transmission

of important safety information on a timely basis to the

appropriate organizations.

Except for the deficiencies discussed above and in the

Surveillance section of this report, management's efforts in

the area of maintenance have improved significantly and have

resulted in increased reliability of the plant safety systems

during this SALP period.

12

2.

Conclusion

Category 1

3.

Board Recommendation

The licensee's management is encouraged to continue its support

of the maintenance program.

D.

SURVEILLANCE

1.

Analysis

During the current SALP assessment period 205 hours0.00237 days <br />0.0569 hours <br />3.38955e-4 weeks <br />7.80025e-5 months <br /> of direct

inspection effort were applied in the area of surveillances at

San Onofre Units 1, 2 and 3. One violation was identified:

Failure to assure that equipment made inoperable by planned

surveillance activities is returned to service in an operable

status with required test procedures completed (Inspection

Report 84-11, Level IV).

The summary assessment of individual Unit activities is as

follows:

Unit 1

Unit 1 was in Mode 5 for the entire assessment period and the

surveillance program requirements were therefore minimal. No

significant failures or errors in the program were noted.

Units 2 and 3

Although only one violation was identified on Units 2 and 3,

the following five major program weaknesses were identified in

the licensee's surveillance programs:

o

Inadequate formal communications within the

instrumentation and control (I&C) maintenance

organizations.

o

Inadequate knowledge of equipment control requirements by

I&C technicians.

o

Poor procedure compliance by I&C technicians.

o

Inadequate surveillance procedures in that:

1)

Procedures lacked detailed steps to properly restore

the system under test to an operable status.

2)

Procedure failed to provide a second independent

verification of actions requiring independent

verification.

13

The above weaknesses were identified as the result of the

investigation of the following events, which occurred during

the SALP period:

a.

February 3, 1984:

An I&C technician signed the applicable

equipment control from ECF 30242 indicating that the Plant

Protection System response time surveillance testing was

complete. However, based on the review of the restoration

step of the surveillance procedure S023-II-3.1 and the

maintenance order and interviewing the licensee's

personnel, work was not completed until February 16, 1984.

This occurrence resulted in a violation and the licensee

initiated retraining of I&C technicians in the area of

equipment control.

b.

February 28, 1984:

While troubleshooting an inoperable

Reactor Trip Breaker (RTB), an I&C technician identified

that eight leads in the plant protection system cabinets,

which supply power to the RTB's shunt trip devices, had

been left disconnected during the completion of the

restoration section of surveillance procedure S023-II-3.1

(18 month response test) on February 16, 1984. Underlying

causes for this event included improper informal

communication practices between I&C technicians as well as

inadequate procedures due to failure to provide

independent verification and proper system restoration

steps.

c.

March 9, 1984:

Inadvertent initiation of a Safety

Injection Actuation Signal, Containment Cooling Actuation

Signal, and a Containment Spray Actuation Signal due to

the technician's failure to reset the trip in a previously

tested channel before testing the second channel. The

licensee's corrective actions included revising the

affected procedure to include independent verification of

the resetting of each channel.

d.

July 23, 1984:

Inadvertent initiation of the ESF Main

Steam Isolation Signal, when the I&C technician failed to

reset the trip in a previously tested channel before

testing the second channel. The licensee's corrective

action included revising the procedure to eliminate

assumed knowledge and practices of I&C technicians.

The licensee's management has pursued the completion of several

programs to eliminate the above noted weaknesses. The licensee

dedicated considerable resources to complete review of

safety-related surveillance procedures on all three units in

order to include proper restoration steps and independent

verification requirements in the procedures. The licensee

responded aggressively in communicating to all station

personnel each individual's responsibility to strictly adhere

to procedures and require formal communications in the

performance of all procedures. The licensee completed training

0

14

on equipment control requirements and has already demonstrated

improvements in this area. These corrective actions were

timely, well planned and appear to be effective based on

licensee performance during the last four months of the

evaluation period.

The licensee surveillance program was successful in properly

identifying reportable events which, with few exceptions, were

promptly reported. A total of 89 Licensee Event Reports

(LER's) on Units 2 and 3 were submitted during this period. Of

these, 20 represented errors which occurred in the

implementation of the surveillance program. Most of the errors

were due to technician errors during the performance of the

surveillance activities. Overall, the surveillance program has

shown an improved effectiveness over the previous SALP

evaluation period in the area of reducing technician errors

during the performance of the surveillance activities. Roughly

the same number of errors were made, however, the number of

surveillances performed during the period was more than double

that of the previous SALP period due to the fact that Unit 3

did not achieve initial criticality until this evaluation

period.

The scheduling and tracking of the surveillance program by the

Operations department has been excellent and the proper

assignment of priority items has been consistent.

Technician staffing for the period was supplemented by

contracted technicians to complete the large workload for 3

units. The licensee's training programs for technicians have

become more specialized with four distinct groups of

technicians within the licensee's staff. The four groups which

include approximately 200 technicians are:

Instrumentation and

Control, Computer, Radiological Monitor and Electrical Test.

The shortage of technicians in the industry has been recognized

by the licensee and management has aggressively pursued

obtaining the best qualified technicians available throughout

the country. Turnover of technicians is beginning to stabilize

and this should result in additional improvement in the

surveillance program with improved work task efficiency.

Overall, the training and qualification program for technicians

is adequate, but requires continuous attention and evaluation

by management until technician experience levels are improved.

2.

Conclusion

Category 2 -

No change from previous SALP perod.

3.

Board Recommendation

The licensee should continue to closely monitor and enforce

formal communications and procedural adherence by the working

level technicians, and to continue efforts to stabilize the

15

g

turnover of technicians and gradually eliminate the reliance on

large numbers of contract technicians.

E.

Fire Protection

1.

Analysis

During the current SALP assessment period 2 inspections

totaling 87 hours0.00101 days <br />0.0242 hours <br />1.438492e-4 weeks <br />3.31035e-5 months <br /> of direct inspection effort were applied in

the area of fire protection at San Onofre Units 1, 2, and 3.

In addition the resident inspectors provided continuing

observations in this area. Three violations were identified as

follows:

o

Failure to provide indication of reactor coolant cold leg

temperature on the essential plant parameter monitor panel

which is used if a fire makes the control room unavailable

(Units 2 & 3).

o

Failure to wrap redundant equipment power cables found to

be within 20 feet of each other with a one-hour rated fire

resistant material (Unit 3).

o

Failure to provide required fire protection for safe

shutdown equipment (Unit 3).

The above violations were corrected in a timely manner.

The licensee has demonstrated aggressive management involvement

in this area by the aggressive pursuit of a complete review of

the Fire Hazards Analysis (FHA). This review consisted of a

verification of plant conformance to this document and a

comprehensive review of this document for conformance to NRC

requirements. This activity has been essentially completed for

Units 2&3 with the submittal of the revised document to NRR for

approval. In addition, as a result of this work, 5 LERs were

identified which covered a number of cases wherein plant

configuration was not consistent with the FHA or NRC

requirements. The licensee is currently doing a similar effort

on Unit 1.

The licensee's staffing in this area appeared adequate and

included a large number of fire patrol personnel, a station

fire brigade, and an adequate management staff.

The training in this area was adequate and the fire watch

personnel appeared alert, knowledgeable and responsible. The

station has its own fire department which has been at the

station all year. The licensee's reporting of fire protection

system discrepancies appeared aggressive.

The licensee did have several LER's in this area -

21 on Unit

2, 3 on Unit 3 and 0 on Unit 1. Of these, three were caused by

personnel error, three were caused by defective procedure,

16

three were caused by component failure, and seven were caused

by design manufacturing or installation error. These LER's

appear to result in part due to a large amount of retrofit work

and the FHA review.

2.

Conclusion

Overall the licensee's performance in this areas has been

aggressive and responsive to NRC concerns; however, due to the

number of violations in this area, the failure on occasion to

perform required surveillances, the failure to ensure

compensation measures on occasion and the failure to ensure

configuration conformance to the FHA and NRC requirement during

initial construction on Units 2&3, this area is evaluated

Category 2.

3.

Board Recommendation

The licensee should aggressively pursue the completion of the

FRA evaluation on Unit 1 and should continue to emphasize fire

protection, particularly in light of the extensive retrofit

work.

F.

Emergency Preparedness

1.

Analysis

During the appraisal period, Region V conducted a routine

inspection of the SONGS emergency preparedness program and an

appraisal of the Units 2/3 Emergency Response Facilities (ERF)

and observed an emergency preparedness exercise that involved

the Units 2/3 facility as well as areas common for the site.

This inspection effort totaled 599 hours0.00693 days <br />0.166 hours <br />9.9041e-4 weeks <br />2.279195e-4 months <br /> onsite (Unit 1-54

hours, Unit 2-344 hours and Unit 3-201 hours).

No violations

of NRC requirements or significant deficiencies were identified

during the scope of this inspection effort. During this

appraisal period, however, one violation having impact in the

area of emergency preparedness was cited. This is discussed in

Section A, Unit 2/3 Operations.

