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Category:Memoranda
MONTHYEARML24124A0342024-05-0101 May 2024 Summary of Public Meeting Concerning Annual Assessment of Catawba Nuclear Station Units 1 and 2, McGuire Nuclear Station Units 1 and 2, Oconee Nuclear Station Units 1, 2, and 3, Brunswick Steam Electric Plant Units 1 and 2, Shearon Harris ML24047A2092024-02-22022 February 2024 Calendar Year 2023 Baseline Inspection Completion ML23118A2852023-05-0202 May 2023 Public Meeting Summary - 2022 Annual Assessment Meeting Regarding Catawba Nuclear Station, McGuire Nuclear and Oconee Nuclear Station ML22300A0742023-01-11011 January 2023 Final Environmental Assessment and Finding of No Significant Impact for the Duke Energys Updated Decommissioning Funding Plans Submitted in Accordance with 10 CFR 72.30(C) for Catawba Nuclear Station Independent Spent Fuel Storage Installat ML21099A0932021-04-0909 April 2021 Public Meeting Summary - 2020 Annual Assessment Meeting Regarding Catawba, McGuire, and Oconee Nuclear Stations ML20141L4172020-05-20020 May 2020 EOC Public Meeting Summary ML19098B4482019-04-0808 April 2019 Public Meeting Summary ML18117A2212018-04-27027 April 2018 Summary of Public Meeting with Catawba Nuclear Station Concerning Annual Assessment of Units 1 and 2 for Period of January 01, 2017 - December 21, 2017 ML17107A0642017-04-17017 April 2017 Summary of Public Meeting with Catawba, Units 1 and 2 ML16111B2472016-04-28028 April 2016 Request for Additional Information Re. License Amendment Request to Revise TS 5.5.2 Containment Leakage Rate Testing Program ML16088A2042016-03-28028 March 2016 Memo T Bowers from s Ruffin, Technical Assistance Requests - Review 2015 Tri-Annual Decommissioning Funding Plans for Multiple Independent Spent Fuel Storage Installations W/ Encl 2 (Template) ML16088A2052016-03-28028 March 2016 Enclosure 1 - (72.30 DFP Reviews to Be Completed 2015) - Memo T Bowers from s Ruffin, Technial Assistance Requests - Review 2015 Tri-Annual Decommissioning Funding Plans for Multiple Independent Spent Fuel Storage Installations ML16081A3352016-03-17017 March 2016 Summary of Meeting with Public Concerning Annual Assessment of Catawba Nuclear Station, Units 1 and 2 ML15253A4032016-03-11011 March 2016 Recommendation for Dispositioning Proposed Generic Issue on the Effects of Downstream Dam Failures on Nuclear Power Plants ML15244B2522015-08-31031 August 2015 Report on Trip to Catawba on August 26-27, 2015 ML15106A0302015-04-15015 April 2015 Meeting Summary with Public to Discuss the Annual Assessment of Catawba Nuclear Station, Units 1 and 2 ML14126A6792014-05-0606 May 2014 Summary of Public Meeting with Catawba, Units 1 & 2 to Discuss Annual Assessment ML14077A1312014-03-18018 March 2014 Special Inspection Charter to Evaluate the Abnormal Rotation of the Piston Crankshaft Bearings on the Catawba Unit 1 Diesel Generators ML13295A3062013-10-22022 October 2013 Meeting Notice with Duke Energy Carolinas, LLC Discuss the Planned Modifications Related to the Fukushima Flood Hazard Reevaluations for the Sites Operated by Duke Energy Carolinas, LLC ML13135A5962013-05-16016 May 2013 Cancelled 05/23/2013 Notice of Forthcoming Pre-Application Meeting with Duke Energy Carolinas, Llc. to Discuss a Proposed License Amendment Request Concerning Methodology Report DPC-NE-3001-P for Catawba and McGuire Nuclear Stations ML13127A4352013-05-0909 May 2013 Notice of Forthcoming Pre-Application Meeting with Duke Energy Carolinas, Llc. to Discuss a Proposed License Amendment Request Concerning Methodology Report DPC-NE-3001-P for Catawba and McGuire Nuclear Stations ML13072B2022013-03-19019 March 2013 Meeting Notice with Duke Energy Concerning NFPA-805 Performance-Based Standard for Fire Protection for Light Water Reactor Electric Generating Plants License Amendment Request for Catawba, McGuire, and H. B. Robinson ML12300A4032012-10-26026 October 2012 11/8/2012 Meeting Notice with Duke Energy to Discuss NRC Order on Mitigation Strategies for Beyond-design-Basis External Events ML12284A4612012-10-12012 October 2012 Forthcoming Meeting Notice with Duke Energy to Discuss NRC Order on Mitigation Strategies for Beyond-Design-Basis External Events ML12103A3522012-04-10010 April 2012 Special Inspection Charter to Evaluate Catawba Loss of Offsite Power ML1106603302011-03-0707 March 2011 Notice of Meeting with Duke Energy to Present Status of Licensing Submittals Regarding Implementation of