ML030280343

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IR 05000254-02-008, 05000265-02-008, on 10/01-12/28/02, Exelon Nuclear; Quad Cities Nuclear Power Station; Units 1 and 2. Adverse Weather, Refueling and Outage Activities, Identification and Resolution of Problems, and Event Followup
ML030280343
Person / Time
Site: Quad Cities  Constellation icon.png
Issue date: 01/27/2003
From: Ring M
NRC/RGN-III/DRP/RPB1
To: Skolds J
Exelon Generation Co
References
IR-02-008
Download: ML030280343 (54)


See also: IR 05000254/2002008

Text

January 27, 2003

Mr. John L. Skolds, President

Exelon Nuclear

Exelon Generation Company, LLC

Quad Cities Nuclear Power Station

4300 Winfield Road

Warrenville, IL 60555

SUBJECT:

QUAD CITIES NUCLEAR POWER STATION, UNITS 1 AND 2

NRC INTEGRATED INSPECTION REPORT 50-254/02-08; 50-265/02-08

Dear Mr. Skolds:

On December 28, 2002, the U. S. Nuclear Regulatory Commission (NRC) completed an

integrated inspection at your Quad Cities Nuclear Power Station, Units 1 and 2. The enclosed

report documents the inspection findings which were discussed on December 31, 2002, with

Mr. Tulon and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, the inspectors identified seven issues of very low safety

significance (Green). Three of these issues were determined to involve violations of NRC

requirements. However, because of their very low safety significance and because they have

been entered into your corrective action program, the NRC is treating these issues as Non-

Cited Violations in accordance with Section VI.A.1 of the NRCs Enforcement Policy.

If you contest the subject or severity of a Non-Cited Violation, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the

U.S. Nuclear Regulation Commission, ATTN: Document Control Desk, Washington, DC

20555-0001, with a copy to the Regional Administrator, U.S. Nuclear Regulatory Commission -

Region III, 801 Warrenville Road, Lisle, IL 60532-4351; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the Resident

Inspector Office at the Quad Cities Nuclear Power Station.

Since the terrorist attacks on September 11, 2001, the NRC has issued two Orders (dated

February 25, 2002, and January 7, 2003) and several threat advisories to licensees of

commercial power reactors to strengthen licensee capabilities, improve security force

readiness, and enhance access authorization. The NRC also issued Temporary Instruction

2515/148 on August 28, 2002, that provided guidance to inspectors to audit and inspect

licensee implementation of the interim compensatory measures (ICMs) required by the

February 25th Order. Phase 1 of TI 2515/148 was completed at all commercial nuclear power

J. Skolds

-2-

reactors during calendar year (CY) 02, and the remaining inspections are scheduled for

completion in CY 03. Additionally, table-top security drills were conducted at several licensees

to evaluate the impact of expanded adversary characteristics and the ICMs on licensee

protection and mitigative strategies. Information gained and discrepancies identified during the

audits and drills were reviewed and dispositioned by the Office of Nuclear Security and Incident

Response. For CY 03, the NRC will continue to monitor overall safeguards and security

controls and conduct inspections, and will resume force-on-force exercises at selected power

plants. Should threat conditions change, the NRC may issue additional Orders, advisories, and

temporary instructions to ensure adequate safety is being maintained at all commercial nuclear

power reactors.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter

and its enclosure will be available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRC's

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Mark A. Ring, Chief

Branch 1

Division of Reactor Projects

Docket Nos. 50-254; 50-265

License Nos. DPR-29; DPR-30

Enclosure:

Inspection Report 50-254/02-08; 50-265/02-08

See Attached Distribution

DOCUMENT NAME: G:\\quad\\ML030280343.wpd

To receive a copy of this document, indicate in the box:"C" = Copy without enclosure "E"= Copy with enclosure"N"= No copy

OFFICE

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NAME

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MRing

DATE

01/24/03

01/27/03

OFFICIAL RECORD COPY

J. Skolds

-3-

cc w/encl:

Site Vice President - Quad Cities Nuclear Power Station

Quad Cities Nuclear Power Station Plant Manager

Regulatory Assurance Manager - Quad Cities

Chief Operating Officer

Senior Vice President - Nuclear Services

Senior Vice President - Mid-West Regional

Operating Group

Vice President - Mid-West Operations Support

Vice President - Licensing and Regulatory Affairs

Director Licensing - Mid-West Regional

Operating Group

Manager Licensing - Dresden and Quad Cities

Senior Counsel, Nuclear, Mid-West Regional

Operating Group

Document Control Desk - Licensing

Vice President - Law and Regulatory Affairs

Mid American Energy Company

M. Aguilar, Assistant Attorney General

Illinois Department of Nuclear Safety

State Liaison Officer, State of Illinois

State Liaison Officer, State of Iowa

Chairman, Illinois Commerce Commission

W. Leach, Manager of Nuclear

MidAmerican Energy Company

J. Skolds

-4-

ADAMS Distribution:

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U. S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

50-254; 50-265

License Nos:

DPR-29; DPR-30

Report No:

50-254/02-08; 50-265/02-08

Licensee:

Exelon Nuclear

Facility:

Quad Cities Nuclear Power Station, Units 1 and 2

Location:

22710 206th Avenue North

Cordova, IL 61242

Dates:

October 1 through December 28, 2002

Inspectors:

K. Stoedter, Senior Resident Inspector

M. Kurth, Resident Inspector

J. House, Radiation Protection Inspector

D. Jones, Engineering Inspector

R. Kopriva, Senior Project Engineer, Region IV

P. Lougheed, Engineering Inspector

D. Nelson, Radiation Protection Inspector

P. Pelke, Reactor Engineer

G. Pirtle, Physical Security Inspector

T. Ploski, Senior Emergency Preparedness Inspector

S. Sheldon, Engineering Inspector

T. Steadham, Reactor Engineer

Approved by:

Mark Ring, Chief

Branch 1

Division of Reactor Projects

2

SUMMARY OF FINDINGS

IR 05000254/2002-008, 05000265/2002-008; Exelon Nuclear; on 10/01-12/28/02, Quad Cities

Nuclear Power Station; Units 1 & 2. Adverse Weather, Refueling and Outage Activities,

Identification and Resolution of Problems, and Event Followup.

This report covers a 3-month period of baseline resident inspection and announced baseline

inspections on Temporary Instruction 2515/148, radiation protection, inservice inspection, and

emergency preparedness. The inspection was conducted by regional inspectors and the

resident inspectors. Three Severity Level IV Non-Cited Violations (NCV) and seven Green

Findings were identified. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using Inspection Manual Chapter 0609, Significance Determination

Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a

severity level after NRC management review. The NRCs program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 3, dated July 2000.

A.

Inspector-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green. The failure to identify the proper plant air supply prior to installing moisture

separator decontamination equipment (air powered vacuum) resulted in two unexpected

instrument air system transients on October 14 and 15, 2002. The work package did not

contain equipment identification numbers to aid in identifying the proper air supply. In

addition, the individual instructed to identify the air supply failed to perform self-checking

activities that could have identified the inappropriate selection of instrument air for the

equipment installation rather than service air.

This finding was more than minor because it affected the loss of instrument air initiating

event frequency. The finding was of very low safety significance because the exposure

time was short and all mitigating systems needed to address a loss of instrument air

were available. No violation of NRC requirements occurred due to the instrument air

system being non-safety-related. (Section 1R20.1)

Green. The failure to adequately correct deficiencies in the 1B reactor recirculation

motor generator voltage regulator resulted in a pump trip and power transient on

December 6, 2002. On November 29 and December 3, the licensee initiated two

condition reports due to the motor generator voltage regulator failing to meet acceptance

criteria during tuning activities. The inspectors determined that the licensee had not

adequately considered changes made to the voltage regulator during the outage and

power ascension which resulted in inappropriately concluding that the failure to meet the

acceptance criteria was acceptable.

This finding was determined to be more than minor because the reactor recirculation

pump trip was a precursor to a significant transient. This finding was considered to be of

very low safety significance since it did not: contribute to the likelihood of both a reactor

trip and that mitigating equipment would not be available, contribute to the likelihood of a

3

loss of coolant accident, increase the likelihood of a fire or flood, or increase the

frequency of core damage scenarios using other plant specific analyses.

(Section 4OA2.1)

Cornerstone: Mitigating Systems

Green. A self-revealing failure occurred on October 16, 2002, when the safe shutdown

makeup pump room cooler strainer became clogged with duck weed. The inspectors

determined that twice per shift rounds to verify strainer operability and multiple strainer

cleanings were not effective in ensuring continued operability of this equipment. In

addition, control room personnel were not immediately notified of the clogged strainer via

a control room alarm or a local alarm due to a system design deficiency.

This finding was more than minor because the strainer clogging impacted the operability

of the safe shutdown makeup pump which can be used when responding to initiating

events. In addition, the system design issues created a situation where operations

personnel were unaware of equipment operability issues. This finding was of very low

safety significance because the total exposure time was short, all other mitigating

systems were available, and the safe shutdown makeup pump could have been

recovered if needed. No violation of NRC requirements occurred due to the safe

shutdown makeup only being of augmented quality per the licensees Quality Assurance

Report. (Section 1R01.2)

Green. During the 1A stator water heat exchanger tube bundle replacement on

November 11, 2002, approximately 200 gallons of water were released as the tube

bundle was pulled from the heat exchanger. The water migrated to the Unit 1 emergency

diesel generator room below and tripped the circulating oil pump and turbocharger

lubricating oil pump rendering the diesel inoperable. The work package used to perform

the work did not contain information regarding the large amounts of water that may be

present in the heat exchanger. In addition, information regarding the amount of water

present in the heat exchanger was not communicated to the contractors performing the

work even though this information was well known by operations and maintenance

personnel.

This finding was more than minor because the inadequate work instructions and poor

communications resulted in a situation which impacted the operability, availability, and

reliability of the emergency diesel generator. The finding was of very low safety

significance since the loss of the emergency diesel generator did not result in an actual

loss of safety function of a system and did not result in an actual loss of safety function of

a single train for greater than the Technical Specification Allowed Outage Time. No

violations of NRC requirements were identified due to the stator water heat exchanger

being non-safety-related. (Section 1R20.2)

Green. The inspectors identified a Non-Cited Violation of 10 CFR Part 50, Appendix B,

Criterion V, due to the failure to adhere to procedural requirements regarding the

erection of scaffolding near safety-related equipment. On November 6, 2002, the

inspectors identified numerous examples where scaffolding was in contact with residual

heat removal system piping and valves.

4

This finding was more than minor since multiple examples of scaffolding erection

deficiencies were identified which indicated that workers routinely failed to follow

scaffolding erection procedural requirements. This finding was determined to be of very

low safety significance since the scaffolding did not result in an actual loss of safety

function of any system. (Section 1R20.4)

Green. A loose wire caused a condition that would have resulted in the failure of the 2B

residual heat removal system to automatically start when required and would have

resulted in the diversion of water from the 2A residual heat removal system if an

emergency core cooling system actuation signal was received while the 2B residual heat

removal system was operating in torus cooling. One Non-Cited Violation of Technical Specification 3.5.1 was identified. The licensee determined that the wire was loosened

during the February 2002 refueling outage. The impact of the loose wire was not

addressed until October 2002 even though unexpected equipment performance was

experienced on three previous occasions.

This finding was more than minor since the loose wire impacted the operability,

availability, reliability, and capability of the residual heat removal system. The finding

was determined to be of very low risk significance since the both trains of the residual

heat removal system were recoverable using simple operator actions and all remaining

mitigating systems equipment were available. (Section 4OA3.2)

Cornerstone: Barrier Integrity

Green. The failure to adhere to procedure precautions and perform timely control room

panel monitoring resulted in the inadvertent isolation of the reactor water cleanup system

while the system was being used to remove decay heat from the Unit 1 reactor vessel. A

Non-Cited Violation of Technical Specification 5.4.1 was identified.

This finding was determined to be more than minor because the isolation impacted the

reactor water cleanup systems continued ability to provide cooling of the reactor fuel and

fuel cladding while the Unit 1 reactor was in a shutdown condition. The finding was of

very low safety significance since the isolation did not significantly degrade the licensees

ability to recover decay heat removal through the use of the reactor water cleanup or

residual heat removal systems once the isolation occurred. (Section 1R20.3)

B.

Licensee-Identified Violations

Licensee-Identified Violations of very low safety significance have been reviewed by the

inspectors. Corrective actions taken or planned by the licensee have been entered into

the corrective action program. These violations and corrective action tracking numbers

are listed in Section 4OA7 of this report.

