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Category:Letter
MONTHYEARML25052A0882025-02-27027 February 2025 Regulatory Audit Plan in Support of License Amendment Request to Use Online Monitoring Methodology ML25051A1762025-02-26026 February 2025 Regulatory Audit Plan in Support of License Amendment Request to Adopt Risk-Informed Completion Times CNL-25-010, Clinch River, Sequoyah, Units 1 and 2, Watts Bar, Units 1 and 2, Response to Request for Additional Information - TVA Request for Approval of Revision 43 to TVA Fleet Quality Assurance Program Description2025-02-26026 February 2025 Clinch River, Sequoyah, Units 1 and 2, Watts Bar, Units 1 and 2, Response to Request for Additional Information - TVA Request for Approval of Revision 43 to TVA Fleet Quality Assurance Program Description ML25050A0422025-02-14014 February 2025 57484-EN 57484 - Final Report Notification Pursuant to 10 CFR 21.21 Regarding Limitorque SMB-00 Torque Switch Assemblies IR 05000390/20240042025-02-13013 February 2025 Integrated Inspection Report 05000390/2024004 and 05000391/2024004 and Apparent Violation CNL-25-026, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2025-02-12012 February 2025 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions CNL-25-028, Supplement to Application to Revise Function 5 of Technical Specification Table 3.3.2-1, Engineered Safety Feature Actuation System Instrumentation, for (SQN-TS-23-02 & WBN-TS-23-08) (EPID L-2023-LLA-01752025-02-12012 February 2025 Supplement to Application to Revise Function 5 of Technical Specification Table 3.3.2-1, Engineered Safety Feature Actuation System Instrumentation, for (SQN-TS-23-02 & WBN-TS-23-08) (EPID L-2023-LLA-0175 IR 05000390/20244032025-01-31031 January 2025 Watts Barr Nuclear Plant - Material Control and Accounting Program Inspection Report 05000390/2024403 and 05000391/2024403 (Public) CNL-25-009, And Watts Bar Nuclear Plant, Units 1 and 2 - Organization Topical Report, TVA-NPOD89-A, Revision 262025-01-29029 January 2025 And Watts Bar Nuclear Plant, Units 1 and 2 - Organization Topical Report, TVA-NPOD89-A, Revision 26 05000391/LER-2025-001, Loss of the Control Room Emergency Air Temperature Control System Due to Chiller Valve Malfunction2025-01-21021 January 2025 Loss of the Control Room Emergency Air Temperature Control System Due to Chiller Valve Malfunction IR 05000390/20254022025-01-17017 January 2025 Information Request for the Cybersecurity Baseline Inspection Notification to Perform Inspection 05000390/2025402 05000391/2025402 CNL-25-012, Supplement to License Amendment Request for Adoption of Technical Specification Task Force Traveler TSTF-276-A, Revision 2, Regarding TS 3.8.1 AC Sources - Operating to Clarify Requirements for Diesel Generator .2025-01-16016 January 2025 Supplement to License Amendment Request for Adoption of Technical Specification Task Force Traveler TSTF-276-A, Revision 2, Regarding TS 3.8.1 AC Sources - Operating to Clarify Requirements for Diesel Generator . IR 05000391/20240402025-01-16016 January 2025 95001 Supplemental Inspection Report 05000391/2024040 and Follow-Up Assessment Letter CNL-24-076, Response to Request for Additional Information Regarding Application to Modify the Technical Specifications for Main Control Room Chiller Completion Time Extension (WBN-TS-23-13)2025-01-16016 January 2025 Response to Request for Additional Information Regarding Application to Modify the Technical Specifications for Main Control Room Chiller Completion Time Extension (WBN-TS-23-13) ML25006A1172025-01-10010 January 2025 – Review of the Fall 2023 Steam Generator Tube Inspection Report (EPID-L-2024-LRO-0022) ML24354A1582025-01-0303 January 2025 Reissue Technical Specification Pages for Amendment No. 170 to Facility Operating License No. NPF-90 CNL-25-001, License Amendment Request to Revise Technical Specifications to Adopt Risk-Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b2024-12-27027 December 2024 License Amendment Request to Revise Technical Specifications to Adopt Risk-Informed Completion Times TSTF-505, Revision 2, Provide Risk-Informed Extended Completion Times - RITSTF Initiative 4b ML24312A3222024-12-23023 December 2024 Issuance of Amendment Nos. 334, 357, & 317; 368 & 362; 172 & 77 Regarding Revision to TS 5.4 & 5.7.1 ML24312A0052024-12-23023 December 2024 Issuance of Amendment No. 171 Regarding Extension of Facility Operating License Expiration Date to Recapture Low-Power Operating License Testing Time ML24285A2072024-12-17017 December 2024 Amendment Nos. 170 and 76 Regarding the Revision of Technical Specifications 2.0, 3.0, 3.1, 3.2, 3.3, 3.4, and 5.9.5 by Adopting Various Technical Specifications Task Force Travelers CNL-24-009, Brown Ferry Nuclear Plant, Units 1, 2 & 3; Sequoyah Nuclear Plant, Units 1 & 2 and Watts Bar Plant, Units 1 & 2 - Triennial Decommission Funding Plans for Independent Spent Fuel Storage Installations2024-12-17017 December 2024 Brown Ferry Nuclear Plant, Units 1, 2 & 3; Sequoyah Nuclear Plant, Units 1 & 2 and Watts Bar Plant, Units 1 & 2 - Triennial Decommission Funding Plans for Independent Spent Fuel Storage Installations CNL-24-082, Central Emergency Control Center Emergency Plan Implementing Procedure