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Category:Annual Operating Report
MONTHYEARL-2022-070, 2021 Annual Radiological Environmental Operating Report2022-05-0303 May 2022 2021 Annual Radiological Environmental Operating Report L-2022-031, Annual Radioactive Effluent Release Report2022-03-0101 March 2022 Annual Radioactive Effluent Release Report L-2021-066, CFR 50.46 Annual Reporting of Changes to, or Errors in Emergency Core Cooling System Models or Applications2021-04-14014 April 2021 CFR 50.46 Annual Reporting of Changes to, or Errors in Emergency Core Cooling System Models or Applications L-2020-041, 10 CFR 50.46 Annual Reporting of Changes to, or Errors in Emergency Core Cooling System Models or Applications2020-04-14014 April 2020 10 CFR 50.46 Annual Reporting of Changes to, or Errors in Emergency Core Cooling System Models or Applications L-2019-057, Cf~ 50.46 Annual Reporting of Changes to, or Errors in Emergency Core Cooling System Models or Applications2019-03-19019 March 2019 Cf~ 50.46 Annual Reporting of Changes to, or Errors in Emergency Core Cooling System Models or Applications L-2019-017, Submittal of 2018 Annual Radioactive Effluent Release Report2019-02-27027 February 2019 Submittal of 2018 Annual Radioactive Effluent Release Report L-2019-031, Enclosure 3: Turkey Point Units 3 and 4, 2018 Annual Remediation/Restoration Report2018-12-31031 December 2018 Enclosure 3: Turkey Point Units 3 and 4, 2018 Annual Remediation/Restoration Report L-2018-100, Submittal of 10 CFR 50.59(d)(2) Summary Report2018-04-25025 April 2018 Submittal of 10 CFR 50.59(d)(2) Summary Report L-2018-063, CFR 50.46 Annual Reporting and 30-day Notification of Changes or Errors in Emergency Core Cooling System Models or Applications2018-03-26026 March 2018 CFR 50.46 Annual Reporting and 30-day Notification of Changes or Errors in Emergency Core Cooling System Models or Applications L-2017-030, Submittal of 2016 Annual Report of Reactor Coolant Specific Activity Limits2017-02-28028 February 2017 Submittal of 2016 Annual Report of Reactor Coolant Specific Activity Limits L-2017-029, Submittal of 2016 Annual Radioactive Effluent Release Report2017-02-28028 February 2017 Submittal of 2016 Annual Radioactive Effluent Release Report L-2016-080, Transmittal of 10 CFR 50.46, Acceptance Criteria for Emergency Core Cooling Systems in Light Water Nuclear Power Reactors - 2015 Annual Report2016-04-0808 April 2016 Transmittal of 10 CFR 50.46, Acceptance Criteria for Emergency Core Cooling Systems in Light Water Nuclear Power Reactors - 2015 Annual Report L-2012-159, Submittal of 2012 Annual Radiological Environmental Operating Report2013-05-14014 May 2013 Submittal of 2012 Annual Radiological Environmental Operating Report L-2012-189, Annual Radiological Environmental Operating Report2012-05-0202 May 2012 Annual Radiological Environmental Operating Report L-2012-204, CFR 50.46, Acceptance Criteria for Emergency Core Cooling Systems in Light Water Nuclear Power Reactors - 2011 Annual Report2012-04-30030 April 2012 CFR 50.46, Acceptance Criteria for Emergency Core Cooling Systems in Light Water Nuclear Power Reactors - 2011 Annual Report L-2011-160, 2010 Annual Radiological Environmental Operating Report2011-05-0909 May 2011 2010 Annual Radiological Environmental Operating Report L-2010-031, Re-Submittal of the 2009 Annual Radioactive Effluent Release Report2010-12-15015 December 2010 Re-Submittal of the 2009 Annual Radioactive Effluent Release Report L-2010-077, 2009 Annual Radiological Environmental Operating Report2010-05-14014 May 2010 2009 Annual Radiological Environmental Operating Report L-2010-074, 10 CFR 50.46, Acceptance Criteria for Emergency Core Cooling Systems in Light Water Nuclear Power Reactors, 2009 Annual Report2010-04-15015 April 2010 10 CFR 50.46, Acceptance Criteria for Emergency Core Cooling Systems in Light Water Nuclear Power Reactors, 2009 Annual Report L-2010-031, Turkey Point, Units 3 & 4, 2009 Annual Radioactive Effluent Release Report2010-02-26026 February 2010 Turkey Point, Units 3 & 4, 2009 Annual Radioactive Effluent Release Report ML1006106212010-02-26026 February 2010 2009 Annual Radioactive Effluent Release Report L-2010-030, Annual Report of Reactor Coolant Specific Activity Limits2010-02-22022 February 2010 Annual Report of Reactor Coolant Specific Activity