5

REPORT DETAILS

Summary of Plant Status

Unit 1 began the inspection period operating at reduced power levels due to entering

coastdown. On November 5 operations personnel shut down Unit 1 and began a refueling

outage. Major activities accomplished during the outage included implementation of an

extended power uprate, replacement of the high pressure turbine rotor, modifications to the

reactor steam dryer, installation of new condensate demineralizers, and upgrading the high and

low pressure feedwater heaters. Unit 1 achieved criticality on November 25 and was

synchronized the grid the following day. On December 2 the licensee began power uprate

testing. During the multi-day testing evolution, an unisolable leak developed on the 1B reactor

feedwater pump. Operations personnel lowered reactor power to 85 percent to complete the

leak repairs. On December 6 the operators restored reactor power to 94 percent and began

additional power uprate testing. Upon reaching 97 percent power, the 1B reactor recirculation

pump tripped due to motor generator set overcurrent on two out of three phases. The pump

trip resulted in reducing reactor power to approximately 35 percent. The licensee completed

repairs to the reactor recirculation pump on December 9 and continued with the power

ascension. Unit 1 achieved and maintained the maximum post-extended power uprate power

level on December 11. Engineering and operations personnel completed all required power

uprate testing later the same week.

Unit 2 entered the inspection period operating at the maximum achievable power level. On

October 7 operations personnel lowered reactor power to approximately 80 percent to repair a

leak on the 2A reactor feedwater pump suction relief valve. Unit 2 returned to its maximum

power level on October 9. On November 8 and December 5, operations personnel lowered

reactor power to approximately 85 percent to conduct turbine valve testing. In both cases the

unit was returned to maximum power levels within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

1.

REACTOR SAFETY

Cornerstone: Initiating Events, Mitigating Systems, and Barrier Integrity

1R01 Adverse Weather Protection (71111.01)

.1

Routine Cold Weather Preparations

a.

Inspection Scope

From October 29 through November 1, 2002, the inspectors assessed the stations

readiness for cold weather conditions by conducting detailed inspections on the ice melt

valve and the heat tracing system. The inspectors chose the ice melt valve for inspection

due to its importance in preventing the freezing of water for the service water, circulating

water, fire water, residual heat removal service water and emergency diesel generator

service water systems. The heat tracing system was chosen because of its importance

in maintaining the operability of safety-related piping exposed to extreme temperature

conditions. The inspectors reviewed the Updated Safety Analysis Report, and seasonal

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readiness and adverse weather procedures to determine the operational requirements of

the ice melt valve and heat tracing systems during cold weather conditions. The

inspectors compared this information to the licensees seasonal readiness open items

list, system readiness reports, and open maintenance work requests to ensure that none

of the items on these lists impacted the ability of the ice melt valve and heat tracing

system to perform their intended functions. The inspectors performed a review of

previously initiated condition reports related to cold weather conditions and performed a

plant walkdown to ensure that the items documented in the condition reports had been

appropriately corrected.

b.

Findings

No findings of significance were identified.

.2

Review of Site Specific Weather Condition

a.

Inspection Scope

On October 16, 2002, the safe shutdown makeup pump experienced a self-revealing

failure when the room cooler service water strainer became fouled with duck weed. The

safe shutdown makeup pump system is one of three high pressure systems that can be

used to inject water into the reactor during accident conditions. The safe shutdown

makeup pump is classified as a risk significant system under the Maintenance Rule and

is credited as an injection source in the Appendix R (Fire Protection) Safe Shutdown

Analysis. Between October 16 and November 5, 2002, the inspectors performed an

in-office review of Condition Report 127679, the apparent cause evaluation, operations

logs, and procedures associated with the safe shutdown makeup pump to determine past

system performance and the reason for the failure. The inspectors interviewed

operations, maintenance, and engineering personnel to assess the service water strainer

clogging frequency during increased river debris conditions. The inspectors also

conducted an inspection of the safe shutdown makeup pump room, including the room

cooler and service water systems, to monitor room cooler performance.

b.

Findings

The inspectors identified one Green finding due to an inadequate system design which

prevented operations personnel from immediately discovering that the safe shutdown

makeup pump room cooler service water strainer was clogged with duck weed.

Under normal conditions, operations personnel conducted periodic checks of the safe

shutdown makeup pump room cooler service water duplex strainer. When the duplex

strainers differential pressure reached 10 psid or greater, operations personnel were

required to swap duplex strainers and notify maintenance to clean the fouled strainer.

During increased river debris conditions, operations personnel were required to check the

duplex strainer differential pressure twice per shift.

On October 16, 2002, an operator entered the safe shutdown makeup pump room,

noticed that the room seemed warmer than normal, and that the room cooler was not in

operation. Since the room cooler was needed to support continued operability of the

7

safe shutdown makeup pump, control room personnel entered Technical Specification 3.7.9. Troubleshooting determined that the safe shutdown makeup pump

room cooler was not operating due to the both sides of the service water duplex strainer

being fouled.

The inspectors questioned various personnel to determine why operations was not

immediately notified of the safe shutdown makeup pump room cooler malfunction via a

local or control room alarm. The inspectors were informed that the safe shutdown

makeup pump room cooler circuitry was designed without any local or control room alarm

functions which could be used to notify personnel of equipment malfunctions. Due to this

inadequate design, operations personnel were relying on operator rounds to ensure

continued operability of the safe shutdown makeup pump and its associated support

equipment.

The inspectors determined that the failure to ensure the safe shutdown makeup pump

room cooler circuitry was adequately designed to warn personnel of equipment

malfunctions was more than minor because it: (1) involved the design control and

protection against external factors attributes of the mitigating systems cornerstone; and

(2) affected the cornerstone objective of ensuring the operability, availability, reliability,

and function of a system that responded to initiating events to prevent undesirable

consequences.

The inspectors also determined that this finding should be evaluated using the

significance determination process described in Inspection Manual Chapter 0609,

Significance Determination Process. The inspectors conducted a Phase 1 screening

and determined that a Phase 2 evaluation was required since the strainer clogging and

design inadequacy resulted in an actual loss of safety function of a system.

The inspectors used the risk-informed inspection notebook for Quad Cities Nuclear

Power Station, Units 1 and 2, Revision 1, dated May 2, 2002, to complete the Phase 2

evaluation. The inspectors determined that the exposure time was less than 3 days

since approximately 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> elapsed between the time the room cooler was last

verified to be operable and the time the operator discovered the abnormally warm room.

For each significance determination process worksheet completed, the inspectors

assumed that all mitigating capability was available except for the safe shutdown makeup

pump. The inspectors allowed credit for recovery since the duplex strainer could have

been cleaned, and the room cooler re-started, using manual actions. Using these

assumptions the inspectors evaluated 22 core damage sequences. Worksheet results

ranged from 8 to 18 points. The most dominant core damage sequences involved:

(1) the loss of instrument air with the residual heat removal system available for

containment heat removal; (2) a transient with the loss of the power conversion system

and the automatic depressurization system available; and (3) a loss of service water with

the residual heat removal system available for containment heat removal. The inspectors

concluded that the final significance determination process result for this finding was

8 points; therefore, this finding was considered to be of very low risk significance (Green)

(FIN 50-254/02-08-01; 50-265/02-08-01). The inadequate design issue did not constitute

a violation of NRC requirements since the licensees quality assurance program

considered the safe shutdown makeup pump and its associated support equipment to be

8

of augmented quality. This issue was entered into the licensees corrective action

program as Condition Report 127679.

1R05 Fire Protection (71111.05)

a.

Inspection Scope

During the inspection period, the inspectors conducted in-plant walkdowns of the

following risk-significant fire zones to identify any fire protection degradations:

Fire Zone 8.2.3.A, Unit 1 Turbine Building Control Rod Drive Pumps;

Fire Zone 8.2.6.A, Unit 1 Turbine Building Hallway;

Fire Zone 1.1.1.6, Unit 1/2 Reactor Building Refuel Floor;

Fire Zone 8.2.6.B, Unit 1 Turbine Building Low Pressure Heater Bay;

Fire Zone 11.3.3, Unit 2 Reactor Building Northwest Corner Room, Core Spray;

Fire Zone 11.3.2, Unit 2 Reactor Building Southeast Corner Room, 2B Residual

Heat Removal Room; and

Fire Zone 11.3.4, Unit 2 Reactor Building Northeast Corner Room, 2A Residual

Heat Removal Room.

During the walkdowns the inspectors verified that transient combustibles were controlled

in accordance with the licensees procedures. The inspectors observed the physical

condition of fire suppression devices and passive fire protection equipment such as fire

doors, barriers, and penetration seals. The inspectors observed the condition and

location of fire extinguishers, hoses, and telephones against the Pre-Fire Plan zone

maps. The physical condition of passive fire protection features such as fire doors, fire

dampers, fire barriers, fire zone penetration seals, and fire retardant structural steel

coatings were also inspected to verify proper installation and physical condition.

b.

Findings

No findings of significance were identified.

1R08 Inservice Inspection Activities (71111.08)

a.

Inspection Scope

The inspectors conducted a review of the licensees inservice inspection program for

monitoring degradation of the reactor coolant system boundary and the risk significant

piping system boundaries. Specifically, the inspectors conducted a record review of the

following examinations:

WELD #

SYSTEM

NDE TYPE

23S-S9

High Pressure Coolant Injection

Ultrasonic Testing

23S-F4

High Pressure Coolant Injection

Ultrasonic Testing

30C-F27

Main Steam

Ultrasonic Testing

10BD-S8

Residual Heat Removal

Ultrasonic Testing

CRDH Pipe-Pipe

Reactor Pressure Vessel

Penetrant Testing

9

FW-1

High Pressure Coolant Injection Turbine

Radiographic Testing

These examinations were evaluated for compliance with the American Society of

Mechanical Engineers Boiler and Pressure Vessel Code requirements. The inspectors

also reviewed inservice inspection procedures, equipment certifications, personnel

certifications, and NIS-2 forms for Code repairs performed during the last outage to

confirm that American Society of Mechanical Engineers Code requirements were met.

A sample of inservice inspection related problems documented in the licensees

corrective action program, was also reviewed to assess conformance with 10 CFR

Part 50, Appendix B, Criterion XVI, Corrective Action, requirements. In addition, the

inspectors determined that operating experience was correctly assessed for applicability

by the inservice inspection group.

b.

Findings

The licensee discovered that they had missed inspections of the control rod drive

housing welds (Action Report 00113995). Further discussions of this issue with NRC

staff was documented in Action Report 00132057. This issue will be an Unresolved Item

pending further review of the American Society of Mechanical Engineers Code

requirements (URI 50-254/02-08-02; 50-265/02-08-02).

1R11 Licensed Operator Requalification (71111.11)

a.

Inspection Scope

On October 9, 2002, the inspectors observed an operations crew during a requalification

examination on the simulator using Scenario 00-28, Torus Narrow Range Instrument

Failure, Loss of Coolant Accident Inside Containment, and an Anticipated Transient

Without Scram, Revision 10.

The inspectors evaluated crew performance in the areas of:

clarity and formality of communications;

ability to take timely and conservative actions;

prioritization, interpretation, and verification of alarms;

procedure use;

control board manipulations;

oversight and direction from supervisors; and

group dynamics.

Crew performance in these areas was compared to licensee management expectations

and guidelines as presented in the following documents:

OP-AA-101-111, Rules and Responsibilities of On-Shift Personnel, Revision 0;

OP-AA-103-102, Watchstanding Practices, Revision 0;

OP-AA-103-103, Operation of Plant Equipment, Revision 0;

OP-AA-103-104, Reactivity Management Controls, Revision 0; and

10

OP-AA-104-101, Communications, Revision 0.

The inspectors verified that the crew completed the critical tasks listed in the above

scenario. The inspectors also attended meetings with the licensees evaluators to ensure

that weaknesses noted by the inspectors were noticed by the evaluators and discussed

with the crew.

b.

Findings

No findings of significance were identified.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation (71111.13)

a.

Inspection Scope

The inspectors reviewed the documents listed in the List of Documents Reviewed

section of this report to determine if the risk associated with the activities listed below

agreed with the results provided by the licensees risk assessment tool. In each case,

the inspectors conducted walkdowns to ensure that redundant mitigating systems and/or

barrier integrity equipment credited by the licensees risk assessment remained available.

When compensatory actions were required, the inspectors conducted plant inspections

to validate that the compensatory actions were appropriately implemented. The

inspectors also discussed emergent work activities with the shift manager and work week

manager to ensure that these additional activities did not change the risk assessment

results.

Maintenance Activity Assessed

Week Inspected

125 Volt DC Charger Load Testing

December 9, 2002

Risk Associated with U1 High Pressure Coolant Injection Out

of Service Due to Emergent Work

December 9, 2002

U2 Core Spray Semiannual Logic Test

December 9, 2002

b.