Revision2024-12-17017 December 2024 Central Emergency Control Center Emergency Plan Implementing Procedure Revision ML24352A0092024-12-16016 December 2024 Investigation Summary, Office of Investigations Case Number 2-2023-007 IR 05000390/20243012024-12-16016 December 2024 NRC Operator License Examination Report 05000390/2024301 and 05000391/2024301 ML24346A3982024-12-16016 December 2024 NRC Examination Results Summary Examination Report 05000390/2024301 and 05000391/2024301 CNL-24-072, Request for Alternative to Extend First Containment Inservice Inspection Interval2024-12-12012 December 2024 Request for Alternative to Extend First Containment Inservice Inspection Interval CNL-24-075, Response to Request for Additional Information for Application to Revise Function 5 of Technical Specification Table 3.3.2-1, Engineered Safety Feature Actuation System Instrumentation, for the Sequoyah and Watts Bar (SQN-TSTS-23-02 and W2024-11-27027 November 2024 Response to Request for Additional Information for Application to Revise Function 5 of Technical Specification Table 3.3.2-1, Engineered Safety Feature Actuation System Instrumentation, for the Sequoyah and Watts Bar (SQN-TSTS-23-02 and WBN ML24297A4632024-11-21021 November 2024 – Environmental Assessment and Finding of No Significant Impact Related to Recapture of Low-Power Testing Time CNL-24-080, Response to Request for Additional Information Regarding Application to Revise Updated Final Safety Analysis Report Regarding Changes to Hydrologic Analysis (WBN-19-011)2024-11-20020 November 2024 Response to Request for Additional Information Regarding Application to Revise Updated Final Safety Analysis Report Regarding Changes to Hydrologic Analysis (WBN-19-011) IR 05000390/20240032024-11-13013 November 2024 Integrated Inspection Report 05000390/2024003, 05000391/2024003 & 07201048/2024001 CNL-24-021, Application to Revise Technical Specification Limiting Condition of Operation 3.5.2, ECCS – Operating, Note 1 to Include Residual Heat Removal Pump Flow Paths (SQN-TS-23-04 and WBN-TS-23-020)2024-11-12012 November 2024 Application to Revise Technical Specification Limiting Condition of Operation 3.5.2, ECCS – Operating, Note 1 to Include Residual Heat Removal Pump Flow Paths (SQN-TS-23-04 and WBN-TS-23-020) IR 05000390/20250102024-11-0404 November 2024 Notification of an NRC (FPTI) (NRC Inspection Report 05000390/2025010 0500039/ 2025010) (RFI) CNL-24-014, License Amendment Request to Revise the Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 Technical Specifications to Use Online Monitoring Methodology (SQN-TS-24-02 and WBN-TS-23-22)2024-11-0404 November 2024 License Amendment Request to Revise the Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 Technical Specifications to Use Online Monitoring Methodology (SQN-TS-24-02 and WBN-TS-23-22) CNL-24-064, Response to Request for Additional Information Regarding the Watts Bar Nuclear Plant, Unit 2 Steam Generator Tube Inspection Report for U2R52024-11-0404 November 2024 Response to Request for Additional Information Regarding the Watts Bar Nuclear Plant, Unit 2 Steam Generator Tube Inspection Report for U2R5 CNL-24-074, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-10-23023 October 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24290A1202024-10-17017 October 2024 Operator Licensing Examination Approval 05000390/2024301 and 05000391/2024301 ML24282B0412024-10-15015 October 2024 Request for Withholding Information from Public Disclosure for Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 ML24261C0062024-10-0404 October 2024 Correction to Amendment No. 134 to Facility Operating License No. NPF-90 and Amendment No. 38 to Facility Operating License No. NPF-96 ML24260A1682024-10-0404 October 2024 Regulatory Audit Summary Related to Request to Add and Revise Notes Related to Technical Specification Table 3.3.2-1, Function 5 ML24284A1072024-09-26026 September 2024 Affidavit for Request for Withholding Information from Public Disclosure for Sequoyah Nuclear Plant, Units 1 and 2, and Watts Bar Nuclear Plant, Units 1 and 2 CNL-24-047, Decommitment of Flood Mode Mitigation Improvement Systems2024-09-24024 September 2024 Decommitment of Flood Mode Mitigation Improvement Systems CNL-24-060, Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description2024-09-24024 September 2024 Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description ML24262A0602024-09-23023 September 2024 Summary of August 19, 2024, Meeting with Tennessee Valley Authority Regarding a Proposed Supplement to the Tennessee Valley Authority Nuclear Quality Assurance Plan CNL-24-065, Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-09-18018 September 2024 Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions 05000390/LER-2024-002, Automatic Reactor Trip Due to Main Generator Protection Relay Actuation2024-09-0505 September 2024 Automatic Reactor Trip Due to Main Generator Protection Relay Actuation IR 05000390/20240052024-08-28028 August 2024 Updated Inspection Plan and Assessment Follow-Up Letter for Watts Bar Nuclear Plant, Units 1 and 2 - Report 05000390-2024005 and 05000391-2024005 ML24218A1442024-08-27027 August 2024 Issuance of Amendment Nos. 169 and 75 Regarding