Limits L-2009-044, Annual Radioactive Effluent Release Report2009-02-26026 February 2009 Annual Radioactive Effluent Release Report L-2008-122, CFR 50.46, Acceptance Criteria for Emergency Core Cooling Systems in Light Water Nuclear Power Reactors - 2007 Annual Report2008-05-28028 May 2008 CFR 50.46, Acceptance Criteria for Emergency Core Cooling Systems in Light Water Nuclear Power Reactors - 2007 Annual Report L-2008-037, Annual Report of Reactor Coolant Specific Activity Limits2008-02-22022 February 2008 Annual Report of Reactor Coolant Specific Activity Limits L-2007-026, Annual Report of Reactor Coolant Specific Activity Limits for 20062007-02-27027 February 2007 Annual Report of Reactor Coolant Specific Activity Limits for 2006 L-2006-107, 2005 Annual Radiological Environmental Operating Report2006-05-15015 May 2006 2005 Annual Radiological Environmental Operating Report L-2006-090, Annual Radioactive Effluent Release Report2006-03-31031 March 2006 Annual Radioactive Effluent Release Report L-2004-116, CFR 50.46, Acceptance Criteria for Emergency Core Cooling Systems in Light Water Nuclear Power Reactors - Annual Report for 20032004-05-26026 May 2004 CFR 50.46, Acceptance Criteria for Emergency Core Cooling Systems in Light Water Nuclear Power Reactors - Annual Report for 2003 L-2004-108, CFR 50.59 Report2004-05-0303 May 2004 CFR 50.59 Report L-2004-051, Annual Reports of Occupational Exposure and Reactor Coolant Specific Activity Limits2004-02-24024 February 2004 Annual Reports of Occupational Exposure and Reactor Coolant Specific Activity Limits L-2003-298, Plants - Submittal of Price Anderson Guarantees/Annual Financial Report2003-12-26026 December 2003 Plants - Submittal of Price Anderson Guarantees/Annual Financial Report L-2003-112, Annual Radiological Environmental Operating Report2003-05-0808 May 2003 Annual Radiological Environmental Operating Report ML18228A4461978-03-0303 March 1978 03/03/1978 Letter Attached 1977 Turkey Point Annual Operating Report ML18227D4121978-03-0303 March 1978 Transmitting 1977 Turkey Point Annual Operating Report 2022-05-03
[Table view] Category:Letter type:L
MONTHYEARL-2024-010, Point Units 3 and 4, Seabrook, Duane Arnold, and Point Beach Units 1 and 2, Nuclear Property Insurance - 10 CFR 50.54(w)(3)2024-01-25025 January 2024 Point Units 3 and 4, Seabrook, Duane Arnold, and Point Beach Units 1 and 2, Nuclear Property Insurance - 10 CFR 50.54(w)(3) L-2024-007, Inservice Inspection Program Owner'S Activity Report (OAR-1)2024-01-18018 January 2024 Inservice Inspection Program Owner'S Activity Report (OAR-1) L-2023-173, Quality Assurance Topical Report (FPL-1) Revision 30 Update2023-12-15015 December 2023 Quality Assurance Topical Report (FPL-1) Revision 30 Update L-2023-166, Turkey Points Units 3 and 4, Correction to the 2022 Annual Radioactive Effluent Release Report2023-12-0606 December 2023 Turkey Points Units 3 and 4, Correction to the 2022 Annual Radioactive Effluent Release Report L-2023-172, Supplement to Exemption Request Regarding Enhanced Weapons. Firearms Background Checks. and Security Event Notifications Final Rule2023-11-29029 November 2023 Supplement to Exemption Request Regarding Enhanced Weapons. Firearms Background Checks. and Security Event Notifications Final Rule L-2023-155, Supplement to Response to Request for Additional Information, Revised NextEra Common Emergency Plan, and Revised Site-Specific Emergency Plan Annexes Regarding License Amendment Request for Common Emergency Plan Consistent with NUREG-06542023-11-28028 November 2023 Supplement to Response to Request for Additional Information, Revised NextEra Common Emergency Plan, and Revised Site-Specific Emergency Plan Annexes Regarding License Amendment Request for Common Emergency Plan Consistent with NUREG-0654, L-2023-146, Part 73 Exemption Request Regarding Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Final Rule2023-11-16016 November 2023 Part 73 Exemption Request Regarding Enhanced Weapons, Firearms Background Checks, and Security Event Notifications Final Rule L-2023-078, License Amendment Request 278, Incorporate Advanced Fuel Products, Extend Surveillance Intervals and 10 CFR 50.46 Exemption Request to Facilitate Transition to 24-Month Fuel Cycles2023-11-15015 November 2023 License Amendment Request 278, Incorporate Advanced Fuel Products, Extend