Potential Problems with Crosby Safety Relief Valves Used on Diesel Generator Air Start Receiver TanksML031140248 |
Person / Time |
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Site: |
Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Mcguire, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Big Rock Point, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, 05000000, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant |
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Issue date: |
03/09/1990 |
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From: |
Rossi C Office of Nuclear Reactor Regulation |
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To: |
|
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References |
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IN-90-018, NUDOCS 9003050043 |
Download: ML031140248 (5) |
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Similar Documents at Beaver Valley, Millstone, Hatch, Monticello, Calvert Cliffs, Dresden, Davis Besse, Peach Bottom, Browns Ferry, Salem, Oconee, Mcguire, Nine Mile Point, Palisades, Palo Verde, Perry, Indian Point, Fermi, Kewaunee, Catawba, Harris, Wolf Creek, Saint Lucie, Point Beach, Oyster Creek, Watts Bar, Hope Creek, Grand Gulf, Cooper, Sequoyah, Byron, Pilgrim, Arkansas Nuclear, Three Mile Island, Braidwood, Susquehanna, Summer, Prairie Island, Columbia, Seabrook, Brunswick, Surry, Limerick, North Anna, Turkey Point, River Bend, Vermont Yankee, Crystal River, Haddam Neck, Ginna, Diablo Canyon, Callaway, Vogtle, Waterford, Duane Arnold, Farley, Robinson, Clinton, South Texas, San Onofre, Cook, Comanche Peak, Yankee Rowe, Maine Yankee, Quad Cities, Humboldt Bay, La Crosse, Big Rock Point, Rancho Seco, Zion, Midland, Bellefonte, Fort Calhoun, FitzPatrick, McGuire, LaSalle, 05000000, Fort Saint Vrain, Shoreham, Satsop, Trojan, Atlantic Nuclear Power Plant |
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Mclaughlin on NRC, Regarding NRC Information Notice 2006-13: Groundwater Contamination 2020-09-03 The following query condition could not be considered due to this wiki's restrictions on query size or depth: <code> [[:Beaver Valley]] OR [[:Millstone]] OR [[:Hatch]] OR [[:Monticello]] OR [[:Calvert Cliffs]] OR [[:Dresden]] OR [[:Davis Besse]] OR [[:Peach Bottom]] OR [[:Browns Ferry]] OR [[:Salem]] OR [[:Oconee]] OR [[:Mcguire]] OR [[:Nine Mile Point]] OR [[:Palisades]] OR [[:Palo Verde]] OR [[:Perry]] OR [[:Indian Point]] OR [[:Fermi]] OR [[:Kewaunee]] OR [[:Catawba]] OR [[:Harris]] OR [[:Wolf Creek]] OR [[:Saint Lucie]] OR [[:Point Beach]] OR [[:Oyster Creek]] OR [[:Watts Bar]] OR [[:Hope Creek]] OR [[:Grand Gulf]] OR [[:Cooper]] OR [[:Sequoyah]] OR [[:Byron]] OR [[:Pilgrim]] OR [[:Arkansas Nuclear]] OR [[:Three Mile Island]] OR [[:Braidwood]] OR [[:Susquehanna]] OR [[:Summer]] OR [[:Prairie Island]] OR [[:Columbia]] OR [[:Seabrook]] OR [[:Brunswick]] OR [[:Surry]] OR [[:Limerick]] OR [[:North Anna]] OR [[:Turkey Point]] OR [[:River Bend]] OR [[:Vermont Yankee]] OR [[:Crystal River]] OR [[:Haddam Neck]] OR [[:Ginna]] OR [[:Diablo Canyon]] OR [[:Callaway]] OR [[:Vogtle]] OR [[:Waterford]] OR [[:Duane Arnold]] OR [[:Farley]] OR [[:Robinson]] OR [[:Clinton]] OR [[:South Texas]] OR [[:San Onofre]] OR [[:Cook]] OR [[:Comanche Peak]] OR [[:Yankee Rowe]] OR [[:Maine Yankee]] OR [[:Quad Cities]] OR [[:Humboldt Bay]] OR [[:La Crosse]] OR [[:Big Rock Point]] OR [[:Rancho Seco]] OR [[:Zion]] OR [[:Midland]] OR [[:Bellefonte]] OR [[:Fort Calhoun]] OR [[:FitzPatrick]] OR [[:McGuire]] OR [[:LaSalle]] OR [[:05000000]] OR [[:Fort Saint Vrain]] OR [[:Shoreham]] OR [[:Satsop]] OR [[:Trojan]] OR [[:Atlantic Nuclear Power Plant]] </code>.