The licensee's management has continued its support of the

emergency preparedness program. When asked, management readily

volunteered to be the first facility to have an NRC Emergency

Response Facilities (ERF) Appraisal. The inspection effort

confirmed the licensee's ability to adequately address

technical issues related to emergency preparedness and provide

a sound solution. SCE's response to NRC initiatives was timely

and aggressive as demonstrated by their evaluation of, and

action on suggested improvements resulting from the ERF

appraisal. The staff assigned to the emergency preparedness

program and those persons filling positions in the emergency

response organization are ample in numbers and these positions

are well defined. The licensee has a well defined emergency

17

0

preparedness training program that has been implemented and

appropriately documented.

2.

Conclusion

Category 1 - No change from previous SALP period

3.

Board Recommendation

The licensee's management is encouraged to continue its support

of the emergency preparedness program.

G.

Security

1.

Analysis

From June 1, 1983 through September 30, 1984, Region V

conducted six Safeguards inspections at San Onofre Nuclear

Generating Station for a total of 244 hours0.00282 days <br />0.0678 hours <br />4.034392e-4 weeks <br />9.2842e-5 months <br /> of inspection

effort. One inspection was a Material Control and Accounting

inspection and the remaining five inspections were in the

Physical Security area. Throughout the reporting period, all

three units at SONGS were inspected and no violations were

identified. Of the total inspection effort (244 hours0.00282 days <br />0.0678 hours <br />4.034392e-4 weeks <br />9.2842e-5 months <br />), 173

hours were devoted to routine inspection activities and 71

hours were devoted to reactive effort.

Physical security inspections during this SALP period showed

licensee management to be actively involved in the overall

security program. The entire management staff worked steadily

to improve the Security Plan. This effort resulted in a

complete rewrite and approval of the station Security Plan and

implementing procedures together with numerous improvements in

the Station Security Program.

Staffing of the security organization was judged by NRC to be

very adequate.

SONGS continued to effectively utilize a

uniformed security force comprised of both proprietary and

contract personnel. The security management staff was

responsive to NRC initiatives, demonstrated an understanding of

safety/security issues, and actively supported the total

Safety/Security Interface Program. The individual Security

Officers demonstrated a thorough understanding of security

requirements and a desire to comply with these requirements.

An effective program for the reporting and analysis of

reportable events was in place.

2.

Conclusion

Category 1 -

Improvement over previous SALP period.

g

18

3.

Board Recommendations

Licensee management is encouraged to maintain their support of

the station security program.

H.

Refueling

1.

Analysis

No refueling activities were conducted during the assessment

period.

2.

Conclusions

Not applicable

3.

Board Recommendation

Not applicable

I.

Quality Programs and Administrative Controls

1.

Analysis

Quality Programs

Management involvement in quality programs and administrative

controls has been apparent with substantial progress being made

during the assessment period to implement a unified and

consistent quality assurance program applicable to all three

units at SONGS. The SONGS-1 and SONGS-2/3 site quality

assurance groups were reorganized under the common control of

the site Quality Assurance Manager which has improved

communication and control. Various initiatives such as a June

1984 Unit 1 return-to-service audit, a special quality

assurance Construction Surveillance Program, a

Retrofit/Startup/Outage and Maintenance quality assurance group

upgrading of procedures, twenty-four hour quality control

coverage, and quality assurance involvement in a SONGS-1

technical specification surveillance requirement review

demonstrated a strong commitment to prior planning and the

assignment of priorities. The SONGS-1 quality assurance

organization manning level was increased above the previous

manning level for Mode 5 operation and maintenance, and

experienced quality assurance personnel were assigned to

SONGS-1 during modification activities. Various computer

tracking systems were developed to enhance the quality

assurance organization's ability to accurately maintain the

status of activities.

Corporate management was found to be frequently involved in

site activities and special corporate quality assurance audits

were performed on SONGS-1 material/equipment supplier

qualifications and the interface aspects of SCE/Bechtel/Impell

19

design/analysis activities. Inspections in the areas of

design, design changes and modifications revealed strengths in

administrative controls, procedures and implementation.

Discussions with onsite engineering personnel revealed that

they had undergone training and indoctrination in the

engineering and QA procedures applicable to the work to which

they were assigned.

During the special team inspection, Station Orders and selected

Administrative, Engineering, General, Emergency, Abnormal and

Alarm response procedures applicable to Unit No. 1 were

examined. The procedures were found to be detailed and

consistent with industry and regulatory guidelines as to

format, scope, and content. At the end of the SALP period, the

licensee was developing administrative controls to more clearly

define (1) the use of "N/A" in procedures and (2) the process

for expediting issuance of temporary procedure changes.

The licensee is very responsive to NRC concerns in the area of

quality assurance. Investigations of quality assurance

concerns are thorough and timely when the potential for safety

significance exists. Corrective actions are generally

conservative reflecting consideration of the root and

contributing causes. These attributes were clearly

demonstrated recently by the licensee's response following NRC

identification of the installation of some potentially

nonconforming pipe fittings.

Event Review and Independent Offsite Review Groups

The effectiveness of licensee event review groups and

independent offsite review committees was examined during this

assessment period. Post trip/transient reviews were conducted

in accordance with applicable procedures with the cause of the

event and proposed corrective actions to prevent recurrence

identified in all cases. Station incident reports were well

written, accurate descriptions of the events with causes,

corrective actions, and reportability clearly identified.

Management review of station incident reports was prompt and

well documented. Proposed corrective actions were entered on a

tracking system to ensure resolution.

The Independent Safety Engineering Group (ISEG) is physically

located onsite and functions to examine plant operating

characteristics, NRC issuances, industry advisories, Licensee

Event Reports and other sources of plant design and operating

experience information which may indicate areas for improving

plant safety.

ISEG activities are reported offsite by the ISEG

supervisor to the Manager of Nuclear Safety. The licensee has

divided ISEG responsibilities into two programmatic areas:

surveillance of plant activities and review and analysis of

operating experience reports.

g

20

ISEG surveillances were well researched and the findings or

recommendations well documented. The quality of the

surveillances reflected the high experience level (20 years

average) of the ISEG engineers. The surveillances were

directed towards and appeared to be contributing to the goal of

enhancing plant operations and nuclear safety by recommending

solutions to existing or potential problems.

ISEG personnel

initially attempted to resolve actual or potential problems at

the individual station engineer level. Cooperation between

station operations and engineering and ISEG appears

satisfactory. Where disagreements have developed, appropriate

management involvement by the ISEG Supervisor and Manager of

Nuclear Safety was apparent.

The independent offsite review groups (Nuclear Safety Group and

Nuclear Audit and Review Committee) appeared to be effectively

assessing the safety implications of station events.

Individual safety reviews are adequately documented and

checklists used in the reviews are well developed and

comprehensive. Programs to quantify and improve nuclear

safety, which exceed technical specification requirements, are

underway and demonstrate aggressive action by the Nuclear

Safety Group and Licensee Management to enhance nuclear safety.

Licensee event review groups and independent offsite review

groups demonstrate conservatism and a clear understanding of

safety issues in their reviews. Staffing is ample and

experience levels exceed technical specification requirements

in all cases. Monthly management reports examined did not

adequately reflect the independent conclusions or judgments

which had been arrived at during the individual safety reviews,

but the licensee has initiated corrective action in this

regard.

Unit 1 Modifications

During the current SALP assessment period, 982 hours0.0114 days <br />0.273 hours <br />0.00162 weeks <br />3.73651e-4 months <br /> of direct

inspection effort were applied in the area of plant

modification effort. This inspection effort resulted in the

citation of one violation. The major plant modification effort

for the period involved the return to service effort for Unit

1. Extensive field inspections were performed by the NRC

during this period, including a large effort by Lawrence

Livermore National Laboratory (LLL) and a Region V team

inspection.

Findings as a result of the above effort identified a weakness

in the Quality Control inspection effort used for the seismic

modifications work in that minor welding deficiencies were not

being properly documented. The licensee responded to this

finding by forming a reinspection task force in order to

discover if any additional deficiencies existed. All

identified deficiencies have been corrected.

21

In the area of environmental qualification, a Notice of

Violation was issued against the design of the reactor head

vent system because SCE engineering had failed to specify on

the installation drawings the conduit fittings needed for

sealing of the electrical conductors where they enter the valve

solenoid operator. The licensee took immediate corrective

action and was responsive to NRC concerns.

Three Licensee Event Reports (LER) were received during this

period. The areas addressed by the LER's were as follows:

o

Modification to existing plant system.

o

Delinquent temporary change notice approvals.

o

Corrosion of reinforcing steel.

The LER's submitted were reported in a timely manner with

events adequately identified. Analysis of the intake structure

event was described in detail and provided valuable information

to the NRC.

The licensee currently has a large work force dedicated to

completing plant modifications in the following areas:

TMI

modifications on Unit 2, plant betterment modifications

(particularly Condensate Demineralizer Buildings), and

Radiation Monitoring System design changes, plus several

hundred other design changes to be implemented as a result of

minor deficiencies identified during the Startup period which

ended in March, 1984.