Surveillance Intervals and 10 CFR 50.46 Exemption Request to Facilitate Transition to 24-Month Fuel Cycles L-2023-077, License Amendment Request 277 Updated Spent Fuel Pool Criticality Analysis2023-10-11011 October 2023 License Amendment Request 277 Updated Spent Fuel Pool Criticality Analysis L-2023-110, Response to Requests for Additional Information Regarding License Amendment Request No. 276, Revise Fire Protection Program in Support of Reactor Coolant Pump Seal Replacement Project2023-08-25025 August 2023 Response to Requests for Additional Information Regarding License Amendment Request No. 276, Revise Fire Protection Program in Support of Reactor Coolant Pump Seal Replacement Project L-2023-115, Inservice Inspection Program Owner'S Activity Report (OAR-1)2023-08-21021 August 2023 Inservice Inspection Program Owner'S Activity Report (OAR-1) L-2023-114, Proposed Turkey Point Units 6 and 7; Seabrook Station; Point Beach Units 1 and 2 - Official Service List Update2023-08-17017 August 2023 Proposed Turkey Point Units 6 and 7; Seabrook Station; Point Beach Units 1 and 2 - Official Service List Update L-2023-098, and Point Beach Units 1 and 2 - Response to Request for Additional Information Regarding License Amendment Request for Common Emergency Plan Consistent with NUREG-0654, Revision 22023-08-0707 August 2023 and Point Beach Units 1 and 2 - Response to Request for Additional Information Regarding License Amendment Request for Common Emergency Plan Consistent with NUREG-0654, Revision 2 L-2023-094, Response to Requests for Additional Information Regarding License Amendment Request No. 276, Revise Fire Protection Program in Support of Reactor Coolant Pump Seal Replacement Project2023-07-27027 July 2023 Response to Requests for Additional Information Regarding License Amendment Request No. 276, Revise Fire Protection Program in Support of Reactor Coolant Pump Seal Replacement Project L-2023-087, Florida Power & Light/Nextera Energy, Results of the Safety Culture Program Effectiveness Review, March 20, 2023 (ADAMS Accession No. ML22340A452)2023-06-29029 June 2023 Florida Power & Light/Nextera Energy, Results of the Safety Culture Program Effectiveness Review, March 20, 2023 (ADAMS Accession No. ML22340A452) L-2023-086, Request Temporary Suspension of Turkey Point License Amendment Request 274, Reactor Protection System, Engineered Safety Features Actuation System, and Nuclear Instrumentation.2023-06-28028 June 2023 Request Temporary Suspension of Turkey Point License Amendment Request 274, Reactor Protection System, Engineered Safety Features Actuation System, and Nuclear Instrumentation. L-2023-074, Addendum to 2021 Decommissioning Funding Status Reports / Independent Spent Fuel Storage Installation Ctsfsi) Financial Assurance Update2023-06-0202 June 2023 Addendum to 2021 Decommissioning Funding Status Reports / Independent Spent Fuel Storage Installation Ctsfsi) Financial Assurance Update L-2023-069, Response to Requests for Additional Information Regarding License Amendment Request No. 276, Revise Fire Protection Program in Support of Reactor Coolant Pump Seal Replacement Project2023-05-31031 May 2023 Response to Requests for Additional Information Regarding License Amendment Request No. 276, Revise Fire Protection Program in Support of Reactor Coolant Pump Seal Replacement Project L-2023-072, Preparation and Scheduling of Operator Licensing Examinations2023-05-22022 May 2023 Preparation and Scheduling of Operator Licensing Examinations L-2023-071, NextEra Energy Quality Assurance Topical Report (FPL-1) Revision 29 and Florida Power and Light Company Quality Assurance Program Description for 10 CFR Part 52 Licenses (FPL-2) Revision 11, Annual Submittal2023-05-22022 May 2023 NextEra Energy Quality Assurance Topical Report (FPL-1) Revision 29 and Florida Power and Light Company Quality Assurance Program Description for 10 CFR Part 52 Licenses (FPL-2) Revision 11, Annual Submittal L-2023-061, 2022 Annual Radiological Environmental Operating Report2023-05-12012 May 2023 2022 Annual Radiological Environmental Operating Report L-2023-062, Cycle 33 Core Operating Limits Report2023-04-27027 April 2023 Cycle 33 Core Operating Limits Report L-2023-060, Radiological Emergency Plan, Revision 752023-04-26026 April 2023 Radiological Emergency Plan, Revision 75 L-2023-054, Submittal of Periodic