[Table view]The following query condition could not be considered due to this wiki's restrictions on query size or depth: <code> [[:Beaver Valley]] OR [[:Millstone]] OR [[:Hatch]] OR [[:Monticello]] OR [[:Calvert Cliffs]] OR [[:Dresden]] OR [[:Davis Besse]] OR [[:Peach Bottom]] OR [[:Browns Ferry]] OR [[:Salem]] OR [[:Oconee]] OR [[:Mcguire]] OR [[:Nine Mile Point]] OR [[:Palisades]] OR [[:Palo Verde]] OR [[:Perry]] OR [[:Indian Point]] OR [[:Fermi]] OR [[:Kewaunee]] OR [[:Catawba]] OR [[:Harris]] OR [[:Wolf Creek]] OR [[:Saint Lucie]] OR [[:Point Beach]] OR [[:Oyster Creek]] OR [[:Watts Bar]] OR [[:Hope Creek]] OR [[:Grand Gulf]] OR [[:Cooper]] OR [[:Sequoyah]] OR [[:Byron]] OR [[:Pilgrim]] OR [[:Arkansas Nuclear]] OR [[:Three Mile Island]] OR [[:Braidwood]] OR [[:Susquehanna]] OR [[:Summer]] OR [[:Prairie Island]] OR [[:Columbia]] OR [[:Seabrook]] OR [[:Brunswick]] OR [[:Surry]] OR [[:Limerick]] OR [[:North Anna]] OR [[:Turkey Point]] OR [[:River Bend]] OR [[:Vermont Yankee]] OR [[:Crystal River]] OR [[:Haddam Neck]] OR [[:Ginna]] OR [[:Diablo Canyon]] OR [[:Callaway]] OR [[:Vogtle]] OR [[:Waterford]] OR [[:Duane Arnold]] OR [[:Farley]] OR [[:Robinson]] OR [[:Clinton]] OR [[:South Texas]] OR [[:San Onofre]] OR [[:Cook]] OR [[:Comanche Peak]] OR [[:Yankee Rowe]] OR [[:Maine Yankee]] OR [[:Quad Cities]] OR [[:Humboldt Bay]] OR [[:La Crosse]] OR [[:Big Rock Point]] OR [[:Rancho Seco]] OR [[:Zion]] OR [[:Midland]] OR [[:Bellefonte]] OR [[:Fort Calhoun]] OR [[:FitzPatrick]] OR [[:McGuire]] OR [[:LaSalle]] OR [[:05000000]] OR [[:Fort Saint Vrain]] OR [[:Shoreham]] OR [[:Satsop]] OR [[:Trojan]] OR [[:Atlantic Nuclear Power Plant]] </code>. |
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C. 20555 March 9. 1990
NRC INFORMATION NOTICE NO. 90-18: POTENTIAL PROBLEMS WITH CROSBY SAFETY
RELIEF VALVES USED ON DIESEL GENERATOR
AIR START RECEIVER TANKS
Addressees
All holders of operating licenses or construction permits for nuclear power
reactors.
Purpose
This information notice is intended to alert addressees to potential problems
with Crosby safety relief valves that could result in a loss of starting'alt
to the emergency diesel generators (EDGs). It is expected that'recipients
will review the information for applicability to their facilities and consider
actions, as appropriate, to avoid similar problems. However, suggestions
contained in this Information notice do not constitute NRC requirements'
therefore, no specific action or written response is required.