As a result of the large amount of construction/rework activity

ongoing on Units 2 and 3, the licensee has maintained a large

Unit 2 and 3 Projects construction/maintenance organization

onsite separate from the Station Maintenance organization. The

Project organization still includes a large contractor work

force of approximately 1500 engineers and maintenance

craftsmen, which are primarily supervised by Bechtel and

Catalytic construction companies. Due to the complexity of the

organization and the relatively high turnover rate of craft

workers, the licensee has experienced difficulties in managing

proper housekeeping in areas of construction and equipment

alterations. A decline in housekeeping standards occurred

during the last four months of the SALP period as the level of

Project supervised construction increased. The decline in

housekeeping was primarily noted in radiologically controlled

areas in the Safety Equipment Buildings to the extent that a

housekeeping violation was cited. The underlying cause for the

degrading trend in housekeeping was the lack of adequate

direction by the licensee's management as to which

organizations were responsible for housekeeping in the

radiologically controlled areas. The licensee has implemented

interim corrective actions and developed additional long term

corrective actions to upgrade plant housekeeping conditions.

22

2.

Conclusion

Category 1 (This area was not separately evaluated during the

previous SALP period).

3.

Board Recommendation

The licensee's management is encouraged to continue its support

of the quality assurance program and independent review groups

and to enhance the effort directed toward preventing

operational and equipment control problems of the type

discussed in Section A, Plant Operations.

J.

Licensing Activities

1.

Analysis -

Unit 1

This evaluation represents the integrated inputs of the

Operating Reactor Project Manager (ORPM) and those technical

reviewers who expended significant amounts of effort on SONGS-1

licensing actions during the current rating period.

The basis of this appraisal was the licensee's performance in

support of licensing actions that were either completed or

active during the current rating period. These actions,

consisting of amendment requests, exemption requests, responses

to generic letters, TMI items, and other actions, are

classified as follows:

Thirteen completed Multi-Plant Actions included in this

category are:

-

Decay Heat Removal Capability Technical Specifications

-

Radiological Effluent Technical Specifications

-

Containment Purge and Vent

-

Reactor Vessel Cavity Seal Ring Missile Potential

-

Automatic Actuation of Shunt Trip Attachment

-

Thermal Mechanical Report

-

Potential for Voiding in RCS

-

Containment Pressure Instrument

-

Containment Water Level Monitor

-

Containment Hydrogen Monitor

-

Automatic PORV Isolation

-

Report on PORV's

-

ECCS Outages

Seven completed Plant-Specific Actions included in this

category are:

-

Two revisions to station physical security plan

-

Technical Specifications on Coolant Activity Sampling

-

Evaluation of Spent Fuel Pool Racks

-

Steam Generator Inspection Program and License Condition

23

-

Revisions to Appendix B (Environmental) Technical

Specifications

-

Revision to Boron Concentration Limits in Cold Shutdown

and Refueling

Other major activities during the review period were the

seismic reevaluation program and SEP.

The licensee's performance evaluation is based on a

consideration of seven evaluation criteria given in the NRC

Manual Chapter. For most of the licensing issues considered in

this evaluation, only four of the evaluation criteria were of

significance. Therefore, the composite rating is based on the

following evaluation criteria:

-

Management involvement

-

Approach to resolution of technical issues

-

Responsiveness to NRC initiatives

-

Staffing

With the exception of Enforcement History, for which there were

no bases within NRR for evaluation, the remaining evaluation

criteria below were judged to apply only to a few licensing

activities.

-

Reportable events

-

Training

a.

Management Involvement and Control in Assuring Quality

San Onofre 1 has remained in the cold shutdown mode

throughout the evaluation period. During the first

several months of this period, a general slowdown of

licensee activity, both in plant modifications and in

licensing, was in effect. Meanwhile, SCE management was

developing plans and schedules for plant restart and for

long-term plant retrofit.

Management involvement over the last several months has

been very apparent; particularly with respect to issues

directly related to restart. There is evidence of

planning and assignment of priorities and that

decision-making is generally handled at the appropriate

level of management.

The licensee has proposed an "Integrated Living Schedule"

to establish priorities for plant backfits and to track

progress in completing these actions. This system should

be of benefit to both the NRC and the licensee.

As a result of the long shutdown, uncertainty about the

schedule for return to service and the resultant reduction

in effort during the beginning of the review period, many

licensing issues are not yet resolved. Increased

24

management attention should continue in the next

evaluation period to minimize schedule slippages such that

these issues can be completed.

On the basis of these observations, a rating Category of 2

is assigned to this attribute.

b.

Approach to Resolution of Technical Issues from a Safety

Standpoint

In the approach to resolution of technical issues from a

safety standpoint, the licensee's responses are generally

sound and viable. For example, for the Radiological

Effluent Technical Specifications, plant personnel showed

good understanding of the issues and were cooperative in

resolving them.

In the area of seismic reevaluation, the licensee is using

state-of-the-art analysis methodology and criteria; the

licensee has demonstrated clear understanding of the

issues.

For responses to generic letters, the licensee has

generally followed the guidelines provided with exceptions

dictated by unique features of the plant design.

For the SEP Integrated Assessment, the licensee has

provided responses to support the adequacy of the existing

plant design in many areas and, where warranted, has

proposed evaluation programs or other corrective measures

to resolve the open issues. These proposals are generally

sound and reflect an adequate degree of conservatism.

The overall rating for this category, based on inputs from

twelve subject areas, is Category 2.

c.

Responsiveness to NRC Initiatives

During the first several months of the review period,

licensee efforts to resolve outstanding licensing issues

were minimal for the reasons described above. However,

beginning in early 1984, the licensee has made great

strides in reducing the backlog of actions. This is

demonstrated by the large number of actions that have been

closed out and by the eleven license amendments that have

been issued since December. In addition to the completed

actions listed above, the licensee has submitted license

amendment applications for technical specifications on

NUREG-0737 items (Generic Letters 82-16 and 83-37),

Reportable Events (Generic Letter 83-43), Auxiliary

Feedwater System (TMI II.E.1.1 and II.E.1.2) and dc Power

Surveillance. These submittals generally proposed

resolutions which were acceptable to the staff, but in

several instances, it was necessary to request further

25

information to support some of the requested changes. The

licensee has been generally responsive to NRC requests for

information either by conference calls, meetings or by

letter, although schedule slips have occurred.

Although overall responsiveness has been good, delays for

some TMI Action Plan items will result in San Onofre 1

being one of the last plants to resolve these issues.

Most of these delays arise from the slowdown period

mentioned above and from the licensee devoting attention

to issues required for plant restart. The overall rating

for this criterion is Category 2.

d.

Enforcement

No basis exists for an NRR evaluation of this attribute.

e.

Reportable Events

Only one topic was evaluated with regard to reportable

events. This one evaluation (Category 1) was judged to be

too limited a sample to provide an overall rating.

f.

Staffing

A rating of Category 2 was assigned to this attribute.

The level of staffing is considered adequate, with some

delays of submittals that could be attributable to

staffing levels.

g.

Training and Qualifications

This attribute was judged to apply to only a few actions.

A rating of Category 1 was assigned for those instances

where a rating was applied.

2.

Analysis Units 2 and 3

The basis of this appraisal was the licensee's performance in

support of licensing actions that were either completed or

active during the current rating period. These actions,

consisting of amendment requests, exemption requests, responses

to generic letters, TMI items, and other actions, are

classified as follows:

Completed Multi-Plant Actions in this category include:

-

Thermal-Mechanical Report

-

Potential for Voiding in RCS

-

Relief Valve and Safety Valve Testing

-

Control of Heavy Loads (Phase I)

-

NUREG-0737 Technical Specifications

-

Technical Support Center

26

-

Emergency Operations Facility

-

Operational Support Center

Completed Plant-Specific Actions in this category include:

-

Two revisions to station physical security plan

-

Issuance of a full power license amendment for Unit 3

-

Revised Technical Specifications for:

1.

Natural Circulation Test Exceptions

2.

Rod Bow Penalty Factors

3.

ESFAS Subgroup Relay Surveillance

4.

Allowed containment purge time

5.

Setting of Pressurizer Code Safety Valve

6.

Fire Protection equipment changes

-

Two exceptions to the regulations relating to

Appendix E and 10 CFR 70.24.

The licensee's performance evaluation is based on a

consideration of seven evaluation criteria given in the NRC

Manual Chapter. For most of the licensing issues considered in

this evaluation, only four of the evaluation criteria were of

significance. Therefore, the composite rating is based on the

following evaluation criteria:

-

Management involvement

-

Approach to resolution of technical issues

-

Responsiveness to NRC initiatives

With the exceptions of Enforcement History and Staffing for

which were no bases within NRR for evaluation, the remaining

evaluation criteria of

-

Reportable events

-

Training

were judged to apply only to a few licensing activities.

a.

Management Involvement and Control in Assuring Quality

During the evaluation period San Onofre Unit 2 has been in

commercial operation, and Unit 3 has received a full power

license, completed startup testing, and has begun the

first cycle of commercial operation. During this time

period, management involvement with licensing activities

has been evident. Specifically, as a result of previous

difficulties with the technical specifications, SCE has

submitted a large number of requests for changes to

improve the technical specifications. This represents an

improvement over past evaluation periods.