Reports2023-04-12012 April 2023 Submittal of Periodic Reports L-2023-049, Correction to U4R33 Steam Generator Tube Inspection Report2023-03-30030 March 2023 Correction to U4R33 Steam Generator Tube Inspection Report L-2023-021, Units, 1 and 2, Turkey Point, Units 3 and 4, Seabrook Station and Point Beach, Units 1 and 2 - Decommissioning Funding Status Reports / Independent Spent Fuel Storage Installation (ISFSI) Financial Assurance Update2023-03-28028 March 2023 Units, 1 and 2, Turkey Point, Units 3 and 4, Seabrook Station and Point Beach, Units 1 and 2 - Decommissioning Funding Status Reports / Independent Spent Fuel Storage Installation (ISFSI) Financial Assurance Update L-2023-028, and Point Beach Units 1 and 2, 10 CFR 50.46 Annual Reporting of Changes to, or Errors in Emergency Core Cooling System Models or Applications2023-03-27027 March 2023 and Point Beach Units 1 and 2, 10 CFR 50.46 Annual Reporting of Changes to, or Errors in Emergency Core Cooling System Models or Applications L-2023-025, Fleet Relief Request (Frr) 23-01, Proposed Alternative to ASME Section XI Authorizing Implementation of ASME Code Case N-752-12023-03-15015 March 2023 Fleet Relief Request (Frr) 23-01, Proposed Alternative to ASME Section XI Authorizing Implementation of ASME Code Case N-752-1 L-2023-029, and Point Beach Units 1 and 2 Nuclear Property Insurance - 10 CFR 50.54(w)(3)2023-03-10010 March 2023 and Point Beach Units 1 and 2 Nuclear Property Insurance - 10 CFR 50.54(w)(3) L-2023-040, Response to Requests for Additional Information (Rals) and Requests for Confirmation of Information (Rc Ls) Following Regulatory Audit of Subsequent License Renewal Application2023-03-0303 March 2023 Response to Requests for Additional Information (Rals) and Requests for Confirmation of Information (Rc Ls) Following Regulatory Audit of Subsequent License Renewal Application L-2023-037, Annual Radioactive Effluent Release Report2023-03-0101 March 2023 Annual Radioactive Effluent Release Report L-2023-017, Radiological Emergency Plan Revision 73 and Revision 7 42023-02-17017 February 2023 Radiological Emergency Plan Revision 73 and Revision 7 4 L-2023-010, Supplemental Information Regarding License Amendment Request 274, Reactor Protection System, Engineered Safety Features Actuation System, and Nuclear Instrumentation System Replacement Project - Submittal of RPS / ESFAS / Nis2023-02-10010 February 2023 Supplemental Information Regarding License Amendment Request 274, Reactor Protection System, Engineered Safety Features Actuation System, and Nuclear Instrumentation System Replacement Project - Submittal of RPS / ESFAS / Nis L-2023-004, Supplemental Information Regarding License Amendment Request 274, Reactor Protection System, Engineered Safety Features Actuation System, and Nuclear Instrumentation System Replacement Project - Submittal of Huma Factors Results2023-01-17017 January 2023 Supplemental Information Regarding License Amendment Request 274, Reactor Protection System, Engineered Safety Features Actuation System, and Nuclear Instrumentation System Replacement Project - Submittal of Huma Factors Results L-2022-185, Turkey Points, Units 3 & 4; Seabrook Station; and Point Beach, Units 1 and 2 - Supplement to License Amendment Request for Common Emergency Plan Consistent with NUREG-0654, Revision 22022-12-0909 December 2022 Turkey Points, Units 3 & 4; Seabrook Station; and Point Beach, Units 1 and 2 - Supplement to License Amendment Request for Common Emergency Plan Consistent with NUREG-0654, Revision 2 L-2022-181, Response to Request for Additional Information Regarding License Amendment Request for the Technical Specifications Conversion to NUREG-1431, Revision 52022-12-0101 December 2022 Response to Request for Additional Information Regarding License Amendment Request for the Technical Specifications Conversion to NUREG-1431, Revision 5 L-2022-182, Emergency Response Data System (Eros) Changes2022-11-17017 November 2022 Emergency Response Data System (Eros) Changes L-2022-180, CFR 140.21 Licensee Guarantees of Payment of Deferred Premiums2022-11-0909 November 2022 CFR 140.21 Licensee Guarantees of Payment of Deferred Premiums L-2022-168, and Point Beach Units 1 and 2 - 10 CFR 50.46 - Emergency Core Cooling System LBLOCA 30-Day Report2022-10-26026 October 2022 and Point Beach Units 1 and 2 - 10 CFR 