National Fire Protection Association Standard 805, Requirements at Catawba Nuclear Station, Units 1 and 2 and McGuire Nuclear Station ML1029306502010-10-20020 October 2010 Notice of Forthcoming Conference Call with Duke Energy Carolinas, LLC Regarding McGuire Nuclear Station, Units 1 and 2 and Catawba Nuclear Station, Units 1 and 2, ML1021400692010-08-0404 August 2010 Notice of Meeting with Duke Energy to Discuss Duke Energy'S Assessment of the Results of the Catawba Baseline Inspection Conducted by the NRC ML1015804072010-06-0808 June 2010 the Nuclear Regulatory Commission Staff Spot-Check Review of Duke Energy'S Ownership Interest of Catawba, Units 1 and 2, McGuire, Units 1 and 2, and Oconee, Units 1, 2 and 3 on May 20, 2010 - Finding of No Potential Issues in Bank Statement ML1015804682010-06-0808 June 2010 the Nuclear Regulatory Commission Staff Spot Check Review of North Carolina Electric Membership Corporation'S Ownership Interest of Catawba Nuclear Station Units 1 and 2 on May 20, 2010 - Finding of No Potential Issues in Bank Statements ML1015900402010-06-0808 June 2010 the Nuclear Regulatory Commission Staff Spot-Check Review of Piedmont Municipal Power Agency'S Ownership Interest of Catawba Nuclear Station Units 1 and 2 on May 19, 2010 - Finding of No Potential Issues in Bank Statements ML1012604632010-05-0707 May 2010 Notice of Forthcoming Conference Call with Duke Energy Carolinas, LLC (Duke) to Discuss Duke'S Responses to Generic Letter 2004-02 at Catawba 1 and 2 and McGuire 1 and 2 ML0926700202009-10-0707 October 2009 Summary of Conference Call with Duke Regarding Responses to Generic Letter (GL) 2004-02 ML0925404602009-09-10010 September 2009 Summary of Phone Call with Industry to Issues Related to Eccentricity of the Steam Generator Tube-to-Tubesheet Joints in the Finite Element Model Used for the Technical Basis of the Permanent Alternate Repair Criteria License Amendment Requ ML0922908922009-08-18018 August 2009 Notice of Conference Call with Duke Energy Carolinas, LLC (Duke), Regarding Catawba Nuclear Station, Units 1 and 2 (Catawba 1 and 2) and McGuire Nuclear Station Units 1 and 2 ML0831009482008-11-10010 November 2008 Notice of Meeting with Duke Energy Carolinas, LLC, (Duke), Catawba, Units 1 and 2, and McGuire, Units 1 and 2 ML0831107952008-11-0606 November 2008 Cancellation of Meeting with Duke Energy Carolinas, LLC, to Discuss the Request for Additional Information Generic Letter 2004-04, Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents. ML0829701832008-10-30030 October 2008 Notice of Meeting with Duke Energy Carolinas, LLC, to Discuss the Request for Additional Information Generic Letter 2004-04, Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents ... ML0818301542008-07-0101 July 2008 Notice of Meeting with Duke Energy Carolinas, LLC to Discuss Transition to ASME NQA-1-1994 ML0817903662008-06-27027 June 2008 Safety Evaluation by the Office of Nuclear Reactor Regulation Application for Direct Transfer of Facility Operating License Catawaba Nuclear Station, Unit 1 ML0807400842008-03-14014 March 2008 Draft Regulatory Guide for Comment ML0800201632008-01-0303 January 2008 Cancelled - Meeting with Duke Power Company ML0800202162008-01-0303 January 2008 Forthcoming Meeting with Duke Power Company LLC Catawba Nuclear Station to Discuss the Relief Request Dated October 26, 2006 (Agencywide Documents Access and Management System Accession No. ML063120211) ML0733711662007-12-0303 December 2007 Notice of Meeting with Progress Energy & Duke Energy Regarding Fire Probabilistic Risk Assessment for the Pilot Plants Transitioning to the National Fire Protection Association Standard NFPA 805 ML0628401062006-10-18018 October 2006 Staff'S Review of CLIIP Amendment to Adopt TSTF-372 ML0614505462006-05-25025 May 2006 Revised Augmented Inspection Team Charter ML0614303612006-05-23023 May 2006 Augmented Inspection Team Charter for Catawba, Units 1 and 2 ML0533900722005-12-0707 December 2005 Notice of Forthcoming Meeting with Duke Energy Corporation, to Discuss Reload Design and Safety Analysis Methodology Report Submittals ML0524103052005-09-0606 September 2005 08/18/05 - Summary of Public Meeting on Mspi/Rop Topics for August 17/18, 2005 ML0524503412005-09-0202 September 2005 Notice of Meeting with Duke Energy Corp, Regarding RAIs on Nuclear Service Water System for Catawba, Units 1 and 2 2024-05-01