Findings

No findings of significance were identified.

1R14 Personnel Performance During Non-routine Plant Evolutions (71111.14)

a.

Inspection Scope

On October 7, 2002, the inspectors observed control room activities associated with a

Unit 2 power reduction to repair a steam leak on a reactor feedwater pump. The

inspectors determined by direct observation and a review of procedural requirements that

reactivity manipulations were verified by a second licensed operator, that operations

personnel were complying with procedures and Technical Specifications, and that plant

11

parameters were as expected for each operating condition.

b.

Findings

No findings of significance were identified.

1R15 Operability Evaluations (71111.15)

a.

Inspection Scope

The inspectors assessed the following operability evaluations or issues associated with

equipment operability:

Operability Evaluation for Condition Report 124350, Certain General Electric

480 Volt Breakers not Properly Modeled in ELMS-DC Database, dated

September 24, 2002;

Discussions Regarding a Lack of Inservice Inspections on Control Rod Drive

Housing Welds During October and November 2002 (see Condition

Report 132057); and

Operability Evaluation for Condition Report 131936, Potential Failure of

Belleville Springs in Main Steam Isolation Valves 2-0203-2B and 2-0203-2C,

dated November 20, 2002.

The inspectors reviewed the technical adequacy of each evaluation against the Technical

Specifications, the Updated Final Safety Analysis Report, and other design information;

determined whether compensatory measures, if needed, were taken; and determined

whether the evaluations were consistent with the requirements of LS-AA-105,

Operability Determination Process, Revision 0.

In addition, the inspectors reviewed selected issues that the licensee entered into its

corrective action program to verify that identified problems were being entered into the

program with the appropriate characterization and significance.

b.

Findings

No findings of significance were identified.

1R16 Operator Work-Arounds (71111.16)

Semi-Annual Review

a.

Inspection Scope

The inspectors performed a semi-annual review of all operator workarounds and

challenges identified as of October 10, 2002. The inspectors assessed the cumulative

effects of the workarounds and challenges by performing the following:

12

The inspectors compared workaround and challenge information to the normal,

abnormal, and emergency operating procedures to ensure that operations

personnel maintained the ability to correctly respond to plant transients in a

timely manner;

The inspectors utilized system knowledge, a review of plant procedures, and

interviews with operations personnel to ensure that the workarounds and

challenges previously identified did not adversely impact system reliability and

availability, create the potential for system misoperation, or result in a

workaround that impacted multiple mitigating equipment; and

The inspectors reviewed the equipment status tag log, degraded equipment log,

temporary configuration change report, and open operability determination report

for potential operator workarounds and challenges that had not been previously

identified or assessed for potential impact on normal plant operation or transient

response.

In addition to the above, the inspectors reviewed selected issues that the licensee

entered into its corrective action program to verify that identified problems were being

entered into the program with the appropriate characterization and significance.

b.

Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications (71111.17)

a.

Inspection Scope

In October and November 2002, the inspectors reviewed the technical adequacy of

multiple modifications associated with the Unit 1 extended power uprate. A list of the

specific modification packages reviewed is included in the List of Documents Reviewed

section of this report.

The inspectors verified that modification preparation, staging, and implementation did not

impair the operations departments ability to complete emergency and abnormal

operating procedure actions when required, to monitor key safety functions, or to

respond to a loss of key safety functions. The inspectors reviewed the design adequacy

of the modification by verifying the following:

energy requirements were able to be supplied by supporting systems under

accident and event conditions;

replacement components were compatible with physical interfaces;

replacement component properties met functional requirements under event and

accident conditions;

replacement components were environmentally and seismically qualified;

sequence changes remained bounded by the accident analyses and loading on

support systems was acceptable;

13

structures, systems, and components response times were sufficient to serve

accident and event functional requirements assumed by the design analyses;

control signals were appropriate under accident and event conditions; and

affected operations procedures were revised and training needs were evaluated

in accordance with station administrative procedures.

The inspectors also verified that the post modification testing demonstrated system

operability by verifying no unintended system interactions occurred, system performance

characteristics met the design basis, and post-modification testing results met all

acceptance criteria.

b.

Findings

No findings of significance were identified.

1R19 Post Maintenance Testing (71111.19)

a.

Inspection Scope

The inspectors observed and/or reviewed the following post maintenance testing

activities during this inspection period:

Post Maintenance Activity

Date Inspected

Testing Following Modification of the 1A Standby Liquid

Control Pump

October 18, 2002

Testing Following Replacement of the High Pressure

Coolant Injection Turning Gear Time Delay Relay

October 24, 2002

For each post maintenance testing activity selected, the inspectors reviewed the

Technical Specifications and Updated Final Safety Analysis Report against the

maintenance work package to determine the safety function(s) that may have been

affected by the maintenance. Following this review, the inspectors verified that the

licensees post maintenance test procedure adequately tested the safety function(s)

affected by the maintenance, that the procedures acceptance criteria were consistent

with licensing and design basis information, and that the procedure was properly

reviewed and approved. When possible, the inspectors observed the post maintenance

testing activity and verified that the structure, system, or component operated as

expected; test equipment, when used, was adequately calibrated and within its current

calibration cycle; test equipment used was within its required range and accuracy;

jumpers and lifted leads were appropriately controlled; test results were accurate,

complete, and valid; test equipment was removed after testing; and any problems

identified during testing were appropriately documented.

b.

Findings

No findings of significance were identified.

14

1R20 Refueling and Outage Activities (71111.20)

.1

Pre-Outage Work Creates Unexpected Transients in Instrument Air System

a.

Inspection Scope

The inspectors interviewed licensee personnel and reviewed work requests, condition

reports, and procedures to determine the circumstances which led to two unexpected

instrument air transients on October 24 and 25, 2002.

b.

Findings

The inspectors identified one Green finding due to inadequate procedures and the failure

to properly self-check prior to connecting temporary plant equipment to plant air systems.

These deficiencies resulted in two separate instrument air system transients.

On October 14, 2002, a chemistry individual assisted a vendor in routing hoses for the

moisture separator decontamination project by identifying the water and air connections

to be used as directed by Work Order 369947, Task 09. Ten days later, the vendor

directed several pipefitters to connect a decontamination skid to the air and water

connections previously identified. Later the same afternoon, the vendor began using an

air powered vacuum as part of the decontamination activities. Operations personnel

immediately noticed abnormal fluctuations in instrument air pressure but were unaware

an air powered vacuum was being used in the plant. The operators responded to the

pressure fluctuations as required by procedure. However, they were unable to dispatch

individuals to the field to search for the cause of the pressure fluctuations prior to the

fluctuations stopping.

The next morning vendor personnel began using the same air powered vacuum. At

9:05 a.m., control room personnel received an alarm indicating that the Unit 2 backup

service air valve was open. The operators discovered that the Unit 1A and Unit 1/2

instrument air compressors were continuously loaded and instrument air pressures were

noted to be cycling between 91 and 98 pounds per square inch. Control room personnel

dispatched several non-licensed operators and the field supervisor into the plant to

observe air compressor operation and to look for possible air leaks. Operations

personnel also started the Unit 2 instrument air compressor to assist in stabilizing the

transient.

Approximately 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after noticing the pressure fluctuations, a non-licensed operator

discovered the vendor using the air powered vacuum. Additional investigation found that

the vacuum had been powered using instrument air rather than service air. The

non-licensed operator stopped the decontamination activities and closed the instrument

air isolation valve. Instrument air pressures returned to normal.

A subsequent interview of the chemistry individual determined that an inadequate work

procedure and improper self-checking contributed to connecting the air powered vacuum

to the instrument air system rather than the service air system. Although Work Order 369947, Task 09, contained steps for the chemistry individual to assist in routing

the hoses, specific equipment identification numbers were not provided. The chemistry

15

individual stated that when he located the service water connection a Chicago fitting was

present on the end of the line to allow the hose to be easily connected to the piping.

When looking for the air connection, the chemistry individual noticed an air valve with a

Chicago fitting installed on the end of the piping. The chemistry individual immediately

assumed that this was the air supply line to be used during the decontamination project.

Although the valve was properly labeled as an instrument air valve, the chemistry

individual failed to check the valve tag.

The inspectors determined that connecting the air powered vacuum to the instrument air

system rather than the service air system was more than minor because it: (1) involved

the configuration control attribute of the Initiating Events cornerstone; and (2) affected

the cornerstone objective of limiting the likelihood of those events that upset plant

stability during power operations. The inspectors also determined that the error by the

chemistry individual affected the cross-cutting area of Human Performance because,

despite the inadequate procedure, the valve was properly labeled and self-checking

should have been used to ensure that the proper air supply was identified.

The inspectors determined that this finding could be assessed using the significance

determination process in accordance with Inspection Manual Chapter 0609, Significance

Determination Process, because the issue was associated with degraded conditions that

could concurrently influence mitigating systems equipment and an initiating event. For

the Phase 1 screening, the inspectors answered yes to Question 2 under the Initiating

Events column which required a Phase 2 evaluation to be performed.

Using the Risk-Informed Inspection Notebook for Quad Cities Nuclear Power Station,

Units 1 and 2, Revision 1, dated May 1, 2002, the inspectors determined that the

findings exposure time was less than three days and that the finding increased the

likelihood of a loss of instrument air. These assumptions resulted in raising the Table 1

likelihood rating for a loss of instrument air by one decade or to a point value of 3. For

the loss of instrument air worksheet, the inspectors determined that all mitigating

systems capability was available. This resulted in four core damage sequences between

7 points and 13 points. The most dominant sequence involved the loss of instrument air

with containment heat removal and long-term venting available. The inspectors

concluded that the final significance determination process result for this finding was

7 points; therefore, this finding was considered to be of very low significance

(FIN 50-254/02-08-03; 50-265/02-08-03). No violation of NRC requirements was

identified due to the instrument air system being non-safety-related. This issue was

placed in the licensees corrective action program via Condition Report 128977.

.2

Stator Water Heat Exchanger Work Leads to Unit 1 Diesel Inoperability

a.

Inspection Scope

The inspectors interviewed licensee personnel and reviewed work instructions and

condition reports to determine the circumstances which led to the unexpected

inoperability of the Unit 1 emergency diesel generator.

16

b.

Findings

The inspectors identified one Green finding due to the use of inadequate stator water

heat exchanger work instructions and weak communications which resulted in rendering

the Unit 1 emergency diesel generator inoperable.

On November 11, 2002, contractor personnel were performing work to replace the

Unit 1A stator water heat exchanger tube bundle. Prior to performing this work,

operations personnel had tagged out the heat exchanger for draining purposes. The

contractors also established funnels and hoses for collecting the several gallons of water

expected to be expelled from the heat exchanger as the tube bundle was removed. As

the contractors began removing the tube bundle from the heat exchanger, a large

amount of water (as much as 200 gallons) was expelled from the heat exchanger and

overwhelmed the funnels and hoses. Within minutes the control room received alarms

indicating a problem with the Unit 1 emergency diesel generator. A local operator

reported that water from the heat exchanger had migrated into the diesel room and

caused the circulating oil pump and the turbocharger lubricating oil pump to trip. Since

the operators were unable to fully determine the extent of the water intrusion, the Unit 1

emergency diesel generator was declared inoperable.

Through interviews the inspectors determined that operations personnel were very aware

that a large amount of water would be expelled from the stator water heat exchanger

when the tube bundle was removed. In fact, the inspectors were informed that this was

the reason that the out of service tagout for the stator water heat exchanger was

considered an exceptional tagout. Operations personnel also told the inspectors that

when mechanical maintenance personnel performed a stator water heat exchanger tube

bundle replacement a large trough was used to catch the water. The inspectors

interviewed the contractor personnel performing the heat exchanger work regarding the

information provided by operations. The contractors stated that they were not made

aware of the possibility for a large amount of water or that a trough had been used

previously to catch the water. The inspectors also reviewed Work Order 99183182,

Task 01, Replace Tube Bundle Assembly in the 1-7401-A Stator Water Heat

Exchanger, and found that the work order specifically stated that the heat exchanger

would be isolated and drained.

The inspectors determined that the failure to have adequate stator water heat exchanger

work instructions, and to communicate information regarding the amount of water, was

more than minor because if left uncorrected the inadequate work instructions could

continue to impact the availability, reliability, and capability of safety-related equipment.

The inspectors also determined that the failure to ensure adequate work instructions

were in place prior to removing the tube bundle also affected the cross-cutting area of

Human Performance. Despite multiple individuals being aware that large amounts of

water would be expelled during this work activity, actions were not taken to communicate

this information to the contractors performing the work.