50.46 - Emergency Core Cooling System LBLOCA 30-Day Report L-2022-171, 10 CFR 50.59(d)(2) Summary Report2022-10-20020 October 2022 10 CFR 50.59(d)(2) Summary Report L-2022-167, Submittal of Periodic Reports2022-10-13013 October 2022 Submittal of Periodic Reports L-2022-166, Response to Request for Supplemental Information Regarding License Amendment Request 274, Reactor Protection System, Engineered Safety Features Actuation System, and Nuclear Instrumentation System Replacement2022-10-0505 October 2022 Response to Request for Supplemental Information Regarding License Amendment Request 274, Reactor Protection System, Engineered Safety Features Actuation System, and Nuclear Instrumentation System Replacement L-2022-149, U4R33 Steam Generator Tube Inspection Report2022-10-0404 October 2022 U4R33 Steam Generator Tube Inspection Report L-2022-160, Station,, Point Beach Units 1 and 2, License Amendment Request for Common Emergency Plan Consistent with NUREG-0654, Revision 22022-10-0404 October 2022 Station,, Point Beach Units 1 and 2, License Amendment Request for Common Emergency Plan Consistent with NUREG-0654, Revision 2 L-2022-148, Florida Power & Light Company, Comments on NRC Inspection Procedure (IP) 71111.21 N.03, Commercial Grade Dedication2022-09-16016 September 2022 Florida Power & Light Company, Comments on NRC Inspection Procedure (IP) 71111.21 N.03, Commercial Grade Dedication L-2022-151, Evacuation Time Estimate Study2022-09-15015 September 2022 Evacuation Time Estimate Study L-2022-142, Revised Diversity and Defense-In-Depth Evaluation (D3), Framatome Document No. 51-9324096-0042022-08-19019 August 2022 Revised Diversity and Defense-In-Depth Evaluation (D3), Framatome Document No. 51-9324096-004 L-2022-136, Response to Request for Additional Information Regarding Turkey Point Unit 3 Cycle 32 Steam Generator Tube Inspection Report2022-08-12012 August 2022 Response to Request for Additional Information Regarding Turkey Point Unit 3 Cycle 32 Steam Generator Tube Inspection Report L-2022-109, Inservice Inspection Program - Owner'S Activity Report (OAR-1)2022-06-27027 June 2022 Inservice Inspection Program - Owner'S Activity Report (OAR-1) L-2022-076, Subsequent License Renewal Application - Appendix E Environmental Report Supplement 22022-06-0909 June 2022 Subsequent License Renewal Application - Appendix E Environmental Report Supplement 2 2024-01-25
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0FEB FPL.
2 2 2010 L-2010-030 POWERING TODAY. 10 CFR 50.36 EMPOWERING TOMORROW.,
U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555-0001 Re: Turkey Point Units 3 and 4 Docket Nos. 50-250 and 50-251 2009 Annual Report of Reactor Coolant Specific Activity Limits The 2009 Turkey Point Units 3 and 4 Annual Reactor Coolant System (RCS) Specific Activity Report is submitted herein pursuant to Turkey Point Technical Specification (TS) 6.9.1.2.
For Turkey Point Unit 4: The reactor coolant specific activity limits of less than or equal to 1.0 microcurie per gram Dose Equivalent 1-131 and less than or equal to 100/E-bar microcuries per gram of gross radioactivity defined by Technical Specification 3.4.8.a and 3.4.8.b respectively, were not exceeded for Turkey Point Unit 4 during 2009.
For Turkey Point Unit 3: The reactor coolant specific activity limit of less than or equal to 1.0 microcurie per gram Dose Equivalent 1-131 was exceeded on March 16, 2009 at 0145. The reactor coolant specific activity limit of less than or equal to 100/E-bar microcuries per gram of gross radioactivity was not exceeded during 2009. Per TS 6.9.1.2 reporting requirements, Attachment 1 includes the following information for exceeding TS 3.4.8.a limit of 1.0 microcurie per gram Dose Equivalent 1-131:
(1) Reactor power history starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the first sample in which the limit was exceeded (in graphic and tabular format);
(2) Fuel burnup by core region; (3) Clean-up flow history starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the first sample in which the limit was exceeded; (4) History of degassing operations, if any, starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the first sample in which the limit was exceeded; and (5) The time duration when the specific activity of the primary coolant exceeded 1.0 microcurie per gram Dose Equivalent 1-131.