Technical Specification Surveillance Requirement 3.9.5.1 to Reduce the Residual Heat Removal Flow Rate IR 05000390/20244022024-08-20020 August 2024 – Security Baseline Inspection Report 05000390-2024402 and 05000391/2024402 - Public CNL-24-061, Supplement to Application to Revise Function 5 of Technical Specification Table 3.3.2-1, ‘Engineered Safety Feature Actuation System Instrumentation,’ for the Sequoyah and Watts Bar (SQN-TS-23-02 and WBN-TS-23-08),2024-08-19019 August 2024 Supplement to Application to Revise Function 5 of Technical Specification Table 3.3.2-1, ‘Engineered Safety Feature Actuation System Instrumentation,’ for the Sequoyah and Watts Bar (SQN-TS-23-02 and WBN-TS-23-08), ML24219A0262024-08-12012 August 2024 Request for Withholding Information from Public Disclosure 2025-02-27
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000391/LER-2025-001, Loss of the Control Room Emergency Air Temperature Control System Due to Chiller Valve Malfunction2025-01-21021 January 2025 Loss of the Control Room Emergency Air Temperature Control System Due to Chiller Valve Malfunction 05000390/LER-2024-002, Automatic Reactor Trip Due to Main Generator Protection Relay Actuation2024-09-0505 September 2024 Automatic Reactor Trip Due to Main Generator Protection Relay Actuation 05000391/LER-2024-003, Inoperability of Both Trains of Unit 2 Low Head Safety Injection2024-07-11011 July 2024 Inoperability of Both Trains of Unit 2 Low Head Safety Injection 05000391/LER-2024-002, Re Automatic Reactor Trip Due to Steam Generator 3 Level LO-LO2024-05-0606 May 2024 Re Automatic Reactor Trip Due to Steam Generator 3 Level LO-LO 05000391/LER-2024-001, Automatic Reactor Trip Due to Main Generator Protection Relay Actuation2024-03-27027 March 2024 Automatic Reactor Trip Due to Main Generator Protection Relay Actuation 05000391/LER-2023-003-01, Automatic Reactor Trip Due to Loss of Main Feedwater Regulating Valve Control2024-02-29029 February 2024 Automatic Reactor Trip Due to Loss of Main Feedwater Regulating Valve Control 05000391/LER-2023-003, Automatic Reactor Trip Due to Loss of Main Feedwater Regulating Valve Control2023-10-0303 October 2023 Automatic Reactor Trip Due to Loss of Main Feedwater Regulating Valve Control 05000390/LER-2023-001-01, Inadequate 10 CFR 50.59 Results in Failure to Obtain Prior NRC Approval for Condition Prohibited by Technical Specifications2023-09-27027 September 2023 Inadequate 10 CFR 50.59 Results in Failure to Obtain Prior NRC Approval for Condition Prohibited by Technical Specifications 05000391/LER-2023-002, Automatic Reactor Trip Due to Main Generator Protection Relay Actuation2023-08-24024 August 2023 Automatic Reactor Trip Due to Main Generator Protection Relay Actuation 05000391/LER-2023-001, Unanalyzed Condition Related to Loss of the 2A Emergency Diesel Generator During a Postulated Appendix R Fire2023-07-20020 July 2023 Unanalyzed Condition Related to Loss of the 2A Emergency Diesel Generator During a Postulated Appendix R Fire 05000390/LER-2023-001, Interpretation of Technical Specification (TS) Table 1.1-1 Leads to a Condition Prohibited by TS2023-07-0303 July 2023 Interpretation of Technical Specification (TS) Table 1.1-1 Leads to a Condition Prohibited by TS 05000391/LER-2021-001, Automatic Reactor Trip on Main Turbine Trip Caused by Main Feed Pump Trip Due to Low Condenser Vacuum2021-05-10010 May 2021 Automatic Reactor Trip on Main Turbine Trip Caused by Main Feed Pump Trip Due to Low Condenser Vacuum 05000390/LER-2021-001, Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open2021-04-20020 April 2021 Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open 05000391/LER-2020-004, Steam Generators Degraded Due to Axial Outside Diameter Stress Corrosion Cracking2021-01-0707 January 2021 Steam Generators Degraded Due to Axial Outside Diameter Stress Corrosion Cracking 05000390/LER-2020-005, Automatic Start of the Emergency Diesel Generators Due to an Equipment Failure During Transfer of Power Source for the 2A-A Shutdown Board2021-01-0404 January 2021 Automatic Start of the Emergency Diesel Generators Due to an Equipment Failure During Transfer of Power Source for the 2A-A Shutdown Board 05000391/LER-2020-003, Re Low RHR Flow in Mode 6 Results in a Condition Prohibited by Technical Specifications2020-12-21021 December 2020 Re Low RHR Flow in Mode 6 Results in a Condition Prohibited by Technical Specifications 05000391/LER-2020-002, Re Two Pressurizer Safety Valves Outside of Technical Specification Limits Due to Set Point Drift2020-12-17017 December 2020 Re Two Pressurizer Safety Valves Outside of Technical Specification Limits Due to Set Point Drift 05000390/LER-2020-003, Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open2020-09-10010 September 2020 Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open 05000391/LER-2020-001, Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open2020-07-15015 July 2020 Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open 05000390/LER-2020-002, Automatic Start of the Emergency Diesel Generators Due to an Equipment Failure During Transfer of Power Source for the 1B-B Shutdown Board2020-07-14014 July 2020 Automatic Start of the Emergency Diesel Generators Due