On the basis of these observations, a rating Category of 2

is assigned to this attribute.

27

b.

Approach to Resolution of Technical Issues from a Safety

Standpoint

In the approach to resolution of technical issues from a

safety standpoint, the licensee's responses have, in

general, been acceptable. In the areas of the ESFAS

subgroup relay technical specifictaion change, the steam

generator tube inspection criteria technical specification

changes, the control of heavy loads, and the allowed purge

time technical specification, the licensee's submittals

have been better than average.

The overall rating for this attribute based on inputs from

eight subject areas, is Category 2.

c.

Responsiveness to NRC Initiatives

The licensee has generally been quite responsive to staff

concerns. Requested information has been provided in a

timely manner, has been comprehensive, and has directly

addressed the issues of concern. Licensee responsiveness

was particularly good in addressing the ESFAS subgroup

relay issue, the control of heavy loads issue, and the

steam generator inspection criteria issue.

The overall rating for this attribute is Category 1.

d.

Enforcement

No basis exist for an NRR evaluation of this attribute in

the licensing area.

e.

Reportable Events

Only one topic was evaluated with regard to reportable

events. This one evaluation (Category 1) was judged to be

too limited a sample to provide an overall rating for this

attribute.

f.

Staffing

This attribute was judged to be Category 2, in that the

staffing of the SCE licensing effort appears to be

adequate.

g.

Training and Qualifications

This attribute was judged to apply to only a few actions.

A rating of Category 2 was assigned for those instances

where a rating was applied.

28

3.

Conclusion

In summary, licensee performance in the areas of management

involvement and responsiveness has improved over the rating

period. As a result the backlog of items has been

substantially reduced. Although some Category 1 ratings were

assigned, the majority were Category 2. Therefore, an overall

licensing performance rating of Category 2 has been judged.

4.

Board Recommendation

Continued management attention is recommended to ensure timely

completion of the remaining outstanding licensing issues.

K.

STARTUP TESTING (UNIT 3)

1.

Analysis

During the current SALP assessment period, 233 hours0.0027 days <br />0.0647 hours <br />3.852513e-4 weeks <br />8.86565e-5 months <br /> of direct

inspection effort were applied in the area of startup testing.

The resident inspectors observed startup tests performed by the

licensee on Unit 3 from initial criticality on August 29, 1983

through the completion of testing on March 27, 1984. No

violations were identified in this area.

One Licensee Event Report (LER) was submitted in this area.

This event involved a technician error while performing a

startup test procedure at 20 percent power when the technician

erroneously interrupted power supply voltage to the Reed Switch

Position Transmitters for 23 Control Element Assemblies (CEA)

associated with CEA Calculator No. 2. With the exception of

the technicians error, the startup test program implementation

for Unit 3 went smoothly.

2.

Conclusion

Category 1

3.

Board Recommendation

Not applicable

V.

SUPPORTING DATA AND SUMMARIES

A.

Licensee Activities

SONGS-1 has remained shut down during this assessment period to

accomplish seismic upgrading and TMI action plan items.

The

licensee has requested, by letter dated August 20, 1984, permission

to restart the unit which is scheduled for late November, 1984.

During this assessment period both SONGS 2 and 3 completed power

ascension testing and began full power commercial operation. A

brief summary of key events is as follows:

29

Unit 2 Startup

80%

power testing

May

16 -

June 5, 1983

100%

power testing

June 6 - August 8, 1983

Warranty Run

June 16 -

August 18, 1983

Unit 2 Outages

RCP seal replacement

24 days

6/16 -

7/10/83

18 month surveillance

28 days

11/15 -

12/13/83

RCP seal repair

28 days

1/13 -

2/10/84

Steam generator tube leak 20 days

6/19 -

7/9/84

RCP seal replacement

11 days

7/11 -

7/22/84

Unit 3 Startup

Initial criticality

August 29, 1983

Low power physics testing

August 29 -

September 5, 1983

20%

power

September 25 -

October 9, 1983

50%

power

October 11

-

October 31, 1983

80%

power

November 3

- November 15, 1983

100% power

November 17

-

January 6, 1984

Warranty run

March 18

-

March 27, 1984

Unit 3 Outages

Mode 5 delay for Unit 2

34 days

6/1

-

7/4/83

RCP seal repair

18 mo. surv.

55 days

1/7

-

3/2/84

Scheduled outage

2 days

3/29 -

3/31/84

Turbine generator balance

17 days

5/4 -

5/21/84

RCP seal repair

22 days

6/11 -

7/3/84

Steam generator tube leak

18 days

7/18 -

8/5/84

Significant license amendments are listed in Paragraph IV.J.1.

Major modifications took place on Unit-1 during the extended outage

as follows:

1)

Seismic Upgrade -

the licensee's restart plan provided for

upgrading systems to assure a hot standby plant condition will

be achievable following an earthquake of 0.67g. Completed work

activities include:

o

Structural Steel Members

a

New Auxiliary Feedwater Tank and Piping

o

Electrical Raceway Supports

0

Piping Supports

o

Backup N for Safe Shutdown Valves

o

Cross-connect of Spent Fuel Storage Pool to Charging

System for use as a Makeup Water Source.

30

2)

TMI - The return-to-service effort included completion of

modifications begun during the 1982 shutdown. To resolve TMI

action items these modifications included:

o

Wide Range Stack Gas Monitor

o

Containment H and Water Level Monitors

o

2

Technical Support Center

3)

Saltwater Intake Structure -

Underwater surveillances this

summer by the licensee indicated the possibility of structural

degradation of the walls. Following examination of the

dewatered structure modifications were completed to restore

full structural integrity and repair degraded gate slots. The

intake has been refilled.

4)

The return to service effort included completion of tasks begun

in 1982:

o

480V Halon System

o

Drip Shields in 480V and 4KV rooms.

5)

In addition to the upgrades noted above, the licensee has

included the following within the return to service scope and

has completed all required actions.

o

P&ID Drawing Verification

o

Replacement of Efcomatic Valve Operators

o

Replacement of No. 1 DC Battery

o

Replacement of Saltwater Intake Gates

o

Installation of Saltwater Pump Check Valves

o

Waste Gas System Improvements

o

Replacement of Safety Related Snubbers (Mechanical for

Hydraulics)

B.

Inspection Activities

Inspection activities conducted during the assessment period are

provided in Table 1. In addition to the routine inspection program,

a special team inspection of mechanical, electrical, design and

operations activities associated with hardware modifications, plant

maintenance and performance of shift personnel was conducted in

July, 1984. The team inspection involved 688 hours0.00796 days <br />0.191 hours <br />0.00114 weeks <br />2.61784e-4 months <br /> by twelve NRC

inspectors and 188 hours0.00218 days <br />0.0522 hours <br />3.108466e-4 weeks <br />7.1534e-5 months <br /> by three NRC consultants. No violations of

NRC requirements were identified within the scope of the inspection.

A number of perceived weaknesses were referred to the licensee for

consideration.

A substantial amount of inspection effort, including 230

inspection-hours by two NRC resident inspectors and 756 hours0.00875 days <br />0.21 hours <br />0.00125 weeks <br />2.87658e-4 months <br /> by NRC

contract personnel, was devoted to the seismic modifications on

SONGS-1.

31

C.

Investigations and Allegations Review

1.

Investigations

Inquiries Closed:

1-Hardware deficiencies

1-Falsification of records

Inquiries Open:

4-Falsification of records

2-Illegal drug use

Cases Open:

1-False statements and/or documents

2.

Allegations

All allegations associated with Unit 1 assigned to the Region V

staff are closed with the exception of the following:

o

RV-83-A-36 -

Anchor Bolts

It is currently believed that this allegation has a small

probability for substantiation but it only applies to work

performed from 1979-1981 which predates seismic upgrade

work on SONGS 1.

o

RV-84-A-94 - Reactive Aggregate in the Intake Structures

Based upon concrete testing by the licensee during the

investigation and repair of intake structure corrosion

problems, the Region V staff has seen no evidence that

reactive aggregate was used in the intake structure.

D.

Escalated Enforcement Actions

a.

Civil Penalties: Three civil penalties totaling $165,000 were

issued as described individually below.

1.

Improper isolation of charging pump rendered Unit 3

Emergency Core Cooling System inoperable on 9/29/83.

Level III violation. Civil penalty $20,000.

2.

Failure to follow operating instruction S023-0-36, Control

of System Alignments, associated with the above item.

Level III violation. Civil penalty $20,000.

3.

Improper isolation of Unit 3 containment spray system on

March 4, 1983, which was not discovered until March 17,

1984. Level III violation. Civil penalty $125,000.

b.

Orders

None relating to enforcement.

32

E.

Management Conferences Held During Appraisal Period

a.

Conferences

September 7, 1983

-

SALP Management Meeting

November 21, 1983

-

Enforcement Conference (Discussion of

circumstances behind isolation of the

discharge of the Unit 3 charging pumps

from the Reactor Coolant System

(Report No. 50-362/83-37)

May 9, 1984

-

Enforcement Conference (Discussion of

licensee's enforcement history and the

findings of a special inspection

conducted on March 17-19, 1984 of the

improper isolation of the Unit 3

containment spray system (Report No.

