ML083010454

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IR 05000440-08-004 on 07/01/2008 - 09/30/2008 for Perry
ML083010454
Person / Time
Site: Perry FirstEnergy icon.png
Issue date: 10/27/2008
From: Jamnes Cameron
NRC/RGN-III/DRP/RPB6
To: Bezilla M
FirstEnergy Nuclear Operating Co
References
EA-07-199, FOIA/PA-2010-0209 IR-08-004
Download: ML083010454 (53)


See also: IR 05000440/2008004

Text

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION III

2443 WARRENVILLE ROAD, SUITE 210

LISLE, IL 60532-4352

October 27, 2008

EA-07-199

Mr. Mark Bezilla

Site Vice President

FirstEnergy Nuclear Operating Company

Perry Nuclear Power Plant

P. O. Box 97, 10 Center Road, A-PY-290

Perry, OH 44081-0097

SUBJECT:

PERRY NUCLEAR POWER PLANT NRC INTEGRATED INSPECTION

REPORT 05000440/2008004

Dear Mr. Bezilla:

On September 30, 2008, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Perry Nuclear Power Plant. The enclosed report documents the inspection

findings which were discussed on October 14, 2008, with you and members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, three NRC-identified findings and four self-revealed

findings of very low safety significance were identified (Green). Five of the seven findings

involved violations of NRC requirements. Additionally, three licensee-identified violations are

listed in Section 4OA7 of this report. However, because of the very low safety significance and

because the issues were entered into your corrective action program, the NRC is treating these

issues as Non-Cited Violations (NCVs) in accordance with Section VI.A.1 of the NRCs

Enforcement Policy.

If you contest the subject or severity of any NCV in this report, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the U.S.

Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC

20555-0001; with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission,

Region III, 2443 Warrenville Road, Suite 210, Lisle, IL 60532-4352; the Director, Office of

Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the

NRC Resident Inspectors Office at the Perry Nuclear Power Plant.

M. Bezilla

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Jamnes L. Cameron, Chief

Reactor Projects Branch 6

Docket No. 50-440

License No. NPF-58

Enclosure:

Inspection Report 05000440/2008004

w/Attachment: Supplemental Information

cc w/encl:

J. Hagan, President and Chief Nuclear Officer - FENOC

J. Lash, Senior Vice President of Operations and

Chief Operating Officer - FENOC

D. Pace, Senior Vice President, Fleet Engineering - FENOC

J. Rinckel, Vice President, Fleet Oversight - FENOC

P. Harden, Vice President, Nuclear Support

Director, Fleet Regulatory Affairs - FENOC

Manager, Fleet Licensing - FENOC

Manager, Site Regulatory Compliance - FENOC

D. Jenkins, Attorney, FirstEnergy Corp.

Public Utilities Commission of Ohio

C. OClaire, State Liaison Officer, Ohio Emergency Management Agency

R. Owen, Ohio Department of Health

M. Bezilla

-2-

In accordance with 10 CFR 2.390 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRC's document system

(ADAMS), accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html

(the Public Electronic Reading Room).

Sincerely,

/RA/

Jamnes L. Cameron, Chief

Reactor Projects Branch 6

Docket No. 50-440

License No. NPF-58

Enclosure:

Inspection Report 05000440/2008004

w/Attachment: Supplemental Information

cc w/encl:

J. Hagan, President and Chief Nuclear Officer - FENOC

J. Lash, Senior Vice President of Operations and

Chief Operating Officer - FENOC

D. Pace, Senior Vice President, Fleet Engineering - FENOC

J. Rinckel, Vice President, Fleet Oversight - FENOC

P. Harden, Vice President, Nuclear Support

Director, Fleet Regulatory Affairs - FENOC

Manager, Fleet Licensing - FENOC

Manager, Site Regulatory Compliance - FENOC

D. Jenkins, Attorney, FirstEnergy Corp.

Public Utilities Commission of Ohio

C. OClaire, State Liaison Officer, Ohio Emergency Management Agency

R. Owen, Ohio Department of Health

DOCUMENT NAME: G:\\PERRY\\PERR 2008 004.DOC

G Publicly Available

G Non-Publicly Available

G Sensitive

G Non-Sensitive

To receive a copy of this document, indicate in the concurrence box "C" = Copy without attach/encl "E" =

Copy with attach/encl "N" = No copy

OFFICE

RIII

RIII

RIII

RIII

NAME

JCameron:cms

DATE

10/27/08

OFFICIAL RECORD COPY

Letter to M. Bezilla from J. Cameron dated October 27, 2008

SUBJECT:

PERRY NUCLEAR POWER PLANT NRC INTEGRATED INSPECTION

REPORT 05000440/2008004

DISTRIBUTION:

RidsNrrPMPerry

RidsNrrDorlLpI3-2

RidsNrrDirsIrib Resource

Tamara Bloomer

Mark Satorius

Kenneth Obrien

Jared Heck

Carole Ariano

Linda Linn

Cynthia Pederson

DRPIII

DRSIII

Patricia Buckley

Tammy Tomczak

ROPreports@nrc.gov

Enclosure

U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No:

50-440

License No:

NPF-58

Report No:

050000440/2008004

Licensee:

FirstEnergy Nuclear Operating Company (FENOC)

Facility:

Perry Nuclear Power Plant, Unit 1

Location:

Perry, Ohio

Dates:

July 1, 2008 through September 30, 2008

Inspectors:

M. Franke, Senior Resident Inspector

M. Wilk, Resident Inspector

T. Taylor, Reactor Engineer

J. Robbins, Reactor Engineer

D. Reeser, Operations Engineer

R. Murray, Reactor Engineer

M. Phalen, Health Physicist

R. Baker, Resident Inspector, Duane Arnold Energy Center

Observer:

E. Denison, Ohio Department of Health

Approved by:

Jamnes L. Cameron, Chief

Branch 6

Division of Reactor Projects

Enclosure

TABLE OF CONTENTS

SUMMARY OF FINDINGS .........................................................................................................1

REPORT DETAILS.....................................................................................................................5

Summary of Plant Status.........................................................................................................5

1.

REACTOR SAFETY.....................................................................................................5

1R01

Adverse Weather Protection (71111.01) ............................................................5

1R04

Equipment Alignment (71111.04).......................................................................6

1R05

Fire Protection (71111.05) .................................................................................7

1R06

Flood Protection Measures (71111.06) ............................................................11

1R11

Licensed Operator Requalification Program.....................................................11

1R12

Maintenance Effectiveness (71111.12) ............................................................12

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13)........13

1R15

Operability Evaluations (71111.15) ..................................................................16

1R19

Post-Maintenance Testing (71111.19) .............................................................18

1R22

Surveillance Testing (71111.22).......................................................................19

1EP6

Drill Evaluation (71114.06)...............................................................................21

2.

RADIATION SAFETY.................................................................................................21

2OS1

Access Control to Radiologically Significant Areas (71121.01) ........................21

4.

OTHER ACTIVITIES ..................................................................................................24

4OA1

Performance Indicator Verification (71151)......................................................24

4OA2

Identification and Resolution of Problems (71152)...........................................27

4OA3

Follow-up of Events and Notices of Enforcement Discretion (71153)...............31

4OA6

Meetings..........................................................................................................38

4OA7

Licensee-Identified Violations ..........................................................................38

SUPPLEMENTAL INFORMATION .............................................................................................1

KEY POINTS OF CONTACT ..................................................................................................1

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED .......................................................1

LIST OF DOCUMENTS REVIEWED ......................................................................................3

LIST OF ACRONYMS USED ..................................................................................................8

1

Enclosure

SUMMARY OF FINDINGS

IR 05000440/2008004; 07/01/2008 - 09/30/2008; Fire Protection; Operability Evaluations;

Maintenance Risk Assessments and Emergent Work Control; Identification and Resolution of

Problems; Event Follow-up.

The inspection was conducted by resident and regional inspectors. The report covers a

3-month period of resident inspection. The significance of most findings is indicated by their

color (Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609 Significance

Determination Process (SDP). Findings for which the SDP does not apply may be "Green," or

be assigned a severity level after NRC management review. The NRC's program for

overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, "Reactor Oversight Process," Revision 4, dated July 2006.

A.

Inspector-Identified and Self-Revealed Findings

Cornerstone: Initiating Event

Green. A finding of very low safety significance was self-revealed on July 30, 2008.

While performing inspection and dewatering of an underground vault area, plant workers

inadvertently dropped a man-hole cover into the vault. The 15-foot vault area contained

125 Volts direct current control power conduits that supplied fault protection circuitry for

switchyard breakers. The licensee entered the issue into their corrective action

program.

This finding was considered more than minor because it was related to maintenance risk

assessment and risk management issues. Specifically, the licensee failed to manage

risk for maintenance activities associated with the electrical switchyard that could

increase the likelihood of initiating events by causing a loss of offsite power. The finding

was determined through a SDP analysis to be of very low safety significance as no

mitigation equipment or functions were affected. This finding had a cross-cutting aspect

in the area of Human Performance as defined in IMC 0305 H.4(a), because the

organization failed to ensure the use of human error prevention techniques

commensurate with the risk of the assigned task. No violation of NRC requirements

occurred. (Section 4OA3.2)

Green. A finding of very low safety significance was self-revealed on June 28, 2008,

when high radiation alarms for all four main steam lines were received in the control

room during a plant power maneuver. Specifically, maintenance technicians failed to

adhere to procedures and manipulated a hydrogen water chemistry control system while

performing a surveillance test associated with the plant off-gas system. The off-gas

system surveillance test procedure did not address operation of the hydrogen water

chemistry control system and the technicians were not trained to operate the system.

As part of their immediate corrective actions, the licensee corrected the system lineup to

reduce radiation levels and entered the issue into their corrective action program.

This finding was considered more than minor because the manipulation of plant systems

that are different from those specified in the authorized work procedure would become a

more significant safety concern if left uncorrected. In this case, the finding led to an

unexpected increase in radiation levels in areas accessible to plant personnel and was

associated with the operating equipment lineup of the configuration control attribute of

2

Enclosure

the Initiating Events Cornerstone and adversely affected the cornerstone objective of

limiting the likelihood of events that upset plant stability. The finding was determined

through a SDP analysis to be of very low safety significance as no mitigation equipment

or functions were affected and no actual increase in personnel exposure occurred. This

finding has a cross-cutting aspect in the area of Human Performance as defined in

IMC 0305 H.4(b), because the organization failed to ensure that personnel do not

proceed with a task in the face of uncertainty. No violation of NRC requirements

occurred. (Section 4OA3.3)

Mitigating System

Green. The inspectors identified a finding of very low safety significance and an

associated NCV of 10 CFR 50.65(a)(4) for failure to assess and manage the risk

associated with maintenance activity affecting the low pressure core spray system.

Specifically, the licensee removed floor plugs in the auxiliary building and failed to

implement risk control measures to assure operability of low pressure core spray. As

part of their immediate corrective actions, the licensee personnel re-installed building

floor plugs and returned low pressure core spray to an operable status.

The finding was considered more than minor because the licensee failed to prescribe

significant compensatory measures for external conditions; and if the practice were left

uncorrected, the issue would become a more significant safety concern. The finding

was of very low safety significance because the incremental core damage frequency

associated with the activity was less than 1 X 10-6. This finding has a cross-cutting

aspect in the area of Human Performance as defined in IMC 0305 H.3(a), because the

organization failed to adequately plan work activities that are associated with risk.

(Section 1R13.1)

Green. The inspectors identified a finding of very low safety significance and a NCV of

10 CFR 50.65(a)(4) for failure to implement a procedurally-required risk management

activity for a safety system protected train. The licensee failed to provide required

management oversight of work on emergency closed cooling 'A' while the plant was in

Yellow Risk. The licensee entered the issue into their corrective action program.

The finding was considered more than minor because the licensee failed to effectively

manage significant compensatory measures for an elevated risk condition; and if the

practice were left uncorrected, the issue would become a more significant safety

concern. The finding was of very low safety significance, because the incremental core

damage frequency associated with the activity was less than 1 X 10-6. This finding has a

cross-cutting aspect in the area of Human Performance as defined by IMC 0305 H.3(a),

because the organization failed to adequately plan work activities that are associated

with risk. (Section 1R13.2)

Green. The inspectors identified a finding of very low safety significance and an

associated NCV of the Perry Nuclear Power Plant Operating License Condition C(6).

During a maintenance activity, licensee personnel degraded a fire barrier in a manner

that was contrary to the procedural requirements of the Perry Plant Fire Protection

Program. As part of their immediate corrective action, the licensee restored the fire

barrier and entered the issue into their corrective action program.

3

Enclosure

The inspectors determined that the performance deficiency was more than minor in

accordance with IMC 0612, Appendix B, Issue Disposition Screening, because the

finding was associated with protection against external factors attribute of the Mitigating

Systems Cornerstone and affected the cornerstone objective of ensuring the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, by the inappropriate use of fixed impairments

on the fire doors between the diesel fire pump room and the emergency service water

pumphouse, the licensee removed a fire barrier which could impact safety-related

equipment. The finding was determined to be of very low safety significance during a

Phase 2 SDP review. This finding has a cross-cutting aspect in the area of Human

Performance as defined by IMC 0305 H.4(a), because the licensee did not ensure that

appropriate human error prevention techniques were used. (Section 1R05)

Green. A finding of very low safety significance and associated NCV of 10 CFR Part 50,

Appendix B, Criterion V, Instructions, Procedures, and Drawings, was self-revealed on

August 4, 2008, when contract workers bored a hole into a safety-related structure in an

inappropriate location. The workers did not use documented instructions, procedures, or

drawings when performing the work. As part of their immediate corrective actions, the

licensee conducted worker training and entered the issue into their corrective action

program.