Should there be any questions regarding this information, please contact Robert J. Tomonto, Licensing Manager, at (305) 246-7327.
Sincerely, Michael Kiley Vice President Turkey Point Nuclear Plant SM cc: Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant an FPL Group company
L-2010-030 Attachment I Turkey Point Unit 3 2009 Annual Report RCS Specific Activity
L'-2010-030 Attachment 1 TURKEY POINT UNIT 3 2009 ANNUAL
SUMMARY
REPORT FOR TS 6.9.1.2 REQUIREMENTS PRIMARY COOLANT SPECIFIC ACTIVITY ANALYSES RESULTS Turkey Point Unit 3 Technical Specification (TS) Primary Coolant 6.9.1.2 Requirements Specific Activity Analyses Results
- 1. Reactor power history starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to During operating Cycle 23, Turkey Point the first sample in which the limit was exceeded Unit 3 experienced a fuel defect. During the (in graphic and tabular format) subsequent refueling outage, in March 2009, the defect was located and removed from the core. During shutdown, the RCS Dose Equivalent Iodine (DEQ) limit specified in TS 3.4.8.a was exceeded. Table 1 provides the reactor power history and the reactor coolant system purification flow rates, on 30 minute intervals, starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to exceeding the TS limit. The araphic format is also provided in Fiaure 1.
- 2. Fuel Burnup by Core Region The fuel burnup by core region is provided in Figure 2. Note that, by design, the Turkey Point Unit 3 core design is rotationally symmetrical.
- 3. Clean-Up flow history starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to The clean-up flow history starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> the first sample in which the limit was prior to the first sample in which the limit exceeded. was exceeded is also provided in Table 1, as well as in Figure 1.
- 4. History of degassing operations, if any, The pressurizer steam space degassing is starting 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> prior to the first sample in performed by aligning the pressurizer steam which the limit was exceeded. space sample line to the Volume Control Tank (VCT) in accordance with station procedures. VCT degassing is accomplished by venting the VCT gas space to the waste gas system. Degassing operations were in progress at the time that the TS limit was exceeded. Specifically, the pressurizer steam space degassing commenced on 3/12/09 at 00:23 in preparation for the refueling outage. VCT venting was performed on 3/15/09 at approximately 16:00, and again multiple times on 3/16/09 to support reactor coolant system degassing operations.
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L-2010-030 Attachment 1 TURKEY POINT UNIT 3 2009 ANNUAL
SUMMARY
REPORT FOR TS 6.9.1.2 REQUIREMENTS PRIMARY COOLANT SPECIFIC ACTIVITY ANALYSES RESULTS Turkey Point Unit 3 Technical Specification (TS) Primary Coolant 6.9.1.2 Requirements Specific Activity Analyses Results
- 5. The time duration when the specific activity of As indicated in Table 2, the TS 3.4.8.a limit the primary coolant exceeded 1.0 microcurie of less than or equal to 1.0 microcurie per per gram DOSE EQUIVALENT 1-131 gram Dose Equivalent (DEQ) 1-131 was exceeded on 3/16/09 at 01:45, and cleaned up to below the TS limit of < 1.0 microcurie per gram on 3/16/09 at 0400, with a confirmation sample on 3/16/09 at 0740.
The time duration when the specific activity of the primary coolant exceeded the TS limit was 2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 15 minutes. The maximum observed value of 1.09 DEQ 1-131 was observed in a sample taken approximately 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and 45 minutes after (the reactor was tripped manually at) the start of the Turkey Point Unit 3 Refueling Outage.