50-362/84-16)

August 8, 1984

-

Enforcement Conference (Discussion of

licensee action following issuance of

a Notice of Violation on May 16, 1984

involving improper isolation of the

Unit 3 containment spray system

(Report No. 50-362/84-26)

b.

Confirmation of Action Letters

None

F.

Review of 10 CFR 21 Reports and Licensee Event Reports (LER's)

a.

10 CFR 21 Reports

No 10 CFR 21 reports were submitted by the licensee during the

SALP period. The licensee has completed, or has in progress,

action to evaluate and respond to 10 CFR 21 notifications from

other organizations which may impact San Onofre.

b.

Licensee Event Reports

Analyses of significant LER's have been provided in the

applicable functional area sections of this report. A listing

of LER's received during the assessment period is provided in

Table 2. Additionally, an analysis of LER's for the period of

June 1, 1983 to May 31, 1984 was performed by the Office for

Analysis and Evaluation of Operational Data. The results of

this analysis are presented below.

SAN ONOFRE UNIT 1

The licensee submitted 9 LERs, including revisions, for SONGS-1

during the period, June 1, 1983 to May 31, 1984.

In addition,

33

8 other reports were submitted by the licensee. Based on the

review of the available reports, the findings are as follows:

1.

LER COMPLETENESS

a)

Was the information sufficient to provide a good

understanding of the event?

The LERs provided sufficient information to provide a

clear and adequate description of the occurrence, the

direct consequences, and corrective actions.

b)

Were the LERs coded correctly?

All of the entries reviewed appeared to be

essentially correct and the system codes agreed with

the information in the narrative descriptions. One

typographical error was found.

c)

Was supplementary information provided when needed?

Supplemental information was usually provided for

each of the LERs.

In two cases, supplemental

information was provided in separate letters without

an updated LER. The licensee should be encouraged to

submit an updated LER with supplemental information

to ensure that all information pertaining to a

reportable event is complete and referenced to an

LER.

d)

When follow-up reports are promised, are they

delivered?

The licensee generally provided promised follow-up

information in a timely manner.

e)

Were similar occurrences properly referenced?

None of the LERs referenced previous events.

2.

MULTIPLE EVENT REPORTING IN A SINGLE LER

No LERs contained information in a single LER that should

have been reported in separate LERs.

3.

PROMPT NOTIFICATION FOLLOW-UP REPORTS

Each of the prompt reports were followed-up by LERs or

special reports. It appears that LERs were also submitted

for reportable occurrences identified in Preliminary

Notifications.

34

In summary, our review indicates that based on the stated

criteria, the licensee provided adequate event reports during

the assessment period.

SAN ONOFRE UNITS 2 AND 3

The licensee submitted 237 reports, plus revisions, for the two

units during the period from May 1, 1983 to April 30, 1984.

The review included the following LER numbers:

UNIT 2

UNIT 3 83-037 to 83-156 83-037 to 83-120 84-001 to 84-022 84-001 to 84-013

The LER review followed the general instructions and procedures

of NUREG-0161 and NUREG-1022.

Because of the similarity of

both units, and of their respective LER preparers, this LER

review would be applicable to either unit. The specific review

criteria and findings follow.

1.

LER Completeness

a)

Was the information sufficient to provide a good

understanding of the event?

1983 LERs

The LERs provided sufficient information to provide a

clear and adequate description of the occurrence, the

direct consequences and corrective action. Many LERs

included specific details of the event such as the

time of the event, duration of the event, valve

identification numbers, LCOs that were violated,

etc., to provide a more complete understanding of the

event.

1984 LERs

The abstract described the major occurrences of the

event, including all component or system failures

that contributed to the event and significant

corrective action taken or planned to prevent

recurrence as stated in NUREG-1022.

b)

Were the LERs Coded Correctly?

1983 LERs

The codes the licensee selected were checked against

the narrative description of the event for accuracy.

Except for a few infrequent cases, AEOD agreed with

the licensees selection for the coded fields. When

AEOD disagreed, it was in coded fields of lesser

35

importance to the event described, and the

disagreements occurred randomly, so no licensee

misinterpretation of NUREG-0161 guidance was evident.

In addition, each coded entry was typed and centered

within the code box. There were no typos or

omissions. The form was neat in appearance and

readable.

It was evident that care was used in

preparation.

1984 LERs

With the fewer code boxes there is much less chance

for disagreement.

The only licensee error found was

the omission of an event title and a typo in the

event date for LER 84-06 for Unit 2.

c)

Was Supplemental Information Provided When Needed?

1983 LERs

All of the reports that were required to be reported

immediately contained the mandatory supplemental

information. In addition, a significant number of

reports contained voluntary additional supplementary

information. The attachments that were provided

typically included specific information useful in

assessing the full impact of the event. However, the

licensee's safety discussions were often not

commensurate with our perceived potential

consequences of the event, so it appeared that the

safety analysis was briefest for the most potentially

complicated events.

For instance, LER 83-37 reported

that the feedwater logic circuitry resulted in an

actual trip setpoint of 300 psid higher than assumed

in the FSAR. The licensee's safety explanation was

that public health and safety were not affected.

However, it was noted that the licensee usually

stated the number of available redundant systems and

that reports without attachments did not need

additional explanation.

1984 LERs

The text of the LER satisfied the requirements of

NUREG-1022. The licensee's safety assessment of the

event showed considerable improvement from the 1983

submittals but, in some cases, it still did not

completely discuss the safety consequences and

implications of the event.

36

i

d)

Follow-Up Reports

1983 LERs

The licensee promised to update a significant portion

of the LERs in this assessment period. These reports

were updated; they contained new information and they

were updated correctly in accordance with the

guidelines of NUREG-0161. Many reports were promised

to be updated by a specific date by the licensee; the

updated reports were received by this date.

1984 LERs

The same comments are applicable to the 1984 LERs.

e)

Were Similar Occurrences Properly Referenced?

1983 LERs

Previous LER numbers of events of a similar nature

appeared to be referenced correctly. Because there

were many repetitive events, the licensee would only

reference the last few occurrences in lieu of all

previous occurrences. This is acceptable. The

licensee also freely referenced LER numbers of the

other unit. However, on LERs that did not reference

a previous event, the licensee did not provide a

statement to the effect that this is the first event

of this type. Without this statement, it is

uncertain if this is the first occurrence of the

event, or if the licensee failed to reference

previous occurrences.

1984 LERs

The above comments are also applicable to the 1984

LERs, but the proportion of reports without

references seemed higher.

2.

Multiple Event Reporting in a Single LER

No reviewed LER contained information in a single LER that

should have been reported in separate LERs.

3.

Prompt Notification Follow-Up Reports

Eighteen PNs were issued in the SALP assessment period.

Eleven of these events resulted in an LER and the

remaining seven events were clearly unreportable. So, the

licensee appears to be reporting all events that are

required to be reported.

37

Table 1 - Inspection Activity and Enforcement Summary

(6/01/83 -

9/30/84)

Inspections Conducted

Enforcement Items

Functional

Inspection*

Percent

Severity Level**

Area

Hours

Effort

I II III IV V

1. Plant Operations

3924

61

4

2. Radiological

514

8

2

1

Controls

3. Maintenance

143

2

4. Surveillance

205

3

1

5. Fire Protection

87

1

3

6. Emergency

302

5

Preparedness

7. Security and

154

3

Safeguards

8. Refueling

9. Quality Programs

982

13

1

and Administrative

Controls Affecting

Safety (includes

Unit 1 modifications)

10. Licensing

0

0

11. Startup Testing

233

4

(Unit 3)

TOTALS

6,544

100

0

0

6

6 0

  • Allocation of inspection hours vs. functional areas are approximations based

upon inspection report data. Resident inspector hours not assigned to another

specific area were counted as Plant Operations effort.

(10 CFR Part 2, Appendix C).

38

Table 2 - Licensee Event Reports, Unit 1 (6/01/83 -

9/30/84)

LER No.1

Description

(83-001)

Temporary loss of automatic loading for the #1 diesel generator.

(83-002)

Bent upper lateral braces of the Spent Fuel pit storage racks.83-003

Oil change performed on the wrong charging pump resulted in all

three pumps out of service.

(83-004)

Outside air entering the control room bypassed the Control Room

Emergency Air Treatment System filters and charcoal absorber.

(83-005)

Inadvertent SI resulted in increased RCS pressurize and actuation

of the PORV.83-006

Pressurizer level increase 2 to 3% per day while at 50% due to

(Infor-

increased nitrogen pressure in the VCT.

mational

Report)84-001

Tear gas on the San Onofre Site.84-002

Spurious starting of No. 2 Diesel Generator.84-003

No. I 125-VDC battery less than required capacity.84-004

Results of inspection of the overspeed governoor/fuel

(Infor-

transfer pump on Transamerica Delaval, Inc., Diesel

mational)

Generator No. 2.84-005

Two boric acid flow paths were blocked due to boric acid

solidification in the flow path piping.84-006

Containment Fire Protection System inoperable during ILRT.84-007

Delinquent approvals of temporary change notices.84-008

Corrosion of intake structure

reinforcing steel apparently due to

long term chloride penetration into

the soil.