The finding was determined to be more than minor because the finding was associated

with the design control attribute of Mitigating Systems Cornerstone and affected the

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. Specifically, the

licensee initiated work on a seismically qualified structure in the absence of an approved

work package and degraded the structure. The finding was determined to be of very low

safety significance because it did not result in safety system inoperability. This finding

had a cross-cutting aspect in the area of Human Performance as defined by

IMC 0305 H.4.(a), because the licensee failed to communicate human error prevention

techniques through a pre-job brief and personnel proceeded in the face of unexpected

circumstances. (Section 1R15)

Barrier Integrity

Green. A self-revealed finding of very low safety significance and an associated NCV of

10 CFR Part 50 Appendix B, Criterion 5 , Procedures, was identified on June 1, 2008,

when a containment airlock door seal failed during routine operations. On

March 26, 2008, the licensee failed to implement airlock maintenance procedures

appropriate to the circumstances and this led to a failure of the containment upper

airlock outer door seal. As part of their corrective actions, the licensee (1) conducted

worker training; (2) planned to revise the airlock maintenance procedures to include

additional guidance; (3) planned to increase maintenance frequency for the airlocks; and

(4) planned to reintroduce a requirement to grease the door mechanisms.

The finding was determined to be more than minor because it was associated with the

Procedure Quality attribute of the Barrier Integrity Cornerstone and affected the

cornerstone objective of providing reasonable assurance that physical design barriers

protect the public from radionuclide releases caused by accidents or events. The

inspectors determined that the finding was of very low safety significance because the

upper airlock inner door remained closed and the finding did not represent an actual

4

Enclosure

open pathway in the physical integrity of reactor containment. This finding has a cross-

cutting aspect in the area of Human Performance as defined in IMC 0305, H.2(c),

Resources, because the licensee did not ensure that procedures were complete and

were adequate to assure nuclear safety. (Section 4OA2)

B.

Licensee-Identified Violations

Three violations of very low safety significance that were identified by the licensee have

been reviewed by the inspectors. Corrective actions planned or taken by the licensee

have been entered into the licensees corrective action program. These violations and

corrective action tracking numbers are listed in Section 4OA7 of this report.

5

Enclosure

REPORT DETAILS

Summary of Plant Status

The plant began the inspection period at 100 percent power. On July 1, 2008, operators

reduced reactor power to 67 percent for planned maintenance and testing. The plant returned

to full power operation on July 2, 2008. On August 22, 2008, operators reduced reactor power

to about 93 percent to manage main condenser operations during warm weather conditions.

The plant returned to full power the next day. On September 14, 2008, operators reduced

reactor power to about 95 percent again due to warm weather and returned the plant to full

power on the same day. On September 20, 2008, operators reduced reactor power to about

60 percent for planned maintenance and testing. The plant returned to full power operation on

September 23, 2008. With the exception of planned downpowers for routine surveillance testing

and rod sequence exchanges, the plant remained at 100 percent power for the remainder of the

inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R01 Adverse Weather Protection (71111.01)

.5

Readiness For Impending Adverse Weather Condition - Severe Thunderstorm

Watch/Sighted Waterspout

a.

Inspection Scope

Since thunderstorms with potential tornados and high winds were forecast in the vicinity

of the facility for the week of July 21, 2008, the inspectors reviewed the licensees overall

preparations/protection for the expected weather conditions. The inspectors walked

down the ESW system, in addition to the licensees emergency alternating current (AC)

power systems, because their safety-related functions could be affected or required as a

result of high winds or tornado-generated missiles or the loss of offsite power. The

inspectors evaluated the licensee staffs preparations against the sites procedures and

determined that the staffs actions were adequate. During the inspection, the inspectors

focused on plant specific design features and the licensees procedures used to respond

to specified adverse weather conditions. The inspectors also toured the plant grounds to

look for any loose debris that could become missiles during a tornado. The inspectors

evaluated operator staffing and accessibility of controls and indications for those

systems required to control the plant. Additionally, the inspectors reviewed the Updated

Final Safety Analysis Report (UFSAR) and performance requirements for systems

selected for inspection, and verified that operator actions were appropriate as specified

by plant specific procedures. The inspectors also reviewed a sample of corrective action

program (CAP) items to verify that the licensee identified adverse weather issues at an

appropriate threshold and dispositioned them through the CAP in accordance with

station corrective action procedures. Documents reviewed are listed in the Attachment.

This inspection constituted one sample for readiness for impending adverse weather

conditions as defined in Inspection Procedure (IP) 71111.01-05.

6

Enclosure

b.

Findings

No findings of significance were identified.

.8

Readiness For Impending Adverse Weather Condition - Extreme Heat/Drought

Conditions

a.

Inspection Scope

The inspectors performed a detailed review during the week of July 14, 2008, of the

licensees procedures and preparations for operating the facility during an extended

period of time when ambient outside temperature was high and the ultimate heat sink

was experiencing elevated temperatures. The inspectors focused on plant specific

design features and implementation of the procedures for responding to or mitigating the

effects of these conditions on the operation of the emergency service water (ESW)

system and other selected systems. Inspection activities included a review of the

licensees adverse weather procedures, daily monitoring of the off-normal environmental

conditions, and that operator actions specified by plant specific procedures were

appropriate to ensure operability of the normal and emergency cooling systems.

Documents reviewed are listed in the Attachment.

This inspection constituted one sample for readiness for impending adverse weather

conditions as defined in IP 71111.01-05.

b.

Findings

No findings of significance were identified.

1R04 Equipment Alignment (71111.04)

.1

Quarterly Partial System Walkdowns

a. Inspection Scope

The inspectors performed partial system walkdowns of the following risk-significant

systems:

Division 3 diesel generator system during the week of August 25, 2008;

containment vessel and drywell purge system prior to welding replacement of

local leak rate test penetration V313-V314 test connection valve 1M14F0602,

during the week of September 22, 2008; and

high pressure core spray (HPCS) during a Division 1 outage during the week of

September 29, 2008.

The inspectors selected these systems based on their risk significance relative to the

Reactor Safety Cornerstones at the time they were inspected. The inspectors attempted

to identify any discrepancies that could impact the function of the system, and, therefore,

potentially increase risk. The inspectors reviewed applicable operating procedures,

system diagrams, UFSAR, Technical Specification (TS) requirements, outstanding work

orders (WOs), condition reports (CRs), and the impact of ongoing work activities on

redundant trains of equipment in order to identify conditions that could have rendered

7

Enclosure

the systems incapable of performing their intended functions. The inspectors also

walked down accessible portions of the systems to verify system components and

support equipment were aligned correctly and operable. The inspectors examined the

material condition of the components and observed operating parameters of equipment

to verify that there were no obvious deficiencies. The inspectors also verified that the

licensee had properly identified and resolved equipment alignment problems that could

cause initiating events or impact the capability of mitigating systems or barriers and

entered them into the CAP with the appropriate significance characterization.

Documents reviewed are listed in the Attachment.

These activities constituted three samples for partial system walkdowns as defined in

IP 71111.04-05.

b. Findings

No findings of significance were identified.

.2

Semi-Annual Complete System Walkdown

a. Inspection Scope

During the months of July and August 2008 the inspectors performed a complete system

alignment inspection of the ESW system to verify the functional capability of the system.

This system was selected because it was considered both safety-significant and

risk-significant in the licensees probabilistic risk assessment. The inspectors walked

down the system to review mechanical and electrical equipment lineups, electrical power

availability, system pressure and temperature indications, as appropriate, component

labeling, component lubrication, component and equipment cooling, hangers and

supports, operability of support systems, and to ensure that ancillary equipment or

debris did not interfere with equipment operation. A review of a sample of past and

outstanding WOs was performed to determine whether any deficiencies significantly

affected the system function. In addition, the inspectors reviewed the CAP database to

ensure that system equipment alignment problems were being identified and

appropriately resolved. Documents reviewed are listed in the attachment.

These activities constituted one sample for a complete system walkdown as defined in

IP 71111.04-05.

b. Findings

No findings of significance were identified.

1R05 Fire Protection (71111.05)

.1

Routine Resident Inspector Tours (71111.05Q)

a. Inspection Scope

The inspectors conducted fire protection walkdowns which were focused on availability,

accessibility, and the condition of firefighting equipment in the following risk-significant

plant areas:

8

Enclosure

Fire Zones 1CC-4 A,C,D, and E; Control Complex elevation 638 6;

Fire Zones 1CC-5 A, B and C; Control Complex elevation 654 6;

Emergency Service Water pumphouse;

Fire Zone 1DG-1A, Diesel Generator Building 6206 - Division 2 Diesel

Generator Room;

Fire Zone 1DG-1B, Diesel Generator Building 6206 - Division 3 Diesel

Generator Room;

Fire Zone 1DG-1C, Diesel Generator Building 6206 - Division 1 Diesel

Generator Room; and

Fire Zone 1DG-1D, Diesel Generator Building 6206 - Hallway.

The inspectors reviewed areas to assess if the licensee had implemented a fire

protection program that adequately controlled combustibles and ignition sources within

the plant, effectively maintained fire detection and suppression capability, maintained

passive fire protection features in good material condition, and had implemented

adequate compensatory measures for out of service, degraded or inoperable fire

protection equipment, systems, or features in accordance with the licensees fire plan.

The inspectors selected fire areas based on their overall contribution to internal fire risk

as documented in the plants Individual Plant Examination of External Events with later

additional insights, their potential to impact equipment which could initiate or mitigate a

plant transient, or their impact on the plants ability to respond to a security event. Using

the documents listed in the Attachment, the inspectors verified that fire hoses and

extinguishers were in their designated locations and available for immediate use; that

fire detectors and sprinklers were unobstructed, that transient material loading was

within the analyzed limits; and fire doors, dampers, and penetration seals appeared to

be in satisfactory condition. The inspectors also verified that minor issues identified

during the inspection were entered into the licensees CAP. Documents reviewed are

listed in the attachment.

These activities constituted seven quarterly samples for fire protection as defined in

IP 71111.05-05.

b. Findings

Introduction: The inspectors identified a finding of very low safety significance and an

associated NCV of the Perry Nuclear Power Plant Operating License Condition C(6),

when licensee personnel degraded a fire barrier and failed to adhere to fire protection

program procedures.

Description: On August 18, 2008, while performing a walkdown of the ESW system in

the ESW pumphouse, the inspectors noticed that the double-door access to the diesel

fire pump (DFP) room was propped open. One of the doors was tied open with a rope

and the other was propped open with scaffolding material. Workers were in the process

of moving scaffolding and other material in and out of the DFP room for planned

maintenance. The doors had warning signs identifying them as fire-safety barriers and

also stated the requirement to notify the control room prior to impairing them. The

inspectors questioned the workers whether they were meeting the requirements for

impairing the door. The workers informed the inspectors that it was their understanding

that as long as personnel were in the vicinity of the door, they could impair the door

open.

9

Enclosure

The inspectors discussed this issue with the control room operators and inquired

whether the control room was aware of this specific impairment. Control room personnel

were not aware of an impairment authorized for the DFP door.

The inspectors continued the inspection and were informed by the maintenance services

supervisor that fixed fire impairments were no longer approved without proper

authorization. Licensee personnel removed the fixed impairments, and the doors were

subsequently held open as-needed by personnel in accordance with plant procedures.

The inspectors confirmed with the Secondary Alarm Station, which maintained a list of

current fire impairments, that the fixed impairments for the DFP room were not

requested and not approved in accordance with plant procedures. The inspectors also

confirmed with the fire marshal that there was not an approved impairment for the DFP

fire doors.

The licensee further determined that maintenance personnel had left the area while the

fire doors were impaired and, as such, the degraded fire barrier condition was left

unattended.

Analysis: The inspectors determined that the licensees failure to follow the procedural

requirements of the Perry Plant Fire Protection Program was a performance deficiency

warranting a significance evaluation.

The inspectors determined that the performance deficiency was more than minor in

accordance with IMC 0612, Appendix B, Issue Disposition Screening, because the

finding was associated with protection against external factors attribute of the Mitigating

Systems Cornerstone and affected the cornerstone objective of ensuring the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences. Specifically, by the inappropriate use of fixed impairments

on the fire doors between the DFP room and the ESW pumphouse, licensee personnel

removed a fire barrier affecting the safety-related building.

The inspectors evaluated the finding using IMC 0609, Appendix F, Fire Protection

Significance Determination Process. Because the finding involved fire doors, it was

assigned to the Fire Confinement finding category in accordance with table 1.1.1. The

finding was then assigned a High degradation rating in accordance with step 1.2.

Guidance in IMC 0609, Appendix F, Attachment 2, table A2.2 was also used to make

this determination. Step 1.3 then directed the inspectors to step 1.4 based on the Fire

Confinement category and High Degradation rating. In step 1.4, with an assumed

<3-day duration and a Generic Fire Frequency of 3E-2 based on a diesel generator

building, the resultant CDF (core damage frequency) value of 3E-4 required a Phase 2

analysis.

The inspectors performed a Phase 2 evaluation using IMC 0609, Appendix F, Fire

Protection SDP. The inspectors determined that there was not a credible fire scenario

relating to the performance deficiency associated with the blocked open fire door for the

DFP room. The inspectors evaluated fire scenarios for the diesel fire pump and its

associated fuel supply using a bounding 10 MegaWatt (MW) fire (the uppermost fire bin

size from IMC 0609, Appendix F, Table 2.3.1, Mapping of General Fire Scenario

Characterization Type Bins to Fire Intensity Characteristics). For evaluating fire

scenarios involving radiant heat, the inspectors used IMC 0609, Appendix F,

10

Enclosure

Table 2.3.2, Calculated Values (in feet) for Use in the Ball and Column Zone of

Influence Chart for Fires in an Open Location from Walls. The inspectors noted that

there was no equipment important to safety outside the fire door to the diesel fire pump

room within the radial zone of influence for a 10 MW fire. In addition, there was no

equipment inside the fire door within the radial zone of influence for a 200 kW fire

(the 98th percentile bin for a small electrical fire or solid and transient combustible fire).