Description of Circumstances
On March 13, 1989, Cooper Industries was made aware of circumstances at Perry
Unit 1 that led to the Division I EDG being declared inoperable. A Crosby
safety relief valve on'one of the two EDG starting air receiving tanks was
inadvertently hit during maintenance activities. The force of the impact
caused the valve to open and blow down both air receiving tanks. The safety
relief valve did not reseat until approximately 30 psig below the EDG automatic
start lockout signal. On January 12, 1990, Cooper Industries learned that a
similar event had occurred at Comanche Peak. On January 17, 1990, Cooper
Industries'submitted a 10 CFR Part 21 report on the affected safety relief
valves (Crosby style JMBU and JRU safety relief valves).
Discussion of Safety Significance:
Although Crosby-style JMBU and JRU safety relief valves were designed to meet
the requirements of Section VIII of the ASME Boiler and Pressure Vessel Code, they were not seismically qualified. In addition, the blowdown characteristics
of the valves were not consistent with the functional requirements of the
system in which they were installed. Cooper Industries has recommended re- placing these valves with seismically-qualified valves that have the proper
blowdown reseat characteristics.
9003043 Z.A
IN 90-18
March 9, 1990 All licensees with Transamerica Delaval Inc. (TDI) diesel generators were
notified of this problem by Cooper Industries via the Part 21 notification.
However, Crosby safety relief valves (style JMBU, JRU, and possibly non-code
style JMB) may be installed on EDGs manufactured by other vendors. Licensees
may wish to verify that the relief valves installed in their EDG air start
systems have appropriate qualifications and characteristics.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact the
technical contact listed below or the appropriate NRR project manager.
'ar es E. Rossi, a ector
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical Contact:
John Thompson, NRR
(301) 492-1175 Attachment: List of Recently Issued NRC Information Notices
.1 . Attachment
IN 90-18 March 9, 1990 LIST OF RECENTLY ISSUED
NRC INFORMATION NOTICES
Information Date ot
Notice No. Subject Issuance Issued to
90-17 Weight and Center of 3/8/90 All holders of OLs
Gravity Discrepancies or CPs for nuclear
for Copes-Vulcan Valves power reactors.
89-59, Suppliers of Potentially 3/7/90 All holders of OLs
Supp. 2 Misrepresented Fasteners or CPs for nuclear
power reactors.
90-16 Compliance with New 3/7/90 All materials licensees.
Decommissioning Rule
90-15 Reciprocity: Notification 3/7/90 All holders of NRC
of Agreement State Radiation materials licenses
Control Directors Before which authorize use
Beginning Work in Agreement of radioactive
States material at temporary
job sites.90-14_ Accidental Disposal of 3L6190 All U.S. NRC byproduct
Radioactive Materials material licensees.
90-13 Importance of Review and 3/5/90 All holders of OLs
Analysis of Safeguards or CPs for nuclear
Event Logs power reactors.
90-12 Monitoring or Interruption 2/28/90 All holders of OLs
of Plant Communications or CPs for nuclear
power reactors.
90-11 Maintenance Deficiency 2/28/90 All holders of OLs
Associated with Solenoid- or CPs for nuclear
Operated Valves power reactors.
90-10 Primary Water Stress 2/23/90 All holders of OLs
Corrosion Cracking (PWSCC) or CPs for PWRs.
of Inconel 600
90-09 Extended Interim Storage of 2/5/90 All holders of NRC
Low-Level Radioactive Waste materials licenses.
by Fuel Cycle and Materials
Licensees
OL = Operating License
CP = Construction Permit
IN 90-18 March 9, 1990 All licensees with Transamerica Delaval Inc. (TD) diesel generators were
notified of this problem by Cooper Industries via the Part 21 notification.
However, Crosby safety relief valves (style JMBU, JRU, and possibly non-code
style JMB) may be installed on EDGs manufactured by other vendors. Licensees
may wish to verify that the relief valves installed in their EDG air start
systems have appropriate qualifications and characteristics.
This Information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact the
technical contact listed below or the appropriate NRR project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical Contact:
John Thompson, NRR
(301) 492-1175 Attachment: List of Recently Issued NRC Information Notices
Document Name: NRC INFORMATION NOTICE
- SEE PREVIOUS PAGE FOR CONCURRENCE
Wg'
OJD /90
k
- EAB:DOEA:NRR *SC/EAB:DOEA:NRR *AC/OEAB:DOEA:NRR*RPB:ADM *C/OGCB:DOEA:NRR
JThompson:fh DFischer PBaranowsky TechEd CBerlinger
02/28/90 02/28/90 02/28/90 02/28/90 03/02/90
IN 90-XX
March xx, 1990 All licensees with Transamerica Delaval Inc. (TDI) diesel generators were
notified of this problem by Cooper Industries via the Part 21 notification.