The Unit 1 emergency diesel generator was normally credited as an emergency power

supply for Unit 1 equipment. At Quad Cities the Unit 1 emergency diesel generator was

also credited as an emergency power source for common equipment such as the

standby gas treatment and control room emergency ventilation systems. When this

17

event occurred, Unit 1 was shut down for a refueling outage. The inspectors reviewed

Inspection Manual Chapter 0609, Appendix G, Shutdown Operations Significance

Determination Process, Table 1 for a boiling water reactor in refueling operations with

reactor vessel level greater than 23 feet. The inspectors determined that the significance

determination process did not apply since the Unit 1/2 emergency diesel generator

remained available to address accident situations while Unit 1 was shut down. In regards

to Unit 2, the inspectors determined that this issue could be assessed using the At Power

Significance Determination Process in accordance with Inspection Manual Chapter 0609,

Significance Determination Process, because the issue was associated with the

operability, availability, reliability, or function of a system or train in a mitigating system.

The inspectors performed a Phase 1 screening and determined that this issue was of

very low risk significance (Green) since the finding did not represent an actual loss of

safety function of a system or an actual loss of safety function of a single train for greater

than its Technical Specification Allowed Outage Time (FIN 50-265/02-08-04). No

violations of NRC requirements were identified due to the stator water heat exchanger

being non-safety related. This issue was included in the licensees corrective action

program as Condition Report 130694.

.3

Untimely Actions Result in Isolation of Decay Heat Removal System

a.

Inspection Scope

The inspectors interviewed operations personnel and reviewed condition reports and

procedures to determine the circumstances that led to an inadvertent isolation of the

reactor water cleanup system while operating in the decay heat removal mode.

b.

Findings

This self-revealing event led to the identification of one Green finding and a Non-Cited

Violation for the failure to adequately implement QCOP 1200-15, Operation of Decay

Heat Removal Mode of RWCU [Reactor Water Cleanup] System, to ensure that the

reactor water cleanup system did not isolate while being used to remove decay heat from

the Unit 1 reactor vessel.

On November 24, 2002, operations personnel conducted hydrostatic testing on the Unit 1

reactor vessel. Upon completion of this test, operations personnel continued to remove

decay heat from the reactor vessel using the reactor water cleanup system rather than

the shutdown cooling mode of the residual heat removal system. At approximately

2:00 p.m., operations personnel made a control room log entry indicating that the reactor

water cleanup system high temperature alarm and system isolation setpoints were set at

140 degrees as directed by QCOP 1200-13, RWCU System High Temperature Isolation

Setpoint Adjustment. Nine hours later the reactor water cleanup system isolated while

operations personnel were attempting to adjust reactor building closed cooling water

system temperature to maintain reactor vessel water temperature within the specified

temperature band. Operations personnel were able to restart one of the reactor water

cleanup pumps within eight minutes. Heatup of the reactor vessel water was minimal

due to the low amount of decay heat present.

18

The inspectors reviewed QCOP 1200-15 and determined that Step D.2 contained a

precaution warning that the reactor water cleanup system would isolate at 140 degrees if

the reactor building closed cooling water heat removal capabilities were exceeded. The

inspectors determined that operator error and a failure to perform adequate control room

panel monitoring resulted in the failure to control reactor building closed cooling water

temperature and prevent the reactor water cleanup system isolation. The inspectors

determined that this issue was more than minor because it: (1) involved the human

performance attribute of the barrier integrity cornerstone; and (2) affected the

cornerstone objective of providing reasonable assurance that physical design barriers

(fuel cladding, reactor coolant system, and containment) protect the public from

radionuclide releases caused by accidents or events. The inspectors also determined

that the operators error affected the cross-cutting area of Human Performance.

The inspectors determined that this issue could be assessed using the significance

determination process since it was associated with maintaining the integrity of fuel

cladding. Since Unit 1 was shut down when this event occurred, the inspectors reviewed

Inspection Manual Chapter 0609, Appendix G, Shutdown Operations Significance

Determination Process, Table 1 for a boiling water reactor in cold shutdown or refueling

operation with a time to boil of greater than 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and reactor coolant system level less

than 23 feet above the top of the flange. Page T-21 of Table 1 required two residual heat

removal shutdown cooling subsystems to be operable with one subsystem in operation.

This statement was being met by operating the reactor water cleanup system in the

decay heat removal mode. The inspectors referred to Page T-22 of Table 1 and

determined that the inadvertent isolation of the reactor water cleanup system while in the

decay heat removal mode of operation was of very low risk significance (Green).

Specifically, the isolation did not significantly degrade the licensees ability to recover

decay heat removal once it was lost since the reactor water cleanup system was easily

recoverable and either residual heat removal shutdown cooling subsystem could have

been started to remove decay heat.

Technical Specification 5.4.1 requires that written procedures be established,

implemented, and maintained covering the applicable procedures recommended in

Regulatory Guide 1.33, Revision 2, Appendix A, February 1978. Section 3.c of

Regulatory Guide 1.33 requires instructions for changing modes of operation for the

shutdown cooling system. Contrary to the above, on November 24, 2002, operations

personnel failed to properly implement QCOP 1200-15 to prevent a reactor water

cleanup system isolation which resulted in changing modes of operation for the shutdown

cooling system. This violation is being treated as a Non-Cited Violation consistent with

Section VI.A.1 of the NRCs Enforcement Policy (NCV 50-254/02-08-05). This issue was

entered into the licensees corrective action program as Condition Report 133054.

.4

Scaffold In Contact With Plant Equipment

a.

Inspection Scope

The inspectors conducted periodic tours of plant facilities and identified multiple

examples of outage related scaffolding that was in contact with plant equipment. The

19

inspectors reviewed scaffolding erection procedures to determine if the scaffolding was

constructed in accordance with procedural requirements.

b.

Findings

The inspectors identified one Green Non-Cited Violation due to the failure to follow

procedural requirements regarding the clearances required when erecting scaffolding

near the residual heat removal system.

During a walkdown of the residual heat removal system on November 6, 2002, the

inspectors identified that scaffolding was in contact with safety-related piping and valves.

The inspectors also identified two other examples of scaffolding erection deficiencies

concerning the Unit 1 torus shell and the Unit 1 reactor recirculation motor generator

sets.

The inspectors reviewed Procedure MA-AA-796-024, Scaffold Installation, Inspection,

and Removal, Revision 1, and determined that scaffolding inspectors were required to

verify that scaffolding was not supported by, in contact with or connected to

safety-related equipment. The inspectors notified licensee personnel each time they

identified an example of deficient scaffold erection. The inspectors noted that the

licensee took timely action to address each scaffold erection issue. However, condition

reports were not written for any of the inspector-identified issues. After several

discussions regarding scaffold erection deficiencies during the resident inspectors

weekly management debrief, the licensee initiated Condition Report 131690 on

November 14, 2002, to document the inspector-identified issues and to determine

whether a common cause existed.

The licensee reviewed each scaffolding example and concluded that the equipment

impacted remained operable. Therefore, each example was considered minor.

However, in accordance with Inspection Manual Chapter 0612, Appendix B, Issue

Dispositioning Screening, and Appendix E, Example of Minor Issues, Example 4.a., the

inspectors determined that the improper scaffolding erection was more than minor

because the number of examples identified demonstrated that workers routinely failed to

follow Procedure MA-AA-796-024.

The inspectors determined that this finding could be assessed using the significance

determination process. The inspectors determined that this finding was of very low

safety significance (Green) since the scaffolding erection deficiencies did not result in a

loss of function per Generic Letter 91-18, did not represent an actual loss of safety

function of a system, did not represent an actual loss of safety function of a single train

for greater than its Technical Specification Allowed Outage Time, did not represent an

actual loss of safety function of one or more non-Technical Specification trains of

equipment designated as risk significant per 10 CFR Part 50.65 for greater than

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />, and did not screen as potentially risk significant due to a seismic, fire, flooding,

or severe weather initiating event.

Criterion V, Instructions, Procedures, and Drawings, of 10 CFR Part 50, Appendix B,

requires that activities affecting quality be performed in accordance with procedures.

Scaffold installation was considered an activity affecting quality and was governed by

20

Procedure MA-AA-796-024. Contrary to the above, on November 6, 2002, the inspectors

identified that the licensee failed to implement Procedure MA-AA-796-024 when erecting

scaffolding near the residual heat removal system. This violation is being treated as a

Non-Cited Violation consistent with Section VI.A.1 of the NRC Enforcement Policy (NCV

50-254/02-08-06). This issue was entered in the licensees corrective action program as

Condition Report 131690.

.5

General Outage Observations

a.

Inspection Scope

The inspectors observed control room activities associated with the shutdown of Unit 1

for a scheduled refueling outage including removing equipment from service, inserting

control rods, completing mode specific surveillance testing, and monitoring reactor

coolant temperature. The inspectors attended daily outage meetings, reviewed outage

control center and control room operator logs, and conducted daily control room tours to

ensure that shutdown safety was maintained throughout the outage, reactor coolant

system instrumentation provided accurate information, the decay heat removal systems

were functioning properly, and inventory and reactivity controls were maintained. The

inspectors conducted periodic observations of outage related work activities to ensure

that work activities were performed in accordance with plant procedures. The inspectors

performed tours of the turbine building, reactor building, and drywell to verify that

procedural requirements regarding fire protection, foreign material exclusion, and the

storage of equipment near safety-related structures, systems, and components were

maintained.

b.

Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors observed surveillance testing activities and/or reviewed completed

surveillance test packages for the tests listed below:

QCOS 6600-49, Division 1 ECCS Automatic Actuation Test;

QCOS 6600-50, Division 2 ECCS Automatic Actuation Test; and

QOS 6500-03, Bus 14-1 Undervoltage Test.

The inspectors verified that the structures, systems, and components tested were

capable of performing their intended safety function by comparing the surveillance

procedure acceptance criteria and results to design basis information contained in

Technical Specifications, the Updated Final Safety Analysis Report, and licensee

procedures. The inspectors verified that the test was performed as written, the test data

was complete and met the requirements of the procedure, and the test equipment range

and accuracy was consistent with the application by observing the performance of the

21

surveillance test. Following test completion, the inspectors conducted a walkdown of the

test area to verify that the test equipment had been removed and that the system was

returned to its normal standby configuration.

b.

Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a.

Inspection Scope

The inspectors reviewed documentation for the following temporary configuration

changes:

Installation of a temporary pump in the Unit 1 drywell equipment drain sump, and

Installation of bladders in the Unit 1 main steam lines to establish secondary

containment.

The inspectors assessed the acceptability of each temporary configuration change by

comparing 10 CFR 50.59 screening and evaluation information against the Updated Final

Safety Analysis Report and Technical Specifications. The comparisons were performed

to ensure that the new configurations remained consistent with design basis information.

The inspectors observed installation and testing of the temporary modifications when

applicable; verified that the modifications were installed as directed; the modifications

operated as expected; modification testing adequately demonstrated continued system

operability, availability, and reliability, and that operation of the modifications did not

impact the operability of any interfacing systems. The inspectors also reviewed condition

reports initiated during or following temporary modification installation to ensure that

problems encountered during installation were appropriately resolved.

b.

Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP4 Emergency Action Level and Emergency Plan Changes (71114.04)

a.

Inspection Scope

The inspectors reviewed Revision 15 of the Quad Cities Station Annex to Exelons

Standardized Emergency Plan to determine whether changes identified in Revision 15

reduced the effectiveness of the licensees emergency planning, pending onsite

inspection of the implementation of these changes.

22

b.

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Controls for Radiologically Significant Areas (71121.01)

.1

Plant Walkdowns, Radiological Boundary Verifications and Radiation Work Permit

Reviews

a.

Inspection Scope

The inspectors conducted walkdowns of the radiologically protected area to verify the

adequacy of radiation area boundaries and postings including high and locked high

radiation areas in the Unit 1 and 2 Reactor Buildings including the Unit 1 Drywell, and the

Turbine Building. Confirmatory radiation measurements were taken to verify that these

areas and selected radiation areas were properly posted and controlled in accordance

with 10 CFR Part 20, licensee procedures, and Technical Specifications. The inspectors

walked down areas having the potential for airborne activity and verified the adequacy of

the licensees continuous air monitoring systems and contamination controls. Selected

radiation work permits (RWPs) for radiologically significant work being conducted during

the refueling outage (Q1R17) were reviewed for protective clothing requirements and

electronic dosimetry alarm set points for both dose rate and accumulated dose.

b.

Findings

No findings of significance were identified.

.2

Job-In-Progress Reviews

a.

Inspection Scope

The inspectors observed work occurring on the refueling floor including diving and

refueling operations. Work progress was observed in the reactor building, drywell, low

pressure heater bay and the turbine building. RWP requirements and the As-Low-As-

Reasonably-Achievable (ALARA) briefing packages for selected jobs were reviewed to

assess their adequacy and to determine if job controls were implemented as intended.