2
L-2010-030 Attachment 1 TABLE I Turkey Point Unit 3 History of Reactor Power and Clean-up Flow Reactor Clean-up Flow History Date & Time Power (gpm)
(%)
3/13/09 21:45 100 108 3/13/09 22:15 100 108 3/13/09 22:45 100 107 3/13/09 23:15 100 108 3/13/09 23:45 100 108 3/14/09 00:15 100 108 3/14/09 00:45 100 108 3/14/09 01:15 100 108 3/14/09 01:45 100 107 3/14/09 02:15 100 108 3/14/09 02:45 100 108 3/14/09 03:15 100 108 3/14/09 03:45 100 108 3/14/09 04:15 100 108 3/14/09 04:45 100 108 3/14/09 05:15 100 108 3/14/09 05:45 100 108 3/14/09 06:15 100 108 3/14/09 06:45 100 108 3/14/09 07:15 100 108 3/14/09 07:45 100 108 3/14/09 08:15 100 108 3/14/09 08:45 100 108 3/14/09 09:15 100 108 3/14/09 09:45 100 108 3/14/09 10:15 100 108 3/14/09 10:45 100 108 3/14/09 11:15 100 108 3/14/09 11:45 100 108 3/14/09 12:15 100 108 3/14/09 12:45 100 108 3/14/09 13:15 100 108 3/14/09 13:45 100 108 3/14/09 14:15 100 108 3/14/09 14:45 100 108 3/14/09 15:15 100 108 3/14/09 15:45 100 108 3/14/09 16:15 100 108 3/14/09 16:45 100 108 3/14/09 17:15 100 107 3/14/09 17:45 100 107 3/14/09 18:15 100 107 1
L-2010-030 Attachment 1 TABLE I Turkey Point Unit 3 History of Reactor Power and Clean-up Flow Date & Time Reactor Power Clean-up Flow History
(%) (gpm) 3/14/09 18:45 100 107 3/14/09 19:15 100 108 3/14/09 19:45 100 108 3/14/09 20:15 100 108 3/14/09 20:45 100 108 3/14/09 21:15 100 108 3/14/09 21:45 100 108 3/14/09 22:15 100 108 3/14/09 22:45 100 108 3/14/09 23:15 100 108 3/14/09 23:45 100 108 3/15/09 00:15 98 108 3/15/09 00:45 95 107 3/15/09 01:15 90 107 3/15/09 01:45 87 108 3/15/09 02:15 82 108 3/15/09 02:45 77 108 3/15/09 03:15 75 107 3/15/09 03:45 70 108 3/15/09 04:15 66 108 3/15/09 04:45 61 108 3/15/09 05:15 57 108 3/15/09 05:45 53 108 3/15/09 06:15 50 108 3/15/09 06:45 49 108 3/15/09 07:15 49 108 3/15/09 07:45 50 108 3/15/09 08:15 50 108 3/15/09 08:45 50 108 3/15/09 09:15 50 108 3/15/09 09:45 50 107 3/15/09 10:15 50 108 3/15/09 10:45 50 108 3/15/09 11:15 50 108 3/15/09 11:45 50 108 3/15/09 12:15 51 108 3/15/09 12:45 51 108 3/15/09 13:15 51 108 3/15/09 13:45 51 108 3/15/09 14:15 51 108 3/15/09 14:45 51 108 3/15/09 15:15 50 108 2
L-2010-030 Attachment 1 TABLE I Turkey Point Unit 3 History of Reactor Power and Clean-up Flow Reactor Reamowr Clean-up Flow History Date & Time Power
(%)(gm (gpm) 3/15/09 15:45 50 108 3/15/09 16:15 50 108 3/15/09 16:45 51 108 3/15/09 17:15 50 108 3/15/09 17:45 50 108 3/15/09 18:15 50 108 3/15/09 18:45 50 107 3/15/09 19:15 50 108 3/15/09 19:45 50 108 3/15/09 20:15 48 108 3/15/09 20:45 44 108 3/15/09 21:15 38 108 3/15/09 21:45 34 107 3/15/09 22:15 30 108 3/15/09 22:45 29 107 3/15/09 23:15 24 108 3/15/09 23:45 23 108 3/16/09 00:15 0 108 3/16/09 00:45 0 108 3/16/09 01:15 0 109 3/16/09 01:45 0 108 3/16/09 02:15 0 107 3
L-2010-030, Attachment 1 Table 2 Turkey Point Unit 3 Specific Activity of Primary Coolant Exceeded TS Limit 3.4.8 . ,-
[1 microcurie per gram Dose Equivalent Iodine (1-131)]
DEQ 1-131 Date & Time (Microcurie per gram) 15-Mar-09 04:00:00 6.35E-03 15-Mar-09 08:00:00 1.01 E-02 15-Mar-09 12:00:00 1.08E-02 15-Mar-09 16:00:00 1.06E-02 15-Mar-09 20:00:00 1.06E-02 16-Mar-09 00:30:00 7.25E-01 2
Date &/Time 16-Mar-09 01:45:00 1.09E+00 Technical Specification 16-Mar-09 04:00:00 1.OOE+00 3.4.8/limit (1 microcurie per 16-Mar-09 07:40:00 6.99E-01 gram DEQ 1-131) was exceeded 16-Mar-09 11:30:00 5.35E-01 16-Mar-09 15:40:00 4.51E-01 16-Mar-09 20:00:00 3.67E-01 17-Mar-09 00:15:00 2.30E-01 17-Mar-09 02:00:00 1.82E-01 17-Mar-09 04:05:00 1.50E-01 17-Mar-09 08:00:00 1.02E-01 17-Mar-09 12:00:00 8.1OE-02
L-2010-030, Attachment 1 FIGURE 1 Reactor Power and Clean-up Flow Rate Prior to Turkey Point Unit 3 Iodine (1-131) Spike on 3116109 iiI~ ___________ ___________
-Izu
_1%
1004 ----------------------- ------------ - ---
80 ---- ------------------
60 1 .-----------------------.