The inspectors noted that there was no equipment directly above the door which could

be adversely affected by a plume originating near the fire door. The inspectors also

evaluated the potential for a damaging hot gas layer to develop from a 10 MW fire using

a CFAST (Consolidated Fire and Smoke Transport) fire simulation (publicly available

from www.nist.gov). Based on the simulation results, the inspectors determined that a

hot gas layer of approximately 588 degrees Fahrenheit (°F) could develop over the

period of 30 minutes. Such a temperature was below the damage threshold (625 °F) for

thermoset cables such as those used at the Perry Nuclear Power Plant. The CFAST

simulation was based on the ESW pump house having dimensions of 103 feet by 55 feet

by 65 feet high, and that the ESW pumphouse had five louvered ventilation openings of

7 feet wide by 5 feet high (four located 35 feet above the floor and one located 25 feet

above the floor), four louvered ventilation openings of 7 feet wide by 5.5 feet high

(located 50 feet above the floor). The inspectors assumed an opening fraction of 0.1 for

the louvered ventilation openings to be representative of closed ventilation louvers.

Mechanical ventilation, which would provide additional cooling, was not considered. The

CFAST default settings for the fuel (i.e., methane with a 0.3 radiative fraction) were used

for the 10 MW fire specified. As such, the inspectors considered the issue to be of very

low safety significance (i.e., Green) because there was not a credible fire scenario

associated with the performance deficiency.

This finding has a cross-cutting aspect in the area of Human Performance, H.4(a),

because the licensee did not ensure that appropriate human error prevention techniques

were used. Specifically, the pre-job brief did not adequately detail the appropriate

procedural requirements for fire impairments.

Enforcement: Perry Nuclear Power Plant Operating License Condition C(6) states, in

part, that FENOC shall implement and maintain in effect all provisions of the approved

fire protection program. As stated in Perry Administrative Procedure (PAP)-1910, "Fire

Protection Program", Revision 15, work and activities in the plant which present a

potential for creating fire hazards are controlled by this and other plant administrative

procedures/instructions. The control processes include, among other things, impairment

permits. Fire Protection Instruction (FPI)-A-C01, "Fire Protection Program Control

Processes," outlines the specific procedure to request fire impairments. Contrary to the

operating license condition as implemented through the procedures above, the licensee

utilized fixed fire door impairments without proper authorization or controls. Because

this violation was of very low safety significance and it was entered into the licensees

CAP as CR 08-44968, this violation is being treated as NCV, consistent with Section

VI.A.1 of the NRC Enforcement Policy (NCV 05000440/2008004-01).

11

Enclosure

1R06 Flood Protection Measures (71111.06)

.1

Internal Flooding

a. Inspection Scope

The inspectors reviewed selected risk important plant design features and licensee

procedures intended to protect the plant and its safety-related equipment from internal

flooding events. The inspectors reviewed flood analyses and design documents,

including the UFSAR, engineering calculations, and abnormal operating procedures to

identify licensee commitments. The specific documents reviewed are listed in the

Attachment to this report. In addition, the inspectors reviewed licensee drawings to

identify areas and equipment that may be affected by internal flooding caused by the

failure or misalignment of nearby sources of water, such as the fire suppression or the

circulating water systems. The inspectors also reviewed the licensees corrective action

documents with respect to past flood-related items identified in the CAP to verify the

adequacy of the corrective actions. The inspectors performed a walkdown of the

auxiliary building and the modification associated with the alternate decay heat removal

(ADHR) installation during the weeks of August 4 and 11, 2008, to assess the adequacy

of watertight doors and verify drains and sumps were clear of debris and were operable,

and that the licensee complied with its commitments. Documents reviewed are listed in

the attachment.

This inspection constituted one sample for internal flooding as defined in

IP 71111.06-05.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification Program

.1

Resident Inspector Quarterly Review (71111.11Q)

a. Inspection Scope

On July 23, 2008, the inspectors observed a crew of licensed operators in the plants

simulator during licensed operator requalification examinations to verify that operator

performance was adequate, evaluators were identifying and documenting crew

performance problems and training was being conducted in accordance with licensee

procedures. The inspectors evaluated the following areas:

licensed operator performance;

clarity and formality of communications;

ability to take timely actions in the conservative direction;

prioritization, interpretation, and verification of annunciator alarms;

correct use and implementation of abnormal and emergency procedures;

control board manipulations;

oversight and direction from supervisors; and

ability to identify and implement appropriate TS actions and Emergency Plan

actions and notifications.

12

Enclosure

The crews performance in these areas was compared to pre-established operator action

expectations and successful critical task completion requirements. Documents reviewed

are listed in the Attachment.

This inspection constitutes one quarterly sample for the licensed operator requalification

program as defined in IP 71111.11.

b. Findings and observations

After completing a training cycle for High Intensity Training, the licensee revised the

Plant Emergency Instruction flow charts to Emergency Operating Procedures in order to

be in alignment with industry standards. The licensee planned to fully implement the

new Emergency Operating Procedures after completion of the training cycle.

1R12 Maintenance Effectiveness (71111.12)

.1

Routine Quarterly Evaluations (71111.12Q)

a. Inspection Scope

The inspectors evaluated degraded performance issues involving the risk-significant

HPCS system. The inspectors reviewed events such as where ineffective equipment

maintenance had resulted in valid or invalid automatic actuations of engineered

safeguards systems and independently verified the licensee's actions to address system

performance or condition problems in terms of the following:

implementing appropriate work practices;

identifying and addressing common cause failures;

scoping of systems in accordance with 10 CFR 50.65(b) of the maintenance rule;

characterizing system reliability issues for performance;

charging unavailability for performance;

trending key parameters for condition monitoring;

ensuring 10 CFR 50.65(a)(1) or (a)(2) classification or re-classification; and

verifying appropriate performance criteria for structures, systems, and

components/functions classified as (a)(2) or appropriate and adequate goals and

corrective actions for systems classified as (a)(1).

The inspectors assessed performance issues with respect to the reliability, availability,

and condition monitoring of the system. In addition, the inspectors verified maintenance

effectiveness issues were entered into the CAP with the appropriate significance

characterization. Documents reviewed are listed in the Attachment.

This inspection constitutes one quarterly sample for maintenance effectiveness as

defined in IP 71111.12-05.

b. Findings

No findings of significance were identified.

13

Enclosure

1R13 Maintenance Risk Assessments and Emergent Work Control (71111.13)

.1

Maintenance Risk Assessments and Emergent Work Control

a. Inspection Scope

The inspectors reviewed the licensee's evaluation and management of plant risk, for the

maintenance and emergent work activities affecting risk-significant and safety-related

equipment listed below to verify that the appropriate risk assessments were performed

prior to removing equipment for work:

suppression pool level instrument 'A' during the week of July 7, 2008;

diesel fire pump battery replacement during the week of July 28, 2008;

auxiliary building modifications during the week of August 4, 2008; and

motor feedwater pump during the week of August 4, 2008.

These activities were selected based on their potential risk significance relative to the

Reactor Safety Cornerstone. As applicable for each activity, the inspectors verified that

risk assessments were performed as required by 10 CFR 50.56(a)(4) and were accurate

and complete. When emergent work was performed, the inspectors verified that the

plant risk was promptly reassessed and managed. The inspectors reviewed the scope

of maintenance work, discussed the results of the assessment with the licensee's

probabilistic risk analyst or shift technical advisor, and verified plant conditions were

consistent with the risk assessment. The inspectors also reviewed TS requirements and

walked down portions of redundant safety systems, when applicable, to verify risk

analysis assumptions were valid and applicable requirements were met. Documents

reviewed are listed in the Attachment.

These activities constituted four samples for maintenance risk assessments and

emergent work controls as defined in IP 71111.13-05.

b. Findings

(1) Introduction: The inspectors identified a finding of very low safety significance and an

associated NCV of 10 CFR 50.65(a)(4) for failure to implement compensatory measures

for a risk management activity. The licensee failed to implement prescribed risk controls

associated with work affecting the low pressure core spray (LPCS) system.

Description: On August 6, 2008, during a plant tour, the inspectors were verifying the

licensees configuration control and compensatory measures for removal of auxiliary

building floor plugs following a tornado warning for Lake County earlier that morning.

Control room operators provided the inspectors with Engineering Evaluation Requests

p(EER) 600250251, 600308906, and 600472744 for the floor plug removal, which

provided the operators guidance and compensatory measures for addressing auxiliary

building and LPCS operability. The inspectors determined that the following hatch plugs

were removed: 620' West elevation; 620' East elevation; and 599' East elevation. The

inspectors noted that the three EERs did not allow the concurrent removal of all three

plugs and informed the control room operators of this observation. After a review of the

configuration against the engineering evaluations, the Shift Manager declared LPCS

inoperable and ordered the replacement of two of the building floor plugs.

14

Enclosure

The inspectors observed that the removal of the 620 East and 599 East elevation floor

plugs, which are above the LPCS pump motor, provided a direct vertical path to the

LPCS pump. In the near vicinity of the floor plug opening at ground level was a building

roll-up door that had no unique missile shield function as specified by Updated Safety

Analysis Report (USAR) Table 3.5-6. The inspectors considered that, during a high wind

event, a missile could enter the roll-up door that was near the floor plug opening. From

that location, the missile could drop unhindered onto the LPCS pump motor. The

inspectors also noted that workers had left a significant amount of equipment and

materials in the vicinity of the openings above the LPCS pump.

As stated in PAP-0205, Operability of Plant Systems, section 3.1, Revision 18,

administrative controls are those actions taken to control system or component

configuration in accordance with TS action requirements. The licensee did not have any

administrative controls delineated for this specific floor plug configuration for tornado or

high wind warnings. The licensee evaluation for the configuration of all three floor plugs

removed, update to EER 600472744, stated that LPCS should be conservatively

declared inoperable during high wind warnings. The licensee documented the issue in

CR 08-44524.

Analysis: The inspectors determined that the failure to implement administrative controls

for missile protection for a risk management activity was a performance deficiency. The

finding was determined to be more than minor because it was related to risk

management issues and met the guidance of IMC 0612, Appendix B, Section 3,

question (2) and question (5)(i), dated September 20, 2007. Specifically, the licensee

failed to provide administrative controls related to work affecting LPCS.

The inspectors, using IMC 0609, Appendix K, Maintenance Risk Assessment and

Risk Management SDP, Flowchart 2, dated May 19, 2005, determined that the finding

was of very low safety significance. The time that the plant was exposed to high wind

warnings was approximately four hours. The incremental core damage probability for

the duration of the procedure and for the critical step was less than 1 X 10-6. This finding

had a cross-cutting aspect in the area of Human Performance as defined in IMC 0305,

H.3(a), because the organization failed to adequately plan work activities that are

associated with risk.

Enforcement: 10 CFR 50.65(a)(4) requires the licensee to assess and manage the risk

associated with removing the barriers around the LPCS system. Contrary to this, the

licensee failed to manage the risk associated with the floor plug configuration in the

auxiliary building in that it was not in accordance with any of the licensee risk

evaluations, which resulted in not having appropriate administrative controls for high

winds. Because the violation was of very low safety significance and the issue was

entered into the licensees CAP (CR 08-44524), this violation is being treated as an

NCV, consistent with Section VI.A of the NRC Enforcement Policy

(NCV 05000440/2008004-02).

(2) Introduction: The inspectors identified a finding of very low safety significance and an

associated NCV of 10 CFR 50.65(a)(4) for failure to implement a procedurally-required

risk management activity for a protected train. The licensee performed work on

emergency closed cooling (ECC) 'A' when it was considered a protected train during a

Yellow Risk plant condition.

15

Enclosure

Description: On June 11, 2008, during a plant tour, the inspectors were verifying PNPP

No. 10244, "Protected Equipment Posting Checklist for RCIC Outage (Yellow)," dated

June 19, 2006, and observed work being performed on ECC 'A' heat exchanger near the

isolation valves. The ECC 'A' was listed as a protected train on checklist PNPP

No. 10244. The inspectors determined that the shift manager was not aware of the

activity and the engineers did not realize the component they were working on was

protected for risk-management reasons. After the inspectors notified the shift manager

of the work, the shift manager then provided the required controls to the activity

supervisor and work on ECC 'A' was authorized with the appropriate restraints. The

licensee also revised the protected train posting requirements for ECC A to include the

affected components. The licensee later determined that the work was authorized 3

days earlier, but that this was before the plant entered Yellow Risk and before ECC A

was considered protected.

Nuclear Operating Procedure (NOP)-OP-1007, Risk Determination, Section 4.16.3,

Revision 5, states for protected equipment that, "work is prohibited in these areas,

unless authorized." It further states, "Individuals needing to perform work in these

posted areas shall contact the Shift Manager or designee for permission to enter these

areas to perform work." In addition, licensee procedure PYBP-POS-2-2, "Protected

Equipment Postings," Section 4.3.1, Revision 6, further states that, "Work should not

normally be scheduled in posted areas as part of a routine workweek." The evolution

witnessed by the inspectors was related to a scheduled task of heat exchanger testing.

The licensee documented the issue in the CAP as CR 08-42164.

The inspectors noted other similar risk management issues during the inspection period

and were concerned whether the identified issues were representative of a

programmatic issue. In one example, on July 1, 2008, the inspectors identified that the

licensee had failed to post the annulus exhaust gas treatment system (AEGTS) 'A' as

protected equipment prior to removing AEGTS 'B' from service at approximately

3:30 a.m. for scheduled maintenance. The inspectors questioned the shift manager at

about 7:30 a.m. on July 1, 2008, to determine whether AEGTS 'A' was posted as a

protected train. The shift manager determined that AEGTS 'A' was not posted, but said

that the subsystem should be posted as protected in accordance with PYBP-POS-2-2.

Section 4.1.1 of PYBP-POS-2-2, stated that, "When a component is out-of-service for

greater than four hours and failure of the remaining component would cause entry into

Technical Specification (TS) 3.0.3," that protected equipment postings should be used.

In accordance with Perry TS 3.6.4.3, the loss of both trains of AEGTS requires entry into

limiting condition for operation (LCO) TS 3.0.3. The shift manager ordered the posting of

AEGTS A. At about 10:00 a.m., the inspectors performed a follow-up field walkdown to

verify the new postings and found that, while operators had subsequently posted

AEGTS 'A' in the control room, they had not posted the AEGTS 'A' room in the field. The

operators had considered the postings complete. The inspectors noted that this was

also contrary to PYBP-POS-2-2. The inspectors informed the shift manager of the

observation. At about 10:45 a.m., licensee personnel completed postings for AEGTS 'A'.