The inspectors determined if dosimetry placement, alarm set points, job site radiological

surveys, radiological exposure estimates, contamination controls, airborne monitoring for

radioactive materials, and postings were adequate given the jobs radiological conditions.

b.

Findings

No findings of significance were identified.

23

20S2 ALARA Planning and Controls (71121.02)

.1

Inspection Planning

a.

Inspection Scope

The inspectors reviewed the plants exposure history and trends, its three year rolling

average dose and the impact of source term on radiological exposure under outage

conditions, in order to assess radiological challenges for the current outage. The

licensees processes to estimate and track radiological exposure were discussed with

radiation protection management to determine if the licensees practices were

appropriate.

b.

Findings

No findings of significance were identified.

.2

Radiological Work Planning

a.

Inspection Scope

The inspectors reviewed the stations processes for radiological work planning and

scheduling, and evaluated the dose projection methodologies and practices implemented

for the Q1R17 refueling outage, to verify that the technical bases for outage dose

estimates were adequate. Specifically, the inspectors reviewed radiologically significant

RWP/ALARA planning packages to verify that person-hour estimates, job history files,

lessons learned, and industry experiences were utilized in the ALARA planning process.

The inspectors also reviewed total effective dose equivalent ALARA evaluations to

assess the licensees analysis of evolutions involving potential airborne activity for the

use of respiratory protection equipment. The inspectors also attended ALARA committee

meetings and shift turnovers to further assess inter-departmental coordination and

ownership in the radiological work/ALARA planning and scheduling processes.

b.

Findings

No findings of significance were identified.

.3

Job Site Inspection and ALARA Control

a.

Inspection Scope

The inspectors reviewed jobs being performed in areas of elevated dose rates, examined

exposure estimates and work sites, and evaluated selected RWPs along with the

associated ALARA briefing packages to verify that worker radiological exposure was

minimized. Protective clothing requirements, dosimeter use including radiotelemetry

dosimetry, and electronic dosimeter alarm set points were evaluated for consistency with

RWP packages. The use of engineering controls were also reviewed to verify that

worker exposures were maintained ALARA.

24

The inspectors attended selected pre-job ALARA and work control briefings, and

observed portions of work evolutions directly and by using the licensees remote closed

circuit monitoring system in order to verify that adequate work controls were in place to

maintain worker exposures ALARA. During job site walkdowns, radworkers and

supervisors were observed to determine if low dose waiting areas were being used

appropriately, and to evaluate the effectiveness of job supervision including equipment

staging, use of shielding, availability of tools, and work crew size.

b.

Findings

No findings of significance were identified.

.4

Radiation Dose Estimates and Exposure Tracking Systems

a.

Inspection Scope

The inspectors reviewed the licensees Unit 1 outage dose goals and dose trending

records, and evaluated the licensees method for adjusting dose estimates to verify that

the licensee had implemented sound radiation protection principles and properly

identified work control problems. The inspectors also attended site ALARA committee

meetings that discussed and approved dose adjustments for radiological work activities

to assess the adequacy of management involvement in the ALARA program.

b.

Findings

No findings of significance were identified.

.5

Identification and Resolution of Problems

a.

Inspection Scope

The inspectors evaluated the effectiveness of the stations problem identification and

resolution processes to identify, characterize and prioritize problems, and to develop and

implement corrective actions. The evaluation included review of: (1) the results of a

focus area self-assessment of the ALARA Planning and Control Program performed

during 2002; (2) a Nuclear Oversight continuous assessment report along with field

observation reports of the radiation protection program (access control and ALARA

programs) that were completed in calendar years 2001 and 2002; and (3) the licensees

condition report (CR) database and individual CRs related to the access control and

ALARA programs for years 2001 and 2002.

The licensees corrective action program for radiation protection issues was evaluated to

verify that problems were appropriately prioritized and resolved in a timely manner,

commensurate with their importance based on safety and risk. This evaluation included

procedure and documentation reviews, discussions of the program with cognizant

licensee personnel, and observing management meetings in which CRs were evaluated.

25

b.

Findings

No findings of significance were identified.

Cornerstone: Public Radiation Safety

2PS2 Radioactive Material Processing and Transportation (71122.02)

.1

Walkdown of Radioactive Waste Systems

a.

Inspection Scope

The inspectors reviewed the liquid and solid radioactive waste system description in the

Final Safety Analysis Report and the most recent information regarding the types and

amounts of radioactive waste generated and disposed. The inspectors performed

walkdowns of the liquid and solid radwaste processing systems to verify that the systems

agreed with the descriptions in the Final Safety Analysis Report and the Process Control

Program, and to assess the material condition and operability of the systems. The

inspectors reviewed the current processes for transferring waste resins into shipping

containers to determine if appropriate waste stream mixing and/or sampling procedures

were utilized. The inspectors also reviewed the methodologies for waste concentration

averaging to determine if representative samples of the waste product were provided for

the purposes of waste classification in 10 CFR 61.55. During this inspection, the

licensee was not conducting waste processing.

b.

Findings

No findings of significance were identified.

.2

Waste Characterization and Classification

a.

Inspection Scope

The inspectors reviewed the licensees radiochemical sample analysis results for each of

the licensees waste streams, including dry active waste, resins, and filters. The

inspectors also reviewed the licensees use of scaling factors to quantify difficult-to-

measure radionuclides (e.g., pure alpha or beta emitting radionuclides). The reviews

were conducted to verify that the licensees program assured compliance with 10 CFR 61.55 and 10 CFR 61.56, as required by Appendix G of 10 CFR Part 20. The inspectors

also reviewed the licensees waste characterization and classification program to ensure

that the waste stream composition data accounted for changing operational parameters

and thus remained valid between the annual sample analysis updates.

b.

Findings

No findings of significance were identified.

26

.3

Shipment Preparation

a.

Inspection Scope

Since there were no radioactive materials shipped from the site during the inspection, the

inspectors reviewed the records of training provided to personnel responsible for the

conduct of radioactive waste processing and radioactive shipment preparation activities.

The review was conducted to verify that the licensees program provided training

consistent with NRC and Department of Transportation requirements.

b.

Findings

No findings of significance were identified.

.4

Shipping Records

a.

Inspection Scope

The inspectors reviewed five non-excepted package shipment documents completed

during years 2001 and 2002, to verify compliance with NRC and Department of

Transportation requirements (i.e., 10 CFR Parts 20 and 71 and 49 CFR Parts 172 and

173).

b.

Findings

No findings of significance were identified.

.5

Identification and Resolution of Problems

a.

Inspection Scope

The inspectors reviewed 2002 focus area self-assessments of the Radioactive Material

Transportation and Radioactive Waste Processing Programs to evaluate the

effectiveness of the self-assessment process to identify, characterize, and prioritize

problems. The inspectors also reviewed corrective action documentation to verify that

previous radioactive waste and radioactive materials shipping related issues were

adequately addressed. The inspectors also selectively reviewed year 2002 CRs that

addressed radioactive waste processing and radioactive materials shipping program

deficiencies to verify that the licensee had effectively implemented the corrective action

program.

b.

Findings

No findings of significance were identified.

27

4.

OTHER ACTIVITIES

4OA1 Performance Indicator Verification (71151)

Cornerstone: Mitigating Systems

.1

High Pressure Coolant Injection Safety System Unavailability

a.

Inspection Scope

The inspectors reviewed control room logs, condition reports, and the licensees monthly

submittals of performance indicator information to verify the high pressure coolant

injection safety system unavailability for both units from August 2001 to August 2002.

The inspectors verified that the licensee accurately reported system performance as

defined in the applicable revision of Nuclear Energy Institute Document 99-02,

Regulatory Assessment Performance Indicator Guideline.

b.

Findings

No findings of significance were identified.

Cornerstone: Barrier Integrity

.2

Reactor Coolant System Activity

a.

Inspection Scope

The inspectors reviewed the licensees reactor coolant system activity performance

indicator to verify that the information reported by the licensee was accurate. The

inspectors reviewed the licensees reactor coolant sample results for maximum dose

equivalent iodine-131 for the previous 4 quarters, and the licensees sampling and

analysis procedures. The inspectors also observed a chemistry technician obtain and

analyze a reactor coolant sample.

b.

Findings

No findings of significance were identified.

Cornerstone: Occupational Radiation Safety

.3

Occupational Exposure Control Effectiveness

a.

Inspection Scope

The inspectors reviewed the licensees determination of performance indicators for the

occupational radiation safety cornerstone to verify that the licensee accurately

determined these performance indicators had all occurrences required. The inspectors

reviewed CRs for the year 2002 and access control transactions for the year 2002.

28

During plant walkdowns the inspectors also verified the adequacy of postings and

controls for locked high radiation areas, which contributed to the Occupational Exposure

Control Effectiveness performance indicator.

b.

Findings

No findings of significance were identified.

Cornerstone: Public Radiation Safety

.4

RETS/ODCM Radiological Effluents

a.

Inspection Scope

The inspectors reviewed the licensees determination of performance indicators for the

Radiological Effluent Technical Specification/Offsite Dose Calculation Manual

Radiological Effluent Occurrences. The inspectors reviewed CRs for the year 2002 and

quarterly offsite dose calculations for radiological effluents for the previous 4 quarters.

b.

Findings

No findings of significance were identified.

4OA2 Identification and Resolution of Problems (71152)

.1

1B Reactor Recirculation Pump Trips on Overcurrent Condition

a.

Inspection Scope

The inspectors assessed the circumstances surrounding the 1B reactor recirculation

pump trip by interviewing site personnel and reviewing condition reports. The inspectors

also reviewed the 1B reactor recirculation pump maintenance work history to determine if

the current pump trip was similar to previous trips.

b.

Findings

The inspectors identified one Green finding due to the failure to correct previously

identified deficiencies with the 1B reactor recirculation motor generator voltage regulator.

On December 6, 2002, the 1B reactor recirculation pump tripped on an overcurrent

condition. The licensee determined that voltage regulator instabilities caused by a lack of

adequate capacitance in the regulator circuitry caused the pump trip. The inspectors

reviewed Condition Reports 133549 and 133856 initiated on November 29 and

December 3, 2002, respectively. The inspectors determined that both of the condition

reports were written because the 1B reactor recirculation motor generator set failed to

meet the acceptance criteria specified in Procedure MA-AB-772-301 during voltage

regulator tuning activities.

29

The licensee evaluated the information in both condition reports and determined that

continued operation of the 1B reactor recirculation pump was acceptable since the

voltage regulator performance was similar to the performance experienced from

February to November 2002. The licensee planned to add additional capacitance to the

voltage regulator circuitry at a later date. The inspectors reviewed the licensees decision

to continue operating the 1B reactor recirculation pump and determined that previous

and current operating conditions had changed. During the Unit 1 refueling outage, the

licensee adjusted the voltage regulator stability and gain potentiometers on numerous

occasions. However, it did not appear that the licensee adequately considered these

subtle differences in performance prior to continuing operation.

The inspectors reviewed the 1B reactor recirculation pump maintenance work history and

discovered that the pump had tripped twice in November 2000. The licensees

investigation determined that the pump trips occurred due to equipment failures and a

lack of understanding for how the voltage regulator functioned. Corrective actions to

prevent recurrence included component replacements and voltage regulator performance

training. Based on the 1B reactor recirculation pump trip of December 6, 2002, the

inspectors determined that the licensees corrective actions to prevent recurrence were

ineffective.

The failure to adequately address the 1B reactor recirculation motor generator voltage

regulator failures was more than minor because the resulting pump trips could be

reasonably viewed as a precursor to a significant event. The inspectors determined that

this finding could be assessed using the significance determination process for the same

reason. The inspectors conducted a Phase 1 screening and determined that this finding

was of very low safety significance (Green) because it did not: (1) contribute to the

likelihood of a primary or secondary system loss of coolant accident initiator;

(2) contribute to both the likelihood of a reactor trip and the likelihood that mitigation

equipment or functions would not be available; (3) increase the likelihood of a fire or

internal/external flood; or (4) increase the frequency of core damage scenarios of

concern using the Individual Plant Examination for External Events or other plant specific

analyses (FIN 50-254/02-08-07). This issue was not subject to NRC enforcement since

the reactor recirculation pump and the motor generator voltage regulator are non-safety-

related components.

After the December 6, 2002, pump trip the licensee added approximately

500 microfarads of capacitance to the voltage regulator circuit and established an

administrative limit which prevented operating the 1B reactor recirculation pump at

greater than 92 percent speed. The licensee planned to install additional circuit

capacitance on approximately January 6, 2003.

.2

Routine Review of Identification and Resolution of Problems

a.