1 The 1983 reports enclosed in parenthesis were 14-day LERs; the reports

not enclosed by a parenthesis were 30-day LERs. All 1984 reports were

submitted pursuant to a 30-day reporting requirement.

(

39

Table 2 -

Licensee Event Reports, Unit 2 (6/01/83 -

9/30/84)

LER No.

Description

(83-10)*

Failure of control room emergency air cleanup system to

maintain the required positive pressure due to air leakage

from control room boundary.83-043

Failure of the auxiliary feedwater feedwater pump to manually

start.83-044

Kirk key interlock operation of HPSI pumps found to have an

electrical continuity within breaker contacts.83-045

Reactor trip circuit breaker associated with Plant Protection

System channel A tripped open, rendering channel A inoperable.83-046

Reactor Coolant Cold Leg Temperature was observed outside the

limits.

83-047*

Inoperable Toxic Gas Isolation System train "A" due to a

discharged battery supply and a misaligned alarm setpoint.

83-048*

Pilot flames of trains "A" and "B" Toxic Gas Isolation System

butane/propane monitors experienced persistent flame-out.

83-049*

Emergency Chiller failed to start following an invalad TGIS

due to misalignment of its supply breaker in its cubicle.83-050

Core protection calculator declared inoperable since it

experienced more than two automatic restarts during

the preceeding 12-hour interval.

83-051*

Control room emergency air cleanup system train A inoperable

due to failure of the control room complex isolation damper

to close.83-052

Purge/vent stack radiation monitor inoperable for greater

(Special

than 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

report)83-053

Inoperable containment atmosphere gaseous radioactivity monitors

due to unauthorized manipulation of the set point controller.83-054

Misaligned control element assembly (CEA) due to sluggishness

of CEA grippers.

83-055*

Excess oxygen concentration in the waste gas holdup system.

40

Table 2 - Licensee Event Reports, Unit 2 (Cont'd)

LER No.

Description 83-056

Inoperable core protection calculator (CPC) D due to the loss

of a CPC cabinet cooling fan (due to a degraded power supply).

83-057*

Inoperable fire panel due to a smoke detector that was

incorrectly rewired following HVAC and lighting work.83-058

Inoperable core protection calculator channel B attributed to

a multipurpose acquisition and control system error Code 10.83-059

Inoperable train A component cooling water system (CCWS) due

to a broken oil feeder line for a CCWS pump.

83-060*

Failure to maintain a continous fire watch while the deluge

water spray system was inoperable.83-061

Inoperable core protection calculator Channel C due to cold leg

temperature resistance to current converter being out of

calibration.83-062

Secondary coolant system sampling and analysis for specific

activity had not been performed in the required time.

(83-063)

Motor-driven AFW pump failed to complete its 48-hour endurance

run.83-064

DNBR not within acceptable limits while the core operating limit

supervisory system was out of service.83-065

Misaligned control element Assemblies (CEA) due to malfunctioning

of the upper gripper on the CEA.83-066

Inoperable control room emergency air cleanup system due to

emergency chilled water unit failure to start.

(83-067)*

Fire panel 3L-198 failed a routine 6-month surveillance and

compensatory measures prescribed were not implemented.

(83-068)

Reactor coolant system hot leg sampling nozzle loads were

determined to exceed stress limits considered acceptable by CE.83-069

Inoperable control element assembly calculator (CEAC) 1 due to

intermittent and erractic position indication from CEA 20.83-070

Turbine-driven auxiliary feedwater pump (AFW) declared inoperable

in order to isolate two steam leaks in the line to the AFW pump.

41

Table 2 -

Licensee Event Reports, Unit 2 (Cont'd)

LER No.1

Description 83-071

Inoperable diesel generator due to failure to start during

surveillance testing.

(83-072)

Circulating water system traveling screen water level differential

pressure was offscale indicating clogging of the screens.

(83-073)

Inoperable core protection calculator (CPC) channels B and D

due to incorrect CPC constants.

(83-074)

While the turbine building sump effluent monitor was inoperable.

A scheduled grab sample was not taken and analyzed while releases

were being made.83-075

Regulating CEA's (Group 6) exceeded the time allowed below the

long term stead state insertion limit.

83-076*

Extinguished pilot flames of trains "A" and "B" toxic gas isolation

system butane/propane monitors.83-077

Inoperable core protection calculator channel D due to several

spurious trips.83-078

Condensate storage tank water level fell below the technical

specification limit due to water demand higher than make-up to

tank.

(83-079)

Failure to maintain one operable isolation valve in a penetration.83-080

Inoperable reactor coolant boronometer due to leaks at its

connection flange and the flange between the flow indicator and

adjacent check valve.83-081

Inoperable turbine stop valve due to failure of the valve to

reopen after stroking closed.

83-082*

Failure of the supervisory circuit for nine zones due to an

inadvertent circuit interruption by a contract electrician.83-083

Inoperable steam generator wide range level indicator due to

gas entrapped in the instrument's sensing line when

last calibrated.

42

Table 2 - Licensee Event Reports, Unit 2 (Cont'd)

LER No.

Description 83-084

Inoperable core protection calculator due to a low power supply

voltage trip.83-085

Transfer of normal power supply to the safety related KV bus

due to an opened breaker.83-086

Indication on subcooled margin monitor "A" failed to zero.83-087

Inoperable control element assembly calculator (CEAC) #1 when CEA

  1. 20 analog position indication appeared faulty.83-088

The power supply voltage on the channel D plant protection system

was found to be out of the specified range.83-089

Inoperable train "B" salt water cooling system (SWCS) when the

flow rate was determined to be less than required.83-090

A misaligned control element assembly due to intermittent loss of

power to the control element drive mechanism control system power

switch.

83-091*

A fire barrier penetration seal in the cable riser room was

discovered to be inoperable due to an error in construction.83-092

On two occasions a containment airborne radiation monitor was

rendered inoperable when the associated sample pump motor

breaker tripped. The redundant monitor was out of service.

83-93

Annual surveillance test for fire suppression valves not completed

within the required surveillance interval, and compensatory

measures prescribed were not implemented.

83-94

Fire detector electrical panel failed the supervisory circuit

surveillance test.

83-95

Heat detectors failed the 6-month surveillance test.83-096

Misaligned control element assembly (CEA) due to dirty contacts

on the CEA timer card.

83-097*

Spurious fire protection system deluge actuation.83-098

Inoperable control element assembly calculator (CEAC) 2 due to

inaccurate position indication on three target CEA's.

43

Table 2 -

Licensee Event Reports, Unit 2 (Cont'd)

LER No.

Description 83-099

Inoperable pressurizer level instrumentation when its recorder

pen failed to track.83-100

Inoperable component cooling water return containment isolation

valve when control power to the valve was lost.

83-101*

Inoperable Toxic Gas Isolation System train B when the chlorine

analyzer spuriously actuated and could not reset.83-102

Misaligned control element assembly due to a malfunction in the

upper gripper.83-103

Tc observed outside the limits following a rapid reduction in

power.83-104

Purge/vent stack monitor discovered to have low flow and was

declared inoperable.

83-105*

Pilot flames of trains "A" and "B" Toxic Gas Isolation System

butane/propane monitors were found extinguished.

(83-106)

QA audit revealed the 125V battery bank had unsatisfactory results

during a surveillance test, but no required actions were taken.83-107

Diesel generator building pre-action flame detector alarmed and

could not be reset.83-108

Turbine governor valve failed to reopen after testing trip

solenoid "A" due to a stuck plunger.83-109

During ISI valve testing, containment isolation valve gave a

steady dual indication following a demand to close, rendering the

valve inoperable.

(83-110)

Failure of train B emergency chiller to start due to a fuse

failure.

83-111*

Inoperable penetration seals of fire rated barriers due to

damage during construction activities.

(83-112)*

Forty-one (41) heat detectors were found in zone 12, but 42 heat

detectors were required by technical specifications.83-113

CEAC 2 had 3 auto-restarts within the previous 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> and a

required channel functional test was not completed within the

time limit.

Table 2 -

Licensee Event Reports, Unit 2 (Cont'd)

LER No.

Description 83-114

Containment isolation valve gave a dual indication of its position

and was rendered inoperable.83-115

During a surveillance the TGIS train "A" amonia analyzer was

declared inoperable due to a change of amplifier gain.83-116

With the core operating limit supervisory system out of service,

calculations indicated DNBR margin was not within allowable limits.

(83-117)

Pressurizer level instrument on essential plant parameters

monitoring system panel varied from its correct reading by 15%.83-118

Containment isolation valve was found locked open.83-119

Tc dropped below technical specification limits due to a

restrictive Tc limit.83-120

Failure of the iodine removal system flow control valve to open

due to a cracked o-ring.83-121

With the core operating limit supervisory system out of service,

calculations indicated DNBR margin was not within allowable limits.83-122

CPC channel D had more than 3 auto-restarts in the previous 12 hr.

period and was declared inoperable due to failure of its power

supply.