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May 23, 2006 MEMORANDUM TO: James H. Moorman, Chief Operations Branch Division of Reactor Safety FROM: William D. Travers, Regional Administrator /RA/
SUBJECT:
AUGMENTED INSPECTION TEAM CHARTER An Augmented Inspection Team (AIT) has been established for Catawba Nuclear Station to inspect and assess the facts surrounding a loss of offsite power (LOSP) and subsequent dual unit reactor trip at Catawba on or around May 20, 2006. The team composition is as follows:
Team Leader: J. Moorman, RII Team Members: N. Merriweather, RII M. Cain, RII R. Lewis, RII A. Sabisch, RII The objectives of the inspection are to: (1) review the facts surrounding the LOSP on May 20, 2006, and related plant complications; (2) assess the licensees response and investigation of the event; (3) identify any generic issues associated with the event; and (4) conduct an independent extent of condition review.
For the period during which you are leading this inspection and documenting the results, you will report directly to me. The guidance in Inspection Procedure 93800, Augmented Inspection Team, and Management Directive 8.3, NRC Incident Investigation Program, applies to your inspection.
If you have any questions regarding the objectives of the enclosed charter, contact Charles A. Casto at (404) 562-4500.
Enclosure:
AIT Charter Docket Nos.: 50-413 and 50-414 License Nos.: NPF-35 and NPF-52
Contact:
D. Charles Payne, RPB1/DRP (404) 562-4540
OFFICE RII:DRP RII:DRP SIGNATURE DCP CAC1 NAME CPayne CCasto DATE 05/23/2006 05/23/2006 5/ /2006 5/ /2006 5/ /2006 5/ /2006 5/ /2006 E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO Memo to James H. Moorman from William D. Travers dated May 23, 2006.
SUBJECT:
AUGMENTED INSPECTION TEAM CHARTER Distribution:
cc: W. Kane, OEDO S. Lee, OEDO J. Dyer, NRR C. Haney, NRR R. Martin, NRR R. Zimmerman, NSIR L. Plisco, RII C. Casto, RII V. McCree, RII
AUGMENTED INSPECTION TEAM (AIT) CHARTER CATAWBA LOSS OF OFFSITE POWER AND DUAL UNIT REACTOR TRIP Basis for the Formation of the AIT - On May 20, 2006, an electrical fault occurred apparently causing several power circuit breakers (PCB) to open in the Catawba switchyard. This fault apparently caused several other PCBs to open resulting in a loss of offsite power (LOSP) and trip of both Catawba reactors. In accordance with Management Directive 8.3, NRC Incident Investigation Program, deterministic and conditional risk criteria were used to evaluate the level of NRC response for this operational event. The review concluded that the circumstances of the event met the MD 8.3 deterministic criteria due to an apparent single electrical failure causing a loss of offsite power to both operating units and reactor trips. The risk review indicated the CCDP for the event met the criterion for an Augmented Inspection. Subsequently, Region II determined that the appropriate level of NRC response was the conduct of an Augmented Inspection.
This Augmented Inspection is chartered to identify the circumstances surrounding this event and review the licensees actions following discovery of the conditions.
Objectives of the AIT - The objectives of the inspection are to: (1) review the facts surrounding the LOSP on May 20, 2006, and related plant complications; (2) assess the licensees response and investigation of the event; (3) identify any generic issues associated with the event; and (4) conduct an independent extent of condition review.
To accomplish these objectives, the following will be performed:
- a. Develop a complete sequence of events, including applicable management decision points, from the time the LOSP occurred until both units were stabilized.
- b. Identify and evaluate the effectiveness of the immediate actions taken by the licensee in response to this event including the accuracy and timeliness of the licensees classification of the event.
- c. Identify additional actions planned by the licensee in response to this event, including the time line for their completion of the investigation and follow-on analysis.
- d. Assess the circumstances surrounding the multiple lifting and reseat of the Unit 1 and Unit 2 primary power operated relief valves.
- e. Determine if there are any generic issues related to this event which warrant an additional NRC response. Promptly communicate any potential generic issues to regional management.
- f. Document the inspection findings and conclusions in an inspection report within 30 days of the inspection.
Enclosure