Inspection Scope

As discussed in previous sections of this report, the inspectors routinely reviewed issues

during baseline inspection activities and plant status reviews to verify that they were

being entered into the licensees corrective action system at an appropriate threshold,

30

that adequate attention was being given to timely corrective actions, and that adverse

trends were identified and addressed. Issues entered into the licensees corrective

action system as a result of inspectors observations are generally denoted within the

body of the report. Specific issues related to routine problem identification and resolution

were discussed in Sections 1R20.4, 4OA2.1, and 4OA3.2 of this report.

b.

Findings

No findings of significance were identified.

4OA3 Event Follow-up (71153)

.1

(Closed) Licensee Event Report 50-265/02-004: Inadequate Separation in Both Trip

Systems of the Scram Discharge Instrument Volume Input to the Reactor Protection

System.

On August 2, 2002, the licensee determined that an engineering change (EC 24572),

implemented in March 2002 resulted in the failure to maintain electrical separation

between the safety-related reactor protection system cabling and the non-safety-related

plant computer. Upon discovery the licensee entered Technical Specification 3.3.1.1,

Condition B, which allowed 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> to place the reactor protection system in a tripped

condition. The licensee installed a temporary modification within the 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> which

disabled the scram discharge volume input to the plant computer.

The licensee failed to identify this electrical separation issue earlier due to a lack of rigor

during the modification review process. The inspectors determined that this issue was

minor since one channel in each reactor protection trip system remained operable. In the

event that there had been an actual scram discharge volume high level condition,

concurrent with the plant computer cabling and the reactor protection system wiring

shorting together, the scram function would still have been initiated.

.2

(Closed) Licensee Event Report 50-265/02-005: Failure of Low Pressure Coolant

Injection Logic Test due to Detached Wire.

During logic testing on the 2B residual heat removal subsystem on October 7, 2002,

operations personnel were unable to complete a step in QCOS 1000-44, Unit 2 B Loop

Low Pressure Coolant Injection and Containment Cooling Modes of Residual Heat

Removal Non-Outage Logic Test. Troubleshooting identified an unlanded wire that

should have been connected to fuse holder FF-F11 within the residual heat removal logic

circuitry. The licensee determined that the failure of the wire to be connected to the fuse

holder resulted in the 2B residual heat removal subsystem being unable to automatically

start in response to an emergency core cooling system initiation signal. The licensee

also found that if the 2B residual heat removal subsystem was operating in torus spray or

torus cooling certain valves would not have automatically closed upon the receipt of an

emergency core cooling system initiation signal. As a result, low pressure injection from

the 2A residual heat removal subsystem would have been diverted from the reactor

vessel to the torus through the open torus cooling and/or torus spray valves until the

operators manually closed the valves.

31

The inspectors determined that human performance and problem identification and

resolution deficiencies contributed to the failure to identify and correct the residual heat

removal wiring issue. On February 18, 2002, maintenance personnel performed

activities inside the electrical panel containing fuse block FF-F11. The maintenance work

conducted required fuse block FF-F11 to be moved; no wires were de-terminated from

the fuse block. Following the electrical panel maintenance, personnel re-installed fuse

block FF-F11 but did not visually or physically verify the integrity of any wiring

connections. Testing following the maintenance demonstrated that the wiring connected

to fuse block FF-F11 was in contact with the fuse block. However, the licensee believes

the wiring was loose. Instrument maintenance personnel conducted several

surveillances between March 18 and October 7, 2002, with unexpected results. Although

actions were taken to document the unexpected results, the rigor in evaluating these

results was less than adequate since equipment operability was not addressed.

On March 1, 2002, operations personnel completed QCOS 6600-48, Unit 2 Division 2

Emergency Core Cooling System Simulated Automatic Actuation and Diesel Generator

Auto-Start Surveillance. The test completion demonstrated that the wires associated

with fuse block FF-F11 remained in contact with the fuse block. Approximately

2.5 weeks later, instrument maintenance personnel conducted QCIS 1000-13, High

Drywell Pressure Core Spray, Low Pressure Coolant Injection, and Emergency Diesel

Generator Calibration and Functional Test. During this test the instrument technicians

noticed that the residual heat removal lights for high drywell pressure did not illuminate

as expected. One light flickered and extinguished; the other light never illuminated.

Since the light illumination was not part of the QCIS 1000-13 acceptance criteria, the

instrument technicians noted their observation and generated Work Order 421277 to

investigate the light failure. Troubleshooting by the fix-it-now team determined that the

light failures were not caused by burnt out bulbs. No other actions were taken to explain

the significance or cause of the light failure. Instead Work Order 421277 was

re-scheduled for completion during the May 2002 residual heat removal work week

window. Prior to May 2002, Work Order 421277 was re-classified as outage work for

unknown reasons. The inspectors noted that the next Unit 2 refueling outage was not

scheduled until 2004. During performances of QCIS 1000-13 on June 13 and

September 6, 2002, the instrument technicians continued to document the failure of the

residual heat removal lights for high drywell pressure to illuminate. No actions were

taken following the subsequent performances of QCIS 1000-13 due to the licensees

belief that the lights were for indication only.

The inspectors determined that the failure to adequately address the impact of the

extinguished lights were more than minor because it: (1) involved the configuration

control, equipment performance, and human performance attributes of the mitigating

systems cornerstone; and (2) affected the cornerstone objective of ensuring the

availability, reliability, and capability of systems that respond to initiating events to

prevent undesirable consequences.

The inspectors also determined that this finding should be evaluated using the

Significance Determination Process described in Inspection Manual Chapter 0609,

Significance Determination Process, because the finding was associated with the

availability of a mitigating system. The inspectors conducted a Phase 1 screening and

determined that a Phase 2 evaluation was required since the disconnected wire resulted

32

in an actual loss of safety function of a single train for greater than the Technical

Specification Allowed Outage Time. This finding also resulted in an actual loss of safety

function of the residual heat removal system during times when the 2B system was

operating in the torus cooling or torus spray modes.

The inspectors used the risk-informed inspection notebook for Quad Cities Nuclear

Power Station, Units 1 and 2, Revision 1, dated May 2, 2002, to complete the Phase 2

evaluation. The inspectors determined that the exposure time was greater than 30 days

which increased the initiating event likelihood for all initiating events by two orders of

magnitude. For each worksheet the inspectors assumed that all mitigating capability was

available except for both residual heat removal subsystems. The inspectors allowed

credit for recovery since the residual heat removal system could be aligned for low

pressure injection through manual operator actions. This resulted in 11 core damage

sequences between 9 and 14 points. The most dominant core damage sequences

involved: (1) the loss of the power conversion system with high pressure injection

equipment and the core spray system available; (2) a large break loss of coolant accident

with the core spray system available; and (3) a loss of offsite power with the high

pressure injection systems and the core spray system available. The inspectors

concluded that the final significance determination process result for this finding was

9 points; therefore, this finding was considered to be of very low risk significance

(Green).

Technical Specification 3.5.1, Emergency Core Cooling System - Operating, requires

that each emergency core cooling system injection and/or spray subsystem be operable

in Modes 1, 2, and 3. Technical Specification 3.5.1, Condition B, allows one residual

heat removal subsystem to be inoperable for up to 7 days. Condition C of the same

Technical Specification allows both residual heat removal subsystems to be inoperable

for up to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />. The inspectors determined that as of March 18, 2002, the 2B residual

heat removal subsystem, an emergency core cooling system, was inoperable. In

addition, both residual heat removal subsystems were inoperable at various times

between March 18 and October 7, 2002. This determination was based upon the fact

that as of March 18 the licensee was no longer able to ensure that the wire was

adequately secured to fuse block FF-F11. The failure to have both residual heat removal

subsystems operable while operating in Modes 1, 2, and 3 was considered a Non-Cited

Violation of Technical Specification 3.5.1 in accordance with Section VI.A.1 of the NRCs

Enforcement Policy (NCV 50-265/02-08-08). This issue was entered into the licensees

corrective action program as Condition Report 126235.

.4

Unit 1 in Single Loop Operation Due to 1B Reactor Recirculation Pump Trip

On December 6, 2002, the inspectors reviewed the circumstances surrounding the 1B

reactor recirculation pump trip. The inspectors reviewed the timeliness and adequacy of

operator actions during the transient condition. The inspectors determined that the

operators reacted appropriately and followed procedural requirements during the

transient condition. The inspectors also determined through observation that the

operators appropriately implemented procedures to allow the unit to operate in single

33

loop operations during the troubleshooting and reactor recirculation pump restoration

activities. Further information regarding the incident is described in Section 4OA2 of this

report.

4OA4 Cross-Cutting Findings

.1

Human Performance Related Findings

Findings described in Sections 1R20.1, 1R20.2, 1R20.3, and 4OA3.2 of this report had

one or more human performance deficiencies which caused the event to occur. An

individual failed to use self-check techniques when identifying the proper plant air supply

for an air powered vacuum. This error resulted in two separate instrument air transients

on October 24 and 25, 2002 (see Section 1R20.1).

A communications weakness between operations, maintenance and contractor personnel

resulted in a large amount of water being expelled from a stator water heat exchanger

during maintenance. The water migrated to the room below and resulted in the Unit 1

emergency diesel generator being declared inoperable (see Section 1R20.2).

Failure to follow procedures and untimely control room panel monitoring led to the

unexpected isolation of the reactor water cleanup system while the system was being

used to remove decay heat during the Unit 1 refueling outage (see Section 1R20.3).

Lastly, the failure to verify the physical integrity of wiring connections following

maintenance activities led to a condition which resulted in the 2B residual heat removal

system being inoperable for more than 6 months (see Section 4OA3.2).

.2

Problem Identification and Resolution Related Findings

The licensee did not initiate condition reports following the inspectors identification of

multiple scaffolding erection deficiencies (see Section 1R20.4). As a result, additional

scaffolding deficiencies were identified by other plant personnel. Later in the inspection

period, the licensee initiated a condition report encompassing all of the inspector

identified scaffolding issues. Once this action was taken, the licensee began conducting

an evaluation to determine whether a common cause had contributed to some or all of

the identified deficiencies.

Weaknesses in problem evaluation resulted in the failure to correct deficiencies with the

1B reactor recirculation voltage regulator (see Section 4OA2.1). On November 29 and

December 3, 2002, the licensee initiated two condition reports due to the 1B reactor

recirculation pump voltage regulator failing to meet proceduralized acceptance criteria.

During the evaluation of these condition reports, the licensee did not fully consider

changes made to the voltage regulator during the outage and power ascension. These

actions resulted in Unit 1 being at an increased risk for a plant transient and a

subsequent reactor recirculation pump trip on December 6, 2002.

Deficiencies in problem evaluation and prioritization also led to the failure to recognize

that the 2B residual heat removal system was inoperable (see Section 4OA3.2). The

inspectors determined that licensee personnel had at least three prior opportunities to

34

identify this condition prior to discovery of the condition on October 7, 2002. These

opportunities were not acted upon due to the licensees belief that an extinguished light

was for indication only rather than a sign of equipment malfunction.

4OA5 Other Activities

.1

Completion of Appendix A to TI 2515/148, Revision 1

The inspectors completed the pre-inspection audit for interim compensatory measures at

nuclear power plants, dated September 13, 2002.

.2

Power Uprate

a.

Inspection Scope

The inspectors observed control room activities associated with the Unit 1 power uprate

including power ascension testing and surveillance testing. The inspectors also reviewed

daily licensee power uprate observations and evaluations to ensure deficiencies were

adequately evaluated. The inspectors performed tours of the turbine building and reactor

building to assess plant conditions as power ascension activities progressed. The

inspectors reviewed plant modification plans and post-modification testing.

b.

Findings

No findings of significance were identified.

4OA6 Meetings

.1

Exit Meeting

The inspectors presented the inspection results to Mr. T. Tulon and other members of

licensee management at the conclusion of the inspection on December 31, 2002. The

inspectors asked the licensee whether any materials examined during the inspection

should be considered proprietary. No proprietary information was identified.

.2

Interim Exit Meetings

Interim exits were conducted for:

Temporary Instruction 2515/148, Appendix A with Mr. B. Swenson on

October 25, 2002.

Access Control, ALARA Planning and Control, and Radwaste and Transportation

with Mr. T. Tulon on November 15, 2002.

Inservice Inspection with Mr. T. Tulon on November 21, 2002.

35

4OA7 Licensee-Identified Violations

The following violations of very low significance were identified by the licensee and are

violations of NRC requirements which meet the criteria of Section VI of the NRC

Enforcement Manual, NUREG-1600, for being dispositioned as Non-Cited Violations.