to an Equipment Failure During Transfer of Power Source for the 1B-B Shutdown Board 05000390/LER-2020-001, Manual Reactor Trip Due to Lowering Steam Generator Level Caused by a Hand Station Failure2020-04-17017 April 2020 Manual Reactor Trip Due to Lowering Steam Generator Level Caused by a Hand Station Failure 05000390/LER-2019-004, Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open2020-01-13013 January 2020 Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open 05000390/LER-2019-003, Manual Reactor Trip Due to Main Feedwater Regulating Valve Failing Closed2019-10-21021 October 2019 Manual Reactor Trip Due to Main Feedwater Regulating Valve Failing Closed 05000391/LER-2019-002, Breach Due to Penetration Boot Seal Separation Results in Shield Building Inoperability2019-08-19019 August 2019 Breach Due to Penetration Boot Seal Separation Results in Shield Building Inoperability 05000390/LER-2019-002, Loss of Control Room Emergency Air Temperature Control System Due to Air Filter Failure2019-08-0707 August 2019 Loss of Control Room Emergency Air Temperature Control System Due to Air Filter Failure 05000391/LER-2019-001, Regarding Manual Reactor Trip Due to Main Feedwater Regulating Valve Failing Closed2019-07-18018 July 2019 Regarding Manual Reactor Trip Due to Main Feedwater Regulating Valve Failing Closed 05000390/LER-2018-006, Containment Air Return Fan Inoperable for a Time Period Longer than Allowed by Technical Specifications Due to an Inadequate Post Maintenance Test2019-02-11011 February 2019 Containment Air Return Fan Inoperable for a Time Period Longer than Allowed by Technical Specifications Due to an Inadequate Post Maintenance Test 05000390/LER-2018-005, Regarding Manual Reactor Trip Due to Failure of Reactor Coolant Pump to Transfer to Normal Power2018-12-19019 December 2018 Regarding Manual Reactor Trip Due to Failure of Reactor Coolant Pump to Transfer to Normal Power 05000390/LER-2018-004, Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open2018-11-13013 November 2018 Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open 05000391/LER-2018-005, For Watts Bar Nuclear Plant, Unit 2, Automatic Reactor Trip Due to Turbine Control System Card Failure and Throttle Valve Closure2018-10-22022 October 2018 For Watts Bar Nuclear Plant, Unit 2, Automatic Reactor Trip Due to Turbine Control System Card Failure and Throttle Valve Closure 05000391/LER-2018-004, Failure to Implement Annunciator Response Process Results in a Condition Prohibited by Technical Specifications2018-09-21021 September 2018 Failure to Implement Annunciator Response Process Results in a Condition Prohibited by Technical Specifications 05000391/LER-2018-003, Reactor Trip Due to Main Generator Differential Relay Actuation2018-08-21021 August 2018 Reactor Trip Due to Main Generator Differential Relay Actuation 05000391/LER-2018-002, Loss of Shield Building Vacuum Due to Equipment Failure2018-07-0909 July 2018 Loss of Shield Building Vacuum Due to Equipment Failure 05000390/LER-2018-002-01, Shield Building Inoperability Due to Annulus Vacuum Transient2018-06-26026 June 2018 Shield Building Inoperability Due to Annulus Vacuum Transient ML18144A9982018-05-24024 May 2018 Ventilation System Inoperable Due to Main Control Room Door Being Left Open 05000390/LER-2018-002, Regarding Shield Building Inoperability Due to Annulus Vacuum Transient2018-03-19019 March 2018 Regarding Shield Building Inoperability Due to Annulus Vacuum Transient 05000390/LER-2017-016, Regarding System Actuations Due to Opening of Feeder Breaker to the 1B-B 6.9 Kv Shutdown Board2018-02-20020 February 2018 Regarding System Actuations Due to Opening of Feeder Breaker to the 1B-B 6.9 Kv Shutdown Board 05000391/LER-2017-006, Regarding Manual Reactor Trip in Response to Indication of Multiple Dropped Control Rods2018-02-0909 February 2018 Regarding Manual Reactor Trip in Response to Indication of Multiple Dropped Control Rods 05000391/LER-1917-005, Regarding Unplanned Emergency Core Cooling System Injection Into the Reactor Coolant System Due to Personnel Error2018-01-25025 January 2018 Regarding Unplanned Emergency Core Cooling System Injection Into the Reactor Coolant System Due to Personnel Error 05000390/LER-1917-015, Regarding Failure to Enter Limiting Condition of Operation Action Statement Results in a Condition Prohibited by Technical Specifications2018-01-0808 January 2018 Regarding Failure to Enter Limiting Condition of Operation Action Statement Results in a Condition Prohibited by Technical Specifications 05000390/LER-1917-014, Regarding Main Control Room Boundary Door Left Open Leading to a Loss of Safety Function2017-12-20020 December 2017 Regarding Main Control Room Boundary Door Left Open Leading to a Loss of Safety Function 05000390/LER-1917-013, Regarding Incorrectly Adjusted Auxiliary Building Gas Treatment System Damper Leads to a Condition Prohibited by Technical Specifications2017-11-0606 November 2017 Regarding Incorrectly Adjusted Auxiliary Building Gas Treatment System Damper Leads to a Condition Prohibited by Technical Specifications 05000390/LER-1917-011, Regarding Failure to Enter Technical Specification 3.6.3 for Containment Lsolation Valve2017-10-23023 October 2017 