Analysis: The inspectors determined that the failure to implement a

procedurally-required risk-management activity for the ECC A protected train was a

performance deficiency. The finding was determined to be more than minor because it

was related to risk management issues and met the guidance of IMC 0612, Appendix B,

Section 3, question (2) and question (5)(i), dated September 20, 2007. Specifically, the

16

Enclosure

licensee failed to either prohibit work or provide required management oversight of work

on ECC 'A' while the plant was in Yellow Risk.

The inspectors, using IMC 0609, Appendix K, Maintenance Risk Assessment and Risk

Management SDP, flowchart 2, dated May 19, 2005, determined that the finding was of

very low safety significance. The time that the plant was in Yellow Risk was less than

one day, and ECC 'A' was determined to be operable. The incremental core damage

probability for the duration of the procedure and for the critical step was less than

1 X 10 6. This finding had a cross-cutting aspect in the area of Human Performance as

defined in IMC 0305 H.3(a), because the organization failed to adequately plan work

activities that are associated with risk.

Enforcement: 10 CFR 50.65(a)(4) requires the licensee to manage the increase in risk

resulting from maintenance activities. Contrary to this, the inspectors identified that work

was in progress on ECC 'A' when that sub-system was posted as a protected train and

the required administrative controls were not met. Because the violation was of very low

safety significance and the issue was entered into the licensees CAP (CR 08-42164),

this violation is being treated as an NCV, consistent with Section VI.A of the NRC

Enforcement Policy (NCV 05000440/2008004-03).

1R15 Operability Evaluations (71111.15)

.1

Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following issues:

residual heat removal (RHR) 'C' pump minimum flow valve during the week of

July 21, 2008;

Divisional Class 1E safety batteries during the week of August 11, 2008;

ESW 'B' flange material during the week of September 1, 2008;

ADHR core bore during August and September;

ESW building ventilation dampers during the week of September 22, 2008;

reactor water clean-up (RWCU) system through-wall leakage downstream of the

regenerative heat exchanger during the week of September 22, 2008; and

service water make-up to the cooling tower flow path isolation capability while the

inboard isolation valve, OP41F420, was declared inoperable during the week of

September 22, 2008.

The inspectors selected these potential operability issues based on the risk-significance

of the associated components and systems. The inspectors evaluated the technical

adequacy of the evaluations to ensure that TS operability was properly justified and the

subject component or system remained available such that no unrecognized increase in

risk occurred. The inspectors compared the operability and design criteria in the

appropriate sections of the TS and USAR to the licensees evaluations, to determine

whether the components or systems were operable. Where compensatory measures

were required to maintain operability, the inspectors determined whether the measures

in place would function as intended and were properly controlled. The inspectors

determined, where appropriate, compliance with bounding limitations associated with the

evaluations. Additionally, the inspectors also reviewed a sampling of corrective action

17

Enclosure

documents to verify that the licensee was identifying and correcting any deficiencies

associated with operability evaluations. Documents reviewed are listed in the

Attachment.

These inspections constitute seven samples for operability evaluations as defined in

IP 71111.15.-05.

b. Findings

Introduction: A finding of very low safety significance and an associated NCV of

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, was

self-revealed for the failure to have documented instructions, procedures, or drawings

appropriate to the circumstances. The failure to have an approved work package prior

to boring holes in a seismically qualified structure was not in accordance with Perrys

work control procedures.

Description: On August 4, 2008, during dayshift, contractors performing work associated

with the ADHR project prepared to bore a 14-inch hole in the floor of the 599 level of the

auxiliary building. Holes were being drilled in this area in preparation for pipe

installations that were scheduled at a later date. Upon arrival to the work site, the

workers began the set-up process for the boring machine and discovered that some of

the material pre-staged for the job was incorrect. The supervisor then directed the

workers to set-up and bore an 8-inch hole which was located nearby. In preparation for

drilling operations, the floor had been marked-up with representations of the rebar

present in the floor and the locations for the holes on this level associated with the

ADHR project.

The workers placed the boring machine over a crosshair on the floor that was marked

CL AUX-8 and CL AUX-D. These marks indicated the intersection of the centerline of

columns 8 and D in the auxiliary building. The workers assumed that this mark was the

center for the 8-inch hole. This was not the correct location for the 8-inch hole. The

correct location for the 8-inch hole was marked, but was five to six feet away.

The incorrect positioning of the boring equipment was discovered during shift turnover

on August 4. As supervision began looking into this event they discovered that the work

package for the boring of the 8-inch hole had not been released. The only boring work

that had an approved work package was for the 14-inch holes. The 8-inch hole had

been bored without an approved work package.

Analysis: The inspectors determined that boring holes in a seismically qualified structure

without an approved work package was contrary to Perrys work control practices and

was a performance deficiency.

The finding was determined to be more than minor because the finding was associated

with the design control attribute of Mitigating Systems Cornerstone and affected the

cornerstone objective of ensuring the availability, reliability, and capability of systems

that respond to initiating events to prevent undesirable consequences. Specifically, the

licensee initiated work on a seismically qualified structure in the absence of an approved

work package. This instance resulted in the boring of a hole in a location other than that

which was planned, thus placing the structure in an unanalyzed condition. The licensee

18

Enclosure

subsequently conducted an analysis to demonstrate operability for the current

configuration.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of findings, Table 4a for the Mitigating System

Cornerstone. The inspectors answered yes to the question regarding design or

qualification deficiencies confirmed not to result in loss of operability. Therefore this

finding screens as Green, very low safety significance.

This finding has a cross-cutting aspect in the area of human performance because

personnel failed to hold an adequate pre-job brief, did not have proper documentation,

and proceeded in the face of unexpected circumstances. H.4(a)

Enforcement: Criterion V, Instructions, Procedures, and Drawings, of 10 CFR Part 50,

Appendix B, requires, in part, that activities affecting quality be prescribed by

documented instructions, procedures, or drawings, of a type appropriate to the

circumstances and that they be accomplished in accordance with these instructions,

procedures, or drawings. Contrary to this, on August 4, 2008, the licensee failed to have

work instructions appropriate to the circumstances prior to initiating work. Specifically,

the licensee initiated work on a seismically qualified structure in the absence of an

approved work package. Because this violation was of very low safety significance and

it was entered into the licensees CAP as CR 08-4431, this violation is being treated as

an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy

(NCV 05000440/2008004-04).

1R19 Post-Maintenance Testing (71111.19)

.1

Post-Maintenance Testing

a. Inspection Scope

The inspectors reviewed the following post-maintenance activities for review to verify

that procedures and test activities were adequate to ensure system operability and

functional capability:

suppression pool 'A' level instrument line testing during the week of

July 14, 2008;

AEGTS testing during the weeks of July 14 and 28, 2008;

RHR 'C' leak indication during the weeks of August 18 and 29, 2008;

RHR 'C' minimum flow pressure trip unit during the week of September 15, 2008;

service water system make-up to cooling tower inboard isolation valve

troubleshooting and repair following an in-service testing surveillance failure

during the week of September 22, 2008; and

containment atmosphere monitoring system testing requirements following

control room recorder replacements during the week of September 22, 2008.

These activities were selected based upon the structure, system, or component's ability

to impact risk. The inspectors evaluated these activities for the following (as applicable):

the effect of testing on the plant had been adequately addressed; testing was adequate

for the maintenance performed; acceptance criteria were clear and demonstrated

19

Enclosure

operational readiness; test instrumentation was appropriate; tests were performed as

written in accordance with properly reviewed and approved procedures; equipment was

returned to its operational status following testing (temporary modifications or jumpers

required for test performance were properly removed after test completion), and test

documentation was properly evaluated. The inspectors evaluated the activities against

TS, the UFSAR, 10 CFR Part 50 requirements, licensee procedures, and various NRC

generic communications to ensure that the test results adequately ensured that the

equipment met the licensing basis and design requirements. In addition, the inspectors

reviewed corrective action documents associated with post-maintenance tests to

determine whether the licensee was identifying problems and entering them in the CAP

and that the problems were being corrected commensurate with their importance to

safety. Documents reviewed are listed in the Attachment.

This inspection constitutes six samples for post-maintenance testing as defined in

IP 71111.19.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

.1

Surveillance Testing

a. Inspection Scope

The inspectors reviewed the test results for the following activities to determine whether

risk-significant systems and equipment were capable of performing their intended safety

function and to verify testing was conducted in accordance with applicable procedural

and TS requirements:

suppression pool level 'A' testing during the week of June 30, 2008, (routine);

inservice ECC pump and valve inspection during the week of August 4, 2008,

(IST);

emergency diesel generator (EDG) exhaust hallway inspection during the week

of August 4, 2008, (routine);

testing of the diesel driven fire pump ventilation switch during the week of

August 25, 2008, (routine) ;

average power range monitor (APRM) channel calibration testing during the

week of August 25, 2008, (routine) ;

Division 3 EDG testing during the week of September 15, 2008, (routine);

APRM 'A' channel calibration testing during the week of September 15, 2008,

(routine); and

oscillating power range monitor (OPRM) channel 'A' functional testing during the

week of September 22, 2008, (routine).

20

Enclosure

The inspectors observed in plant activities and reviewed procedures and associated

records to determine the following:

did preconditioning occur;

were the effects of the testing adequately addressed by control room personnel

or engineers prior to the commencement of the testing;

were acceptance criteria clearly stated, demonstrated operational readiness, and

consistent with the system design basis;

plant equipment calibration was correct, accurate, and properly documented;

as-left setpoints were within required ranges; and the calibration frequency were

in accordance with TSs, the USAR, procedures, and applicable commitments;

measuring and test equipment calibration was current;

test equipment was used within the required range and accuracy; applicable

prerequisites described in the test procedures were satisfied;

test frequencies met TS requirements to demonstrate operability and reliability;

tests were performed in accordance with the test procedures and other

applicable procedures; jumpers and lifted leads were controlled and restored

where used;

test data and results were accurate, complete, within limits, and valid;

test equipment was removed after testing;

where applicable for inservice testing activities, testing was performed in

accordance with the applicable version of Section XI, American Society of

Mechanical Engineers code, and reference values were consistent with the

system design basis;

where applicable, test results not meeting acceptance criteria were addressed

with an adequate operability evaluation or the system or component was

declared inoperable;

where applicable for safety-related instrument control surveillance tests,

reference setting data were accurately incorporated in the test procedure;

where applicable, actual conditions encountering high resistance electrical

contacts were such that the intended safety function could still be accomplished;

prior procedure changes had not provided an opportunity to identify problems

encountered during the performance of the surveillance or calibration test;

equipment was returned to a position or status required to support the

performance of its safety functions; and

all problems identified during the testing were appropriately documented and

dispositioned in the CAP.

Documents reviewed are listed in the Attachment to this report.

This inspection constituted one in-service testing sample and seven routine surveillance

testing samples as defined in IP 71111.22.

b. Findings:

No findings of significance were identified.

21

Enclosure

1EP6 Drill Evaluation (71114.06)

.1

Training Observation

a.

Inspection Scope

The inspector observed a simulator training evolution for licensed operators on

September 15, 2008, which required emergency plan implementation by a licensee

operations crew. This evolution was planned to be evaluated and included in

performance indicator (PI) data regarding drill and exercise performance. The

inspectors observed event classification and notification activities performed by the crew.

The inspectors also attended the post-evolution critique for the scenario. The focus of

the inspectors activities was to note any weaknesses and deficiencies in the crews

performance and ensure that the licensee evaluators noted the same issues and entered

them into the CAP. As part of the inspection, the inspectors reviewed the scenario

package and other documents listed in the Attachment to this report.

This inspection constituted one sample of a training observation as defined in

IP 71114.06-05.

b.

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas (71121.01)

.1

Review of Licensee PIs for the Occupational Exposure Cornerstone

a.

Inspection Scope

The inspectors reviewed the licensees Occupational Exposure Control Cornerstone PIs

to determine whether the conditions resulting in any PI occurrences had been evaluated

and whether identified problems had been entered into the licensees CAP for resolution.

This inspection constitutes one sample as defined in IP 71121.01-5.

b.

Findings

No findings of significance were identified.

.2

Plant Walkdowns and Radiation Work Permit Reviews

a.

Inspection Scope

The inspectors assessed the adequacy of the licensees internal dose assessment

process for internal exposures in excess of 50 millirem committed effective dose

equivalent. There were no internal exposures greater than 50 millirem committed

effective dose equivalent.

22

Enclosure

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors also reviewed the licensees physical and programmatic controls for

highly activated and/or contaminated materials (non-fuel) stored within the spent fuel

pool or other storage pools.

This inspection constitutes one sample for plant walkdowns and radiation work permit

reviews as defined in IP 71121.01-5.

b.

Findings

No findings of significance were identified.

.3

Problem Identification and Resolution

a.

Inspection Scope

The inspectors reviewed a sample of the licensees self-assessments, audits, licensee

even reports (LERs), and special reports related to the access control program to verify

that identified problems were entered into the CAP for resolution.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors reviewed corrective action reports related to access controls and any

high radiation area radiological incidents (issues that did not count as PI occurrences

identified by the licensee in high radiation areas less than 1R/hr). Staff members were

interviewed and corrective action documents were reviewed to verify that follow-up

activities were being conducted in an effective and timely manner commensurate with

their importance to safety and risk based on the following:

initial problem identification, characterization, and tracking;

disposition of operability/reportability issues;

evaluation of safety significance/risk and priority for resolution;

identification of repetitive problems;

identification of contributing causes;

identification and implementation of effective corrective actions;

resolution of NCVs tracked in the corrective action system; and

implementation/consideration of risk-significant operational experience feedback.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors evaluated the licensees process for problem identification,

characterization, and prioritization and verified that problems were entered into the

CAP and resolved. For repetitive deficiencies and/or significant individual deficiencies

in problem identification and resolution, the inspectors verified that the licensees

self-assessment activities were capable of identifying and addressing these deficiencies.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors reviewed licensee documentation packages for all PI events occurring

since the last inspection to determine if any of these PI events involved dose rates in

23

Enclosure

excess of 25 R/hr at 30 centimeters or in excess of 500 R/hr at 1 meter. Barriers were

evaluated for failure and to determine if there were any barriers left to prevent personnel

access. Unintended exposures exceeding 100 millirem total effective dose equivalent

(or 5 rem shallow dose equivalent or 1.5 rem lens dose equivalent) were evaluated to

determine if there were any regulatory overexposures or if there was a substantial

potential for an overexposure.