Cornerstone: Mitigating Systems

Technical Specification Surveillance Requirement 3.8.4.7 requires that the licensee verify

that battery capacity is adequate to supply, and maintain in an operable status, the

required emergency loads for the design duty cycle every 24 months. As described in

Condition Report 124350, on September 24, 2002, the licensee had not included

charging spring motor loads for certain General Electric 480 Volt breakers as part of the

design duty cycle during previous battery testing. As a result, the license had not

adequately performed the surveillance testing required by Technical Specification

Surveillance Requirement 3.8.4.7.

The licensee entered Technical Specification Surveillance Requirement 3.0.3 in response

to the missed surveillance test. This surveillance requirement allowed the licensee to

delay entry into Technical Specification 3.8.7 due to the discovery of missed

surveillances as long as the a risk evaluation was performed within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> and the

missed surveillance tests were completed within the Technical Specification specified

frequency (in this case 24 months). The inspectors reviewed the licensees risk

assessment and determined that the risk to the plant from the missed surveillances was

very low since calculations showed that adequate battery capacity was available to

supply all required loads. Subsequent testing of the Unit 1 and 2 batteries also

demonstrated that adequate capacity was available to supply the required loads.

36

KEY POINTS OF CONTACT

Licensee

T. Tulon, Site Vice President

B. Swenson, Plant Manager

D. Barker, Radiation Protection Manager

W. Beck, Regulatory Assurance Manager

G. Boerschig, Work Control Manager

R. Gideon, Engineering Manager

K. Hungerford, Wackenhut Project Manager

A. Javorik, Maintenance Manager

M. Karney, Midwest ROG Security Manager

K. Leech, Security Manager

K. Moser, Chemistry/Environ/Radwaste Manager

M. Perito, Operations Manager

M. Snow, Nuclear Oversight Manager

Nuclear Regulatory Commission

M. Ring, Chief, Reactor Projects Branch 1

C. Lyon, Project Manager

K. Ohr, Radiation Protection Supervisor

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-254/02-08-01

FIN

Inadequate Design Leads to Delay in Discovering Safe Shutdown

50-265/02-08-01

Makeup Pump was Inoperable due to Strainer Clogging

50-254/02-08-02

URI

Resolution of American Society of Mechanical Engineers

50-265/02-08-02

Requirements

50-254/02-08-03

FIN

Inadequate Procedure and Self Checking Results in Connecting

50-265/02-08-03

Air Powered Vacuum to Instrument Air System and two Air

Transients

50-265/02-08-04

FIN

Inadequate Procedure and Communication Weaknesses Leads to

Emergency Diesel Generator Inoperability

50-254/02-08-05

NCV

Failure to Follow Procedure and Weak Control Board Monitoring

Leads to Inadvertent Reactor Water Cleanup Isolation

50-254/02-08-06

NCV

Multiple Examples of Scaffolding in Contact with Safety-Related

Equipment

37

50-254/02-08-07

FIN

Weaknesses in Problem Identification and Resolution Leads to 1B

Reactor Recirculation Pump Trip

50-265/02-08-08

NCV

Human Performance and Problem Identification and Resolution

Results in Failure to Discover Impact of Loose Lead on Residual

Heat Removal Inoperability

Closed

50-254/02-08-01

FIN

Inadequate Design Leads to Delay in Discovering Safe Shutdown

50-265/02-08-01

Makeup Pump was Inoperable due to Strainer Clogging

50-254/02-08-03

FIN

Inadequate Procedure and Self Checking Results in Connecting

50-265/02-08-03

Air Powered Vacuum to Instrument Air System and two Air

Transients

50-265/02-08-04

FIN

Inadequate Procedure and Communication Weaknesses Leads to

Emergency Diesel Generator Inoperability

50-254/02-08-05

NCV

Failure to Follow Procedure and Weak Control Board Monitoring

Leads to Inadvertent Reactor Water Cleanup Isolation

50-254/02-08-06

NCV

Multiple Examples of Scaffolding in Contact with Safety-Related

Equipment

50-254/02-08-07

FIN

Weaknesses in Problem Identification and Resolution Leads to 1B

Reactor Recirculation Pump Trip

50-265/02-08-08

NCV

Human Performance and Problem Identification and Resolution

Results in Failure to Discover Impact of Loose Lead on Residual

Heat Removal Inoperability

50-265/02-004

LER

Inadequate Separation in both Trip Systems of the Scram

Discharge Instrument Volume Input to the Reactor Protection

System

50-265/02-005

LER

Failure of Low Pressure Coolant Injection Logic Test due to

Detached Wire

Discussed

None

38

LIST OF ACRONYMS USED

ALARA

As-Low-As-Is-Reasonably-Achievable

ADAMS

Agencywide Documents Access and Management System

CFR

Code of Federal Regulations

CR

Condition Report

FIN

Finding

IMC

Inspection Manual Chapter

NCV

Non-Cited Violation

PARS

Publically Available Records System

RWP

Radiation Work Permit

SDP

Significance Determination Process

39

LIST OF DOCUMENTS REVIEWED

1R01

Adverse Weather

QCOP 0010-01; Winterizing Checklist; Revision 17

QCOP 0010-02; Required Cold Weather Routines; Revision 12

Quad Cities Winter Readiness Operating Experience

IE Bulletin 79-24; Frozen Lines; dated September 27, 1979

Licensees Response to IE Bulletin 79-24; dated October 30, 1979

List of Open Work Requests on the Ice Melt Valve and Heat Tracing System

Winter Readiness 2002-2003 Open Items List

OP-AA-108-109, Attachment 3; System Engineering System Readiness Review; various

dates

Condition Report 79845; Clean Demineralizer Suction Piping Installed At Risk; dated

October 23, 2001

Condition Report 80242; Unit 2 Traveling Screen High Differential Pressure Due to

Shear Pin Failure; dated October 25, 2001

Condition Report 81415; Cold Weather Preparations; dated November 2, 2001

Condition Report 82901; Ice Melt Valve - Limitorque Failure, Damage to Worm/Worm

Gear; dated November 14, 2001

Condition Report 93918; Unit 1 Startup Delayed 24 Hours Due to CIV #1 Stuck Closed;

dated February 4, 2002

Condition Report 98562; High Traveling Screen Differential Pressure Alarm on Unit 2;

dated March 10, 2002

Condition Report 112590; U-1 and 2 HRSS Sample Heat Trace Circuits Turned Off;

dated June 20, 2002

Condition Report 127693; Corrective Action Work Request Canceled; dated October 16,

2002

Condition Report 127842; Need to Inspect Duct for Foreign Material; dated October 17,

2002

40

Condition Report 127679, Safe Shutdown Makeup Pump Room Observed Warmer Than

Usual; dated October 16, 2002

Apparent Cause Evaluation for Condition Report 127679; dated October 25, 2002

QCMPM 2900-01; Unit 1/2 Safe Shutdown Pump Room Air Handling Unit Cooling Service

Water Strainer Preventive Maintenance; Revision 4; dated August 30 - October 31, 2002

Exelon Quality Assurance Topical Report; Revision 69

1R05 Fire Protection

Quad Cities Pre-Plan TB-69; Unit 1 Turbine Building, Elevation 595'-0" Hallway Fire

Zone 8.2.6.A

Quad Cities Pre-Plan TB-66; Unit 1 Turbine Building, Elevation 572'-6" CRD Pumps Fire

Zone 8.2.3.A

Quad Cities Pre-Plan TB-68; Unit 1 Turbine Building, Elevation 595'-0" Low Pressure

Heater Bay Fire Zone 8.2.6.B

Quad Cities Pre-Plan RB-24; Unit 1/2 Reactor Building, Elevation 690'-6" Refuel Floor

Quad Cities Pre-Plan RB-16; Unit 2 reactor Building, Elevation 554'-0" NW Corner

Room - 2A Core Spray Fire Zone 11.3.3

Quad Cities Pre-Plan RB-17; Unit 2 Reactor Building, Elevation 554'-0" SE Corner

Room - 2B RHR Room Fire Zone 11.3.2,

Quad Cities Pre-Plan RB-18; Unit 2 Reactor Building, Elevation 554'-0" NE Corner

Room - 2A RHR Room Fire Zone 11.3.4,

Quad Cities Station Units 1 and 2 Fire Hazards Analysis; dated August 2001

OP-AA-201-001; Fire Marshall Tours; Revision 1

OP-AA-201-004; Fire Prevention for Hot Work; Revision 5

OP-AA-201-008; Pre-Fire Plans; Revision 1

OP-AA-201-009; Control of Transient Combustibles; Revision 2

1R08 Inservice Inspection

ER-AA-335-005; Radiographic Examination; Revision 0

PT-EXLN-104V0; Procedure for Liquid Penetrant Examination Color Contrast (Visible)

Solvent Removable; dated November 7, 2001

41

GE-UT-311; Procedure for Manual Ultrasonic Examination of Nozzle Inner Radii and

Bore; dated January 9, 2001

GE-PDI-UT-1; PDI Generic Procedure for the Ultrasonic Examination of Ferritic Pipe

Welds; dated October 24, 2002

GE-PDI-UT-2; PDI Generic Procedure for the Ultrasonic Examination of Austenitic Pipe

Welds; dated October 24, 2002

ISI Program Plan, Third 10-Year Inspection Interval, Quad Cities Station, Units 1 & 2;

dated May 22, 2001

Quad Cities Generating Station Unit 2, Post Outage (90 Day) Summary Report,

Refueling Outage Q2R16; dated June 3, 2002

Action Report 00132057; NRCs Position Regarding CRD Housing Weld Inspections

Action Report 00113995; Dresden Missed Inspections of CRD Housing Welds

(Condition Report 113590)

Radiographic Examination Report RT-005; dated November 20, 2002

1R11 Licensed Operator Requalification

Scenario 00-28; Torus Narrow Range Instrument Failure, Loss of Coolant Accident

Inside Containment, and an Anticipated Transient Without Scram; Revision 10

QCOA 0201-01; Increasing Drywell Pressure; Revision 15

QCOP 0300-28; Alternate Rod Insertion; Revision 18

QCOA 0400-01; Reactivity Addition; Revision 13

QCOA 3200-01; Reactor Feed Pump Auto Trip; Revision 11

QGA 100; Reactor Pressure Vessel Control; Revision 7

QGA 101; Reactor Pressure Vessel Control (Anticipated Transient Without Scram);

Revision 10

QGA 200; Primary Containment Control; Revision 8

1R13 Maintenance Risk Assessment and Emergent Work

OU-AA-103; Shutdown Safety Management Program; Revision 1

Work Week Safety Profile; Week of December 9, 2002

OU-QC-104; Daily Risk Factor Chart, Attachment 1; Revision 1

42

WC-AA-104; Review and Screening for Production Risk; Revision 4

Online Work Schedules; Week of December 9, 2002

1R14 Non-Routine Evolutions

QCGP 3-1; Reactor Power Operations; Revision 29

QCGP 3-2; Control of Planned Reactor Power Changes; Revision 13

QCGP 4-1; Control Rod Movements and Control Rod Sequences; Revision 22

1R15 Operability Evaluations

Condition Report 132057; NRCs Position Regarding Control Rod Drive Housing Weld

Inspections; dated November 17, 2002

Condition Report 124350; Certain General Electric 480 Volt Breakers not Properly

Modeled in ELMS-DC Database; dated September 24, 2002

Condition Report 131936, Unit 2 Main Steam Isolation Valves 2-0203-2B and 2-0203-2C

Contain Belleville Springs in the Low Liner Assembly Which are Suspect for Potential

Failure; dated November 20, 2002

1R16 Operator Workarounds

OP-AA-101-103; Operator Work-Around Program; Revision 0

List of Open Operator Workarounds and Operator Challenges; dated October 10, 2002

Condition Report 110692; Work on Valve 1-2001-794 Rescheduled due to Welding

Resources and Pipe Interference; dated June 5, 2002

OP-AA-108-102; Equipment Status Tag Log; dated October 11, 2002

Unit 1 Nuclear Station Operator Turnover Checklist; dated October 11, 2002

Unit 2 Nuclear Station Operator Turnover Checklist; dated October 11, 2002

Temporary Configuration Change Report; dated October 11, 2002

Operability Determinations with Open Compensatory Actions or Corrective Actions Log;

dated October 11, 2002

Operator Burden Review; dated July 2002

Operator Burden Review; dated October 2002

43

1R17 Permanent Plant Modifications

Engineering Change Package 24165; Trip Condensate/Booster Pump 1D on Loss of

Coolant Accident and With All four Condensate/Booster Pumps 1A, 1B, 1C, and 1D

Running; dated May 9, 2001

Engineering Change Package 24169; Main Steam Flow High Setpoint Change and

Differential Pressure Switch Replacement; dated January 16, 2001

Engineering Change Package 24420; Reactor Feed Pump and Motor Generator Set

Breaker Time Delay Modification; dated June 5, 2001

Engineering Change Package 337693; Isophase Bus Duct Cooling System Upgrade to

Support Extended Power Uprate Operation

Calculation QDC-3000-I-0986; Main Steam Line High Flow Differential Pressure Switch