Regarding Failure to Enter Technical Specification 3.6.3 for Containment Lsolation Valve 05000390/LER-1917-012, Regarding Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications2017-10-23023 October 2017 Regarding Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications 05000390/LER-1917-010, Regarding Actuation of Turbine Driven Auxiliary Feedwater Pump Due to Loss of 6.9kV Shutdown Board2017-10-10010 October 2017 Regarding Actuation of Turbine Driven Auxiliary Feedwater Pump Due to Loss of 6.9kV Shutdown Board 05000391/LER-1917-004, Regarding Manual Reactor Trip Due to Inoperable Rod Position Indication2017-09-25025 September 2017 Regarding Manual Reactor Trip Due to Inoperable Rod Position Indication 05000390/LER-1917-008, Regarding Shield Building Inoperability and Potential Loss of Safety Function Resulting from Spurious Equipment Operation2017-08-14014 August 2017 Regarding Shield Building Inoperability and Potential Loss of Safety Function Resulting from Spurious Equipment Operation 05000390/LER-1917-007, Regarding Multiple Unreported Potential Loss of Safety Function Events Associated with Inoperable Single Train Systems Due to Misinterpretation of Reporting Guidance2017-08-0808 August 2017 Regarding Multiple Unreported Potential Loss of Safety Function Events Associated with Inoperable Single Train Systems Due to Misinterpretation of Reporting Guidance 05000390/LER-1917-006, Regarding Structural Degradation of 161 Kv Line Pole Leads to a Condition Prohibited by Technical Specifications2017-07-31031 July 2017 Regarding Structural Degradation of 161 Kv Line Pole Leads to a Condition Prohibited by Technical Specifications 05000390/LER-1917-005, Re Isolation of the 1B-B Safety Injection Pump Leads to a Condition Prohibited by Technical Specifications2017-07-10010 July 2017 Re Isolation of the 1B-B Safety Injection Pump Leads to a Condition Prohibited by Technical Specifications 2025-01-21
[Table view] |
text
Tennessee Valley Authority, Post Office Box 2000, Spring City, Tennessee 37381-2000 William R. Lagergren, Jr Site Vice President, Watts Bar Nuclear Plant SFP 1 I )no2 U.S. Nuclear Regulatory Commission 10 CFR 50.73 ATTN:
Document Control Desk Washington, D.C. 20555 Gentlemen:
TENNESSEE VALLEY AUTHORITY -
WATTS BAR NUCLEAR PLANT (WBN)
UNIT 1 -
DOCKET NO. 50-390 -
FACILITY OPERATING LICENSE NPF-90 LICENSEE EVENT REPORT (LER) 50-390/2002-003 The enclosed report provides details of an automatic turbine/reactor trip which occurred on July 13, 2002.
This event resulted from actuation of a Main Transformer differential relay due to a grounded conductor (splice) for a current transformer.
The plant trip and subsequent actuation of an engineered safety feature is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A).
If you should have any questions, please call P. L. Pace at (423) 365-1824.
Sincerely, W. R. Lager 4<n Enclosure cc (Enclosure):
Pnnted nwCydepaper
U.S. Nuclear Regulatory Commission Page 2 SEP 1 1 2002 cc (Enclosures):
NRC Resident Inspector Watts Bar Nuclear Plant 1260 Nuclear Plant Road Spring City, Tennessee 37381 Mr. L. Mark Padovan, Senior Project Manager U.S. Nuclear Regulatory Commission MS 08G9 One White Flint North 11555 Rockville Pike Rockville, Maryland 20852-2738 U.S. Nuclear Regulatory Commission Region II Sam Nunn Atlanta Federal Center 61 Forsyth St., SW, Suite 23T85 Atlanta, Georgia 30303 Institute of Nuclear Power Operations 700 Galleria Parkway, NW Atlanta, Georgia 30339-5957
NRC FORM 366 U.S. NUCLEAR REGULATORY APPROVED BY OMB NO. 3150-0104 EXPIRES 7131/2004 (7.2001 COMMISSION Estimated
- the NRC may not digits/characters for each block) conduct or sponsor, and a person is not required to respond to the
- 1. FACILITY NAME
][2. DOCKET NUMBER lPAGE (31 Watts Bar Nuclear Plant (WBN) UNIT 1 05000 - 390 1 OF 7
- 4. TITLE Automatic Turbine/Reactor Trip Due To Main Transformer Protection Circuit Ground Due To Inadequate Cable Splice
- 5. EVENT DATE
- 6. LER NUMBER
- 7. REPORT DATE
- 8. OTHER FACILITIES INVOLVED MONTH DAY YEAR YEAR SEQUENTIAL REVISION MONTH DAY YEAR FACILITY NAME DOCKET NUMBER NUMBER NUMBER NA 05000 07 13 2002 2002 003 00 09 11 2002 FACILITY NAME DOCKET NUMBER NA l
05000
- 9. OPERATING 1
- 11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR§: (Check one or more)
MODE
= 20.2201b) 20.2203(a)(3)(ii) 50 73(a)(2)(ii)(B)
=50.73(a)(2)(ix)(A)
- 10. POWER 100 20.2201(d) 20.2203(a)(4) 50.73(a)(2)(iii)
_50.73(a)(2)(x)
LEVEL 20.2203(a)(1) 50.36(c)(1)1i)(A)
X 50.73(a)(2)(Iv)(A) 73.711a)(4) 20.2203(a)(2)(i) 50 361)(1)(1A)
=
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HER (Voluntary)
S<tt5_+g Rg 20.2203(a)(2)(ml) 50.46(a)(3)(n1) 150.73(a)(2)(v)(C)
SpecltifyinAbstract below l
20.2203(a)(2)(iv)
=
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_ 50 73(a)(2)(vi)()l
=3 t^R~lqiue.9wL20 2203(a)(3)(i 0 73(a)(2)60l(A) _5 3a()vl)B
- 12. LICENSEE CONTACT FOR THIS LER NAME TELEPHONE NUMBER (Include Area Code)
Charles Touchstone, Licensing Engineer l
(423) 365-3820CAUSE SYSTEM COMPONENT MANUFACTURER EPORTABLE l
CAUSE
YSTEM COMPONENT MANUFACTURER REPORTABLE TOR EPINEX 1 ATTR O
EPORBL
- 14. SUPPLEMENTAL REPORT EXPECTED
- 15. EXPECTED MONTH DAY YEAR YES (If yes, complete EXPECTED SUBMISSION DATE).