This inspection constitutes one sample as defined in IP 71121.01-5.

b.

Findings

No findings of significance were identified.

.4

High Risk Significant, High Dose Rate, High Radiation Area and Very High Radiation

Area Controls

a.

Inspection Scope

The inspectors held discussions with the radiation protection manager concerning high

dose rate/high radiation areas and very high radiation area controls and procedures,

including procedural changes that had occurred since the last inspection, in order to

assess whether any procedure modifications substantially reduced the effectiveness and

level of worker protection.

This inspection constitutes one sample as defined in IP 71121.01-5.

The inspectors discussed with radiation protection supervisors the controls that were in

place for special areas of the plant that had the potential to become very high radiation

areas during certain plant operations. The inspectors assessed if plant operations

required communication beforehand with the radiation protection group, so as to allow

corresponding timely actions to properly post and control the radiation hazards.

This inspection constitutes one sample as defined in IP 71121.01-5.

b.

Findings

No findings of significance were identified.

.5

Radiation Worker Performance

a.

Inspection Scope

The inspectors reviewed radiological problem reports for which the cause of the event

was due to radiation worker errors to determine if there was an observable pattern

traceable to a similar cause and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems. Problems or

issues with planned or completed corrective actions were discussed with the radiation

protection manager.

This inspection constitutes one sample as defined in IP 71121.01-5.

24

Enclosure

b.

Findings

No findings of significance were identified.

.6

Radiation Protection Technician Proficiency

a.

Inspection Scope

The inspectors reviewed radiological problem reports for which the cause of the event

was radiation protection technician error to determine if there was an observable pattern

traceable to a similar cause and to determine if this perspective matched the corrective

action approach taken by the licensee to resolve the reported problems.

This inspection constitutes one sample as defined in IP 71121.01-5.

b. Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

.1

Unplanned Scrams per 7000 Critical Hours

a.

Inspection Scope

The inspectors sampled licensee submittals for the Unplanned Scrams per 7000 Critical

Hours PI for the period from 3rd quarter 2007 through the 2nd quarter 2008. To determine

the accuracy of the PI data reported during those periods, PI definitions and guidance

contained in the NEI 99-02, Regulatory Assessment PI Guideline, Revision 5, was

used. The inspectors reviewed the licensees operator narrative logs, issue reports,

event reports and NRC inspection reports for the period of 3rd quarter 2007 through the

2nd quarter 2008 to validate the accuracy of the submittals. The inspectors also

reviewed the licensees issue report database to determine if any problems had been

identified with the PI data collected or transmitted for this indicator. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one sample for unplanned scrams per 7000 critical hours as

defined in IP 71151-05.

b.

Findings

No findings of significance were identified.

.4

Safety System Functional Failures

a. Inspection Scope

The inspectors sampled licensee submittals for the Safety System Functional Failures PI

for the period from the 3rd quarter 2007 through the 2nd quarter 2008. To determine the

accuracy of the PI data reported during those periods, PI definitions and guidance

25

Enclosure

contained in the Nuclear Energy Institute (NEI) Document 99-02, Regulatory

Assessment PI Guideline, Revision 5, and NUREG-1022, Event Reporting Guidelines

10 CFR 50.72 and 50.73" definitions and guidance, were used. The inspectors reviewed

the licensees operator narrative logs, operability assessments, maintenance rule

records, maintenance WOs, issue reports, event reports and NRC integrated inspection

reports for the period of July 1, 2007 through June 30, 2008, to validate the accuracy of

the submittals. The inspectors also reviewed the licensees issue report database to

determine if any problems had been identified with the PI data collected or transmitted

for this indicator. Documents reviewed are listed in the Attachment to this report.

This inspection constituted one sample for safety system functional failures as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

.9

Mitigating Systems Performance Index - Cooling Water Systems

a. Inspection Scope

The inspectors sampled licensee submittals for the Mitigating Systems Performance

Index (MSPI) - Cooling Water Systems PI for the period from 3rd quarter 2007 through

the 2nd quarter 2008. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in the NEI 99-02, Regulatory

Assessment PI Guideline, Revision 5, was used. The inspectors reviewed the

licensees operator narrative logs, issue reports, MSPI derivation reports, event reports

and NRC integrated inspection reports for the period 3rd quarter 2007 through the

2nd quarter 2008 to validate the accuracy of the submittals. The inspectors reviewed the

MSPI component risk coefficient to determine if it had changed by more than 25 percent

in value since the previous inspection, and if so, that the change was in accordance with

applicable NEI guidance. The inspectors also reviewed the licensees issue report

database to determine if any problems had been identified with the PI data collected or

transmitted for this indicator and none were identified. Documents reviewed are listed in

the Attachment to this report.

This inspection constituted one sample for MSPI cooling water systems as defined in

IP 71151-05.

b. Findings

No findings of significance were identified.

Cornerstone: Public Radiation Safety

.10

Reactor Coolant System Specific Activity

a. Inspection Scope

The inspectors sampled licensee submittals for the Reactor Coolant System Specific

Activity PI for Perry Station Unit 1 for the period from the third quarter 2007 through the

26

Enclosure

second quarter 2008. To determine the accuracy of the PI data reported during those

periods, PI definitions and guidance contained in the NEI 99-02, Regulatory

Assessment PI Guideline, Revision 5, was used. The inspectors reviewed the

licensees reactor coolant system chemistry samples, TS requirements, issue reports,

event reports and NRC Integrated Inspection Reports for the period of July 2007 through

August 2008 to validate the accuracy of the submittals. The inspectors also reviewed

the licensees issue report database to determine if any problems had been identified

with the PI data collected or transmitted for this indicator and none were identified. In

addition to record reviews, the inspectors observed a chemistry technician obtain and

analyze a reactor coolant system sample. Documents reviewed are listed in the

Attachment to this report.

This inspection constituted one sample for reactor coolant system specific activity as

defined in IP 71151-05.

b. Findings

No findings of significance were identified.

.15

Occupational Exposure Control Effectiveness

a. Inspection Scope

The inspectors sampled licensee submittals for the Occupational Radiological

Occurrences PI for the period from the 4th quarter 2007 through the 2nd quarter 2008. To

determine the accuracy of the PI data reported during those periods, PI definitions and

guidance contained in the NEI 99-02, Regulatory Assessment PI Guideline, Revision 5,

was used. The inspectors reviewed the licensees assessment of the PI for occupational

radiation safety to determine if indicator-related data was adequately assessed and

reported. To assess the adequacy of the licensees PI data collection and analyses, the

inspectors discussed with radiation protection staff, the scope and breadth of its data

review, and the results of those reviews. The inspectors independently reviewed

electronic dosimetry dose rate and accumulated dose alarm and dose reports and the

dose assignments for any intakes that occurred during the time period reviewed to

determine if there were potentially unrecognized occurrences. The inspectors also

conducted walkdowns of numerous locked high and very high radiation area entrances

to determine the adequacy of the controls in place for these areas. Documents reviewed

are listed in the Attachment to this report.

This inspection constituted one sample for occupational radiological occurrences as

defined in IP 71151-05.

b. Findings

No findings of significance were identified.

27

Enclosure

4OA2 Identification and Resolution of Problems (71152)

Cornerstone: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

.1

Routine Review of Items Entered Into the CAP

a.

Inspection Scope

As part of the various baseline IPs discussed in previous sections of this report, the

inspectors routinely reviewed issues during baseline inspection activities and plant

status reviews to verify that they were being entered into the licensees CAP at an

appropriate threshold, that adequate attention was being given to timely corrective

actions, and that adverse trends were identified and addressed. Attributes reviewed

included: the complete and accurate identification of the problem; that timeliness was

commensurate with the safety significance; that evaluation and disposition of

performance issues, generic implications, common causes, contributing factors, root

causes, extent-of-condition reviews, and previous occurrence reviews were proper and

adequate; and that the classification, prioritization, focus, and timeliness of corrective

actions were commensurate with safety and sufficient to prevent recurrence of the issue.

Minor issues entered into the licensees CAP as a result of the inspectors observations

are included in the attached List of Documents Reviewed.

These routine reviews for the identification and resolution of problems did not constitute

any additional inspection samples. Instead, by procedure they were considered an

integral part of the inspections performed during the quarter and documented in

Section 1 of this report.

b. Findings

No findings of significance were identified.

.2

Daily Corrective Action Program Reviews

a. Inspection Scope

In order to assist with the identification of repetitive equipment failures and specific

human performance issues for follow-up, the inspectors performed a daily screening of

items entered into the licensees CAP. This review was accomplished through

inspection of the stations daily CR packages.

These daily reviews were performed by procedure as part of the inspectors daily plant

status monitoring activities and, as such, did not constitute any separate inspection

samples.

b. Findings

No findings of significance were identified.

28

Enclosure

.5

Selected Issue Follow-Up Inspection: Containment Airlocks

a. Inspection Scope

The inspectors selected a CR for detailed annual sample review (CR 08-44698). The

CR was associated with an adverse trend of containment airlock failures. The report

was reviewed to ensure that the full extent of the issue was identified, an appropriate

evaluation was performed, and appropriate corrective actions were specified and

prioritized. The inspectors evaluated the report against the requirements of the

licensees CAP as delineated in NOP-LP-2001-01, Condition Report Process,

Revision 8, and 10 CFR Part 50, Appendix B.

This activity constitutes the first of two samples for an in-depth review as defined in

IP 71152-05.

b. Findings

Introduction: A finding of very low safety significance (Green) and an associated NCV of

TS 5.4, Procedures, was self-revealed when a containment airlock door seal failed

during routine operations.

Description: On June 1, 2008, a licensee operator exited the containment building

through the upper airlock. When the operator closed the airlock outer door and operated

the door hand wheel, the light that provided indication for one of the doors seals failed to

illuminate. The operator made additional attempts to operate the door, but the doors

small seal would not inflate. The licensee declared the upper airlock outer door

inoperable and placed administrative controls on the inner door to ensure it was closed.

Licensee personnel inspected the outer doors seal mechanism and determined that a

3-way ball valve, 1P53F0591A, associated with the small seal had failed. The valve

stem had separated from the valve ball.

Licensee maintenance personnel removed the failed valve, noted valve body damage,

and determined that the valve needed to be rebuilt using a new valve body. The ball

valve 1P53F0591A was rebuilt, installed, and then tested with satisfactory results on

June 4, 2008.

Licensee maintenance and engineering personnel investigated the cause of the valve

failure. During inspection of the removed components, licensee personnel noted that

significant metal loss had occurred on the valve stem where it interfaced with the ball

slot. The inner ring of the valve body was also worn. The licensee initially determined

through engineering inspections and interviews with maintenance personnel, that

contrary to valve assembly procedures, a valve stem seal ring may not have been

installed during the last valve assembly. The seal ring was designed to prevent contact

between the stem and the valve body. The lack of a seal ring would have resulted in

metal to metal contact, galling, and damage to the valve during door operations.

The licensee could not find evidence of an installed slip ring during the initial

investigation. However, subsequent licensee laboratory testing results of the valve

internals indicated possible trace amounts of chemical residue on metal valve

component surfaces that could be consistent with the presence of an installed slip ring at

29

Enclosure

some time in the past. The laboratory personnel used an electron microscope to identify

the chemical traces.

The valve had been last worked on March 26, 2008. During this maintenance, a new

valve body was installed and the internals were rebuilt. The new valve body was a

replacement for the original valve body that had been in use for over 20 years.

The inspectors reviewed the March 26, 2008, work documentation and noted that

workers listed two slip rings as used during the work. The inspectors further noted that

the work procedures required the use of four stem slip rings. The inspectors questioned

licensee maintenance personnel on the discrepancy. During interviews with the

inspectors, licensee maintenance personnel stated that they believed all four slip rings

were used but that they mistakenly only documented the use of two slip rings.

The licensee later informed the inspectors that there was not a high level of certainty

whether the laboratory test results supported a conclusion that a slip ring had been

installed. The laboratory had later questioned the accuracy of the results due to the

minute amount of chemicals that were detected.

While the question of whether a stem slip ring was installed per procedure was not

conclusively resolved, the inspectors considered that the valve failed and exhibited

significant degradation in less than 3-months of routine use after it had been replaced.

Therefore, the inspectors determined that the March 26, 2008, procedures associated

with valve maintenance were not appropriate to the circumstances. Specifically, the

maintenance resulted in an unsatisfactory condition of the valve.

Other doors on both upper and lower containment airlocks were potentially affected by

past performance of airlock maintenance procedure Generic Mechanical Instruction

(GMI)-0176, Containment Airlock Door Maintenance. The licensee conducted a review

of the other airlock door seal mechanisms and reworked the lower and upper airlock

door mechanisms. The licensee identified several deficiencies during their rework of the

airlock doors, including: (1) inadequate procedure guidance for mechanism assembly

relative to worker training; (2) failure to grease the door mechanisms due to a dropped

maintenance task; and (3) maintenance frequencies that were not commensurate with

usage frequency of the doors. As part of their corrective action, the licensee

(1) conducted worker training; (2) planned to revise the airlock maintenance procedures

to include additional guidance; (3) planned to increase the maintenance frequency of the

airlocks; and (4) planned to reintroduce a requirement to grease the door mechanisms.

The inspectors previously noted that the licensees maintenance program associated

with the containment airlocks had resulted in frequent airlock failures. A programmatic

deficiency associated with the licensees maintenance and testing of the airlocks was

described in NCV 05000440/2007002-02.

Analysis: The inspectors determined that the failure to implement maintenance

procedures that were appropriate to the circumstances on March 26, 2008, was a

performance deficiency.