83-123*

Two inoperable electrical penetration seals in the auxiliary

building control area.83-124

Inoperable control element assembly calculator (CEAC) 2 due to

spurious position indication from CEA 20.

(83-125)

Three reactor trip breakers demonstrated anomalous behavior

during surveillance testing when their under voltage devices were

tested.83-126

Surveillance of NIS safety channels not completed within the

required surveillance interval.

83-127*

Inoperable fire rated assemblies in various fire zones.83-128

A containment mini-purge in progress, containment airborne

radiation monitor channel C was discovered to be in alarm defeat.

'I

45

Table 2 -

Licensee Event Reports, Unit 2 (Cont'd)

LER No.

Description 83-129

With the core operating limit supervisory system out of service,

calculations indicated DNBR margin was not within allowable limits.

(83-130)*

Train B emergency chiller tripped and was declared inoperable.83-131

With the core operating limit supervisory system out of service,

calculations indicated DNBR margin was not within allowable limits.83-132

Inoperable steam generator remote shutdown monitoring

instrumentation pressure indicator.83-133

During a reactor trip the excore linear power level channel C

failed due to a failed linear amplifier card.83-134

Unacceptable actuation time of the CCW pump sequence timer relay.83-135

Core Protection calculator channel C declared inoperable following

a spurious trip.

83-136*

Inoperable data gathering panel when a ground fault alarm was

received.

83-137*

Train A containment emergency cooling unit failed to meet

acceptance criteria.83-138

Containment isolation valve failed to close during the waste gas

quarterly valve test due to a loose connection on the terminal

block in the closing circuit.

83-139*

TGIS train "B" chlorine analyzer spuriously initiated and was

declared inoperable.83-140

Inoperable electrically driven fire pump due to an open local

controller shut off switch.83-141

Incorrect control element assembly position indication caused a

reactor trip on a low DNBR signal.

83-142*

Inoperable cable tray fire barriers in various fire zones.83-143

Failure to report an inoperable snubber in the time required.

83-144*

Excessive oxygen concentration in the waste gas holdup system.83-145

Inoperable PPS channel C excore safety channel.

(83-146)

Safety injection tanks exceeded their nitrogen pressure limit.

83-147*

Inoperable control room emergency air cleanup system train "A"

when control room fan failed to automatically start on a TGIS

signal.

46

Table 2 -

Licensee Event Reports, Unit 2 (Cont'd)

LER No.

Description

83-148*

Inoperable diesel driven fire pump starting battery due to a low

electrolyte level in the fire pump battery.83-149

Not issued.

83-150*

A power supply overload protection circuit in fire detection Data

Gathering Panel deenergized the panel, rendering it inoperable.83-151

Tc dropped below the allowable limits previous to a manual reactor trip. Following the trip, a condensate storage tank level dropped

below the allowable limit.83-152

Inoperable remote shutdown boronometer due to a failed display.83-153

Reactor trip breaker undervoltage trip device exhibited

(Infor-

scattered and unacceptable response times.

mational)83-154

Inoperable pressurizer level transmitter due to an empty reference

leg.83-155

Inoperable control element assembly calculator (CEAC) 1 due to

spurious position indication on CEA 20.83-156

Inoperable snubber on the main steam supply line to the auxiliary

feed pump turbine. Also, failure to complete the required

engineering evaluation for the steam supply line as required.84-001

Deficiencies in the fire protection program.84-002

Spurious actuation of the containment purge isolation system due

to an electrical noise spike.84-003

Containment purge isolation system actuation due to a conservatively

established setpoint.83-004

Spurious actuation of containment purge isolation system due to

an electrical noise spike.

84-005**

Flow rate estimates required were not being performed.84-006

Spurious Toxic Gas Isolation System actuations.84-007

Spurious main steam isolation signal due to voltage fluctuations.

0470

Table 2 -

Licensee Event Reports, Unit 2 (Cont'd)

1

LER No.

Description 84-008

Failure of plant monitoring system resulted in inadvertent mode 3

entry.

84-009**

Decalibration of calculated static thermal power.84-010

Partial loss of extraction steam feedwater heating resulted in a

reactor power surge.84-011

Containment purge isolation system actuation due to the failure of

containment airborne monitor gaseous channel "C".

84-012**

Spurious Toxic Gas Isolation System actuations.84-013

Containment negative pressure limit exceeded due to

misinterpretation of the venting procedure.

84-014*

Reactor coolant system flow rate verification not determined as

according to technical specifications.

84-015*

Fire protection program discrepancies.84-016

Inadvertent ESF actuations due to a technician error.84-017

Shutdown cooling valve found fully open contrary to surveillance

requirements.

84-018*

Manual control room isolation system actuation when a dirty

filter caused a low flow alarm.84-019

A false position indication caused control element assembly

calculator to generate a reactor trip on low DNBR.84-020

High steam generator level trip.

84-021**

Spurious Toxic Gas Isolation System actuations.

84-022*

Automatic control room isolation system actuation due to electrical

spikes.

84-023*

Automatic control room isolation system actuations due to electrical

spikes.

84-24*

Fire protection program discrepancies.84-025

Reactor trip breaker undervoltage device anomaly.

(Infor

mational)

84-026*

Spurious Toxic Gas Isolation System actuations.

84-027**

Waste gas processing system valve failure resulting in a

release of Xe-133.

480

Table 2 - Licensee Event Reports, Unit 2 (Cont'd)

LER No.

Description

84-028**

Waste gas sampling system valve failure resulting in a release of

Xe-133.

84-029**

Inadvertent de-energization of emergency chiller due to personnel

error.

84-030*

Fire protection program discrepancies.

84-031**

Inoperable emergency chiller due to microswitch malfunction.84-032

Spurious Toxic Gas Isolation System actuations.

84-033**

Leakage through the hydrostatic test boundary valves, pressurized

the entire firemain, causing a break in the piping.84-034

Failure to establish a fire watch.84-035

Containment purge isolation system actuation due to a brief

increase in airborne activity following maintenance.

84-036**

Deficiency with the high pressure safety injection motor

(Infor-

operated loop isolation valves.

mational)

84-037**

Spurious Toxic Gas Isolation System actuations.

84-038**

Spurious control room isolation system actuations due to electrical

noise spikes.

84-039**

Missed in-service inspection test on shutdown cooling heat

exchanger valves.84-040

Main steam isolation system inadvertent actuation due to a

technician error.

84-41*

Fire protection program discrepancies involving cable separation

and fire wraps.84-042

Spurious Toxic Gas Isolation System actuations.84-043

DNBR reactor trip due to erroneous control element assembly

position indication.

84-044**

Actuation of Toxic Gas Isolation System due to fumes from a

cleaning solvent.

49

Table 2 - Licensee Event Reports, Unit 2 (Cont'd)

LER No.1

Description 84-045

Inoperable charging pump due to leakage from a crack on the

cylinder block.

84-046*

Inoperable Component Cooling Water Trains.

84-047*

Spurious control room isolation system actuations due to noise

spikes.84-048

Delinquent Surveillance of the Electrical Power Systems.

1. The 1983 reports enclosed in parenthesis were 14-day LERs; the

reports not enclosed by a parenthesis were 30-day LERs. All 1984

reports were submitted pursuant to a 30-day reporting requirement.

  • Common system LER for Units 2 and 3
    • LER for Unit 2, but applies to Units 2 and 3.

50

Table 2 -

Licensee Events Reports, Unit 3 (6/01/84 -

9/31/84)

LER No.1

Description 83-034

Qualified safety parameter display system found to have the

potential for a loss of indication during and after a seismic

event.83-038

Inoperable fire spray system and fire detection instrumentation

due to corrosion of the panel internals caused by water

intrusion from improper closure of the panel.

(83-039)

See Unit 2, LER No.83-063.

(83-040)

See Unit 2, LER No.83-068.

(83-041)

See Unit 2, LER No.83-072. 83-042

Early warning fire detectors found inoperable due to a melted

element in the fusible heat detector.

(83-043)

Emergency chilled water unit failed to start during Control Room

Emergency Air cleanup system surveillance testing.

(83-044)

Contrary to technical specifications, a manual containment

isolation valve was opened.83-045

Damaged fire barrier penetration seals in the diesel generator

building.

(83-046)

Inoperable diesel generators due to isolation of the normal

diesel fuel supply from the fuel transfer pumps to each of

the day fuel tanks.83-047

Inadvertent actuation the deluge spray system.83-048

See Unit 2, LER No.83-110

83-049

Low volume control tank level due to a lifted relief valve that

failed to reseat.83-050

The outer containment airlock door jammed in the open position.83-051

Low flow readings from the condenser air elector monitor.83-052

See Unit 2, LER No.83-085

83-053

Boronometer declared inoperable due to readings drifting downward.83-054

Inoperable Containment Spray Chemical Storage Tank.

S0

51

Table 2 - Licensee Event Reports, Unit 3 (Cont'd)

LER No.