However, Crosby safety relief valves (style JMBU, JRU, and possibly non-code
style JMB) may be installed on EDMs manufactured by other vendors. Licensees
may wish to verify that the relief valves installed in their EDG air start
systems have appropriate qualifications and characteristics.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact the
technical contact listed below or the appropriate NRR project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical Contact:
John Thompson, NRR
(301) 492-1175 Attachment: List of Recently Issued NRC Information Notices
Document Name: NRC INFORMATION NOTICE
D/DOEA:NRR
CERossi
02/ /90
EABW :NRR XAB:DOEA:NRR AC/OEAB:DOEA:NRR C/OGCB:DOE :NRi
JTh Aj3son:fh DFischer PBaranowsky CBerling
02r/2/90 02/R2 /90 02/2X /90 03p0290
|
---|
|
list | - Information Notice 1990-01, Importance of Proper Response to Self-Identified Violations by Licensees (12 January 1990, Topic: Uranium Hexafluoride)
- Information Notice 1990-02, Potential Degradation of Secondary Containment (22 January 1990)
- Information Notice 1990-03, Malfunction of Borg-Warner Bolted Bonnet Check Valves Caused by Failure of the Swing Arm (23 January 1990, Topic: Liquid penetrant)
- Information Notice 1990-04, Cracking of the Upper Shell-to-Transition Cone Girth Welds in Steam Generators, (26 January 1990, Topic: Nondestructive Examination)
- Information Notice 1990-05, Inter-System Discharge of Reactor Coolant (29 January 1990)
- Information Notice 1990-06, Potential for Loss of Shutdown Cooling While at Low Reactor Coolant Levels (29 January 1990)
- Information Notice 1990-07, New Information Regarding Insulation Material Performance and Debris Blockage of PWR Containment Sumps (30 January 1990)
- Information Notice 1990-08, KR-85 Hazards from Decayed Fuel (1 February 1990)
- Information Notice 1990-08, KR-85 Hazards From Decayed Fuel (1 February 1990)
- Information Notice 1990-09, Extended Interim Storage of Low-Level Radioactive Waste by Fuel Cycle and Materials Licensees (5 February 1990, Topic: Decommissioning Funding Plan)
- Information Notice 1990-10, Primary Water Stress Corrosion Cracking (PWSCC) of Inconel 600 (23 February 1990, Topic: Boric Acid, Hydrostatic, Liquid penetrant)
- Information Notice 1990-10, Primary Water Stress Corrosion Cracking of Inconel 600 (23 February 1990, Topic: Boric Acid, Hydrostatic, Nondestructive Examination, Liquid penetrant)
- Information Notice 1990-11, Maintenance Deficiency Associated with Solenoid-Operated Valves (28 February 1990)
- Information Notice 1990-12, Monitoring or Interruption of Plant Communications (28 February 1990)
- Information Notice 1990-13, Importance of Review and Analysis of Safeguards Event Logs (5 March 1990)
- Information Notice 1990-14, Accidental Disposal of Radioactive Materials (6 March 1990, Topic: Brachytherapy)
- Information Notice 1990-15, Reciprocity Notification of Agreement State Radiation Control Directors Before Beginning Work in Agreement States (17 March 1990, Topic: Uranium Hexafluoride)
- Information Notice 1990-16, Compliance with New Decommissioning Rule (7 March 1990)
- Information Notice 1990-17, Weight and Center of Gravity Discrepancies for Copes-Vulcan Valves (8 March 1990, Topic: Earthquake)
- Information Notice 1990-18, Potential Problems with Crosby Safety Relief Valves Used on Diesel Generator Air Start Receiver Tanks (9 March 1990)
- Information Notice 1990-18, Potential Problems With Crosby Safety Relief Valves Used on Diesel Generator Air Start Receiver Tanks (9 March 1990)
- Information Notice 1990-19, Potential Loss of Effective Volume for Containment Recirculation Spray at PWR Facilities (14 March 1990)
- Information Notice 1990-20, Personnel Injuries Resulting from Improper Operation of Radwaste Incinerators (22 March 1990)