The finding was determined to be more than minor because the finding was associated

with the Procedure Quality attribute of the Barrier Integrity Cornerstone attribute and

affected the cornerstone objective of providing reasonable assurance that physical

30

Enclosure

design barriers (fuel cladding, reactor coolant system, and containment) protect the

public from radionuclide releases caused by accidents or events. Specifically, the

finding resulted in the degradation and failure of a containment door seal.

The inspectors determined the finding could be evaluated using the SDP in accordance

with IMC 0609, Significance Determination Process, Attachment 0609.04, Phase 1 -

Initial Screening and Characterization of findings, Table 4a for the Barrier Integrity

(Containment Barriers) Cornerstone. The inspectors determined that the finding did not

represent an actual open pathway in the physical integrity of reactor containment

because the upper airlock inner door remained closed. Therefore the finding screened

as Green.

This finding has a cross-cutting aspect in the area of Human Performance, H.2.c.,

Resources, because the licensee did not ensure that procedures were complete and

were adequate to assure nuclear safety. Specifically, the implementation of GMI-0176

resulted in the failure of valve 1P53F0591A, associated with a containment airlock seal.

Enforcement: Criterion V, Instructions, Procedures, and Drawings, of 10 CFR Part 50,

Appendix B, requires, in part, that activities affecting quality be prescribed by

documented instructions, procedures, or drawings, of a type appropriate to the

circumstances and be accomplished in accordance with these instructions, procedures,

or drawings. Contrary to this, on March 26, 2008, the licensee failed to implement

airlock maintenance procedures appropriate to the circumstances. Specifically, the

airlock maintenance procedures were not appropriate to the circumstances in that the

implementation of the procedures resulted in failure of the containment upper airlock

inner door seal on June 1, 2008. Because this violation was of very low safety

significance and it was entered into the licensees CAP as CR 08-41097, this violation is

being treated as an NCV, consistent with Section VI.A.1 of the NRC Enforcement Policy

as NCV 05000440/2008004-05, and closes URI 05000440/2008003-01.

.6

Selected Issue Follow-Up Inspection: ESW 'C' Valve Failure Affecting HPCS

a.

Inspection Scope

The inspectors selected a CR for detailed annual sample review (CR 08-40969). The

CR was associated with an inoperability of the HPCS system that was identified on

May 26, 2008. The report was reviewed to ensure that the full extent of the issue was

identified, an appropriate evaluation was performed, and appropriate corrective actions

were specified and prioritized. The inspectors evaluated the report against the

requirements of the licensees CAP as delineated in NOP-LP-2001-01, "Condition

Report Process", Revision 8, and 10 CFR 50, Appendix B.

This activity constitutes the second of two samples for an in-depth review as defined by

IP 71152-05.

b. Findings

A licensee-identified violation is discussed in Section 4OA7 of this report.

31

Enclosure

4OA3 Follow-up of Events and Notices of Enforcement Discretion (71153)

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

.1

(Closed) LER 05000440/2008-001-00: Condition Prohibited by Technical Specifications

Due to Unrecognized Reactor Core Isolation Cooling Inoperability

On January 14, 2008, during preparation for planned maintenance, the licensee

identified that the reactor core isolation cooling (RCIC) flow controller voltage output

changed independently of any alteration in system input. The RCIC system was

declared inoperable. The licensee conducted an investigation that determined several

instances of inadequate voltage output dating back to December 10, 2007. Therefore,

the RCIC system was inoperable for 35 days and the licensee failed to meet the

requirements of TS 3.5.3. As stated in TS 3.5.3, the required action is to verify HPCS is

operable within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />; and restore the RCIC system to operable status in 14 days; or be

in hot standby within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> when neither of these conditions is met. When the

licensee discovered the RCIC system inoperable on January 14, 2008, the licensee did

meet the requirements of TS 3.5.3.

The licensee's investigation and troubleshooting could not determine the exact cause of

the controller output deviation, but listed the possible cause as one of the following four

replaced components: the Bailey 701 flow controller and connector, the power supply,

the ramp generator/signal converter, or the computer input circuit board. The

investigation stated that equipment reliability issues of these components could have

contributed to this failure, but the licensee considers that the anomaly was most likely

introduced into the system during the numerous flow controller changes performed

during November and December 2007.

On April 16, 2008, the licensee observed degraded RCIC flow controller output voltage,

but the output voltage met operability requirements. The licensee investigated the cause

and established a monitoring program to ensure RCIC system operability. On

April 24, 2008, the RCIC flow controller voltage output degraded to a point where the

licensee declared RCIC inoperable. A spare Bailey 701 controller (with previous service

life) was installed, and RCIC was declared operable on April 24, 2008. On

April 25, 2008, the licensee installed new NUS controllers that were designed to replace

the obsolete Bailey 701 controllers.

The Bailey 701 flow controller installed from January to April 2008 was evaluated by the

licensee's Beta lab. The lab was unable to identify the precise failure mechanism, but

concluded that the most likely portions of the controller causing this degradation were

the high output limit circuit (diodes, potentiometers, resistors) and the internal controller

power supply (capacitors, diodes, resistors, transistors, transformer). The investigation

concluded the April 2008 degraded failure was caused by age/cyclic duty degradation of

flow controller subcomponents. The investigation also noted that previous Bailey 701

flow controller failures were attributed to controller subcomponent aging as the major

contributor for the previous controller malfunctions.

The inspectors' discussion with the licensee concerning the two failures of the RCIC

controller system determined that the two inoperability periods mentioned here were due

to different equipment issues, which included the degradation of internal components of

32

Enclosure

the RCIC flow controller. Since the installation of the NUS flow controller, there have

been no observed operability issues with RCIC as of the date of this report.

Licensee corrective actions included replacement of the obsolete Bailey 701 controllers

with NUS controllers, and implemented a 12-year replacement/refurbishment

maintenance requirement of the RCIC flow controllers. This issue was found to be a

licensee-identified violation and is documented in section 4OA7. The licensee

documented the issue in CRs 08-38443 and 08-39111. This LER is closed.

This review represents the first of five samples as defined in IP 71153-05.

.2

Failure to Adequately Manage Risk Associated With Working Around a Risk-Significant

Underground Vault

a. Inspection Scope

The inspectors responded to an incident that occurred during routine maintenance

activities for dewatering underground vaults when the man-hole cover was dropped into

the vault area. The inspectors inspected the circumstance of the event, the impact on

plant safety, licensee response, and regulatory issues.

b. Findings

Introduction: A Green finding (FIN) of very low safety significance was self-revealed

when the licensee failed to manage risk when lifting a man-hole cover for an

underground vault containing risk-significant cables.

Description: On July 30, 2008, while preparing to dewater an underground vault,

man-hole number Eight, licensee personnel inadvertently dropped the man-hole cover

into the vault area. The vault area contained eight electrical conduits used for

indications and switchyard breaker controls affecting offsite power. The purpose of

those controls was fault indication and isolation of the four breakers associated with the

west bus of the switchyard. The licensee determined that the falling cover could have

damaged the control cables and this could have affected controls associated with the

supply of offsite power to the plant and plant stability. Without the fault protection

provided by the circuits, a breaker fault would lead to an off-site circuit protection

response and a loss of offsite power. The licensee determined that the dropped

man-hole cover fell down the side of the vault and did not impact or damage any of the

eight conduits.

The licensee's investigation determined that one of the workers involved with lifting the

man-hole cover was not ready to perform this task when the other technician lifted his

end of the cover. The licensee determined that the pre-job brief did not address the

possibility of dropping the cover and its possible impact to plant operations. Therefore,

the pre-job brief did not identify the removal of the man-hole cover as a critical task

requiring additional oversight. The investigation also identified inadequate

communications between the two workers as a contributing cause because the one

worker did not receive verbal confirmation from the other worker that he was prepared to

lift the cover.

33

Enclosure

The licensee's procedure, NOBP-LP-2604, "Effective Job Briefs," Revision 2, stated, in

4.2.1 (9), that a pre-job brief should summarize the critical steps, error-likely situations;

anticipate the potential errors for each identified critical step; and evaluate and establish

contingencies to prevent and catch errors. This procedure defined a critical step in 3.1

as, "a procedure step or action that, if performed incorrectly, will cause immediate,

irreversible, intolerable harm to plant equipment, people, or significantly impact plant

operation." Contrary to this standard, the licensee failed to identify the lifting of the man-

hole cover as a critical step and therefore did not institute error prevention tools for this

evolution.

Analysis: The inspectors determined that the failure to properly manage risk of the

underground vault was a performance deficiency warranting a significance evaluation in

accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue

Disposition Screening, issued on September 20, 2007. The inspectors determined that

the finding was more than minor because it was related to maintenance risk assessment

and risk management issues. Specifically, the licensee failed to manage risk for

maintenance activities associated with the electrical switchyard, including the

underground vaults, which could increase the likelihood of a loss of offsite power.

The inspectors performed a significance determination of this issue using IMC 0609,

Significance Determination Process, dated January 10, 2008, and IMC 0609.04, Initial

Screening and Characterization of Findings, dated January 10, 2008. The issue

screened as a transient initiator contributor. As such, the finding was of very low safety

significance because all mitigation equipment or functions were available. The primary

cause of this finding was related to the cross-cutting aspect in the area of Human

Performance because the organization failed to ensure the use of human error

prevention techniques commensurate with the risk of the assigned task H.4(a).

Enforcement: The inspectors determined that no violation of regulatory requirements

occurred because the electrical conduits in man-hole number Eight were not a

safety-related system covered by 10 CFR Part 50, Appendix B. The licensee entered

this issue into their CAP, CR 08-43997. (FIN 05000440/2008004-06)

This review represents the second of five samples as defined in IP 71153-05.

.3

Loss of Configuration Control of the Hydrogen Water Chemistry Injection System

Resulting in High Radiation Levels

a. Inspection Scope

The inspectors observed a planned downpower for maintenance and responded to an

incident that occurred during the evolution when operators received High Radiation

alarms for the Main Steam lines. The inspectors reviewed the circumstance of the

event, the impact on plant safety, licensee response, and regulatory issues.

b. Findings

Introduction: A Green finding (FIN) of very low safety significance was self-revealed

when high radiation level alarms were received on the main steam lines during a

reduction in reactor power. Technicians had failed to adhere to surveillance test

34

Enclosure

procedures and the hydrogen water chemistry (HWC) injection system had been

inadvertently placed in manual.

Description: On June 28, 2008, while reducing power to 60 percent power for control

rod exercise, operators received main steam line high radiation level alarms when

reactor power was at 65 percent. Initially, the cause of the high radiation levels was

unknown to plant operators.

Operators responded by stabilizing reactor power and entering Plant Emergency

Instruction PEI-N11, Containment Leakage Control, and Off-Normal Instruction

ONI-J11, Gross Fuel Cladding Failure. Normal radiation levels for the main steam

lines were about 470 millirem per hour, and levels during the event were as high as 740

millirem per hour.

Operators investigating the cause of the high radiation levels determined that the HWC

injection system was in manual mode, and that the system was injecting at a rate

appropriate for 100 percent reactor power. Operators returned the HWC injection

system to automatic mode so that the injection rate would adjust appropriately to reactor

power levels. This returned radiation levels back to the normal range and operators

exited the plant emergency instruction and off-normal procedure.

The licensee's investigation determined that during a surveillance test conducted on

June 12, 2008, technicians used the HWC computer interface panel to monitor system

status in an effort to limit their radiation exposure while performing the test. The

surveillance, SVI-N64-T8021-A, "Main Condenser Offgas H2/O2 Monitor Channel A

Functional," Revision 7, did not allow for the use of the HWC monitor panel during the

surveillance. While using the panel, technicians inadvertently placed the HWC system in

manual mode, and with no procedural guidance to use the panel, they did not ensure

that the HWC system was in the correct mode of operation after completing their activity.

The investigation also determined that technicians considered the use of the HWC

computer interface panel as an undocumented enhancement to the surveillance

procedure to limit their radiation exposure. The technicians did not communicate this

practice to licensee management for proper review.

The licensee's Nuclear Operating Procedure (NOP)-LP-2601, "Procedure Use and

Adherence," Revision 1, states in 4.1.1, "Procedures shall be used and adhered to as

written without deviating from the original intent and purpose." Contrary to this standard,

licensee personnel did not adhere to the surveillance procedure when they manipulated

the HWC system.

Analysis: The inspectors determined that the failure of licensee personnel to adhere to

surveillance test procedures was a performance deficiency warranting a significance

evaluation in accordance with IMC 0612, ?Power Reactor Inspection Reports,

?Appendix B, ?Issue Disposition Screening,? issued on September 20, 2007. The

inspectors determined that the finding was more than minor because it was associated

with the operating equipment lineup of the configuration control attribute of the initiating

events cornerstone and adversely affected the cornerstone objective of limiting the

likelihood of events that upset plant stability. Specifically, the finding resulted in

unexpected high radiation levels in the plant, entrance into plant emergency procedures,

and challenged operators during a plant power maneuver.

35

Enclosure

The inspectors performed a significance determination of this issue using IMC 0609,

Significance Determination Process, dated January 10, 2008, and IMC 0609.04, Initial

Screening and Characterization of Findings, dated January 10, 2008. The issue

screened as a transient initiator contributor. As such, the finding was of very low safety

significance because all mitigation equipment or functions were available. The finding

had a cross-cutting aspect in the area of Human Performance because the licensee

failed to define and effectively communicate expectations regarding procedural

compliance and personnel did not follow procedures. Specifically, the technicians had

considered the manipulation of the HWC system to be an accepted practice though it

was contrary to the test procedure. H.4(b)

Enforcement: The inspectors determined that no violation of regulatory requirements

had occurred because the HWC injection system is not a safety-related system covered

by 10 CFR Part 50, Appendix B. The licensee entered this issue into their CAP as

CR 08-42529. (FIN 0500440/2008004-07)

This review represents the third of five samples as defined in IP 71153-05.