Description 83-055

Core protection calculator channel A was declared inoperable

due to a failed high reactor coolant cold leg temperature input.83-056

Level indication for fuel oil storage tank was discovered to be

off-scale low rendering the associated diesel generator

inoperable.83-057

Inoperable system generator wide range level indicator.83-058

Inoperable containment isolation valve due to poor position

indications.83-059

Inoperable main steam line radiation monitor.83-060

Inoperable control element assembly calculator 1 and core

protection calculator channel B.83-061

Inoperable pressurizer pressure indicator.83-062

Failure of control element assembly shutdown group to maintain

position.83-063

Inoperable steam-driven auxilary feedwater pump due to steam

inlet valve not opening completely.83-064

Inoperable excore logarithmic power safety channel C and B due

to failed connectors.83-065

Inoperable high range in-containment radiation monitor due to

a failed low condition.83-066

Excessive auto restarts of the control element assembly

calculator 2.83-067

Partial trip of the individual supply breaker for part length

CEA 32 rendered the CEA incapable of withdrawal.

(83-068)

Violation of LCO 3.0.4 when mode change was made while control

room cabinet area emergency air conditioning was out for

maintenance.83-069

Inoperable condenser air ejector wide range gas monitors.83-070

Control element assembly calculator inoperable due to control

element assembly is giving spurious indication of rod movement.

52

Table 2 -

Licensee Event Reports, Unit 3 (Cont'd)

LER No.

Description 83-071

Unusual event due to an unidentified leakage of 1.19 gpm.83-072

Containment water level-wide range train B instrumentation

failed during a channel check.

(83-073)

Technical specifications violated when charging and letdown

flows were isolated.83-074

Inoperable containment airborne radiation monitor.83-075

Inoperable low pressure turbine stop valve due to a piece of

wood between the disc and the seat.83-076

Inoperable control element assembly calculator 2.83-077

Fire detection and actuation panel failed a 6-month supervisory

circuit surveillance test.83-078

Inoperable boronometer due to the isolation of the charging and

letdown.83-079

Failure of core protection calculator channel A.83-080

While performing a Reactor Coolant System Water Inventory

Balance, tc dropped below minimum temperature (544 0F).83-081

RCS water inventory balance was not completed within the required

surveillance interval.83-082

Inoperable qualified safety parameter display system train B

due to a failed circuit board.83-083

A diesel generator tripped during surveillance testing and could

not be restarted.83-084

During a monthly surveillance, the auxiliary feedwater flow rate

channel was declared inoperable.83-085

The low pressure turbine no. 1 intercept valve failed the trip

solenoid A and B tests due to a failed logic card in the control

circuit.83-086

Inoperable control element assembly calculator (CEAC) 2 due to

technician error.

53

Table 2 -

Licensee Event Reports, Unit 3 (Cont'd)

LER No.

Description

(83-087)

Plant monitoring system computer failed while the plant was

under special test exception.83-088

Reactor coolant system hot leg sample valve showed intermediate

2

indication and could not be closed from the control room.83-089

AFW pump was declared inoperable to replace a broken torque

switch on the motor operator for a steam inlet valve.83-090

Fire detector electrical panel failed a 6-month surveillance test.83-091

The undervoltage armatures for reactor trip breakers were found

not to be fully picked up.83-092

Core protection calculator B was declared inoperable due to trips

received from a faulty RTD.83-093

Core protection calculator (CPC) and excore linear power level

(ELPL) channel C were declared inoperable while CPC and ELPL

channel D were out of service.83-094

Plant protection system channel C was observed to be in the

tripped condition.83-095

Inoperable channel A accident monitoring instrumentation for the

pressurizer water level indication due to erroneously high level

indication.83-096

AFW pumps rendered inoperable to allow repairs on emergency

feedwater actuation system no. 1 circuitry.83-097

Misaligned control element assemblies (CEA) due to sluggishness

of CEA grippers.83-098

Qualified safety parameter display system channel A was

continuously cycling through the pages of its display, and

was declared inoperable.93-099

Failure of the steam driven auxiliary feedwater pump to start

during a reactor trip due to the pump being in the tripped

condition.83-100

Constant alarm state of containment airborne radiation monitor

rendered the leak detection system gaseous channel inoperable.83-101

Core protection calculator channel B experienced more than 3

auto-restarts within the previous 12-hour period.

0

54

Table 2 -

Licensee Event Reports, Unit 3 (Cont'd)

LER No.

Description 83-102

Failure of channel A of the post Loss of Coolant Accident (LOCA)

hydrogen monitor.83-103

During plant stabalization following a manual trip, the

condensate storage tank level dropped below the technical

specification limit.83-104

Inoperable auxiliary feedwater (AFW) flow rate channel due to

erroneously high AFW flow rate indication when no flow existed.83-105

Mini-purge exhaust containment isolation valve failed to close

within its maximum isolation time.83-106

With the core operating limit supervisory system out of service,

calculations indicated that the DNBR was not within allowable

limits.83-107

Inoperable train A containment emergency cooling unit and train B

diesel generator.83-108

Inoperable qualified safety parameter display system channel A.83-109

Qualified safety parameter display system channel A began

intermittently failing and was declared inoperable.83-110

Misaligned control element assemblies (CEA) due to sluggishness

of CEA grippers.83-111

Reactor coolant system specific activity exceeded 1.0

microcurie/gram dose equivalent 1-131.83-112

Regulating group 6 control element assemblies exceeded the time

allowed below the long term steady state insertion limit.83-113

Failure of control element assembly calculator 2 due to a 83-114

Nitrogen cover pressure in the safety injection tank was below

the minimum value.83-115

Inoperable core protection calculator channel C due to a failed

module card.83-116

Reactor trip breaker under voltage trip device exhibited a

(Infor-

procedurally unacceptable response.

mational

Report)

w

55

Table 2 -

Licensee Event Reports, Unit 3 (Cont'd)

LER No.

Description 83-117

Misaligned control element assembly due to a faulty IC chip on

the rod's timer card.83-118

With the core operating limit supervisory system out of service,

calculations indicated that the DNBB was not within allowable

limits.83-119

Inoperable core protection calculator channel A due to the

multipurpose aquistion and control system error code 10.83-120

During plant stabalization following a manual trip, the

condensate storage tank level dropped below the technical

specification limit.84-001

Precautionary evacuation of personnel due to an inadvertent

release of radioactive material.84-002

Hourly fire watch patrols were suspended following evacuation

of the Penetration Building due to airborne iodine and

noble gas concentrations.84-003

Reactor trip due to control element assembly slipping thirty

inches.84-004

Inadvertent safety injection actuation due to dirty contacts

on the "relay hold" pushbutton.84-005

Reactor Coolant System dose equivalent iodine limits exceeded

(dated

due to iodine spiking following a power change.

2/6/84)84-006

Reactor trip breaker #8 undervoltage device did not actuate.84-007

Spurious Reactor Protection System trip.84-008

Reactor trip on loss of load.84-009

Inoperability of containment spray system.84-010

Spurious Containment Purge Isolation System Actuations84-011

Disconnected leads in plant protection system cabinets.84-012

Failure of main steam isolation valves to meet technical

specification surveillance requirements.

56

Table 2 -

Licensee Event Reports, Unit 3 (Cont'd)

LER No.

Summary Description 84-013

Reactor coolant system dose equivalent iodine limits exceeded

due to iodine spiking following a power change.84-014

Charging pumps inoperable due to the failure of the discharge

check valve and discharge relief valve.84-015

Dose equivalent iodine limits exceeded and RCS samples were

not taken and analyzed as required.84-016

Reactor trip breaker undervoltage trip device exhibited an

unacceptable response time.84-017

High steam generator water level reactor trip during routine

reactor shutdown.84-018

Reactor trip breaker undervoltage trip device exhibited an

(Infor-

unacceptable response time.

mational

Report)84-019

Post maintenance testing on containment isolation valves was

not performed as required.84-020

Missed condenser evacuation system sample because the sample pump

was isolated.84-021

Actuation of the safety relief valve on the nuclear sample system.84-022

Failure in the turbine control system caused a "loss of load"

reactor trip.84-023

Reactor Coolant System Dose equivalent iodine limits exceeded

due to iodine spiking following a power change.84-024

Reactor trip on low DNBR due to hardware failure on one of five

computer boards.84-025

Containment pressure transmitter inoperable due to closed

isolation valve.84-026

Containment purge isolation system actuation due to equipment

failure.84-027

Missed iodine and particulate sample following a reactor trip.84-028

Delinquent processing of overtime request forms.

57

Table 2 -

Licensee Event Reports, Unit 3 (Cont'd)

LER No.

Description 84-029

Reactor power increase above rated power due to partial loss of

extraction system feedwater heating.84-030

Containment purge isolation system actuation due to a spurious

instrument fail signal.84-031

Containment purge isolation system actuation.84-032

High steam generator water level reactor trip during manual

operation of the feedwater control system.84-033

Condensate storage tank flow path blocked.84-034

Fire protection discrepancy due to missing conduit fire wrapping.

1. The 1983 reports enclosed in parenthesis

were 14-day LERs; the reports not enclosed

by a parenthesis were 30-day LERs. All 1984

reports were submitted pursuant to a 30-day

reporting requirement.