- Information Notice 1990-21, Potential Failure of Motor-Operated Butterfly Valves to Operate Because Valve Seat Friction was Underestimated (22 March 1990)
- Information Notice 1990-21, Potential Failure of Motor-Operated Butterfly Valves to Operate Because Valve Seat Friction Was Underestimated (22 March 1990)
- Information Notice 1990-22, Unanticipated Equipment Actuations Following Restoration of Power to Rosemount Transmitter Trip Units (23 March 1990, Topic: Reactor Vessel Water Level)
- Information Notice 1990-23, Improper Installation of Patel Conduit Seals (4 April 1990)
- Information Notice 1990-24, Transportation of Model Spec 2-T Radiographic Exposure Device (10 April 1990)
- Information Notice 1990-24, Transportation of Model SPEC 2-T Radiographic Exposure Device (10 April 1990)
- Information Notice 1990-25, Loss of Vital AC Power With Subsequent Reactor Coolant System Heat-Up (16 April 1990)
- Information Notice 1990-25, Loss of Vital AC Power with Subsequent Reactor Coolant System Heat-Up (16 April 1990)
- Information Notice 1990-26, Inadequate Flow of Essential Service Water to Room Coolers and Heat Exchangers for Engineered Safety-Feature Systems (24 April 1990)
- Information Notice 1990-27, Clarification of the Recent Revisions to the Regulatory Requirements for Packaging of Uranium Hexafluoride (UF6) for Transportation (30 April 1990)
- Information Notice 1990-28, Potential Error In High Steamline Flow Setpoint (30 April 1990)
- Information Notice 1990-28, Potential Error in High Steamline Flow Setpoint (30 April 1990)
- Information Notice 1990-29, Cracking of Cladding and Its Heat-Affected Zone in the Base Metal of a Reactor Vessel Head (30 April 1990, Topic: Nondestructive Examination, Liquid penetrant)
- Information Notice 1990-30, Ultrasonic Inspection Techniques for Dissimilar Metal Welds (1 May 1999, Topic: Dissimilar Metal Weld)
- Information Notice 1990-31, Update on Waste Form and High Integrity Container Topical Report Review Status, Identification of Problems with Cement Solidification, and Reporting of Waste Mishaps (4 May 1990, Topic: Process Control Program)
- Information Notice 1990-31, Update on Waste form and High Integrity Container Topical Report Review Status, Identification of Problems with Cement Solidification, and Reporting of Waste Mishaps (4 May 1990, Topic: Process Control Program)
- Information Notice 1990-32, Surface Crack and Subsurface Indications in the Weld of a Reactor Vessel Head (3 May 1990)
- Information Notice 1990-33, Sources of Unexpected Occupational Radiation Exposures at Spent Fuel Storage Pools (9 May 1990)
- Information Notice 1990-34, Response to False Siren Activations (10 May 1990)
- Information Notice 1990-35, Transportation of Type a Quantities of Non-Fissile Radioactive Materials (24 May 1990)
- Information Notice 1990-37, Sheared Pinion Gear-To-Shaft Keys in Limitorque Motor Actuators (24 May 1990)
- Information Notice 1990-38, License and Fee Requirements for Processing Financial Assurance Submittals for Decommissioning (6 November 1990, Topic: Authorized possession limits)
- Information Notice 1990-39, Recent Problems with Service Water Systems (1 June 1990)
- Information Notice 1990-40, Results of NRC-Sponsored Testing of Motor-Operated Valves (5 June 1990, Topic: Weak link)
- Information Notice 1990-41, Potential Failure of General Electric Magne-Blast Circuit Breakers and Ak Circuit Breakers (12 June 1990)
- Information Notice 1990-42, Failure of Electrical Power Equipment Due to Solar Magnetic Disturbances (19 June 1990)
- Information Notice 1990-43, Mechanical Interference with Thermal Trip Function in GE Molded-Case Circuit Breakers (29 June 1990)
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