.4

(Closed) LER 0500440/2008-003-00: Inoperable High Pressure Core Spray System

Results in Loss of Safety Function

On May 28, 2008, the licensee identified, during an ESW 'C' subsystem draindown

surveillance, that ESW 'C' would fail to maintain system keepfill pressure during a loss of

offsite power event. ESW 'C' supported operation of HPCS, and both ESW 'C' and

HPCS were declared inoperable. The licensee inspected the ESW 'C' discharge check

valve and discharge valve. The licensee concluded the check valve was intermittently

stuck open during the surveillance test. The ESW 'C' discharge valve was not fully

seated and technicians made adjustments to the motor-operated valve (MOV) to ensure

complete closure. On June 1, 2008, repairs were completed and the ESW 'C' passed

the loop draindown surveillance, and both HPCS and ESW 'C' were declared operable.

The HPCS is a single train emergency core cooling system (ECCS) and this unplanned

inoperability represented a condition that could have prevented the fulfillment of the

safety function of HPCS when needed to mitigate the consequences of an accident.

During the licensee's investigation and troubleshooting, personnel observed leakage

past the ESW 'C' discharge valve and determined that the valve was approximately four

degrees from the optimum closed position. The licensee reset the closed limit switch of

the ESW 'C' discharge valve to ensure optimum closure of the valve by the valve motor

operator. The licensee determined that the ESW 'C' discharge valve was removed on

June 29, 2007, when ESW 'C' failed the loop draindown test. Inspection of the

discharge internals identified heavily corroded valve internals, and the ESW 'C'

discharge valve was replaced. The only post-maintenance test conducted was the

surveillance for ESW 'C' loop draindown test. No post-maintenance test was conducted

for leak tightness and proper MOV adjustments.

36

Enclosure

Licensee's corrective actions included adjustment of the MOV closed limit switch, the

development of a leak test and MOV testing, and the performance of this testing during

the next refueling outage. This issue was a licensee-identified violation and is

documented in section 4OA7. The licensee documented the issue in CR 08-40969.

This LER is closed.

This review represented the fourth of five samples as defined in IP 71153-05.

.5

Reactor Water Cleanup (RWCU) Pipe Weld Failure

a. Inspection Scope

During the week of September 22, 2008, the inspectors observed the licensees

response to a crack that developed in a RWCU system pipe weld located downstream of

the non-regenerative heat exchanger. The licensee isolated the RWCU system,

performed additional inspections, and repaired the weld. The inspectors reviewed the

circumstances of the event, the impact on plant safety, the licensees response, and any

regulatory issues.

This review represented the fifth of five samples as defined in IP 71153-05.

b. Findings

No findings of significance were identified.

4OA5 Other Activities

.1

Quarterly Resident Inspector Observations of Security Personnel and Activities

a.

Inspection Scope

During the inspection period, the inspectors conducted observations of security force

personnel and activities to ensure that the activities were consistent with licensee

security procedures and regulatory requirements relating to nuclear plant security.

These observations took place during both normal and off-normal plant working hours.

These quarterly resident inspector observations of security force personnel and activities

did not constitute any additional inspection samples. Rather, they were considered an

integral part of the inspectors' normal plant status reviews and inspection activities.

b.

Findings

No findings of significance were identified.

.2

Independent Effectiveness Assessment of the Training Required by the NRCs

August 15, 2007, Confirmatory Order (92702)

a.

Inspection Scope

On August 15, 2007, the NRC issued Confirmatory Order EA-07-199 (Order) that

formalized commitments made by the FirstEnergy Nuclear Operating Company

37

Enclosure

(FENOC). The FENOC commitments were documented in its July 16, 2007, letter

responding to the NRCs May 14, 2007, Demand for Information (DFI).

The Order required, in part, that the licensee conduct regulatory sensitivity training for

selected FENOC and non-FENOC FirstEnergy employees, to ensure those employees

identify and communicate information that has the potential for regulatory impact at any

FENOC nuclear site or within the nuclear industry, to the NRC. This requirement was

inspected and documented in Inspection Report (IR) 05000440/2007005. That IR also

lists all required Order actions.

As part of the NRCs ongoing activities to monitor the licensees implementation of the

Order, the inspectors interviewed 10 individuals who had received the training in

November 2007 to determine how effective the training had been in delivering its

message. The inspectors posed four questions to each of the individuals:

(1) What did you take away from the training?

(2) Has it changed your daily work activities?

(3) Do you have any specific examples?

(4) Has the training changed how you interact with your peers?

In addition, to determine whether the licensee was following its Business Practice, the

inspectors reviewed the assessment forms generated when an issue was brought to

FENOCs Regulatory Affairs group for evaluation.

b.

Observations and Findings

Based on the documentation reviews and observations, the inspectors concluded that

the training was effective at instilling within the FirstEnergy management an enhanced

awareness/sensitivity to issues, and the need to ensure that any issues that could

potentially impact Davis-Besse, Perry, or Beaver Valley, are promptly brought to

FENOCs attention. Each of the 10 individuals interviewed indicated that they were

much more sensitive to ensuring all potentially affected organizations or individuals are

aware of issues and ongoing activities with specific emphasis on those issues potentially

affecting the nuclear facilities. Each individual indicated that asking who else needs to

be aware of an issue has become a standard practice in day-to-day activities. While

there were few examples of specific issues actually being brought to the attention of

Regulatory Affairs staff, individuals identified numerous items in which they or others had

raised the question of who else needs to be aware of the issue. All individuals indicated

that it has become an expected practice during peer meeting/interactions to question the

extent to which potentially impacted organizations have been informed of issues.

Issues raised to the Regulatory Affairs organization are appropriately reviewed for

applicability to the nuclear facilities. Further, in a proactive move, Regulatory Affairs has

implemented a practice of attending meetings in which issues that could affect the

nuclear facilities would likely arise.

38

Enclosure

These results are also being documented in inspection reports for Davis-Besse

(05000346/2008004), and Beaver Valley (05000334/2007005 and 05000412/2008004).

No findings of significance were identified.

.3

NRC Temporary Instruction (TI 2515/173) Review of the Implementation of the Industry

Ground Water Protection Voluntary Initiative

a. Inspection Scope

The inspector performed a partial review of station implementation of the industry ground

water protection initiative for Objective 2.2 Voluntary Communication. As part of that

review, the inspector evaluated the licensees response to an on-site leak of buried

piping associated with the ESW system, which started on or about April 25, 2008.

This inspection constituted a partial sample as defined in TI 2515/173.

b. Findings

No findings of significance were identified.

4OA6 Meetings

.1

Exit Meeting

The inspectors presented the inspection results to the Site Vice President,

Mr. Mark Bezilla, and other members of licensee management on October 14, 2008.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was identified.

.2

Interim Exit Meeting

The preliminary results of the licensees radiological environmental monitoring and

radioactive material control programs, and verification of the PI for public radiation safety

with the Plant General Manager, Mr. K. Kruger, was held on September 12, 2008.

4OA7 Licensee-Identified Violations

The following violations of very low safety significance (Green) were identified by the

licensee and are violations of NRC requirements, which meets the criteria of Section VI

of the NRC Enforcement Policy, NUREG-1600, for being dispositioned as NCVs.

Cornerstone: Mitigating Systems

Technical Specification (TS) 3.5.3, Emergency Core Cooling Systems (ECCS) and

Reactor Core Isolation Cooling (RCIC) System, Condition A.1, required that when the

RCIC system is inoperable, it must be verified within one hour, by administrative means,

that HPCS system is operable. Condition B.1 of TS 3.5.3 requires that when the

Required Action and associated Completion Times of Condition A are not met the plant

must be in Mode 3 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />. Contrary to this requirement, on

December 11, 2007, the HPCS was declared inoperable for maintenance and the plant

39

Enclosure

remained in Mode 1. Specifically, on January 14, 2008, the licensee discovered that the

RCIC flow controller output voltage did not meet operability requirements and this

condition previously existed since December 10, 2007. Not knowing that TS LCO 3.5.3

was not met, licensee personnel did not make the required mode changes. Upon

discovery, the licensee took immediate actions to restore RCIC operability. The finding

was determined to be of very low safety significance because the system inoperable

time was less than 30 days (CR 08-38443).

10 CFR Part 50, Appendix B, Criterion XI, Test Control, requires, in part, that a test

program shall be established to assure that all testing required to demonstrate that

structures, systems, and components will perform satisfactorily in service is identified

and performed in accordance with written test procedures which incorporate the

requirements and acceptable limits contained in applicable design documents. Contrary

to this, on July 21, 2007, the licensee failed to test the C Emergency Service Water

pump discharge valve for seat leakage following valve replacement. This resulted in

high pressure core spray system inoperability and unavailability in May 2008 due to low

keep-fill system pressure. Immediate corrective actions included repair of the affected

valve. The finding was determined to be of very low safety significance because the

system unavailability time was less than three days. (CR 08-40969)

Cornerstone: Occupational Radiation Safety

Perry Plant TS 5.7.1 states in part, that each high radiation area shall be barricaded and

conspicuously posted as a high radiation area. Contrary to the above, on

June 20, 2008, an unlabeled drum of radioactive material with dose rates of 120 millirem

per hour at 30 centimeters was found unattended in the non-high radiation area

controlled area of the control rod drive rebuild room. A violation of regulatory

requirements occurred when the area was not effectively barricaded, controlled, and

conspicuously posted. This was identified in the licensees CAP as CR 08-42154.

Immediate corrective actions were to label and relocate the drum into a properly posted

and controlled high radiation area. The finding was determined to be of very low safety

significance because it was not an as-low-as-is-reasonably-achievable planning issue,

there was no overexposure nor potential for overexposure, and the licensees ability to

assess dose was not compromised.

ATTACHMENT: SUPPLEMENTAL INFORMATION

1

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee

M. Bezilla, Vice President Nuclear

K. Krueger, Plant General Manager

M. Alfonso, Manager, Chemistry

A. Cayia, Director, Performance Improvement

K. Cimorelli, Director, Maintenance

D. Evans, Manager, Operations

E. Gordon, Radiation Protection Operational Superintendent

J. Grabner, Director, Site Engineering

H. Hanson, Jr., Director, Work and Outage Management

S. Thomas, Manger, Radiation Protection

LIST OF ITEMS OPENED, CLOSED, DISCUSSED

Opened and Closed 05000440/2008004-01

NCV

Impaired Fire Barrier for Safety-Related Building (Section

1R05)05000440/2008004-02

NCV

Failure to Implement Compensatory Measures for a Risk-

Management Activity (Section 1R13.1)05000440/2008004-03

NCV

Failure to Implement a Procedurally-Required Risk

Management Activity for a Protected Train (Section 1R13.2)05000440/2008004-04

NCV

Failure to Use Procedures for Work Affecting Safety

(Section 1R15)05000440/2008004-05

NCV

Adequacy of Airlock Ball Valve Maintenance (4OA2.3)05000440/2008004-06

FIN

Failure to Adequately Manage Risk Associated With

Working Around a Risk-Significant Underground Vault

(Section 4OA3.2)05000440/2008004-07

FIN

Loss of Configuration Control of the Hydrogen Water

Chemistry Injection System Resulting in High Radiation

Levels (Section 4OA3.3)

2

Attachment

Closed

05000440/2008-001-00

LER

Condition Prohibited by Technical Specifications Due to

Unrecognized Reactor Core Isolation Cooling Inoperability

(Section 4OA3)

05000440/2008-003-00

LER

Inoperable High Pressure Core Spray System Results in

Loss of Safety Function 05000440/2008003-01

URI

Adequacy of Airlock Ball Valve Maintenance

(Section 4OA3.2)

Discussed 05000440/2007002-02

NCV

Procedures Inappropriate to Circumstances for Degraded

Containment Lower Airlock Inner Door Seal System

(Section 4OA2.3)

Temporary Instruction

2515/173

TI

Review of the Implementation of the Industry Ground Water

Protection Voluntary Initiative (Section 4OA5)

3

Attachment

LIST OF DOCUMENTS REVIEWED

The following is a partial list of documents reviewed during the inspection. Inclusion on this list

does not imply that the NRC inspector reviewed the documents in their entirety, but rather that

selected sections or portions of the documents were evaluated as part of the overall inspection

effort. Inclusion of a document on this list does not imply NRC acceptance of the document or

any part of it, unless this is stated in the body of the inspection report.