Setpoint Error Analysis; Revision 0

Engineering Change 24432; Extended Power Uprate Project Main Steam Pipe Support

Project Main Steam Pipe Support and Drywell Steel Modifications; Revision 3

1R19 Post Maintenance Testing

QCOS 1100-07; SBLC Pump Flow Rate Test; Unit 1, Revision 22

QOM 1-1100-01; U1 Standby Liquid Control Valve Check List; Revision 9

QCOS 2300-28; HPCI Turning Gear Logic Functional Test; Revision 8

Work Order 416235-01; Replace Agastat Time Delay Relay 1-2300-121 in Panel 901-39;

dated October 22, 2002

Engineering Change Request 51124; Obtain Time Delay Criteria for 2330-121 Relay;

dated September 16, 1998

Drawing 4E-1526; Schematic Control Diagram HPCI System Block Diagram 8 Control

Switch Development; Revision T

Drawing 4E-1527; Schematic Diagram High Pressure Coolant Injection System Sensors

and Auxiliary Relays; Sheet 1; Revision R

Drawing 4E-1527; Schematic Diagram High Pressure Coolant Injection System Sensors

and Auxiliary Relays; Sheet 2; Revision H

Drawing 4E-1527; Schematic Diagram High Pressure Coolant Injection System Sensors

and Auxiliary Relays; Sheet 3; Revision M

Drawing 4E-1532; Schematic Diagram High Pressure Coolant Injection System Turbine

Auxiliary Pumps; Revision AA

44

1R20 Refueling and Outage

Condition Report 128977; Moisture Separator Decon Work Used IA Instead of SA; dated

October 25, 2002

Work Order 369947; Moisture Separator Decontamination Work

Units 1 and 2 Control Room Logs; dated October 24-25, 2002

Condition Report 130694, Stator Water Heat Exchanger Spill; dated November 7, 2002

Out of Service Tagout 00011947

Work Order 99183182, Task 01; Replace Tube Bundle Assembly in the 1-7401-A Stator

Cooling Water Heat Exchanger

Condition Report 133054; Unit 1 RWCU Isolation; dated November 24, 2002

Unit 1 Control Room Logs; dated November 24, 2002

QCOP 1200-15, Operation of Decay Heat Removal Mode of RWCU System; Revision 13

QCOP 1200-13, RWCU System High Temperature Isolation Setpoint Adjustment;

Revision 3

Unit 1 Main Condenser Clearance Order 00011583

Unit 1 High Pressure Coolant Injection Clearance Order 00012820

Procedure OU-AA-103; Shutdown Safety Management Program; Revision 1

Procedure OU-QC-104; Shutdown Safety Management Program Quad Cities Annex;

Revision 2

QCOA 1000-02; Loss of Shutdown Cooling; Revision 12

QCOS 1000-24; Shutdown Cooling Outage Report; Revision 5

QCOP 1000-38; Alternate Shutdown Cooling; Revision 3

QCOA 1000-03; RHR Pump Trip; Revision 6

QCOP 1000-17; Shutdown Cooling, Reactor Temperature Trending; Revision 11

QCOP 1000-05; Shutdown Cooling Operation; Revision 30

QCOP 1200-15; Operation of Decay Heat Removal Mode of Reactor Water Cleanup

System; Revision 13

45

QCGP 1-1; Normal Unit Startup; Revision 44

QCGP 3-1; Reactor Power Operations; Revision 29

OP-AA-108-108; Unit Restart Review; Revision 0

Shutdown Safety Risk Profile Worksheets; dated November 5 - November 25, 2002

Condition Report 131936; Missing Belleville Washer in 1-0203-2C Main Steam Isolation

Valve; dated November 5, 2002

Condition Report 130946; Parts Found in Turbine Stop Valve Strainer; dated

November 8, 2002

Technical Evaluation of Degraded Main Steam Isolation Valve Belleville Springs

Identified During Q1R17

Indication Notification Report Q1R17-02-01; Steam Dryer; dated November 8, 2002

Condition Report 130921; Deformed Steam Dryer Exhaust Skirt and Cracked Tie Bar

Weld; dated November 8, 2002

Engineering Change 24495; Power Uprate - Modify Reactor Vessel Steam Dryer to

Reduce Moisture Carryover; dated November 12, 2002

Letter from Mark O. Lenz and James D. Adam, General Electric to Bruce Phares, Exelon

Nuclear; Re: Quad Cities Unit 1, Jet Pump 16 Slip Joint; dated November 15, 2002

1R22 Surveillance Testing

QOS 6500-03; Undervoltage Functional Test 4 KV Bus 14-1; Revision 21

QCOS 6600-49; Division 1 ECCS Automatic Actuation Test; Revision 5

QCOS 6600-50; Division 1 ECCS Automatic Actuation Test; Revision 6

Technical Specifications

Updated Final Safety Analysis Report

1R23 Temporary Plant Modifications

Engineering Change Request 357803; dated 11/11/02

Engineering Change 339810; Revision 1

Temporary Interim Change Procedure 576; Drywell Equipment Drain Sump Temporary

Pump Installation; dated 11/13/02

46

CC-AA-112; Temporary Configuration Changes; Revision 5

Engineering Change 339708; Installation of Temporary Bladders to Maintain Secondary

Containment; dated November 7, 2002

10 CFR 50.59 Screening QC-S-2002-0376; Installation of Temporary Bladders to

Maintain Secondary Containment; dated November 7, 2002

QCMM 0203-03; Installation, Maintenance, and Removal of Line Plugs in the Main Steam

Line to Provide Secondary Containment with the MSIV Room Part of the Turbine

Building; Revision 0

Updated Final Safety Analysis Report

Technical Specifications

2OS1 Access Control

2OS2 ALARA Planning and Controls

10001409; RWP/ALARA Plan/Work In Progress Review: U1 Moisture Separators:

Chem Decon; Revision 2

10001341; RWP/ALARA Plan: U1 Main Turbine Overhaul/PM; Revision 2

10001253; RWP/ALARA Plan: ERV/SRV/Target Rock Valves: Remove/Replace;

Revision 3

10001289; RWP/ALARA Plan: Overhaul B, C, D Inboard MSIVs; Revision 1

10001909; RWP/ALARA Plan: U1 Steam Dryer Cover Plate Mod: Diving Activities:

Diving Activities; Revision 1

10001362; RWP/ALARA Plan: U1 Reactor Steam Dryer: Mod To Reduce Carryover

(Divers); Revision 0

10001341; RWP-TEDE ALARA Evaluations; Revisions 1 and 2

Trend Charts, Unit 1 Soluble/Insoluble Cobalts 58/60; from June 1998 through

November 2002

Exposure Reduction Charter; Revision 2

Reactor Coolant I-131 Equivalent from May 15, 2002 through October 2, 2002

Reactor Coolant Neptunium 239 from May 15, 2002 through September 4, 2002

Unit 1 Dose Equivalent Iodine from November 5, 2000 through November 5, 2002

47

RP-AA-441; Evaluation and Selection Process For Radiological Respirator Use;

Revision 2

QCCP 0200-01; Reactor Water Iodine Analysis; Revision 11

Performance Indicator Data (Effluents) from October 2001 through September 2002

Performance Indicator Data (Occupational) from October 2001 through September 2002

Dose Equivalent Iodines U1/U2 from October 2001 through September 2002

Drywell Survey Map 579 Elevation; dated November 5, 2002

Drywell Survey Map 592 Elevation; dated November 8, 2002 Drywell Survey Map 614

Elevation; dated November 7, 2002

Drywell Survey Map 640 Elevation; dated November 9, 2002

Drywell Survey Map 652 Elevation; dated November 9, 2002

105357; Nuclear Oversight Identified Deficiencies in RP Documentation Reviews In First

Quarter Assessment; dated April 25, 2002

107216; Contamination Found in Clean Area In U2 5 Rack; dated May 15, 2002

104218; 2B RHR Room Cooler Work Scope Not Properly Communicated To RP; dated

April 16, 2002

103141; Erroneous ED Record Without Proper Follow up Causes RWP Lock; dated

April 10, 2002

127222; Elevated Dose Rates in Rad Waste Basement; dated October 11, 2002

127441; Poor Rad Worker Practices Identified; dated October 17, 2002

128774; High radiation Area Identified in Radwaste Max Recycle; dated October 4, 2002

Q1R17 Dose Estimates; dated November 7, 2002

Q1R17 Outage Dose Estimate Review; dated November 12, 2002

2PS2 Radioactive Material Processing and Transportation

Focus Area Self-Assessment Report, Radioactive Material Transportation; dated

July 30, 2002

Focus Area Self-Assessment Report Radiation, Radwaste; dated May 16, 2002

RW-AA-100; Process Control Program for Radioactive Wastes; Revision 2

48

QCRP 5620-0610; CFR 61 Waste Stream Sampling and Analysis; Revision 2

RP-AA-600; Radioactive Material/Waste Shipments; Revision 5

Shipment No QC-01-307 Type B, Y-III, Irradiated Hardware; dated April 20, 2001

Shipment No QC-01-311 Type B, Y-III, Irradiated Hardware; dated May 4, 2001

Shipment No QC-02-328 Type A, Y-III, Control Rod Drives; dated February 20, 2002

Shipment No QC-02-001 LSA II, Y-III, Dewatered Resin; dated June 4, 2002

Shipment No QC-02-324 SCO I, Safety Valves; dated February 17, 2002

AR 00076148Q2001-02884; RAM Shipping Personnel Not Trained IAW IATA; dated

September 17, 2001

AR 00090308; Improper Unloading of a Radioactive Material Shipment; dated

January 14, 2002

AR 00100601; HIC Dose Rate Higher Than Normal; dated March 22, 2002

AR 00123322; Water in Radioactive Shipment; dated September 18, 2002

4OA1 Performance Indicator Verification

Nuclear Energy Institute Document 99-02; Regulatory Assessment Performance

Indicator Guideline; Revision 2

LS-AA-2050; Monthly Performance Indicator Data Elements for Safety System

Unavailability-High Pressure Injection (BWR) or High Pressure Safety Injection (PWR);

Revision 2; dated August 2001-August 2002

4OA3 Event Followup

Updated Safety Analysis Report

Technical Specifications

Condition Report 126235; While Performing QCOS 1000-44 2B RHR Logic Test, Could

Not Complete Step H.4.1.1; dated October 7, 2002

Prompt Investigation for Condition Report 126235; Disconnected Lead Found During U2

LPCI Logic Test; dated October 7, 2002

Management Review Committee Update; RHR Logic Test Failure due to Detached Lead;

dated October 29, 2002

49

QCOP 0202-21, Unit 1 Reactor Recirculation System Shutdown of One Pump,

Revision 4

QCOP 0202-07, Reactor Recirculation Single Loop Operation Determination of Total

Core Flow, Revision 12

QCOP 0202-02, Reactor Recirculation System Startup, Revision 24

QCOP 0202-13, Reactor Recirculation Flow Control Line Determination, Revision 7

TIC-510, Quad Cities Unit 1 EPU Power Ascension Test Procedure

Engineering Change 24495; Power Uprate - Modify Reactor Vessel Steam Dryer to

Reduce Moisture Carryover; dated November 12, 2002

Engineering Change 337693; Isophase Bus Duct Cooling Modification; dated

October 4, 2002

Work Order 453748; Remove and replace Modified Standby Liquid Control Relief Valves

for EPU

EC 24165; Trip Condensate/Booster Pump 1D on Loss of Coolant Accident and With All

Four Condensate/Booster Pumps 1A, 1B, 1C, and 1D Running; dated May 9, 2001

EC 24169; Main Steam Flow High Setpoint Change and Differential Pressure Switch

Replacement; dated January 16, 2001

EC 24420; Reactor Feed Pump and Motor Generator Set Breaker Time Delay

Modification; dated June 5, 2001

Calculation QDC-3000-I-0986; Main Steam Line High Flow Differential Pressure Switch

Setpoint Error Analysis; Revision 0

EC 24432; Extended Power Uprate Project Main Steam Pipe Support Project Main

Steam Pipe Support and Drywell Steel Modifications; Revision 3

4OA7 Licensee-Identified Violations

Condition Report 124350; Certain General Electric 480 Volt Breakers not Properly

Modeled in ELMS-DC Database; dated September 24, 2002

Risk Management Documentation Number SA-1114; Technical Specification Surveillance

Requirement 3.0.3 Risk Evaluation of Revised 125 V Direct Current Profile; dated

October 4, 2002