X INO SUBMISSION DATE Abstract (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines)
On July 13, 2002, at approximately 1622 EDT, while the plant was in Mode 1, at 100% power, Watts Bar Unit 1 experienced an automatic turbine/reactor trip when a C-Phase Main Transformer differential relay actuated This occurred because a bolted cable splice associated with a C-phase current transformer (CT) came into contact with the CT junction box; thereby shorting the differential relay protection circuit to ground.
The apparent factors contributing to this short circuit condition include temperature, cable splice material, vibration, and configuration of the splice inside the junction box.
All control rods inserted properly in response to the reactor trip. The Auxiliary Feedwater (AFW) System actuated in response to the trip, as designed. Plant response was in accordance with design with no complications. Operations shift personnel performance was in accordance with applicable procedures.
Subject to confirmatory laboratory testing, the root cause of this event was determined to be inadequate work instructions that allowed lower temperature rated tape to be used on a cable replacement and/or inadequate application of splice material. Corrective actions include revision and training on TVA's engineering and maintenance procedures for high temperature jacketing material, laboratory analysis of damaged splices, and reinspection and taping of similar vulnerable cable splices.
NRC FORM 366 (7-2001)U.S. NUCLEAR REGULATORY COMMISSION (4-951 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET LER NUMBER (6)
PAGE (3)
YEYEAR SEQUENTIAL l REVISION Watts Bar Nuclear Plant (WBN) Unit 1 05000390 NUMBER 2 OF 7
__ I1 2002--
003 00 TEXT lIf more space Is required, use additional copies of NRC Form 366A) (17)
I.
PLANT CONDITION(S)
Watts Bar Unit 1 was in power operation at approximately 100 percent reactor power
11. DESCRIPTION OF EVENT
A. Event:
While operating at 1 00% power, Watts Bar Unit 1 experienced an automatic turbine/reactor trip at 1622:24 EDT on July 13, 2002, when a C-Phase Main Transformer differential relay (Energy Industry Identification System (EIIS) code 87) actuated. This occurred because the metal portion of a bolted splice associated with a C-phase current transformer (CT, EIIS code XCT) came into contact with the CT junction box; thereby shorting the differential relay protection circuit to ground causing actuation of the main transformer protection function. The apparent factors contributing to this short circuit condition include temperature, cable splice material, vibration, and configuration of the splice inside the junction box. Problem Evaluation Report (PER) 02-009532-000 was initiated to document this event in the TVA Corrective Action Program.
All control rods inserted properly in response to the reactor trip. The Auxiliary Feedwater (AFW)
System (EIIS code BA) actuated in response to the trip, as designed.
During the February/March 2002 refueling outage for Watts Bar Unit 1, the Main Generator bushing box was disassembled to repair hydrogen leaks identified at the end of the previous refueling outage.
While performing this activity, installed cables from the manufacturer's junction box to the related current transformers were observed to be damaged, apparently due to heat. The installed cabling was rated for 75 degrees C (167 degrees F). A Work Order (WO) was initiated to replace the damaged cable sections with higher temperature rated cables (250 degrees C/482 degrees F). The WO specified bolted splices configured with Scotch 70 tape as an insulating material and Scotch 33+
tape as a jacketing material. It was not recognized that the temperature rating of the Scotch 33+ tape was questionable for the operating environmental conditions within the junction box. As is typical in cable installation, sufficient pigtail and field cable lengths were retained to facilitate any future re-splicing. In order to store this excess length of cable inside the junction box, it was necessary to train (coil) the cable 180 degrees from entry to the junction box. The as-left configuration of the splice involved in this event had its tip (bolted end) lying against a wall of the junction box at approximately a 45 degree angle, and under some pressure. The applicable TVA Engineering Specification G-38 requires that cables be supported so there is no mechanical load on the splice. On July 13, 2002, after about four months of full power operation, a fault occurred at the point where the splice was resting against the junction box wall. After re-taping the splice and installing tie wraps to minimize contact with the junction box wall, the plant was restarted and returned to full power operation.
The purpose of Scotch 33+ tape is to provide mechanical protection for the Scotch 70 tape. Scotch 70 tape is a high temperature insulating material. Per G-38, 90 degrees C (194 degrees F) is the temperature rating of Scotch 33+ tape, a PVC tape (thermoplastic material). Based on 3M tapeU.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL l REVISION Watts Bar Nuclear Plant (WBN) Unit 1 05000390 NUMBER l
3 OF 7 2002--
003 00 TEXT (if more space is required, use additional copies of NRC Form 366A) (171 vendor documentation, the actual rating of Scotch 33+ tape is 105 degrees C (220 degrees F).
Nevertheless, this type of material will gradually soften at elevated temperatures. G-38 and plant instructions do not permit the use of tape where environmental temperatures exceed the tape temperature rating, however, the effect of the operating temperatures on the tape was not realized at the time of the cable replacement and the immediate repairs after the trip. Therefore, during the event investigation, and after attaining normal full power conditions, thermocouples and infrared thermography were used to measure temperatures at this and related junction boxes. The highest recorded ambient temperature was 210 degrees F. Even though the temperature rating of 220 degrees F was not exceeded, the temperature rating for Scotch 33+ tape is considered the most significant contributing factor in this event. In other words, the use of this tape marginally within its maximum temperature limit, may not in itself always result in a fault. However, as a result of other environmental conditions, the conductor portion of the splice shorted to the junction box. Once the protective cover provided by the Scotch 33+ tape was degraded (softened at higher temperature), the Scotch 70 tape became susceptible to cut-through by the lugging material, given the vibration and the physical loading. Since the actual splice was not removed for analysis (an issue being addressed separately), it will be removed at the next available opportunity and sent for laboratory analysis to validate the above assumptions.