1R01 Adverse Weather

ONI-ZZZ-1; Tornado or High Winds; Revision 8

IOI-0015; Seasonal Variations; Revision 14

1R04 Equipment Alignment

VLI R-45; Division 3 Diesel Generator Fuel Oil System (Unit 1); Revision 3

VLI R-47; Division 3 Diesel Generator Lube Oil System (Unit 1); Revision 3

SDM E-22B; High Pressure Core Spray Diesel Generator System; Revision 8

GCI-0016; Scaffolding Erection, Modification or Dismantling Guidelines, Revision 14

CR 08-35043; Division 3 Diesel Governor Oil Level; dated February 5, 2008

CR 08-45038; Fire Impairment Not Prepared for Div 3 DG Exhaust Damper Work;

dated 19 August 2008

USAR Section 9.2.1; Emergency Service Water System; Revision 14

System Description Manual (SDM) P45; Emergency Service Water System; Revision 9

SDM P48; Service Water/Emergency Service Water System Chlorination; Revision 4

CR 08-44095; ESW B Pump has Plexiglass Installed Behind Coupling Guard; dated 7/31/08

CR 08-44079; ESW B Pump Discharge Insulation Separated at Pipe and Pump; dated 7/31/08

VLI-P45; Emergency Service Water System; Revision 7

CR 07-12624; NRC Question on Construction Deficiency Tag Found Hanging on 2P42 HX

supports

CR 08-42723; Sodium Hypochlorite Leak in ESW Supply Line in ESW Pumphouse

USAR Section 9.4.6; Revision 14

SDM M14; Containment Vessel and Drywell Purge System; Revision 5

SOI-M14; Containment Vessel and Drywell Purge System; Revision 18

VLI M14; Containment Vessel and Drywell Purge System (Unit 1); Revision 6

Drawing 912-0604; Containment Vessel and Drywell Purge; Revision BB

VLI E22A; High Pressure Core Spray; Revision 7

Engineering Evaluation Request 600491029; Scaffold in ESW Diesel Fire Pump House; dated

September 10, 2008

1R05 Fire Protection (Annual/Quarterly)

FPI-0IB; Intermediate Building; Revision 5

FPI-1AB; Auxiliary Building; Revision 2

FPI-0CC; Control Complex; Revision 7

FPI-A-A02, "Periodic Fire Inspections," Revision 5

PAP-1910, "Fire Protection Program," Revision 15

PAP-0204, "Housekeeping/Cleanliness Control Program," Revision 20

Drawing D-926-002; Emergency Service Water Pumphouse; Revision E

Drawing D-926-001; Emergency Service Water Pumphouse; Revision K

CR-08-44968; NRC ID'd: NRC Identified Door Open Without Fire Impairment; dated 8/18/08

FPI-A-C01; Fire Protection Program Control Processes (Hot Work Permits, Transient

Combustible Permits, Impairment Permits, and Fire Watches); Revision 10

The Operating License

4

Attachment

FPI-1DG, Diesel Generator Building; Revision 5

Perry USAR for Unit 1, Appendix 9A, Fire Protection Evaluation Plan (Section 9A.4.5, Diesel

Generator Building); Revision 12

CR 08-45442; Unplanned Fire Impairment For F-3C Fire Barrier; dated August 27, 2008

CR 08-45405; Unplanned Fire Impairment For CC-323; dated August 27, 2008

1R11 Licensed Operator Requalification Program

OTLC-3058200809_PY-SGC4; July 23, 2008 Scenario Guide; dated July 21, 2008

1R12 Maintenance Effectiveness

CR 08-41083; Failure of HPCS Test Valve To SP To Fully Stroke Open On The First Attempt;

dated May 31, 2008

CR 08-40520; HPCS Discharge Strainer Blowdown Valve Indicating Light Out; dated

May 18, 2008

CR 08-37864; Discrepancies In PTI-M39-P0002, HPCS Pump Room Cooler Performance

Testing; dated April 7, 2009

Perry Nuclear Power Plant - Maintenance Rule Items List

1R13 Maintenance Risk Assessments and Emergent Work Control

Perry Work Implementation Schedule; Week 10, Period 5

Perry Work Implementation Schedule; Week 1, Period 6

Perry Work Implementation Schedule; Week 2, Period 6

Notification 600472744; Tornado External Missiles and Flooding

Engineering Evaluation Request; Notification # 600250251

Engineering Evaluation Request; Notification # 600308906

Engineering Evaluation Request; Notification # 600472744

CR 05-02081; RFA Request Engineering Evaluate Removal Of Floor Plug; dated

March 11, 2005

1R15 Operability Evaluations

CR 08-44299; Failure to Meet Acceptance Criteria of SVI-R42T5214; dated August 5, 2008

Prompt Operability Determination Form; CR 08-44299; dated August 6, 2008

Prompt Operability Determination Form; CR 08-44262; dated August 8, 2008

CR 08-46155; Seal task Freq Exceeds EQ Calc Life For ESW Ventilation Damper Actuators;

dated September 11, 2008

CR 01-4102; 1M32F0040B Damper Shaft Exhibits Undercut Exceeding Code Acceptance

Criteria; dated November 28, 2001

CR 08-46155; Seal Task Frequency Exceeds EQ Calculation for ESW Ventilation Damper

Actuators; dated September 11, 2008

CR 08-46302; Hydramotors Have A Grace Period Longer Than Allowed By Commitment Letter

L00631; dated September 12, 2008

LER 86-021-00; Hydraulic Seal Failures Result In Inoperable Diesel Generator Building

Ventilation Dampers

SDM G33; Reactor Water Clean-up System; Revision 9

SDM E31; Leak Detection System; Revision 8

SDM P41; Service Water System; Revision 9

PAP-0205; Operability of Plant Systems; Revision 18

WO 200272885; Perform SVI-P41-T2001 (92D) Service Water to Cooling Towers Isolation

Valve Operability Test; dated September 22, 2008

CR 08-46484; Rising Trend in Containment Radwaste Sump In Leakage; dated

September 17, 2008

5

Attachment

CR 08-46546; RWCU Delta Flow Rate Met Threshold for Duty Team Phone Call; dated

September 19, 2008

CR 08-46613; RWCU Leakage Identified in the RWCU Heat Exchanger Room; dated

September 19, 2008

CR 08-46680; SW to Cooling Tower Inboard Isolation Valve Failed to Close During

Surveillance; dated September 22, 2008

CR 01-3384; RFA-Retest Requirements (Why Stroke Valves Twice); dated September 20, 2001

CR 08-45326; Incorrect Gaskets Found on ESW Screen Wash Pump; dated August 26, 2008

CR 08-46852; Functionality Assessment Not Requested for Leak in RWCU Piping; dated

September 25, 2008

CR 08-46986; Unsatisfactory Draft Functionality Assessment; dated September 24, 2008

1R19 Post-Maintenance Testing

WO 200329040; Suppression Pool Level A Wet Leg; dated July 14, 2008

Problem Solving Plan; CR 08-43008 Suppression Pool Instruments Read Incorrectly Following

SVI-E51-T11295E; Revision 0

CR 08-42640; Suppression Pool Level Instruments; dated July 1, 2008

CR 08-43008; Suppression Pool Level A Instrument Read Low After Testing Repeat Issue;

dated July 9, 2008

CR 08-42637; A Suppression Pool Instrument Read Lower Following Venting; dated

July 1, 2008

WO 200328695; Troubleshoot Cause of Multiple AEGTS 'A' Low Flow Alarms; dated

July 14, 2008

CR 08-42798; AEGTS Fan A Low Flow Alarms; dated July 3, 2008

CR 06-00267, New Transmitter Installation Results in Gross Fail Operation Deficiency; dated

January 18, 2006

CR 07-30597, Unplanned Tech Spec Entry Due to Hi Gross Fail Locked In; dated

November 27, 2007

CR 08-46223, Received Gross Fail High During Norma Surveillance Flow Testing; dated

September 13, 2008

ICI-B21-1, Rosemount Master Trip Unit (510DU) and (710DU); Revision 5

SVI-E12-T1195-C, LPCI Pump C Low Flow (Bypass) Channel Calibration for 1E12-N052C;

Revisions 5 and 6

SVI-E51-T1293-A, RCIC Actuation - CST Low Level Channel A Calibration for 1E51-N035A;

Revisions 4 and Revision 5

SVI-P41-T2001; Service Water to Cooling Towers Isolation Valve Operability Test; Revision 6

SVI-G43-T1305E; Accident Monitoring Suppression Pool Water Level Channel Calibration;

Revision 3

WO 200340028; Perform Visual Inspections of OP41F0420 MOV Operator Identify Deficiencies,

and Cycle Valve Remotely for Testing; dated September 23, 2008

WO 200203776; Perform Service Water to Cooling Towers Isolation Valve Operability Test SVI

for PMT of Valve P41F0420; dated September 25, 2008

WO 200201001; Perform Recorder Replacements Utilizing ECP 06-0016-01 which superseded

ECP 04-0043 & ECP 06-0069; dated September 23, 2008

ECP 06-0016-001; Replace Recorders 1G43R0093A, 1G43R0073A, 1D23R0250A,

1D23R0180A, 1M51R0090 and 1M51R0091 with New Recorders 1G43R0103A,

1D23R0281A and 1M51R0731; dated January 27, 2008

CR 08-46680; SW to Cooling Tower Inboard Isolation Valve Failed to Close During

Surveillance; dated September 22, 2008

CR 06-01466; Westronics Recorder Series 1220B ECP Problems; dated March 29, 2006

6

Attachment

CA 05-00013; Suppression Pool Level High Range Recorder Blue Pen Failed; dated

January 1, 2005

1R22 Surveillance Testing

WO 200274103; SVI-P42T2001A; Emergency Closed Cooling System A Pump and Valve

Operability; dated August 4, 2008

WO 200314659; Visual Inspection of the Emergency Diesel Generator hallway; dated

August 2008

SOI-E22B, Division 3 Diesel Generator; Revision 23

SVI-E22-T1319, Diesel Generator Start and Load Division 3; Revision 14

SVI-C51-T0030-G, APRM G Channel Calibration for 1C51-K605G; Revision 9

SVI-C51-T0051A; OPRM Channel A Functional For 1C51-K603A; Revision 4

WO 200269152; Perform SVI-C61-T1200 (184D) OPRM Channel A Functional for 1C51-K603A;

dated September 25, 2008

1EP6 Drill Evaluation

OTLC-3058200810-PY-SGC2; dated August 22, 2008

2OS1 Access Control to Radiologically Significant Areas

CR 07-26352; Potential LHRA Issues Associated with the Spent Fuel Clean-Out Project; dated

September 2007

CR 07-26415; Container Identified Tied Off to handrail in Fuel Handling Building; dated

September 2007

CR 07-26726; Locked High Radiation Area Key/Door Controls; dated September 2007

CR 07-26930; Change Management Failed to Identify a Change in VHRA Key (Inventory

Frequency); dated September 2007

CR 08-42154; Elevated Dose Rates on Unlabeled Drum; dated June 2008

HPI-C0010; Radiation Protection Support of Plant Startup; Revision 5

HPI-C0014; Radlock Key Issue; Revision 0

HPI-L0009; Discrete Particle Control; Revision 4

IOI-17; Drywell Entry and Access Control; Revision 10

NOP-WM-7025; High Radiation Area Program; Revision 02

NOP-WM-7003; Radiation Work Permit (RWP); Revision 04

4OA1 Performance Indicator Verification

Perry Safety System Functional Failures; July 2007

Perry Safety System Functional Failures; August 2007

Perry Safety System Functional Failures; September 2007

Perry Safety System Functional Failures; October 2007

Perry Safety System Functional Failures; November 2007

Perry Safety System Functional Failures; December 2007

Perry Safety System Functional Failures; January 2008

Perry Safety System Functional Failures; February 2008

Perry Safety System Functional Failures; March 2008

Perry Safety System Functional Failures; April 2008

Perry Safety System Functional Failures; May 2008

Perry Safety System Functional Failures; June 2008

LER 2007-003; Improper Containment Floor Grating Installation Results in an Unanalyzed

Condition; dated October 26, 2007

NOBP-LP-4012; NRC Performance Indicators; Revisions 3

7

Attachment

SVI-P35-T3011; Perry Operations Manual Surveillance Instruction; Dose Equivalent Iodine

Analysis; Revision 6

4OA2 Identification and Resolution of Problems

WO 200273140; Penetration Pressurization Valve Operability Test; dated March 27, 2008

CR 08-43113; Condition Report 08-41101 Did Not Identify The Airlock Ball Valve Failure Cause;

dated July 11, 2008

CR 08-41097; Upper Air Lock Outer Door Unplanned Tech Spec Entry; dated June 1, 2008

CR 08-41101; P53-Upper Airlock Outer Door Outer Seal; dated June 1, 2008

WO 200176053; Upper Containment Airlock Outer Door Tubing; dated March 29, 2008

WO 200249806; Upper Containment Airlock Outer Door Ball Valve; dated March 29, 2008

WO 200324733; 3-Way Valve Outer Door Small Seal Upper; dated June 4, 2008

WO 200324651; Upper Containment Airlock Outer Door Seal; dated June 2, 2008

CR 08-46177; RWCU Inlet Conductivity Reading Erratic; dated September 12, 2008

CR 08-46160; 1N25-N226B Yarway Pegged High MSR 1B DT Alarm; dated

September 11, 2008

CR 08-40969; High Pressure Core Spray Inoperable; dated May 28, 2008

WO 200272874; HPCS ESW Pump Discharge Check Valve; dated May 31, 2008

WO 200176053; Upper Containment Outer Door; dated March 29, 2008

CR 08-43678; Upper Airlock Order Contains Parts Discrepancy Used In Ball Valve Rebuild;

dated July 23, 2008

CR 08-43422; Near Miss Incident Concerning SAM9; dated July 18, 2008

4OA3 Follow-up of Events and Notices of Enforcement Discretion

CR 08-38443; RCIC Controller Output Computer Point, Decreasing Trend; dated April 16, 2008

CR 08-3911; Unplanned Tech Spec Entry RCIC System Controller Failure; dated April 24, 2008

4OA5 Other Activities

CR 08-39814; ESW Coupling Leak - Division 2; dated May 2008

CR 08-43250; Perry Response to NRC Tritium Inquiry; dated July 2008

FirstEnergy Groundwater Field Sampling Plan, Perry Nuclear Power Plant; dated August 2007

NOP-OP-2012; Groundwater Monitoring; Revisions 01 and 02

8

Attachment

LIST OF ACRONYMS USED

°F

degrees Fahrenheit

AC

alternating current

ADHR

alternate decay heat removal

AEGTS

annulus exhaust gas treatment system

APRM

average power range monitor

CAP

Corrective Action Program

CFR

Code of Federal Regulations

CR

condition report

DFI

Demand for Information

DFP

diesel fire pump

ECC

emergency closed cooling

EDG

emergency diesel generator

EER

Engineering Evaluation Request

ESW

emergency service water

FENOC

FirstEnergy Nuclear Operating Company

FIN

Finding

FPI

Fire Protection Instruction

GMI

Generic Mechanical Instruction

HPCS

high pressure core spray

HWC

hydrogen water chemistry

IMC

Inspection Manual Chapter

IP

Inspection Procedure

IR

Inspection Report

LCO

limiting condition for operation

LER

Licensee Event Report

LPCS

low pressure core spray

MOV

motor-operated valve

MSPI

mitigating systems performance index

MW

MegaWatt

NCV

non-cited violation

NEI

Nuclear Energy Institute

NOP

Nuclear Operating Procedure

NRC

Nuclear Regulatory Commission

OPRM

oscillating power range monitor

PAP

Perry Administrative Procedure

PI

performance indicator

RCIC

reactor core isolation cooling

RHR

residual heat removal

RWCU

reactor water cleanup

SDP

Significance Determination Process

SVI

Surveillance Instruction

TI

Temporary Instruction

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

USAR

Updated Safety Analysis Report

WO

work order