L.-.. --....... --------
40 .......................--........................................................................ --------------------------------................
20 ---------- ----------------------- ------------------------ ------
7 ---- -----
0 3/12/09 12:00 3/13/09 0:00 3/13/09 12:00 3/14/09 0:00 3/14/09 12:00 3/15/09 0:00 3/15/09 12:00 3/16/09 0:00 3/16/09 12:00
-- %Power- Letdown Flow (gpm)
L-2010-030, Attachment 1 Figure 2 '
Fuel Burnup by Turkey Point Unit 3 Core Region 16381 MWD/MTU 47 PPM 1.478 CORE F-DELTA-H 1.747 CORE FQ I
dAB z2T 1 ZbA 7A 18DB ZJD 0.972 1.113 1.351 1,017 1.011 1.370 0.900 0,339 01891 1.172 1.437 1,071 1.098 1,467 1.055 0,595 53420 39940 22060 49270 50670 22760 36430 43240 1,018 1.356 1.696 1,237 1.256 1.738 1.233 0.714 24E 24E 24C 025D 24A 2D5E 23A 1.113 1.130 1.121 1.393 I1.160 1.191 1.0800 0.295 1.172 1.177 1.167 1.478 1.250 1.285 1.310 0.553 39940 39290 40700 22650 35020 37170 17430 42520 1.356 1.364 1.352 1.747 1,452 1.511 1.554 0.672 AbA ZbA Z38 Z11E 2 c 1.351 1.121 1.336 1.004 1.155 1.331 0.719 1.437 1.167 1.427 1.059 1.231 1.465 0.983 22060 40590 21670 51780 41060 21820 33190 1.696 1.352 1.681 1.213 1.436 1.737 1.146 23A 25D 238 248 25C 25B 23C 1.017 1,391 1.004 1.092 1.332 1.135 0.418 1.071 1.475 1.059 1.134 1.459 1.388 0.775 49270 22590 51900 39350 22100 19560 43960 1.237 1.744 1.213 1.311 1.726 1.645 0.992 23B 24A 24E 25C 239 23C 1.011 1.160 1.155 1.332 0,935 0.461 1.088 1.250 1.231 1.459 1.015 0.807 50670 35000 41040 22090 43050 44870 1.256 1.453 1.436 1.726 1.167 0.928
- dbD Z11D ZbD ZbB .&Jc 1.370 1.192 1.331 1.135 0.461 1.467 1.296 1.465 1.398 0.906 22760 37150 21920 18550 44960 1.738 1.513 1.737 1.645 0.926 ii. ___________ IL ___________ IL .11 24C 25B 24C 23C 0.900 1.090 0.719 0.419 1.055 1.310 0.994 0.774 36430 17450 33190 43940 1.233 1.555 1.147 0.091 23A 0.339 0.296 NpI ASSEMBoL POWER REGION 0.585 0.554 AD ASSEMBLY BURNUP 43240 42560 SO ASSEMBLY PQ 1
0.714 0.674
] PhZL QVAflUUA REGION NUMBER OF POWER BURNUPS REGION NUMBER OF POWER BURNUPS IDENT. ASSEMBLIES SHARING TOTAL CYCLE IDENT. ASSEMBLIES SHARING TOTAL CYCLE 22B 1 0.972 53420 13940 24C 20 0.916 36820 14970 23A 12 0.529 44790 8260 24D 8 1.191 37160 20270 23B 16 0.963 49320 15710 24E 16 1.139 40090 19170 23C 16 0.439 44410 6610 2SA 8 1.344 21860 21860 23D 4 0.339 43240 4990 25B 16 1.108 18000 19000 24A 9 1.160 35010 19620 25C 8 1.332 22090 22090 24B 4 1.092 39350 17960 25D 20 1.359 22330 22330 CYCLE 23 - 16381 MWD/MTU