B. Inoperable Structures, Components, or SVstems that Contributed to the Event:
There were no structures, components, or systems inoperable at the start of the event that contributed to the event.
C. Dates and Approximate Times of Maior Occurrences:
DATE i
4 trACTION M
P 4
1/14/1999 Engineering issues generic substitution data sheet (GSDS) for high temperature cable based on Design Change EDC 50105.
2/28/2002 Maintenance identifies cable damage due to high temperature environment.
2/28/2002 Actual operating temperature is unknown.
2/28/2002 Maintenance initiates PER 02-002480 to document condition.
2/28/2002 Maintenance initiates WO 02-002582-000 to replace cable.
3/12/2002 Cable is replaced with high temperature cable.
3/12/2002 Cables are spliced with Scotch 70 and Scotch 33+ as jacketing material.
7/13/2002 Cable splice fails causing spurious operation of the generator differential relay.
7/13/2002 Turbine trip/reactor trip. (1622 EDT)
D. Other Systems or Secondary Functions Affected
There were no other plant systems or secondary functions directly affected by the subject event.U.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISION Watts Bar Nuclear Plant (WBN) Unit 1 05000390 NUMBER 4 OF 7 l
2002--
003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) 1171 E.
Method of Discovery
The turbine/reactor trip was an automatic response to actuation of the C-Phase Main Transformer differential relay protection circuit.
F. Operator Actions
Operations personnel correctly responded to the reactor trip in accordance with Emergency Procedure E-0, "Reactor Trip or Safety Injection." The involved personnel transitioned when required into the appropriate emergency and abnormal procedures to properly stabilize the unit in Mode 3.
G. SafetV System Responses:
The Watts Bar Unit 1 reactor automatically tripped following a turbine trip caused by actuation of the C-Phase Main Transformer differential relay. All control rods inserted properly and the Auxiliary Feedwater (AFW) System started, as required, in response to the reactor trip. The AFW system was the only engineered safety feature (ESF) equipment required to respond to this event. The AFW System was subsequently placed in manual control by procedure to reduce feedwater flow to control plant cooldown.
11. CAUSE OF THE EVENT
A. Immediate Cause:
The automatic turbine/reactor trip resulted from actuation of a C-Phase Main Transformer differential relay protection circuit. The metal portion of a bolted cable splice associated with the C-phase current transformer (CT) came into contact with the CT junction box; thereby shorting the differential protection relay circuit to ground causing actuation of the differential relay. The direct cause of the equipment failure was determined to be a combination of several factors. These factors are temperature, cable splice material (Scotch 33+), vibration, and configuration of the splice inside the junction box adjacent to the main generator current transformer.
B. Root Cause:
Subject to confirmatory laboratory testing, the root cause of this event was determined to be inadequate work instructions that allowed lower temperature rated tape to be used on a cable replacement splice because the operating environmental conditions within the junction box were unknown, and/or inadequate application of splice material. Because conclusive information was not collected during the post-trip recovery activities, the root cause of this event cannot be verified until an outage occurs that permits additional inspection of the affected junction box.U.S. NUCLEAR REGULATORY COMMISSION (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISION Watts Bar Nuclear Plant (WBN) Unit 1 05000390 NUMBER 5 OF 7 l
2002--
003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (171 C. Contributing Factor:
There was no contributing factor for this event.
IV. ASSESSMENT OF SAFETY CONSEQUENCES
The plant experienced a loss of load event. The main generator's C phase main transformer differential relay tripped. This resulted in a turbine trip. A direct reactor trip occurred as a result of the turbine trip.
The main condenser steam dump valves opened per design to accommodate the excess steam generation and the pressurizer pressure control system functioned properly. As a result, reactor coolant temperature and pressure did not increase significantly.
This event is compared to the "Loss of External Load and/or Turbine Trip" event (Ref: FSAR Section 15.2.7). The complete loss of load/turbine trip from full power is examined primarily to show the adequacy of the pressure relieving devices and also to demonstrate that the Reactor Protection System (RPS, EIIS code JG) provides protection against departure from nucleate boiling (DNB). The design and licensing basis analysis does not credit operation of the steam dump system or steam generator power-operated relief valves (PORVs). The sudden reduction in steam flow results in an increase in pressure and temperature in the steam generator shell. As a result, the heat transfer rate in the steam generator is reduced, causing the reactor coolant temperature to rise, which causes coolant expansion, pressurizer insurge, and Reactor Coolant System (RCS, EIIS code AB) pressure rise. Unless the transient RCS response to the loss of external electrical load and/or turbine trip event is terminated by manual or automatic action, the resultant reactor coolant temperature rise could eventually result in DNB and/or a challenge to the integrity of the Reactor Coolant Pressure Boundary (RCPB) or the Main Steam System Pressure Boundary. To avert the possible damage that might otherwise result from this event, the RPS is designed to automatically terminate any such transient before the DNB ratio (DNBR) falls below the safety analysis limit value and before the peak pressures exceed the values at which the integrity of the pressure boundaries would be jeopardized.
Unlike the design and licensing basis analysis, in the actual event, the main condenser steam dump valves opened per design and the pressurizer pressure control system functioned properly. As a result it was not necessary for the steam generator PORVs to operate. Pressurizer level did not increase and pressurizer pressure did not increase in a manner that would challenge the pressurizer PORVs or safety valves. Also in the actual event, RCS temperature did not rise; but rather dropped to an average temperature of 559 degrees F. Since a direct reactor trip occurred as a result of the turbine trip, it was not necessary for the RPS to initiate a reactor trip by the RPS trip signals of OTAT, High Pressurizer Pressure, High Pressurizer Water Level, or Low-Low Steam Generator Water Level. Therefore the DNB safety analysis limit value was never challenged.
In summary, the FSAR critical parameter plots of pressurizer pressure, pressurizer water volume, RCS inlet and average temperature, and steam generator pressure bound the values that actually occurred during the actual event. DNBR was never challenged during the event because no increasing RCS temperature excursions occurred. Therefore, the actual plant response for this event falls within the bounds of the design basis response.U.S. NUCLEAR REGULATORY COMMISSION (4.95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET LER NUMBER (6) lPAGE (3)
YEAR l SEQUENTIAL REVISION Watts Bar Nuclear Plant (WBN) Unit 1 05000390 NUMBER 6 OF 7 I 2002--
003 00 TEXT (it more space is required, use additional copies of NRC Form 366A) 117)
V. CORRECTIVE ACTIONS
A. Immediate Corrective Actions:
Work Order WO 02-009536-000 was initiated to perform troubleshooting. Based on troubleshooting, 3 cable splices were taped over, damaged cable was repaired using Scotch 70 and 33+, and a protective material was placed where the cables enter the junction boxes. Additionally the cables splices were wrapped to minimize contact with the junction box walls.
The extent of condition was determined to be limited to 13 cables that contain a splice in the same environment that caused the initial cable damage. These cables, including the damaged cable/splice (Cable 1G20), are all associated with the generator CTs. The corrective actions discussed above for the troubleshooting WO 02-009536-000 include these 13 cables/splices. At the time of repair, it was not recognized that the lower temperature rated tape was potentially inappropriate for the environmental conditions within the junction box. However, the corrective actions performed should provide sufficient protection to prevent the reoccurrence of a cable/splice fault as an interim measure.
Longer-term corrective actions for the splices are discussed in Section V.B.
B. Corrective Actions to Prevent Recurrence:
The following actions are tracked under TVA's corrective action program and therefore, are not considered to be regulatory commitments:
- 1. Issued exception to G-38 to allow the use of high temperature jacketing tape (Scotch 69) in turbine building areas at WBN.
- 2.
Provided a Lessons Learned meeting with personnel responsible for splicing cables on the root causes of this event.
- 3.
Revise GSDS 3087 to require use of the high temperature jacketing material.
- 4.
Revise General Engineering Specification G-38 to provide for a high temperature jacketing material to use on splices located in high temperature environments.
- 5. Revise and conduct training on applicable Maintenance Instructions to include the use of Scotch 70 and the high temperature jacketing material required by G-38.
- 6.
Inspect/Re-work splices identified by the extent of condition with new high temperature jacketing material. All splices associated with this event must be preserved for further analysis. This action will be completed the next time the generator is offline.
- 7.
Send cable splices (identified in CA-6) that were identified as damaged to the Central Laboratory for testing to determine the cause of the splice damage.U.S. NUCLEAR REGULATORY COMMISSItON (4-95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISION Watts Bar Nuclear Plant (WBN) Unit 1 05000390 NUMBER 7 OF 7 l
2002--
003 00 TEXT (If more space is required, use additional copies of NRC Form 366A) (171
VI. ADDITIONAL INFORMATION
A.
Failed Components:
There were no additional failed components from those discussed above.
B.
Previous LERs on Similar Events:
A review was performed of previous WBN LERs for any similar events. WBN has not experienced any prior turbine/reactor trips due to ground faults involving cable/splice problems. A previous similar plant trip occurred during 1997 when the main generator circuit breaker opened due to problems with the A phase main transformer high side potential device. However, since no anomalies have been identified with the plant response to the current event, no further comparison of these events is necessary.
C.
Additional Information
None D.
Safety System Functional Failure Consideration:
The subject cable/splice failure is not safety significant. The 13 cables discussed in Section V.A are not safety related. Therefore, this event does not constitute a safety system functional failure in accordance with NEI 99-02 E.
Loss Of Normal Heat Removal Consideration:
This event did not result in loss of normal heat removal capability.
VII.
COMMITMENTS
None
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05000390/LER-2002-001, Re Loss of RHR Flow Path in Mode 6 with Reduced RCS Level | Re Loss of RHR Flow Path in Mode 6 with Reduced RCS Level | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | 05000390/LER-2002-002, Re Missing Auxiliary Feedwater Guard Pipe Inspection Covers | Re Missing Auxiliary Feedwater Guard Pipe Inspection Covers | | 05000390/LER-2002-003, Automatic Turbine/Reactor Trip Due to Main Transformer Protection Circuit Ground Due to Inadequate Cable Splice | Automatic Turbine/Reactor Trip Due to Main Transformer Protection Circuit Ground Due to Inadequate Cable Splice | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2) | 05000390/LER-2002-004, Partial Loss of Offsite Power | Partial Loss of Offsite Power | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000390/LER-2002-005, For Watts Bar Nuclear Plant (WBN) Unit 1, Loss of Offsite Power Due to a Fire at the Watts Bar Hydroelectric Generating Plant (Wbh) | For Watts Bar Nuclear Plant (WBN) Unit 1, Loss of Offsite Power Due to a Fire at the Watts Bar Hydroelectric Generating Plant (Wbh) | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(i) |
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